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            .                                               .,,
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                                                                                            '
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        p Ktog                               UNITE 3 STATES                                       l
p Ktog
                Do
UNITE 3 STATES
                                                                  .
.
                '
l
                                    NUCLEAR REGULATORY COMMISSION                                  !
Do
  ,8         -
NUCLEAR REGULATORY COMMISSION
                  ,                             REGION 11                                          I
'
  g               ,j                     101 MARIETTA STREET.N.W.         .
REGION 11
  *               t                     ATLANTA, GEORGIA 30323 a
,8
  \, * * * * /
-
    Report Nos. 50-325/87-03 and 50-324/87-03
,
    Licensee: Carolina Power and Light Company
g
                    P. O. Box 1551
,j
                    Raleigh, NC 27602
101 MARIETTA STREET.N.W.
    Docket Nos.: 50-325 and 50-324                       License Nos.: DPR-71 and DPR-62
.
    Facility Name: Brunswick 1 and 2
*
    Inspection Conducted: February 1 - 28, 1987 and March 3-4, 1987
t
    Inspectors:
ATLANTA, GEORGIA 30323 a
                g
\\, * * * * /
                      .I. N &
Report Nos. 50-325/87-03 and 50-324/87-03
                      , H. Ruland
Licensee: Carolina Power and Light Company
                                                                                3/16/f7
P. O. Box 1551
                                                                                Date Signed
Raleigh, NC 27602
                    9.6.d
Docket Nos.: 50-325 and 50-324
                @ LM W. Garner ,
License Nos.: DPR-71 and DPR-62
                                                                                slu tt?
Facility Name: Brunswick 1 and 2
                                                                                Date Signed       ,
Inspection Conducted: February 1 - 28, 1987 and March 3-4, 1987
    Approved by:        .  .                                                  3 /2(> [87
.I. N &
              g P4 Division
3/16/f7
                      E. Fredrickson, Section Chief                           Date Signed
Inspectors:
                              of Reactor Projects
g
                                              SUMMARY
, H. Ruland
    Scope:       This routine safety inspection involved the areas of maintenance
Date Signed
    observation, surveillance observation, operational safety verification, onsite
9.6.d
    Licensee Event Reports (LER) review, in-office LER review, followup on
slu tt?
    inspector identified and unresolved items, Limitorque Operators, spent fuel
@ LM W. Garner ,
    storage capacity, and refueling activities.
Date Signed
    Results: One violation - failure to maintain Unit 2 PWR spent fuel storage
,
    capacity, paragraph 11,
3 /2(> [87
                                                                                                  1
Approved by:
        0704130291 870330
.
        PDR     ADOCK 0D000324
.
        0                     PDR
g P4 E. Fredrickson, Section Chief
Date Signed
Division of Reactor Projects
SUMMARY
Scope:
This routine safety inspection involved the areas of maintenance
observation, surveillance observation, operational safety verification, onsite
Licensee Event Reports (LER) review, in-office LER review, followup on
inspector identified and unresolved items, Limitorque Operators, spent fuel
storage capacity, and refueling activities.
Results:
One violation - failure to maintain Unit 2 PWR spent fuel storage
capacity, paragraph 11,
1
0704130291 870330
PDR
ADOCK 0D000324
0
PDR
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- - -
- - -


                                            ,           _ _ .                                                   _ _ _ _ - _ _ _ _ .
,
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_
_ _ _ - _ _ _ _ .
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                                    REPORT DETAILS
REPORT DETAILS
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    1. Persons Contacted
1.
      Licensee Employees
Persons Contacted
      P. Howe, Vice President - Brunswick Nuclear Project
Licensee Employees
l     C. Dietz, General Manager - Brunswick Nuclear Project
P. Howe, Vice President - Brunswick Nuclear Project
l
C. Dietz, General Manager - Brunswick Nuclear Project
T. Wyllie, Manager - Engineering and Construction
'
'
      T. Wyllie, Manager - Engineering and Construction
J. Holder, Manager - Outages
      J. Holder, Manager - Outages
R. Eckstein, Manager - Technical Support
      R. Eckstein, Manager - Technical Support
E. Bishop, Manager - Operations
      E. Bishop, Manager - Operations
l
l     L. Jones, Director - Quality Assurance (QA)/ Quality Control (QC)-
L. Jones, Director - Quality Assurance (QA)/ Quality Control (QC)-
      R. Helme, Director - Onsite Nuclear Safety - BSEP
R. Helme, Director - Onsite Nuclear Safety - BSEP
      J. Chase, Assistant to General Manager
J. Chase, Assistant to General Manager
      J. O'Sullivan, Manager - Maintenance
J. O'Sullivan, Manager - Maintenance
      G. Cheatham, Manager - Environmental & Radiation Control
G. Cheatham, Manager - Environmental & Radiation Control
      J. Smith, Manager - Administrative Support
J. Smith, Manager - Administrative Support
      K. Enzor, Director - Regulatory Compliance
K. Enzor, Director - Regulatory Compliance
      A. Hegler, Superintendent - Operations
A. Hegler, Superintendent - Operations
,      W. Hogle, Engineering Supervisor
W. Hogle, Engineering Supervisor
l     B. Wilson, Engineering Supervisor
,
l     B. Parks, Engineering Supervisor
l
      R.Creech,I&C/ElectricalMaintenanceSupervisor(Unit 2)
B. Wilson, Engineering Supervisor
      R. Warden, ISC/ Electrical Maintenance Supervisor (Unit 1)
l
      W. Dorman, Supervisor - QA
B. Parks, Engineering Supervisor
      W. Hatcher Supervisor - Security
R.Creech,I&C/ElectricalMaintenanceSupervisor(Unit 2)
      R. Kitchen,MechanicalMaintenanceSupervisor(Unit 2)
R. Warden, ISC/ Electrical Maintenance Supervisor (Unit 1)
!     C. Treubel, Mechanical Maintenance Supervisor (Unit 1)
W. Dorman, Supervisor - QA
      R. Poulk, Senior NRC Regulatory Specialist
W. Hatcher Supervisor - Security
      W. Murray, Senior Engineer - Nuclear Licensing Unit
R. Kitchen,MechanicalMaintenanceSupervisor(Unit 2)
;      Otiler licensee employees contacted included construction craftsmen,
!
C. Treubel, Mechanical Maintenance Supervisor (Unit 1)
R. Poulk, Senior NRC Regulatory Specialist
W. Murray, Senior Engineer - Nuclear Licensing Unit
Otiler licensee employees contacted included construction craftsmen,
;
engineers, technicians, operators, office personnel, and security force
'
'
      engineers, technicians, operators, office personnel, and security force
members.
      members.
1
1
    2. ExitInterview(30703)
2.
l     The inspection scope and findings were summarized on March 3,1987, with
ExitInterview(30703)
l
The inspection scope and findings were summarized on March 3,1987, with
the general manager and vice-president. The violation, excess capacity in
'
'
      the general manager and vice-president. The violation, excess capacity in
the Unit 2 spent fuel pool (paragraph 11), was discussed in detail. The
      the Unit 2 spent fuel pool (paragraph 11), was discussed in detail. The
i
i     inspector stated that the item was unresolved pending inspector discussion
inspector stated that the item was unresolved pending inspector discussion
      with regional management.    On March 4, 1987, the licensee was informed by
'
'
      the inspector that the spent fuel pool issue was a violation.                                         The
with regional management.
i     licensee agreed to address the issue of board walkdowns/ reviews
On March 4, 1987, the licensee was informed by
      (paragraph 6) along with the response to the violation. The licensee
the inspector that the spent fuel pool issue was a violation.
l     acknowledged the findings without exception. The licensee did not
The
l     identify as proprietary any of the materials provided to or reviewed by
i
      the inspectors during the inspection.
licensee agreed to address the issue of board walkdowns/ reviews
                                                                      _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ .
(paragraph 6) along with the response to the violation.
The licensee
l
acknowledged the findings without exception.
The licensee did not
l
identify as proprietary any of the materials provided to or reviewed by
the inspectors during the inspection.
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                                            2
2
    3. Followup on Previous Enforcement Matters (92702)
3.
      Not inspected.
Followup on Previous Enforcement Matters (92702)
;   4. Maintenance Observation (62703)
Not inspected.
      The inspectors observed maintenance activities and reviewed records to
;
      verify that work was conducted in accordance with approved procedures,
4.
      Technical Specifications, and applicable industry codes and standards. The
Maintenance Observation (62703)
      inspectors also verified that:       redundant components were operable;
The inspectors observed maintenance activities and reviewed records to
      administrative controls were followed; tagouts were adequate; personnel
verify that work was conducted in accordance with approved procedures,
      were qualified; correct replacement parts were used; radiological controls
Technical Specifications, and applicable industry codes and standards. The
      were proper; fire protection was adequate; quality control hold points
inspectors also verified that:
      were adequate and observed; adequate post-maintenance testing was
redundant components were operable;
      performed; and independent verification requirements were implemented.
administrative controls were followed; tagouts were adequate; personnel
      The inspectors independently verified that selected equipment was properly
were qualified; correct replacement parts were used; radiological controls
      returned to service.
were proper; fire protection was adequate; quality control hold points
      Outstanding work requests were reviewed to ensure that the licensee gave
were adequate and observed; adequate post-maintenance testing was
      priority to safety-related maintenance.
performed; and independent verification requirements were implemented.
The inspectors independently verified that selected equipment was properly
returned to service.
Outstanding work requests were reviewed to ensure that the licensee gave
priority to safety-related maintenance.
.
.
      The inspectors observed / reviewed portions of the following maintenance
The inspectors observed / reviewed portions of the following maintenance
      activities:
activities:
            MP-09           Dryer / Separator, Cattle Chute, and Fuel Pool Gates
MP-09
                            Removal and Installation.
Dryer / Separator, Cattle Chute, and Fuel Pool Gates
              OLP-NVT001     Topaz Static Inverter and Lambda Power Supply.
Removal and Installation.
              WR&A-87-AGEB1 Repair of Unit 2 Annunciation Horn Circuit.
OLP-NVT001
      During performance of work request 87-AGEB1, the inspector observed a
Topaz Static Inverter and Lambda Power Supply.
      communication problem between operations and maintenance personnel. At
WR&A-87-AGEB1 Repair of Unit 2 Annunciation Horn Circuit.
During performance of work request 87-AGEB1, the inspector observed a
communication problem between operations and maintenance personnel.
At
first, the annunciator horn being repaired, could not be silenced. Later,
'
'
      first, the annunciator horn being repaired, could not be silenced. Later,
j
j      the horn stopper' continuously sounding and would not sound when another
the horn stopper' continuously sounding and would not sound when another
!     annunciator came in. Operations was aware of this and took proper
!
      compensatory actions, e. g., assigned sections of the board to individuals
annunciator came in.
      to note when a new annunciator came in. The first problem was correctly
Operations was aware of this and took proper
      conmunicated to maintenance; however, the change in symptoms was not.
compensatory actions, e. g., assigned sections of the board to individuals
      Operations assumed the change was due to Instrumentation and Control (I&C)
to note when a new annunciator came in.
      trouble shooting activities.     The inspector informed the maintenance
The first problem was correctly
      personnel of the second item approximately 30 minutes after it happened.
conmunicated to maintenance; however, the change in symptoms was not.
      Although the inspector was confident that the problem would have been
Operations assumed the change was due to Instrumentation and Control (I&C)
      fixed, the failure of operations personnel to recognize that a new
trouble shooting activities.
      condition existed versus a condition induced by I&C personnel performing
The inspector informed the maintenance
      trouble shooting or repair, was a concern. Inadequate communication can
personnel of the second item approximately 30 minutes after it happened.
      noticeably increase the length of time an unsatisfactory condition exists.
Although the inspector was confident that the problem would have been
      This matter was discussed with cognizant supervision.
fixed, the failure of operations personnel to recognize that a new
      No violations or deviations were identified.
condition existed versus a condition induced by I&C personnel performing
trouble shooting or repair, was a concern.
Inadequate communication can
noticeably increase the length of time an unsatisfactory condition exists.
This matter was discussed with cognizant supervision.
No violations or deviations were identified.


                                                                                                            <
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                      5.   SurveillanceObservation(61726)
5.
                            The inspectors observed surveillance testing required by Technical
SurveillanceObservation(61726)
                            Specifications. Through observation and record review, the inspectors
The inspectors observed surveillance testing required by Technical
                            verified that: tests conformed to Technical Specification requirements;
Specifications.
                            administrative controls were followed; personnel were qualified;
Through observation and record review, the inspectors
                              instrumentation was calibrated; and data was accurate and complete.                         The
verified that:
                              inspectors independently verified selected test results and proper return
tests conformed to Technical Specification requirements;
                            to service of equipment.
administrative controls were followed; personnel were qualified;
                            The inspectors witnessed / reviewed portions of the following test
instrumentation was calibrated; and data was accurate and complete.
                            activities:
The
                                                        IMST-DG12R     Diesel Generator DG-2 Loading Test.
inspectors independently verified selected test results and proper return
                                                        2MST-APRM12   Average Power Range Monitor (APRM), (Ch. 8, D & F)
to service of equipment.
                                                                      Channel Functional Test (Reactor Protection System
The inspectors witnessed / reviewed portions of the following test
                                                                      (RPS) Inputs].
activities:
                                                        2MST-ATWS22M   Anticipated Transcient Without Scram (ATWS) Reactor
IMST-DG12R
                                                                      High Pressure Trip Instrument Channel Calibration.
Diesel Generator DG-2 Loading Test.
                                                        2MST-RHR21M   Residual Heat Removal (RHR) - Low Pressure Coolant
2MST-APRM12
                                                                      Injection (LPCI), Core Spray System (CSS) and HPCI Hi
Average Power Range Monitor (APRM), (Ch. 8, D & F)
                                                                      Drywell Pressure Trip Unit Channel Calibration.
Channel Functional Test (Reactor Protection System
                                                        PT-12.8       Electrical Power Systems Operability Test.
(RPS) Inputs].
                              During performance of IMST-DG12R on February 17, 1987, the licensee
2MST-ATWS22M
                                identified that step 7.4.30 had not been performed correctly. The step
Anticipated Transcient Without Scram (ATWS) Reactor
                              requires stopping of the core spray pump while supplying rated flow to
High Pressure Trip Instrument Channel Calibration.
                              verify that the DG does not trip.                         This is a surveillance requirement
2MST-RHR21M
                              specified in Technical Specification (TS) .4.8.1.1.2.d.2. The operator
Residual Heat Removal (RHR) - Low Pressure Coolant
                                reduced the flow prior to stopping the pumb. This is the method normally
Injection (LPCI), Core Spray System (CSS) and HPCI Hi
                              used to stop the pump as required by either the quarterly required
Drywell Pressure Trip Unit Channel Calibration.
                              Surveillance Test Procedure PT-07.2.4b, or the Operating Procedure OP-18.
PT-12.8
                              The licensee verified that during another performance of MST-DG12R, the
Electrical Power Systems Operability Test.
                                step was satisfactorily performed. This item meets all the requirements
During performance of IMST-DG12R on February 17, 1987, the licensee
                                to be considered as a licensee identified violation. The licensee is
identified that step 7.4.30 had not been performed correctly.
                                preparing an Operating Experience Report (0ER) to address the root cause
The step
                                of the communication failure between the I&C personnel in charge of the
requires stopping of the core spray pump while supplying rated flow to
                                test and the control operator. The inspector plans to review the OER when
verify that the DG does not trip.
                                issued.                     This is an Inspector Followup Item:     Review of IMST-DG12R
This is a surveillance requirement
                                ProcedureViolationOER(325/87-03-03).
specified in Technical Specification (TS) .4.8.1.1.2.d.2.
                              One licensee identified violation and no deviations were identified.
The operator
                      6.     Operational Safety Verification (71707)                                                         )
reduced the flow prior to stopping the pumb. This is the method normally
                                                                                                                              T
used to stop the pump as required by either the quarterly required
. _ - _ _ - _ _ _        _ _ - _ _ _ _ _ _ _ _ _ _ - _
Surveillance Test Procedure PT-07.2.4b, or the Operating Procedure OP-18.
The licensee verified that during another performance of MST-DG12R, the
step was satisfactorily performed.
This item meets all the requirements
to be considered as a licensee identified violation.
The licensee is
preparing an Operating Experience Report (0ER) to address the root cause
of the communication failure between the I&C personnel in charge of the
test and the control operator. The inspector plans to review the OER when
issued.
This is an Inspector Followup Item:
Review of IMST-DG12R
ProcedureViolationOER(325/87-03-03).
One licensee identified violation and no deviations were identified.
6.
Operational Safety Verification (71707)
)
T
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                                                      4
4
1-
1-
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:               The inspectors verified conformance with regulatory requirements by direct
:
The inspectors verified conformance with regulatory requirements by direct
. observations of activities, facility tours, discussions with personnel,
,
,
              . observations of activities, facility tours, discussions with personnel,
reviewing of records and independent-verification.of safety. system status.
                reviewing of records and independent-verification.of safety. system status.
1
1
!
!             The inspectors verified that control room manning requirements of 10 CFR
The inspectors verified that control room manning requirements of 10 CFR
50.54 and the Technical Specifications were-met. . Control room, shift
<
<
                50.54 and the Technical Specifications were-met. . Control room, shift
supervisor, and clearance logs were reviewed to obtain information-
<
<
                supervisor, and clearance logs were reviewed to obtain information-
j
j              concerning operating trends and out of service safety systems to ensure
concerning operating trends and out of service safety systems to ensure
'
that there were no conflicts with Technical Specifications Limiting
                that there were no conflicts with Technical Specifications Limiting
:              Conditions for Operations. Direct observations were conducted of control
'
'
                room panels, instrumentation and recorder traces important to safety to
:
a              verify operability and that parameters were within~ Technical Specification
Conditions for Operations.
]               limits. The inspectors observed shift turnovers to verify that continuity
Direct observations were conducted of control
;.              of system status was maintained. :The' inspectors verified the status of
'
                selected control room annunciators.
room panels, instrumentation and recorder traces important to safety to
verify operability and that parameters were within~ Technical Specification
a
]
limits. The inspectors observed shift turnovers to verify that continuity
of system status was maintained. :The' inspectors verified the status of
;.
selected control room annunciators.
1
1
i               Operability of ' a selected Engineered ' Safety Feature (ESF) train was -
i
i               verified by insuring that:       each accessible valve in the flow path was in
Operability of ' a selected Engineered ' Safety Feature (ESF) train was -
;             its correct position; each power supply' and breaker,. including control
i
                room fuses, were aligned for components that must activate upon initiation
verified by insuring that:
;               signal; removal of power from those - ESF motor-operated valves, so
each accessible valve in the flow path was in
                identified by Technical Specifications, was completed; there was. no
;
                                                                  ~
its correct position; each power supply' and breaker,. including control
room fuses, were aligned for components that must activate upon initiation
;
signal; removal of power from those - ESF motor-operated valves, so
1
1
identified by Technical Specifications, was completed; there was. no
~
1
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                leakage of major components; there was proper lubrication and cooling
leakage of major components; there was proper lubrication and cooling
i              water available; and a condition did. not exist which might prevent
water available; and a condition did. not exist which might prevent
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                fulfillment of the system's functional requirements. Instrumentation
fulfillment of the system's functional requirements.
i               essential to system actuation or performance was. verified operable by
Instrumentation
                observing on-scale indication and proper instrument valve lineup, if
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essential to system actuation or performance was. verified operable by
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j               accessible.
observing on-scale indication and proper instrument valve lineup, if
                The     inspectors verified     that the licensee's health physics
j
J               policies / procedures were followed.     This includod a review of area
accessible.
The
inspectors verified
that the licensee's health physics
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policies / procedures were followed.
This includod a review of area
surveys, radiation work permits, posting, and instrument calibration.
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,
                surveys, radiation work permits, posting, and instrument calibration.
The inspectors verified that:
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the security. organization was properly
    .
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                The inspectors verified that:       the security. organization was properly
.
{              manned and security personnel were capable of performing their assigned
manned and security personnel were capable of performing their assigned
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functions; persons and packages were checked prior to entry into the
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                functions; persons and packages were checked prior to entry into the
!              protected area (PA); vehicles were properly authorized, searched and
;              escorted within the PA; persons within the PA ~ displayed photo
:              identification badges; personnel in vital areas were authorized; and
                effective compensatory measures were employed when required.
!
!
i               On February 1, -1987, the inspector found a vital area door closed but           !
protected area (PA); vehicles were properly authorized, searched and
;
escorted within the PA; persons within the PA ~ displayed photo
identification badges; personnel in vital areas were authorized; and
:
effective compensatory measures were employed when required.
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On February 1, -1987, the inspector found a vital area door closed but
unlatched.
While an unauthorized person could have opened the door, the
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                unlatched.      While an unauthorized person could have opened the door, the    l
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security computer would have detected the intrusion, enabling the security
                security computer would have detected the intrusion, enabling the security       j
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>              force to respond. The inspector reported the condition to security. A
force to respond.
{               security member responded in a timely manner, verified the condition and
The inspector reported the condition to security.
                took action as required.
A
                                                                                                  .
>
i              The inspectors also observed plant housekeeping controls, verified
{
!               position of certain containment isolation valves, and verified ' the
security member responded in a timely manner, verified the condition and
i               operability of onsite and offsite emergency power sources.-
took action as required.
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The inspectors also observed plant housekeeping controls, verified
!
position of certain containment isolation valves, and verified ' the
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operability of onsite and offsite emergency power sources.-
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On February 2,1987, the inspector observed the Unit 2 A and 6 trains of
        On February 2,1987, the inspector observed the Unit 2 A and 6 trains of
Standby Gas Treatment (SBGT) system with loose blower and motor pedestal
        Standby Gas Treatment (SBGT) system with loose blower and motor pedestal
mounting rubber bushing retaining bolts.
        mounting rubber bushing retaining bolts. The licensee issued work
The licensee issued work
        requests 87-ADJIl and 87-ADJJ1 to correct the deficiency. The licensee
requests 87-ADJIl and 87-ADJJ1 to correct the deficiency.
        inspected Unit I and issued work requests ADJK1 and ADJL1 to correct
The licensee
        similar deficiencies on Unit 1 SBGT trains A and B. Technical support
inspected Unit I and issued work requests ADJK1 and ADJL1 to correct
        reviewed the "as found" condition and determined that the condition had
similar deficiencies on Unit 1 SBGT trains A and B.
        not rendered the SBGT trains inoperable.
Technical support
        On February 12, 1987, at 7:50 a.m., the inspector found valve 1-E11-F007B,
reviewed the "as found" condition and determined that the condition had
        the Division II RHR minimuni flow valve, open instead of closed. The valve
not rendered the SBGT trains inoperable.
        had remained open after the licensee had performed OP-17, RHR Operating
On February 12, 1987, at 7:50 a.m., the inspector found valve 1-E11-F007B,
        Procedure   Section 8.7, draining the suppression pool to radwaste.
the Division II RHR minimuni flow valve, open instead of closed. The valve
        Valve]-Ell F007B auto-opened when the RHR pump was started, but no
had remained open after the licensee had performed OP-17, RHR Operating
        procedure step existed to manually reshut the valve. Thus, the valve was
Procedure
        in the position required by the last procedure performed on the RHR
Section 8.7, draining the suppression pool to radwaste.
        system.   However, the licensee reported that the evolution had occurred
Valve]-Ell F007B auto-opened when the RHR pump was started, but no
        two shifts prior to discovery.     Therefore, three shifts and two shift
procedure step existed to manually reshut the valve. Thus, the valve was
        turnovers failed to identify the mi:; positioned valve.   The Plant General
in the position required by the last procedure performed on the RHR
        Manager agreed to address this issue, weakness in board walkdowns and
system.
        board review after valve manipulations, when responding to the violation
However, the licensee reported that the evolution had occurred
        issued with this report.   This is an Inspector Followup Item: Inadequate
two shifts prior to discovery.
        Board Walkdown and Review (325/87-03-04).
Therefore, three shifts and two shift
        No violations or deviations were identified.
turnovers failed to identify the mi:; positioned valve.
    7. Onsite Review of Licensee Event Reports (92700)
The Plant General
        The listed Licensee Event Reports (LERs) were reviewed to verify that the
Manager agreed to address this issue, weakness in board walkdowns and
        inforr.ation provided met NRC reporting requirements. The verification
board review after valve manipulations, when responding to the violation
        included adequacy of event description and corrective action taken or
issued with this report.
        planned, existence of potential generic problems and the relative safety
This is an Inspector Followup Item:
        significance of the event.     Onsite inspections were performed and
Inadequate
        concluded that necessary corrective actions have been taken in accordance
Board Walkdown and Review (325/87-03-04).
        with existing requirements, licensee conditions and commitments.
No violations or deviations were identified.
        (CLOSED)   LER 1-86-13, Control Building Emergency Air Filtration System
7.
        Start Due to Corrosion on Radiation Monitor Sensor Converter. The
Onsite Review of Licensee Event Reports (92700)
        inspector verified that the applicable Maintenance Procedure, MI-26-11A,
The listed Licensee Event Reports (LERs) were reviewed to verify that the
        was revised July 29, 1986, to include inspection for corrosion as
inforr.ation provided met NRC reporting requirements.
        comitted to in the LER.     A sign-off on the data sheet was also provided
The verification
        to document the review.
included adequacy of event description and corrective action taken or
        (OPEN)   LER 1-87-01, Failure of Unit 1 HPCI System Turbine Steam Supply
planned, existence of potential generic problems and the relative safety
        Valve E41-F002 to Open. The licensee discovered a failed auxiliary
significance of the event.
        contact adder block assembly during the followup to the valve failure.
Onsite inspections were performed and
        The auxiliary contact block assemblies are attached to the main contactor
concluded that necessary corrective actions have been taken in accordance
        in each breaker compartment, with from one to six auxiliary blocks per
with existing requirements, licensee conditions and commitments.
        breaker. There are over 3000 auxiliary contact blocks on site in both Q
(CLOSED)
        and non Q app'eications. The licensee sent several auxiliary contact
LER 1-86-13, Control Building Emergency Air Filtration System
        blocks to General Electric (GE) for failure analysis. GE reported to the
Start Due to Corrosion on Radiation Monitor Sensor Converter.
                                                                                    .
The
inspector verified that the applicable Maintenance Procedure, MI-26-11A,
was revised July 29, 1986, to include inspection for corrosion as
comitted to in the LER.
A sign-off on the data sheet was also provided
to document the review.
(OPEN)
LER 1-87-01, Failure of Unit 1 HPCI System Turbine Steam Supply
Valve E41-F002 to Open.
The licensee discovered a failed auxiliary
contact adder block assembly during the followup to the valve failure.
The auxiliary contact block assemblies are attached to the main contactor
in each breaker compartment, with from one to six auxiliary blocks per
breaker.
There are over 3000 auxiliary contact blocks on site in both Q
and non Q app'eications.
The licensee sent several auxiliary contact
blocks to General Electric (GE) for failure analysis. GE reported to the
.


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licensee that the supplied blocks (CR205X100E) failed because dimensional
      licensee that the supplied blocks (CR205X100E) failed because dimensional
problems caused excess wear of the movable plunger, allowing the plunger
      problems caused excess wear of the movable plunger, allowing the plunger
to eventually stick inside the block, preventing the contact and thus the
      to eventually stick inside the block, preventing the contact and thus the
valve from moving.
      valve from moving.
Further licensee investigation revealed a potential generic problem with
      Further licensee investigation revealed a potential generic problem with
the auxiliary cor. tact adder block.
      the auxiliary cor. tact adder block. Maintenance record searches by the
Maintenance record searches by the
      licensee turned up over 50 potential auxiliary contactor problems since
licensee turned up over 50 potential auxiliary contactor problems since
      1982. GE has redesigned the auxiliary contact adder block (new part No.
1982.
      CR305X100E) and it appears that the new design is not susceptible to the
GE has redesigned the auxiliary contact adder block (new part No.
      binding problem. Further inspection of this item will be conducted after
CR305X100E) and it appears that the new design is not susceptible to the
      the licensee issues an LER supplement due May 22, 1987.
binding problem.
      (CLOSED)     LER 2-86-13, Failure to Prcperly Verify Reactor Protection
Further inspection of this item will be conducted after
      System (RPS) Shorting Links Installed During Testing Causes Full RPS Trip
the licensee issues an LER supplement due May 22, 1987.
      During Refueling. The in5pector verified via the training report that
(CLOSED)
      members of the I&C crews were trained on proper verification of
LER 2-86-13, Failure to Prcperly Verify Reactor Protection
      installation of the RPS shorting links.       The training class syllabus
System (RPS) Shorting Links Installed During Testing Causes Full RPS Trip
      adequately addressed the item. It required class participants to field
During Refueling.
      verify that the shorting links were in place.
The in5pector verified via the training report that
      (CLOSED)                                         . Level Scram During Pipe
members of the I&C crews were trained on proper verification of
      Flushing Due LER
installation of the RPS shorting links.
                      to 2-86-16,
The training class syllabus
                        PersonnelAutomatic
adequately addressed the item.
                                    Error. TheLowinspect
It required class participants to field
                                                  Water,'or verified that the lesson
verify that the shorting links were in place.
      plan associated with the committed real time training satisfactorily
(CLOSED)
      discussed the circumstances surrounding the event and the lessons which
LER 2-86-16, Automatic Low Water,'or verified that the lesson
      can be learned.
. Level Scram During Pipe
        (CLOSED)   LER 2-86-24, Inadvertent Emergency Core Cooling System (ECCS)
Flushing Due to Personnel Error.
      Actuation During Refueling Outage Due to Personnel Error. The inspector
The inspect
      reviewed the documentation which demonstrated that new tags were
plan associated with the committed real time training satisfactorily
        installed. The inspector visually verified that the tags were in place on
discussed the circumstances surrounding the event and the lessons which
      the Unit 1 Division ECCS inverters and power supplies on February 24,
can be learned.
      1987.
(CLOSED)
      No violations or deviations were identified.
LER 2-86-24, Inadvertent Emergency Core Cooling System (ECCS)
    8. In Office LER Review (90712)
Actuation During Refueling Outage Due to Personnel Error.
      The listed LERs were reviewed to verify that the information provided met
The inspector
      NRC reporting requirements. The verification included adequacy of event
reviewed the documentation which demonstrated that new tags were
      description and corrective action taken or planned, existance of potential
installed. The inspector visually verified that the tags were in place on
      generic problems and the relative safety significance of the avent.
the Unit 1 Division ECCS inverters and power supplies on February 24,
        (CLOSED) LER 1-86-17, Late Performance of Required Hourly Fire Watches.
1987.
        (CLOSED)   LER 1-86-18, Output Breaker EPA-2, Reactor Protection System
No violations or deviations were identified.
        (RPS) Motor Generator 1A, Tripped Unexpectedly to De-energize RPS Bus A;
8.
      Cause - Undetermined.
In Office LER Review (90712)
The listed LERs were reviewed to verify that the information provided met
NRC reporting requirements.
The verification included adequacy of event
description and corrective action taken or planned, existance of potential
generic problems and the relative safety significance of the avent.
(CLOSED) LER 1-86-17, Late Performance of Required Hourly Fire Watches.
(CLOSED)
LER 1-86-18, Output Breaker EPA-2, Reactor Protection System
(RPS) Motor Generator 1A, Tripped Unexpectedly to De-energize RPS Bus A;
Cause - Undetermined.


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(CLOSED)
        (CLOSED)   LER 1-86-23, Technical Specification (TS) 3.0.3 Entered Due to
LER 1-86-23, Technical Specification (TS) 3.0.3 Entered Due to
        Inoperability of the Unit 1 Reactor Core Spray Subsystem B and RHR Low
Inoperability of the Unit 1 Reactor Core Spray Subsystem B and RHR Low
        Pressure Coolant Injection Loop.
Pressure Coolant Injection Loop.
        (CLOSED)   LER 1-86-32, Failure to Functionally Test Relay TR/2 in Logic
(CLOSED)
        Channels A2, A4, B2 and B4 Primary Containment Isolation Instruments
LER 1-86-32, Failure to Functionally Test Relay TR/2 in Logic
        B21-TS-3229-3232; Procedure Deficiency.
Channels A2, A4, B2 and B4 Primary Containment Isolation Instruments
        (CLOSED)   LER 2-86-04, Primary Containment Group 6 Isolation / Automatic
B21-TS-3229-3232; Procedure Deficiency.
        Isolation of Reactor Building Ventilation System and Automatic Starting of
(CLOSED)
        Standby Gas Treatment System Occurred; Cause - Electrical Shorting.
LER 2-86-04, Primary Containment Group 6 Isolation / Automatic
        (CLOSED)   LER 2-86-07, High Radiation Alarm Trip of Reactor Building
Isolation of Reactor Building Ventilation System and Automatic Starting of
        Ventilation Exhaust Radiation Monitor D12-RM-N010B; Due to Electrical
Standby Gas Treatment System Occurred; Cause - Electrical Shorting.
        Grounding of the Monitor Power Lead.
(CLOSED)
        (CLOSED)   LER 2-86-09, Upscale Trip of Instrument Trip Unit to Reactor
LER 2-86-07, High Radiation Alarm Trip of Reactor Building
        Building Exhaust Ventilation Monitor D12-RM-N010B: Cause Could Not Be
Ventilation Exhaust Radiation Monitor D12-RM-N010B; Due to Electrical
        Determined.
Grounding of the Monitor Power Lead.
        (CLOSED)     LER 2-86-11, Reactor Water Cleanup System Inlet Primary
(CLOSED)
        Containment Outboard Isolation Valve, Automatically Closed; Cause - Fuse
LER 2-86-09, Upscale Trip of Instrument Trip Unit to Reactor
        F18 Blew.
Building Exhaust Ventilation Monitor D12-RM-N010B: Cause Could Not Be
        (CLOSED)   LER 2-86-14, Upscale Trip of Reactor Power Intermediate Range
Determined.
        Monitor D Occurred When Control Rod 02-19 Was Selected in Reactor Manual
(CLOSED)
        Control System While Performing PT-18.1; Cause - Electronic Noise Spike.
LER 2-86-11, Reactor Water Cleanup System Inlet Primary
        (CLOSED)   LER 2-86-22, Unit 2 Shutdown in Accordance With TS 3.4.1.1 Due
Containment Outboard Isolation Valve, Automatically Closed; Cause - Fuse
        to a Lockout / Trip of the Recirculation Pump Motor Generator Set.
F18 Blew.
        No violations or deviations were identified.
(CLOSED)
    9. Followup on Inspector Identified and Unresolved Items (92701)
LER 2-86-14, Upscale Trip of Reactor Power Intermediate Range
        (OPEN) Inspector Followup Item, (325/84-04-01 and 324/84-04-01), Licensee
Monitor D Occurred When Control Rod 02-19 Was Selected in Reactor Manual
        to Identify and Repair Cab *ie Tray Raceway Z Clamps Problems. The I clamps
Control System While Performing PT-18.1; Cause - Electronic Noise Spike.
        secure the tray to the horizontal tray support.     The inspector reviewed
(CLOSED)
        completed work requests 1-E84-1658 and 2-E84-2009 which documented
LER 2-86-22, Unit 2 Shutdown in Accordance With TS 3.4.1.1 Due
        completion of this particular inspection and repair. The inspector         '
to a Lockout / Trip of the Recirculation Pump Motor Generator Set.
        performed an inspection of safety related cable trays 50F/DA and 50M/DA in
No violations or deviations were identified.
        the Unit 2 control room on February 22. Of twenty four Z clamps installed
9.
        on these trays, five were bent such that they were not engaged with the
Followup on Inspector Identified and Unresolved Items (92701)
        tray top, four others had loose I clamp nuts, and three others were turned
(OPEN) Inspector Followup Item, (325/84-04-01 and 324/84-04-01), Licensee
        to the side. In addition, two Z clamps were missing. The inspector also
to Identify and Repair Cab *ie Tray Raceway Z Clamps Problems. The I clamps
        observed several tray covers which were not in their proper place. Based
secure the tray to the horizontal tray support.
        on discussions with the architect / engineer, the licensee determined that
The inspector reviewed
        the "as found" condition of these two trays would not render the raceway
completed work requests 1-E84-1658 and 2-E84-2009 which documented
        inoperble or adversely effect the cables in the trays.
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completion of this particular inspection and repair.
The inspector
performed an inspection of safety related cable trays 50F/DA and 50M/DA in
the Unit 2 control room on February 22. Of twenty four Z clamps installed
on these trays, five were bent such that they were not engaged with the
tray top, four others had loose I clamp nuts, and three others were turned
to the side.
In addition, two Z clamps were missing. The inspector also
observed several tray covers which were not in their proper place. Based
on discussions with the architect / engineer, the licensee determined that
the "as found" condition of these two trays would not render the raceway
inoperble or adversely effect the cables in the trays.


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8
            Discussion with Quality Assurance (QA) personnel revealed that an
Discussion with Quality Assurance (QA) personnel revealed that an
            outstanding non-conformance report (NCR), number E-86-002, involving cable
outstanding non-conformance report (NCR), number E-86-002, involving cable
            tray covers had been issued on July 1,1986, but a review of the NCR
tray covers had been issued on July 1,1986, but a review of the NCR
            responses by the QC supervisor and the inspector showed that poor work
responses by the QC supervisor and the inspector showed that poor work
            control practices which allowed the 2 clamp problems to occur had not been
control practices which allowed the 2 clamp problems to occur had not been
            specifically addressed. Hence, both the licensee and the inspector have
specifically addressed.
            determined that the responses were inadequate. On February 27, 1987,
Hence, both the licensee and the inspector have
            licensee QA issued a Notice of Deficiency against this NCR in accordance
determined that the responses were inadequate.
            with QA procedure 0QA-104, which required correction of the inadequate
On February 27, 1987,
            response within seven days.
licensee QA issued a Notice of Deficiency against this NCR in accordance
            This item will remain open pending final resolution of NCR E-86-002 and
with QA procedure 0QA-104, which required correction of the inadequate
            the Notice of Deficiency and subsequent review by the inspector.
response within seven days.
            No violations or deviations were identified.
This item will remain open pending final resolution of NCR E-86-002 and
      10. LimitorqueOperators(71707)
the Notice of Deficiency and subsequent review by the inspector.
            The licensee has recently procured information from Limitorque Corporation
No violations or deviations were identified.
            concerning actuator sizing and settings on both safety and non-safety
10. LimitorqueOperators(71707)
            related valves. The data was recently reviewed (December - January) and
The licensee has recently procured information from Limitorque Corporation
            compiled from original design documents into a new format at the
concerning actuator sizing and settings on both safety and non-safety
            licensee's request. Review of the data sheets showed that Limitorque was
related valves.
            now recommending upgrade of some actuator motors to a larger size.
The data was recently reviewed (December - January) and
            Apparently, Limitorque had used 100% full voltage to size the motors,
compiled from original design documents into a new format at the
            instead of the currently specified degraded supply of 85%. Reviews of
licensee's request.
            documents between the licensee, the valve manufacturer and the valve
Review of the data sheets showed that Limitorque was
            manufacturer's subcontractor (Limitorque), has not been able to determine
now recommending upgrade of some actuator motors to a larger size.
            what was specified to Limitorque (or by whom) when the original plant
Apparently, Limitorque had used 100% full voltage to size the motors,
            equipment was procured. The licensee has evaluated this condition on the
instead of the currently specified degraded supply of 85%.
            applicable safety related valves and has determined that these valves
Reviews of
            would function under design conditions.       The affected valves are:
documents between the licensee, the valve manufacturer and the valve
            E41-F002, High Pressure Coolant Injection (HPCI) inboard steam line
manufacturer's subcontractor (Limitorque), has not been able to determine
            isolation valve; E41-F004, HPCI condensate storage tank suction valve;
what was specified to Limitorque (or by whom) when the original plant
            E41-F008, HPCI full flow test isolation valve; E11-F017A and B, RHR system
equipment was procured.
            outboard isolation valves; and E11-F024A and B, suppression pool test
The licensee has evaluated this condition on the
            return isolation valve. The inspector has reviewed the justification for
applicable safety related valves and has determined that these valves
            continued operation for Unit 2 contained in Engineering Evaluation
would function under design conditions.
            EER-87-0088. In summary, the evaluation concludes that no safety problem
The affected valves are:
            exists based upon either application and/or electrical distribution
E41-F002, High Pressure Coolant Injection (HPCI) inboard steam line
            voltage studies. The voltage studies determined that the degraded voltage
isolation valve; E41-F004, HPCI condensate storage tank suction valve;
            of some of the valves would not drop below 85%. Under these anticipated
E41-F008, HPCI full flow test isolation valve; E11-F017A and B, RHR system
            voltages, there is no motor sizing concern. In addition, contact with the
outboard isolation valves; and E11-F024A and B, suppression pool test
            applicable valve vendors, Anchor Darling and Rockwell, revealed that they
return isolation valve.
            perfonn their own sizing and setting calculations.     Of three valves.
The inspector has reviewed the justification for
            reviewed by Anchor Darling, a degraded voltage of 85% was used. A list of
continued operation for Unit 2 contained in Engineering Evaluation
            the other valves has been supplied to the vendors to verify exactly what
EER-87-0088.
In summary, the evaluation concludes that no safety problem
exists based upon either application and/or electrical distribution
voltage studies. The voltage studies determined that the degraded voltage
of some of the valves would not drop below 85%.
Under these anticipated
voltages, there is no motor sizing concern.
In addition, contact with the
applicable valve vendors, Anchor Darling and Rockwell, revealed that they
perfonn their own sizing and setting calculations.
Of three valves.
reviewed by Anchor Darling, a degraded voltage of 85% was used. A list of
the other valves has been supplied to the vendors to verify exactly what
value was used.
,
,
            value was used.
The licensee has contracted with B&W to review the Limitoroue data sheets,
            The licensee has contracted with B&W to review the Limitoroue data sheets,
calculations and generally assist in resolving the concerns. Their review
            calculations and generally assist in resolving the concerns. Their review
- . _ - , . _ -
                                                                      - . _ - , . _ -


                                                                                      _ - _ _ _
_ - _ _ _
          .
.
.
  .-
.-
                                                9
.
          has indicated potential problems with Limitorque data sheets.       Two DC
9
          motor powered actuators had been treated as AC powered.     In addition, one
has indicated potential problems with Limitorque data sheets.
          of these had the wrong pull-out efficiency used for the overall unit ratio
Two DC
          (motor design speed-RPM / actuator speed RPM). Apparently the wrong value
motor powered actuators had been treated as AC powered.
          had been taken from the Limitorque Gate and Globe Valve Efficiency Chart.
In addition, one
          The actuators involved were SMB-3 and SMB-000. Another valve with an
of these had the wrong pull-out efficiency used for the overall unit ratio
          SMB-5T actuator also had the wrong pull-out efficiency used in the torque
(motor design speed-RPM / actuator speed RPM).
          switch calculation. This was attributed to using the wrong motor speed
Apparently the wrong value
          when obtaining values from the Gate and Globe Valve Efficiency Chart.
had been taken from the Limitorque Gate and Globe Valve Efficiency Chart.
          The licensee is continuing his review. This is an Inspector Followup
The actuators involved were SMB-3 and SMB-000.
          Item: Potential Problems with Limitorque Data Sheets (324/87-03-02).
Another valve with an
          No violations or deviations were identified.
SMB-5T actuator also had the wrong pull-out efficiency used in the torque
    11. Spent Fuel Storage Capacity (59095)
switch calculation.
          The inspectors reviewed the available storage capacity in the Unit 1 and
This was attributed to using the wrong motor speed
          Unit 2 spent fuel storage pools to determine if full core offload
when obtaining values from the Gate and Globe Valve Efficiency Chart.
          capability existed for each unit.       Based on discussions with licensee
The licensee is continuing his review.
          personnel and review of the licensee's fuel map, full offload capability
This is an Inspector Followup
          (560 assemblies) existed. Unit 2 Spent Fuel Pool (SFP) has room for 566
Item: Potential Problems with Limitorque Data Sheets (324/87-03-02).
          more BWR assemblies:
No violations or deviations were identified.
                          1839     allowed by TS
11. Spent Fuel Storage Capacity (59095)
                        -
The inspectors reviewed the available storage capacity in the Unit 1 and
                            36      displaced by a PWR rack
Unit 2 spent fuel storage pools to determine if full core offload
                        - 36       rack not installed
capability existed for each unit.
                        -
Based on discussions with licensee
                              I      contains stuck blade guide
personnel and review of the licensee's fuel map, full offload capability
                        -
(560 assemblies) existed.
                              2     boral sample stations
Unit 2 Spent Fuel Pool (SFP) has room for 566
                        - 442       not yet installed
more BWR assemblies:
                          1322     available spaces
1839
                        - 756       assemblies in pool
allowed by TS
                          ~566     BWR spaces available
36
          Unit 1 SFP has room for 925 more BWR assemblies:
displaced by a PWR rack
                          1803     allowed by TS
-
                        -  36     rack not installed
- 36
                        -   2     boral sample stations
rack not installed
                          T7EE     available spaces
I
                        - 840       assemblies in pool
contains stuck blade guide
                            975     BWR spaces available
-
          The above data is as of February 15, 1987.
-
          The inspector noted that each SFP contained 10 PWR spent fuel modules each
2
          capable of storing 16 assemblies for a PWR capacity in each pool of 160
boral sample stations
          PWR assemblies. The Unit 1 SFP contained 160 assemblies while the Unit 2
- 442
          pool contained 144 assemblies. However, Unit 2 Technical Specification
not yet installed
          5.6.3 states that, "the fuel storage pool is designed and shall be
1322
          maintained with a storage capacity limited to no more than 144 PWR fuel
available spaces
- 756
assemblies in pool
~566
BWR spaces available
Unit 1 SFP has room for 925 more BWR assemblies:
1803
allowed by TS
36
rack not installed
-
2
boral sample stations
-
T7EE
available spaces
- 840
assemblies in pool
975
BWR spaces available
The above data is as of February 15, 1987.
The inspector noted that each SFP contained 10 PWR spent fuel modules each
capable of storing 16 assemblies for a PWR capacity in each pool of 160
PWR assemblies.
The Unit 1 SFP contained 160 assemblies while the Unit 2
pool contained 144 assemblies.
However, Unit 2 Technical Specification
5.6.3 states that, "the fuel storage pool is designed and shall be
maintained with a storage capacity limited to no more than 144 PWR fuel


,_                                                                                               ,
,
            .
,_
              ..
..
                                                          10
.
10
I
I
                    assemblies and 1839 BWR fual assemblies.   The extra 16 storage locations
assemblies and 1839 BWR fual assemblies.
                      in the Unit 2 SFP pose no safety problem since the Unit 1 SFP has been
The extra 16 storage locations
                    reviewed and approved by NRR, contains 160 PWR assemblies and locations,
in the Unit 2 SFP pose no safety problem since the Unit 1 SFP has been
                    also contains additional high density racks, and is essentially identical
reviewed and approved by NRR, contains 160 PWR assemblies and locations,
                    to the Unit 2 SFP. The excess storage capacity in the Unit 2 SFP is a
also contains additional high density racks, and is essentially identical
                    violation of TS 5.6.3: Failure to Meet TS 5.6.3 Regarding Spent Fuel Pool
to the Unit 2 SFP.
l                   PWR Capacity (324/87-03-01).
The excess storage capacity in the Unit 2 SFP is a
violation of TS 5.6.3:
Failure to Meet TS 5.6.3 Regarding Spent Fuel Pool
l
PWR Capacity (324/87-03-01).
!
!
j                    One violation and no deviations were identified.
One violation and no deviations were identified.
                12. RefuelingActivities(60705)
j
                    Selected refueling activities were witnessed and reviewed by the
12. RefuelingActivities(60705)
                      inspector. These included verification that:
Selected refueling activities were witnessed and reviewed by the
                      -    The fuel pool gates were removed per MP-09.
inspector. These included verification that:
l                     -
The fuel pool gates were removed per MP-09.
                            Surveillance requirements of Technical Specification 4.9.6 associated
-
l
-
Surveillance requirements of Technical Specification 4.9.6 associated
l
l
                            with refueling bridge interlocks were performed prior to fuel
with refueling bridge interlocks were performed prior to fuel
                            movement.
movement.
                      -    Number of operable SRM's per Technical Specification 3.9.2.a. and b.
Number of operable SRM's per Technical Specification 3.9.2.a. and b.
                            were maintained.
-
                      -    Continues communications between the refueling bridge and the control
were maintained.
                            room were established per Technical Specification 3.9.5.
Continues communications between the refueling bridge and the control
                      -
-
                            Fuel movements were conducted in accordance with operating procedures
room were established per Technical Specification 3.9.5.
                            and the Fuel Movement Sheets.
-
                      The last activity was performed during a two hour inspection conducted on
Fuel movements were conducted in accordance with operating procedures
                      the refueling bridge during fuel movements.
and the Fuel Movement Sheets.
                      No violations or deviations were identified.
The last activity was performed during a two hour inspection conducted on
the refueling bridge during fuel movements.
No violations or deviations were identified.
l
l
i
i
.
.
                                                                                                    l
                                                                                                    1
  _ _ _ _ _
}}
}}

Latest revision as of 20:17, 23 May 2025

Safety Insp Repts 50-324/87-03 & 50-325/87-03 on 870201-28, 0303-04.Violation Noted:Failure to Maintain Unit 2 PWR Fuel Storage Capacity
ML20206D280
Person / Time
Site: Brunswick  
Issue date: 03/26/1987
From: Fredrickson P, Garner L, Ruland W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20206D205 List:
References
50-324-87-03, 50-324-87-3, 50-325-87-03, 50-325-87-3, NUDOCS 8704130291
Download: ML20206D280 (11)


See also: IR 05000324/1987003

Text

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UNITE 3 STATES

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NUCLEAR REGULATORY COMMISSION

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REGION 11

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101 MARIETTA STREET.N.W.

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ATLANTA, GEORGIA 30323 a

\\, * * * * /

Report Nos. 50-325/87-03 and 50-324/87-03

Licensee: Carolina Power and Light Company

P. O. Box 1551

Raleigh, NC 27602

Docket Nos.: 50-325 and 50-324

License Nos.: DPR-71 and DPR-62

Facility Name: Brunswick 1 and 2

Inspection Conducted: February 1 - 28, 1987 and March 3-4, 1987

.I. N &

3/16/f7

Inspectors:

g

, H. Ruland

Date Signed

9.6.d

slu tt?

@ LM W. Garner ,

Date Signed

,

3 /2(> [87

Approved by:

.

.

g P4 E. Fredrickson, Section Chief

Date Signed

Division of Reactor Projects

SUMMARY

Scope:

This routine safety inspection involved the areas of maintenance

observation, surveillance observation, operational safety verification, onsite

Licensee Event Reports (LER) review, in-office LER review, followup on

inspector identified and unresolved items, Limitorque Operators, spent fuel

storage capacity, and refueling activities.

Results:

One violation - failure to maintain Unit 2 PWR spent fuel storage

capacity, paragraph 11,

1

0704130291 870330

PDR

ADOCK 0D000324

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PDR

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REPORT DETAILS

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1.

Persons Contacted

Licensee Employees

P. Howe, Vice President - Brunswick Nuclear Project

l

C. Dietz, General Manager - Brunswick Nuclear Project

T. Wyllie, Manager - Engineering and Construction

'

J. Holder, Manager - Outages

R. Eckstein, Manager - Technical Support

E. Bishop, Manager - Operations

l

L. Jones, Director - Quality Assurance (QA)/ Quality Control (QC)-

R. Helme, Director - Onsite Nuclear Safety - BSEP

J. Chase, Assistant to General Manager

J. O'Sullivan, Manager - Maintenance

G. Cheatham, Manager - Environmental & Radiation Control

J. Smith, Manager - Administrative Support

K. Enzor, Director - Regulatory Compliance

A. Hegler, Superintendent - Operations

W. Hogle, Engineering Supervisor

,

l

B. Wilson, Engineering Supervisor

l

B. Parks, Engineering Supervisor

R.Creech,I&C/ElectricalMaintenanceSupervisor(Unit 2)

R. Warden, ISC/ Electrical Maintenance Supervisor (Unit 1)

W. Dorman, Supervisor - QA

W. Hatcher Supervisor - Security

R. Kitchen,MechanicalMaintenanceSupervisor(Unit 2)

!

C. Treubel, Mechanical Maintenance Supervisor (Unit 1)

R. Poulk, Senior NRC Regulatory Specialist

W. Murray, Senior Engineer - Nuclear Licensing Unit

Otiler licensee employees contacted included construction craftsmen,

engineers, technicians, operators, office personnel, and security force

'

members.

1

2.

ExitInterview(30703)

l

The inspection scope and findings were summarized on March 3,1987, with

the general manager and vice-president. The violation, excess capacity in

'

the Unit 2 spent fuel pool (paragraph 11), was discussed in detail. The

i

inspector stated that the item was unresolved pending inspector discussion

'

with regional management.

On March 4, 1987, the licensee was informed by

the inspector that the spent fuel pool issue was a violation.

The

i

licensee agreed to address the issue of board walkdowns/ reviews

(paragraph 6) along with the response to the violation.

The licensee

l

acknowledged the findings without exception.

The licensee did not

l

identify as proprietary any of the materials provided to or reviewed by

the inspectors during the inspection.

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2

3.

Followup on Previous Enforcement Matters (92702)

Not inspected.

4.

Maintenance Observation (62703)

The inspectors observed maintenance activities and reviewed records to

verify that work was conducted in accordance with approved procedures,

Technical Specifications, and applicable industry codes and standards. The

inspectors also verified that:

redundant components were operable;

administrative controls were followed; tagouts were adequate; personnel

were qualified; correct replacement parts were used; radiological controls

were proper; fire protection was adequate; quality control hold points

were adequate and observed; adequate post-maintenance testing was

performed; and independent verification requirements were implemented.

The inspectors independently verified that selected equipment was properly

returned to service.

Outstanding work requests were reviewed to ensure that the licensee gave

priority to safety-related maintenance.

.

The inspectors observed / reviewed portions of the following maintenance

activities:

MP-09

Dryer / Separator, Cattle Chute, and Fuel Pool Gates

Removal and Installation.

OLP-NVT001

Topaz Static Inverter and Lambda Power Supply.

WR&A-87-AGEB1 Repair of Unit 2 Annunciation Horn Circuit.

During performance of work request 87-AGEB1, the inspector observed a

communication problem between operations and maintenance personnel.

At

first, the annunciator horn being repaired, could not be silenced. Later,

'

j

the horn stopper' continuously sounding and would not sound when another

!

annunciator came in.

Operations was aware of this and took proper

compensatory actions, e. g., assigned sections of the board to individuals

to note when a new annunciator came in.

The first problem was correctly

conmunicated to maintenance; however, the change in symptoms was not.

Operations assumed the change was due to Instrumentation and Control (I&C)

trouble shooting activities.

The inspector informed the maintenance

personnel of the second item approximately 30 minutes after it happened.

Although the inspector was confident that the problem would have been

fixed, the failure of operations personnel to recognize that a new

condition existed versus a condition induced by I&C personnel performing

trouble shooting or repair, was a concern.

Inadequate communication can

noticeably increase the length of time an unsatisfactory condition exists.

This matter was discussed with cognizant supervision.

No violations or deviations were identified.

<

.

..

,

3

5.

SurveillanceObservation(61726)

The inspectors observed surveillance testing required by Technical

Specifications.

Through observation and record review, the inspectors

verified that:

tests conformed to Technical Specification requirements;

administrative controls were followed; personnel were qualified;

instrumentation was calibrated; and data was accurate and complete.

The

inspectors independently verified selected test results and proper return

to service of equipment.

The inspectors witnessed / reviewed portions of the following test

activities:

IMST-DG12R

Diesel Generator DG-2 Loading Test.

2MST-APRM12

Average Power Range Monitor (APRM), (Ch. 8, D & F)

Channel Functional Test (Reactor Protection System

(RPS) Inputs].

2MST-ATWS22M

Anticipated Transcient Without Scram (ATWS) Reactor

High Pressure Trip Instrument Channel Calibration.

2MST-RHR21M

Residual Heat Removal (RHR) - Low Pressure Coolant

Injection (LPCI), Core Spray System (CSS) and HPCI Hi

Drywell Pressure Trip Unit Channel Calibration.

PT-12.8

Electrical Power Systems Operability Test.

During performance of IMST-DG12R on February 17, 1987, the licensee

identified that step 7.4.30 had not been performed correctly.

The step

requires stopping of the core spray pump while supplying rated flow to

verify that the DG does not trip.

This is a surveillance requirement

specified in Technical Specification (TS) .4.8.1.1.2.d.2.

The operator

reduced the flow prior to stopping the pumb. This is the method normally

used to stop the pump as required by either the quarterly required

Surveillance Test Procedure PT-07.2.4b, or the Operating Procedure OP-18.

The licensee verified that during another performance of MST-DG12R, the

step was satisfactorily performed.

This item meets all the requirements

to be considered as a licensee identified violation.

The licensee is

preparing an Operating Experience Report (0ER) to address the root cause

of the communication failure between the I&C personnel in charge of the

test and the control operator. The inspector plans to review the OER when

issued.

This is an Inspector Followup Item:

Review of IMST-DG12R

ProcedureViolationOER(325/87-03-03).

One licensee identified violation and no deviations were identified.

6.

Operational Safety Verification (71707)

)

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The inspectors verified conformance with regulatory requirements by direct

. observations of activities, facility tours, discussions with personnel,

,

reviewing of records and independent-verification.of safety. system status.

1

!

The inspectors verified that control room manning requirements of 10 CFR 50.54 and the Technical Specifications were-met. . Control room, shift

<

supervisor, and clearance logs were reviewed to obtain information-

<

j

concerning operating trends and out of service safety systems to ensure

that there were no conflicts with Technical Specifications Limiting

'

Conditions for Operations.

Direct observations were conducted of control

'

room panels, instrumentation and recorder traces important to safety to

verify operability and that parameters were within~ Technical Specification

a

]

limits. The inspectors observed shift turnovers to verify that continuity

of system status was maintained. :The' inspectors verified the status of

.

selected control room annunciators.

1

i

Operability of ' a selected Engineered ' Safety Feature (ESF) train was -

i

verified by insuring that:

each accessible valve in the flow path was in

its correct position; each power supply' and breaker,. including control

room fuses, were aligned for components that must activate upon initiation

signal; removal of power from those - ESF motor-operated valves, so

1

identified by Technical Specifications, was completed; there was. no

~

1

leakage of major components; there was proper lubrication and cooling

water available; and a condition did. not exist which might prevent

i

.

fulfillment of the system's functional requirements.

Instrumentation

i

essential to system actuation or performance was. verified operable by

'

observing on-scale indication and proper instrument valve lineup, if

j

accessible.

The

inspectors verified

that the licensee's health physics

J

policies / procedures were followed.

This includod a review of area

surveys, radiation work permits, posting, and instrument calibration.

,

The inspectors verified that:

the security. organization was properly

j-

.

manned and security personnel were capable of performing their assigned

'

{

functions; persons and packages were checked prior to entry into the

4

!

protected area (PA); vehicles were properly authorized, searched and

escorted within the PA; persons within the PA ~ displayed photo

identification badges; personnel in vital areas were authorized; and

effective compensatory measures were employed when required.

!

i

On February 1, -1987, the inspector found a vital area door closed but

unlatched.

While an unauthorized person could have opened the door, the

'

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security computer would have detected the intrusion, enabling the security

j

force to respond.

The inspector reported the condition to security.

A

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{

security member responded in a timely manner, verified the condition and

took action as required.

i

The inspectors also observed plant housekeeping controls, verified

!

position of certain containment isolation valves, and verified ' the

i

operability of onsite and offsite emergency power sources.-

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On February 2,1987, the inspector observed the Unit 2 A and 6 trains of

Standby Gas Treatment (SBGT) system with loose blower and motor pedestal

mounting rubber bushing retaining bolts.

The licensee issued work

requests 87-ADJIl and 87-ADJJ1 to correct the deficiency.

The licensee

inspected Unit I and issued work requests ADJK1 and ADJL1 to correct

similar deficiencies on Unit 1 SBGT trains A and B.

Technical support

reviewed the "as found" condition and determined that the condition had

not rendered the SBGT trains inoperable.

On February 12, 1987, at 7:50 a.m., the inspector found valve 1-E11-F007B,

the Division II RHR minimuni flow valve, open instead of closed. The valve

had remained open after the licensee had performed OP-17, RHR Operating

Procedure

Section 8.7, draining the suppression pool to radwaste.

Valve]-Ell F007B auto-opened when the RHR pump was started, but no

procedure step existed to manually reshut the valve. Thus, the valve was

in the position required by the last procedure performed on the RHR

system.

However, the licensee reported that the evolution had occurred

two shifts prior to discovery.

Therefore, three shifts and two shift

turnovers failed to identify the mi:; positioned valve.

The Plant General

Manager agreed to address this issue, weakness in board walkdowns and

board review after valve manipulations, when responding to the violation

issued with this report.

This is an Inspector Followup Item:

Inadequate

Board Walkdown and Review (325/87-03-04).

No violations or deviations were identified.

7.

Onsite Review of Licensee Event Reports (92700)

The listed Licensee Event Reports (LERs) were reviewed to verify that the

inforr.ation provided met NRC reporting requirements.

The verification

included adequacy of event description and corrective action taken or

planned, existence of potential generic problems and the relative safety

significance of the event.

Onsite inspections were performed and

concluded that necessary corrective actions have been taken in accordance

with existing requirements, licensee conditions and commitments.

(CLOSED)

LER 1-86-13, Control Building Emergency Air Filtration System

Start Due to Corrosion on Radiation Monitor Sensor Converter.

The

inspector verified that the applicable Maintenance Procedure, MI-26-11A,

was revised July 29, 1986, to include inspection for corrosion as

comitted to in the LER.

A sign-off on the data sheet was also provided

to document the review.

(OPEN)

LER 1-87-01, Failure of Unit 1 HPCI System Turbine Steam Supply

Valve E41-F002 to Open.

The licensee discovered a failed auxiliary

contact adder block assembly during the followup to the valve failure.

The auxiliary contact block assemblies are attached to the main contactor

in each breaker compartment, with from one to six auxiliary blocks per

breaker.

There are over 3000 auxiliary contact blocks on site in both Q

and non Q app'eications.

The licensee sent several auxiliary contact

blocks to General Electric (GE) for failure analysis. GE reported to the

.

'

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,

6

licensee that the supplied blocks (CR205X100E) failed because dimensional

problems caused excess wear of the movable plunger, allowing the plunger

to eventually stick inside the block, preventing the contact and thus the

valve from moving.

Further licensee investigation revealed a potential generic problem with

the auxiliary cor. tact adder block.

Maintenance record searches by the

licensee turned up over 50 potential auxiliary contactor problems since

1982.

GE has redesigned the auxiliary contact adder block (new part No.

CR305X100E) and it appears that the new design is not susceptible to the

binding problem.

Further inspection of this item will be conducted after

the licensee issues an LER supplement due May 22, 1987.

(CLOSED)

LER 2-86-13, Failure to Prcperly Verify Reactor Protection

System (RPS) Shorting Links Installed During Testing Causes Full RPS Trip

During Refueling.

The in5pector verified via the training report that

members of the I&C crews were trained on proper verification of

installation of the RPS shorting links.

The training class syllabus

adequately addressed the item.

It required class participants to field

verify that the shorting links were in place.

(CLOSED)

LER 2-86-16, Automatic Low Water,'or verified that the lesson

. Level Scram During Pipe

Flushing Due to Personnel Error.

The inspect

plan associated with the committed real time training satisfactorily

discussed the circumstances surrounding the event and the lessons which

can be learned.

(CLOSED)

LER 2-86-24, Inadvertent Emergency Core Cooling System (ECCS)

Actuation During Refueling Outage Due to Personnel Error.

The inspector

reviewed the documentation which demonstrated that new tags were

installed. The inspector visually verified that the tags were in place on

the Unit 1 Division ECCS inverters and power supplies on February 24,

1987.

No violations or deviations were identified.

8.

In Office LER Review (90712)

The listed LERs were reviewed to verify that the information provided met

NRC reporting requirements.

The verification included adequacy of event

description and corrective action taken or planned, existance of potential

generic problems and the relative safety significance of the avent.

(CLOSED) LER 1-86-17, Late Performance of Required Hourly Fire Watches.

(CLOSED)

LER 1-86-18, Output Breaker EPA-2, Reactor Protection System

(RPS) Motor Generator 1A, Tripped Unexpectedly to De-energize RPS Bus A;

Cause - Undetermined.

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(CLOSED)

LER 1-86-23, Technical Specification (TS) 3.0.3 Entered Due to

Inoperability of the Unit 1 Reactor Core Spray Subsystem B and RHR Low

Pressure Coolant Injection Loop.

(CLOSED)

LER 1-86-32, Failure to Functionally Test Relay TR/2 in Logic

Channels A2, A4, B2 and B4 Primary Containment Isolation Instruments

B21-TS-3229-3232; Procedure Deficiency.

(CLOSED)

LER 2-86-04, Primary Containment Group 6 Isolation / Automatic

Isolation of Reactor Building Ventilation System and Automatic Starting of

Standby Gas Treatment System Occurred; Cause - Electrical Shorting.

(CLOSED)

LER 2-86-07, High Radiation Alarm Trip of Reactor Building

Ventilation Exhaust Radiation Monitor D12-RM-N010B; Due to Electrical

Grounding of the Monitor Power Lead.

(CLOSED)

LER 2-86-09, Upscale Trip of Instrument Trip Unit to Reactor

Building Exhaust Ventilation Monitor D12-RM-N010B: Cause Could Not Be

Determined.

(CLOSED)

LER 2-86-11, Reactor Water Cleanup System Inlet Primary

Containment Outboard Isolation Valve, Automatically Closed; Cause - Fuse

F18 Blew.

(CLOSED)

LER 2-86-14, Upscale Trip of Reactor Power Intermediate Range

Monitor D Occurred When Control Rod 02-19 Was Selected in Reactor Manual

Control System While Performing PT-18.1; Cause - Electronic Noise Spike.

(CLOSED)

LER 2-86-22, Unit 2 Shutdown in Accordance With TS 3.4.1.1 Due

to a Lockout / Trip of the Recirculation Pump Motor Generator Set.

No violations or deviations were identified.

9.

Followup on Inspector Identified and Unresolved Items (92701)

(OPEN) Inspector Followup Item, (325/84-04-01 and 324/84-04-01), Licensee

to Identify and Repair Cab *ie Tray Raceway Z Clamps Problems. The I clamps

secure the tray to the horizontal tray support.

The inspector reviewed

completed work requests 1-E84-1658 and 2-E84-2009 which documented

'

completion of this particular inspection and repair.

The inspector

performed an inspection of safety related cable trays 50F/DA and 50M/DA in

the Unit 2 control room on February 22. Of twenty four Z clamps installed

on these trays, five were bent such that they were not engaged with the

tray top, four others had loose I clamp nuts, and three others were turned

to the side.

In addition, two Z clamps were missing. The inspector also

observed several tray covers which were not in their proper place. Based

on discussions with the architect / engineer, the licensee determined that

the "as found" condition of these two trays would not render the raceway

inoperble or adversely effect the cables in the trays.

_ _ _ _ _ _ - _ _ _ _ _ _ _ .

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Discussion with Quality Assurance (QA) personnel revealed that an

outstanding non-conformance report (NCR), number E-86-002, involving cable

tray covers had been issued on July 1,1986, but a review of the NCR

responses by the QC supervisor and the inspector showed that poor work

control practices which allowed the 2 clamp problems to occur had not been

specifically addressed.

Hence, both the licensee and the inspector have

determined that the responses were inadequate.

On February 27, 1987,

licensee QA issued a Notice of Deficiency against this NCR in accordance

with QA procedure 0QA-104, which required correction of the inadequate

response within seven days.

This item will remain open pending final resolution of NCR E-86-002 and

the Notice of Deficiency and subsequent review by the inspector.

No violations or deviations were identified.

10. LimitorqueOperators(71707)

The licensee has recently procured information from Limitorque Corporation

concerning actuator sizing and settings on both safety and non-safety

related valves.

The data was recently reviewed (December - January) and

compiled from original design documents into a new format at the

licensee's request.

Review of the data sheets showed that Limitorque was

now recommending upgrade of some actuator motors to a larger size.

Apparently, Limitorque had used 100% full voltage to size the motors,

instead of the currently specified degraded supply of 85%.

Reviews of

documents between the licensee, the valve manufacturer and the valve

manufacturer's subcontractor (Limitorque), has not been able to determine

what was specified to Limitorque (or by whom) when the original plant

equipment was procured.

The licensee has evaluated this condition on the

applicable safety related valves and has determined that these valves

would function under design conditions.

The affected valves are:

E41-F002, High Pressure Coolant Injection (HPCI) inboard steam line

isolation valve; E41-F004, HPCI condensate storage tank suction valve;

E41-F008, HPCI full flow test isolation valve; E11-F017A and B, RHR system

outboard isolation valves; and E11-F024A and B, suppression pool test

return isolation valve.

The inspector has reviewed the justification for

continued operation for Unit 2 contained in Engineering Evaluation

EER-87-0088.

In summary, the evaluation concludes that no safety problem

exists based upon either application and/or electrical distribution

voltage studies. The voltage studies determined that the degraded voltage

of some of the valves would not drop below 85%.

Under these anticipated

voltages, there is no motor sizing concern.

In addition, contact with the

applicable valve vendors, Anchor Darling and Rockwell, revealed that they

perfonn their own sizing and setting calculations.

Of three valves.

reviewed by Anchor Darling, a degraded voltage of 85% was used. A list of

the other valves has been supplied to the vendors to verify exactly what

value was used.

,

The licensee has contracted with B&W to review the Limitoroue data sheets,

calculations and generally assist in resolving the concerns. Their review

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has indicated potential problems with Limitorque data sheets.

Two DC

motor powered actuators had been treated as AC powered.

In addition, one

of these had the wrong pull-out efficiency used for the overall unit ratio

(motor design speed-RPM / actuator speed RPM).

Apparently the wrong value

had been taken from the Limitorque Gate and Globe Valve Efficiency Chart.

The actuators involved were SMB-3 and SMB-000.

Another valve with an

SMB-5T actuator also had the wrong pull-out efficiency used in the torque

switch calculation.

This was attributed to using the wrong motor speed

when obtaining values from the Gate and Globe Valve Efficiency Chart.

The licensee is continuing his review.

This is an Inspector Followup

Item: Potential Problems with Limitorque Data Sheets (324/87-03-02).

No violations or deviations were identified.

11. Spent Fuel Storage Capacity (59095)

The inspectors reviewed the available storage capacity in the Unit 1 and

Unit 2 spent fuel storage pools to determine if full core offload

capability existed for each unit.

Based on discussions with licensee

personnel and review of the licensee's fuel map, full offload capability

(560 assemblies) existed.

Unit 2 Spent Fuel Pool (SFP) has room for 566

more BWR assemblies:

1839

allowed by TS

36

displaced by a PWR rack

-

- 36

rack not installed

I

contains stuck blade guide

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-

2

boral sample stations

- 442

not yet installed

1322

available spaces

- 756

assemblies in pool

~566

BWR spaces available

Unit 1 SFP has room for 925 more BWR assemblies:

1803

allowed by TS

36

rack not installed

-

2

boral sample stations

-

T7EE

available spaces

- 840

assemblies in pool

975

BWR spaces available

The above data is as of February 15, 1987.

The inspector noted that each SFP contained 10 PWR spent fuel modules each

capable of storing 16 assemblies for a PWR capacity in each pool of 160

PWR assemblies.

The Unit 1 SFP contained 160 assemblies while the Unit 2

pool contained 144 assemblies.

However, Unit 2 Technical Specification 5.6.3 states that, "the fuel storage pool is designed and shall be

maintained with a storage capacity limited to no more than 144 PWR fuel

,

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10

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assemblies and 1839 BWR fual assemblies.

The extra 16 storage locations

in the Unit 2 SFP pose no safety problem since the Unit 1 SFP has been

reviewed and approved by NRR, contains 160 PWR assemblies and locations,

also contains additional high density racks, and is essentially identical

to the Unit 2 SFP.

The excess storage capacity in the Unit 2 SFP is a

violation of TS 5.6.3:

Failure to Meet TS 5.6.3 Regarding Spent Fuel Pool

l

PWR Capacity (324/87-03-01).

!

One violation and no deviations were identified.

j

12. RefuelingActivities(60705)

Selected refueling activities were witnessed and reviewed by the

inspector. These included verification that:

The fuel pool gates were removed per MP-09.

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Surveillance requirements of Technical Specification 4.9.6 associated

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with refueling bridge interlocks were performed prior to fuel

movement.

Number of operable SRM's per Technical Specification 3.9.2.a. and b.

-

were maintained.

Continues communications between the refueling bridge and the control

-

room were established per Technical Specification 3.9.5.

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Fuel movements were conducted in accordance with operating procedures

and the Fuel Movement Sheets.

The last activity was performed during a two hour inspection conducted on

the refueling bridge during fuel movements.

No violations or deviations were identified.

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