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{{#Wiki_filter:.
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. . . . . . . _ ,
        Notice of Violation                     3
Notice of Violation
        withholding of such material, you muit tpecifically identify the portions of
3
        your response that you seek to have witkield and provide in detail the bases
withholding of such material, you muit tpecifically identify the portions of
your response that you seek to have witkield and provide in detail the bases
l
l
for your claim of withholding (e.g., explain why the disclosure of information
'
'
        for your claim of withholding (e.g., explain why the disclosure of information
will create an unwarranted invasion of personal privacy or provide the
        will create an unwarranted invasion of personal privacy or provide the
confidential commercial or financial information).
If safeguards information
,
,
        confidential commercial or financial information). If safeguards information
l      1s necessary to provide an acceptable response, please provide the level of
        protection described in 10 CFR 73.21.
        Dated at Atlanta, Georgia
        this 18th day of August, 1997
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l
                                                                          Enclosure 1
1s necessary to provide an acceptable response, please provide the level of
    .
protection described in 10 CFR 73.21.
      .
Dated at Atlanta, Georgia
                        .
this 18th day of August, 1997
                                              __   .
l
                                                              .. .
Enclosure 1
                                                                                -   ..
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                                                                                  1
1
                        U. S. NUCLEAR REGULATORY COMMISSION
U. S. NUCLEAR REGULATORY COMMISSION
                                        REGION 11
REGION 11
    Docket Nos:     50-413, 50 414
Docket Nos:
    License Nos:   NPF-35. NPF-52
50-413, 50 414
    Report Nos..   50-413/97 09. 50 414/97-09
License Nos:
    Licensee:       Duke Power Company
NPF-35. NPF-52
    Facility:       Catawba Nuclear Station. Units 1 and 2
Report Nos..
    Location:       422 South Church Street
50-413/97 09. 50 414/97-09
l                   Charlotte. NC 28242
Licensee:
    Dates:         June 8 - July 19, 1997
Duke Power Company
    Inspectors:     J. Zeiler. Acting Senior Resident inspector
Facility:
                    R. L. Franovich, Resident inspector
Catawba Nuclear Station. Units 1 and 2
                    M. Giles. Resident inspector (In Training)
Location:
                    N. Economos Region 11 Inspector (Sections M8.1. 2. 3. 4)
422 South Church Street
                    R. M. Moore. Region 11 Inspector (Sections 08.1. E2.1 )
l
    Approved by:   S. M. Shaeffer. Acting Chief
Charlotte. NC 28242
                    Reactor Projects Branch 1
Dates:
                    Division of Reactor Projects
June 8 - July 19, 1997
Inspectors:
J. Zeiler. Acting Senior Resident inspector
R. L. Franovich, Resident inspector
M. Giles. Resident inspector (In Training)
N. Economos Region 11 Inspector (Sections M8.1. 2. 3. 4)
R. M. Moore. Region 11 Inspector (Sections 08.1. E2.1 )
Approved by:
S. M. Shaeffer. Acting Chief
Reactor Projects Branch 1
Division of Reactor Projects
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I
                                                                    Enclosure 2
Enclosure 2
  9708260105 970818
9708260105 970818
  PDR   ADOCK 05000413
PDR
  0               PDR
ADOCK 05000413
          . .
0
                            .
PDR
                                .   .
.
                                                                                -
.
.
.
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-


. _ .   __     _. _ _ _ _ _ _ _
. _ .
                                  _____ - _ _ __ -
__
                                                          EXECUTIVE SUMMARY
_.
                                                  Catawba Nuclear Station. Units 1 & 2
_ _ _ _ _ _ _
                                NRC Inspection Report 50 413/97-09, 50 414/97 09
_____ - _ _ __ -
      This integrated inspection included aspects of licensee operations.
EXECUTIVE SUMMARY
      maintenance, engineering, and plant support. The report covers a 6-week
Catawba Nuclear Station. Units 1 & 2
      period of resident ins)ection; in addition, it includes the results of
NRC Inspection Report 50 413/97-09, 50 414/97 09
      announced inspections ay Regional reactor safety inspectors.
This integrated inspection included aspects of licensee operations.
      Doerations
maintenance, engineering, and plant support.
      e
The report covers a 6-week
            A Non Cited Violation (NCV) was identified for failure to declare three
period of resident ins)ection; in addition, it includes the results of
            ice condenser intermediate deck doors inoperable and log an associated
announced inspections ay Regional reactor safety inspectors.
            Technical Specification Action item Log entry after identifying ice
Doerations
            buildup on the doors. This item along with several other minor human
A Non Cited Violation (NCV) was identified for failure to declare three
            performance weaknesses indicated a need for greater attention to detail
e
            and questioning attitude by operations personnel during the performance
ice condenser intermediate deck doors inoperable and log an associated
            of routine activities (Section 01.1).
Technical Specification Action item Log entry after identifying ice
      e
buildup on the doors.
            The root cause evaluations of a reactor coolant pump trip and subsequent
This item along with several other minor human
            reactor trip were adequatel
performance weaknesses indicated a need for greater attention to detail
            involve human error or nonconservative            y performed.   The cause
and questioning attitude by operations personnel during the performance
                                                                          decision     of theThe
of routine activities (Section 01.1).
                                                                                    making.     trip protective
The root cause evaluations of a reactor coolant pump trip and subsequent
                                                                                                    did not
e
            relaying associated with the short bus of 2TB functioned as designed.
reactor trip were adequatel
            However, a delay in troubleshooting activities to locate the source of
involve human error or non y performed. The cause of the trip did not
            the associated ground indicated that the ground received a low priority
conservative decision making.
            status in the work schedule and that trained personnel were not readily
The protective
            available to troubleshoot ground indications in a timely manner (Section
relaying associated with the short bus of 2TB functioned as designed.
            w.2).
However, a delay in troubleshooting activities to locate the source of
      *
the associated ground indicated that the ground received a low priority
            Control room operators were effective in precluding a turbine runback by
status in the work schedule and that trained personnel were not readily
            reducing reactor power to 50% before the 28 Main Generator Power Circuit
available to troubleshoot ground indications in a timely manner (Section
            Breaker opened on low air pressure. The licensee's root cause
w.2).
            evaluation was detailed, and actions to prevent recurrence were
Control room operators were effective in precluding a turbine runback by
            considered adequate (Section 01.3).
*
      *
reducing reactor power to 50% before the 28 Main Generator Power Circuit
            The decision to deviate from the preferred normal alignment of
Breaker opened on low air pressure.
            Lower Containment Ventilation Unit (LCVU) operation to support
The licensee's root cause
            planned maintenance exhibited non-conservative work scheduling and
evaluation was detailed, and actions to prevent recurrence were
            operatorjudgement. This resulted in lower containment air
considered adequate (Section 01.3).
            temperature increasing slightly above the adjusted Technical
The decision to deviate from the preferred normal alignment of
            Specification limit for a brief period of time.                         The LCVU
*
            operating procedures did not address the adverse impact of
Lower Containment Ventilation Unit (LCVU) operation to support
            removing two LCVUs from service simultaneously, nor did the
planned maintenance exhibited non-conservative work scheduling and
            procedure address the interaction between LCVU operation and
operatorjudgement.
            integrated containment ventilation systems. These procedural
This resulted in lower containment air
            inadequacies were identified as a NCV (Section 01.4).
temperature increasing slightly above the adjusted Technical
      *
Specification limit for a brief period of time.
            A violation (first example) for failure to follow procedure was
The LCVU
            identified related to Operations failure to adequately document 10 CFR
operating procedures did not address the adverse impact of
            50.59 screening evaluations (Section 08.1).
removing two LCVUs from service simultaneously, nor did the
                                                                                                  Enclosure 2
procedure address the interaction between LCVU operation and
integrated containment ventilation systems.
These procedural
inadequacies were identified as a NCV (Section 01.4).
A violation (first example) for failure to follow procedure was
*
identified related to Operations failure to adequately document 10 CFR
50.59 screening evaluations (Section 08.1).
Enclosure 2


                                                    _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _
_ _ _ _ _
                                          2
_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _
Maintenance
2
e      A Failure In!estigation Process (FIP) team was thorough in investigating
Maintenance
        the cause of an electrical flash in a 600 Volt breaker cubicle
A Failure In!estigation Process (FIP) team was thorough in investigating
        associated with Motor Control Center 2MXM. The root cause indicated
        configuration and procedure weaknesses in the method of locking out 600
        Volt breaker cubicles to the maintenance position. Adaquate corrective
        actions to prevent recurrence of this incident were implemented (Section
        M1.1).
e
e
        The licensee's identification of a technician's failure to follow a leak
the cause of an electrical flash in a 600 Volt breaker cubicle
        rate test procedure that resulted in an invaild test of valve 2NV-874
associated with Motor Control Center 2MXM. The root cause indicated
        during the previous refueling outage was an example of good questioning
configuration and procedure weaknesses in the method of locking out 600
        attitude: however, the procedure completion review was untimely. The
Volt breaker cubicles to the maintenance position.
        Plant Operations Review Committee performed a thorough review of
Adaquate corrective
        subsequent activities to aroperly retest the valve. Good engineering
actions to prevent recurrence of this incident were implemented (Section
        support was arovided, bot 1 in developing a leak rate test procedure and
M1.1).
      briefing paccage for the evolution. The failure to follow the leak rate
The licensee's identification of a technician's failure to follow a leak
      test procedure was identified as a Violation (Section M1.2).
e
rate test procedure that resulted in an invaild test of valve 2NV-874
during the previous refueling outage was an example of good questioning
attitude: however, the procedure completion review was untimely.
The
Plant Operations Review Committee performed a thorough review of
subsequent activities to aroperly retest the valve.
Good engineering
support was arovided, bot 1 in developing a leak rate test procedure and
briefing paccage for the evolution.
The failure to follow the leak rate
test procedure was identified as a Violation (Section M1.2).
Enaineerina
Enaineerina
e      The licensee's identification of a discrepancy between primary and
The licensee's identification of a discrepancy between primary and
      secondary thermal power indication exhibited attention to detail in the
e
      review of plant data. Actions to initiate a FIP team to investigate the
secondary thermal power indication exhibited attention to detail in the
      root cause were appropriate and steps to reduce reactor power until the
review of plant data.
      discrepancy was understood were conservative. Replacement of a faulty
Actions to initiate a FIP team to investigate the
      T,,, card was well-planned, coordinated and controlled and executed in
root cause were appropriate and steps to reduce reactor power until the
      an expediticas manner (Section El.1).
discrepancy was understood were conservative.
o      Resolution of Design Base Document (DBD) open items was generally
Replacement of a faulty
      adequate.   However, a violation (second example) for failure to follow
T,,, card was well-planned, coordinated and controlled and executed in
      procedure was identified related to Engineering's failure to enter DBD
an expediticas manner (Section El.1).
      open items into the Problem identification Process as required by
Resolution of Design Base Document (DBD) open items was generally
      procedure and stated in the licensee's response to the Des'.gn Basis
o
      50.54f letter (Section E2.1).
adequate.
e      The licensee's corrective action audit that assessed the resolution of
However, a violation (second example) for failure to follow
      Self-N iated Technical Audit findings was identified as a strength in
procedure was identified related to Engineering's failure to enter DBD
      correc " ve action performance (Section E2.1).
open items into the Problem identification Process as required by
e      The licensee adequately addressed the Emergency Diesel Generator 10 CFR
procedure and stated in the licensee's response to the Des'.gn Basis
      Part 21 issue related to potentially defective intake / exhaust springs
50.54f letter (Section E2.1).
      (Section E2.1).
The licensee's corrective action audit that assessed the resolution of
*     Based on in-office review of the licensee *s March 31, 1997, annual
e
      summary on 10 CFR 50.59 changes, onsite review of the licensee's 10 CFR
Self-N iated Technical Audit findings was identified as a strength in
      50.59 evaluations, and audit of the licensee's procedures, the inspector
correc " ve action performance (Section E2.1).
      concluded that the licensee had complied with t1e provisions of the
The licensee adequately addressed the Emergency Diesel Generator 10 CFR
      regulation for the changes listed in the annual summary (Section E3.1).
e
                                                                                                                          Enclosure 2
Part 21 issue related to potentially defective intake / exhaust springs
(Section E2.1).
*
Based on in-office review of the licensee *s March 31, 1997, annual
summary on 10 CFR 50.59 changes, onsite review of the licensee's 10 CFR
50.59 evaluations, and audit of the licensee's procedures, the inspector
concluded that the licensee had complied with t1e provisions of the
regulation for the changes listed in the annual summary (Section E3.1).
Enclosure 2


                                                                                  -
-
                                                                                      ,
,
                                        3
3
  Plant Suncort
Plant Suncort
  e    Radiological control practices observed during the inspection period
Radiological control practices observed during the inspection period
        were considered to b(. proper (Section R1.1).
e
were considered to b(. proper (Section R1.1).
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                                                                    Enclosure 2
Enclosure 2
                            ,
,
                                            .
.
                                                            -
-
                                                                                -   _
-
_


                  _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _
_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _
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                                                    Reoort Details
Reoort Details
; Summary of Plant Status
Summary of Plant Status
;
,
,
  Unit 1 operated at or near 100% power during the inspection period.
Unit 1 operated at or near 100% power during the inspection period.
l On June 26, a Unit 2 reactor trip occurred on low Reactor Coolant System loop
l
On June 26, a Unit 2 reactor trip occurred on low Reactor Coolant System loop
l
l
flow as a result of an electrical ground fault which de energized the
i
i
  flow as a result of an electrical ground fault which de energized the
electrical bus that powers the "2B' Reactor Coolant Pump (RCP).
  electrical bus that powers the "2B' Reactor Coolant Pump (RCP). The unit was
The unit was
  returned to 100% power operation on June 29. Power was reduce 1 to 50% on July
returned to 100% power operation on June 29.
  2 to preclude a turbine trip / reactor trip u)on the anticipated failure of                     ;
Power was reduce 1 to 50% on July
  Main Generator Power Circuit Breaker (PCB) 23.                   A solenoid (or pilot) valve   '
2 to preclude a turbine trip / reactor trip u)on the anticipated failure of
  associated with the air supply to all three main generator PCB poles had
Main Generator Power Circuit Breaker (PCB) 23.
  failed, rendering the air system unable to deliver air to the breaker. The
A solenoid (or pilot) valve
  solenoid valve was replaced, and the unit was returned to 100% power the
;
  following day. Reactor power was reduced to 99.3% on July 15 in response to a
'
  discrepancy between primary and secondary thermal power indications. The
associated with the air supply to all three main generator PCB poles had
  discrepancy was attributed to feedwater venturi defouling and hot leg
failed, rendering the air system unable to deliver air to the breaker. The
  streaming, and did not reflect an actual temperature difference. The unit
solenoid valve was replaced, and the unit was returned to 100% power the
  returned to 100% power on July 17 and operated at or near 100% power for the
following day.
  remainder of the inspection period.
Reactor power was reduced to 99.3% on July 15 in response to a
  Review of UDdated Final Safety Analysis Report (UFSAR) Commitm_gn_t1
discrepancy between primary and secondary thermal power indications.
  While performing inspections discussed in this report, the inspector reviewed
The
  the applicable portions of the UFSAR that were related to the areas ins)ected.
discrepancy was attributed to feedwater venturi defouling and hot leg
  The inspector verified that the UFSAR wording was consistent with the o) served
streaming, and did not reflect an actual temperature difference. The unit
  plant practices, procedures, and/or parameters.
returned to 100% power on July 17 and operated at or near 100% power for the
                                                    I. Operations
remainder of the inspection period.
  01     Conduct of Operations
Review of UDdated Final Safety Analysis Report (UFSAR) Commitm_gn_t1
  01.1 General Comments (71707)
While performing inspections discussed in this report, the inspector reviewed
        The inspector conducted frequent control room tours to verify proper
the applicable portions of the UFSAR that were related to the areas ins)ected.
        staffing operator attentiveness and communications. and adherence to
The inspector verified that the UFSAR wording was consistent with the o) served
        approved )rocedures. The inspector attended daily operations turnover
plant practices, procedures, and/or parameters.
        and Site )irection meetings to maintain awareness of overall plant
I. Operations
        operations. Operator logs were reviewed to verify operational safety
01
        and compliance with Technical Specifications (TS). Instrumentation,
Conduct of Operations
        computer indications, and safety system lineups were periodically
01.1 General Comments (71707)
        reviewed from the Control Room to assess o)erability. Plant tours were
The inspector conducted frequent control room tours to verify proper
        conducted to observe equipment status and Jousekeeping.                 Problem
staffing operator attentiveness and communications. and adherence to
        Identification Process (PIP) reports were routinely reviewed to assure
approved )rocedures.
        that potential safety concerns and equipment problems were reported and-
The inspector attended daily operations turnover
        resolved,
and Site )irection meetings to maintain awareness of overall plant
        in general, the conduct of operations was professional and safety
operations.
        conscious. Good )lant equipment material conditions ar.d housekee ing
Operator logs were reviewed to verify operational safety
        were noted througaout the report period. However, as addressed b low,
and compliance with Technical Specifications (TS).
        sevcral minor operator human performance deficiencies were identified
Instrumentation,
                                                                                      Enclosure 2
computer indications, and safety system lineups were periodically
reviewed from the Control Room to assess o)erability.
Plant tours were
conducted to observe equipment status and
Jousekeeping.
Problem
Identification Process (PIP) reports were routinely reviewed to assure
that potential safety concerns and equipment problems were reported and-
resolved,
in general, the conduct of operations was professional and safety
conscious. Good )lant equipment material conditions ar.d housekee ing
were noted througaout the report period.
However, as addressed b low,
sevcral minor operator human performance deficiencies were identified
Enclosure 2


_ _ _ _ _ _ _
_ _ _ _ _ _ _
                                                                    .
.
                                                                                        ,
,
                                                  2
2
                involving a failure to enter a TS Action Statement, failure to identify
involving a failure to enter a TS Action Statement, failure to identify
                equipment status anomalies, and failure to properly document a Technical
equipment status anomalies, and failure to properly document a Technical
              Specification Action item Log (TSAIL) entry.
Specification Action item Log (TSAIL) entry.
              Failure to Declare Unit 2 Ice Condenser Intermediate Deck Doors
Failure to Declare Unit 2 Ice Condenser Intermediate Deck Doors
                inoDerable and Enter ADolicable TS Action Statement
inoDerable and Enter ADolicable TS Action Statement
              On June 17 at 2:38 p.m., while performing the weekly TS surveillance on
On June 17 at 2:38 p.m., while performing the weekly TS surveillance on
              the intermediate deck doors the licensee identified that three doors
the intermediate deck doors the licensee identified that three doors
              had ice buildup (reported to be less than one half inch thick). The
had ice buildup (reported to be less than one half inch thick). The
                function of these doors is to open during a des.gn basis accident to
function of these doors is to open during a des.gn basis accident to
              ensure that the containment loss Of Coolant Accident (LOCA) atmos)here     l
ensure that the containment loss Of Coolant Accident (LOCA) atmos)here
              would be diverted through the ice condenser. Upon discovery of t1e ice,
l
              a test procedure discrepancy was entered and a work request was
would be diverted through the ice condenser.
                initiated to remove the ice. However, work to remove the ice or
Upon discovery of t1e ice,
                investigate the extent of the impact on the door opening function was
a test procedure discrepancy was entered and a work request was
              not initiated due to problems with personnel accessing containment
initiated to remove the ice.
              through the containment airlock door. Later that night, the oncoming
However, work to remove the ice or
              Shift Work Manager became aware of the previces day's problem and
investigate the extent of the impact on the door opening function was
              -contacted engineering personnel to perform an operability evaluation of
not initiated due to problems with personnel accessing containment
              the condition. The following morning, the inspector reviewed the
through the containment airlock door.
              results of this evaluation. The evaluation concluded that the " ice
Later that night, the oncoming
              condenser" was operable. This was based primarily-on a previous McGuire
Shift Work Manager became aware of the previces day's problem and
              Nuclear Station analysis that showed up to one-third of the intermediate
-contacted engineering personnel to perform an operability evaluation of
              deck doors could fail to open and there would still be enough ice
the condition.
              condenser flow area for LOCA heat removal. The inspector determined the
The following morning, the inspector reviewed the
              evaluation focused to narrowly on the ice condenser system operability
results of this evaluation.
              and failed to adequately evaluate the operability of the intermediate
The evaluation concluded that the " ice
              deck doors, especially with regard to consideration of information in
condenser" was operable.
              the applicable TS and Bases.
This was based primarily-on a previous McGuire
              TS 3.6.5.3 requires the intermediate deck doors be operable in Modes 1-
Nuclear Station analysis that showed up to one-third of the intermediate
              4. TS Surveillance Recuirement 4.6.5.3.2 requires a 7-day verification
deck doors could fail to open and there would still be enough ice
              that the intermediate ceck doors be closed and free of frost
condenser flow area for LOCA heat removal.
              accumulation. The TS Bases also states that impairment by ice, frost.
The inspector determined the
              or debris is considered to render the doors inoperable, but capable of
evaluation focused to narrowly on the ice condenser system operability
              opening. Based on this, the inspector concluded that operations
and failed to adequately evaluate the operability of the intermediate
              personnel had failed to declare the three doors inopera]le and follow
deck doors, especially with regard to consideration of information in
              the Action Statement of TS 3.6.5.3.a when the problem was initially
the applicable TS and Bases.
              identified. This action statement allowed power operation to continue
TS 3.6.5.3 requires the intermediate deck doors be operable in Modes 1-
              for up to 14 days provided ice bed temperature was monitored at least
4.
              once per four hours and the maximum ice bed temperature was maintained
TS Surveillance Recuirement 4.6.5.3.2 requires a 7-day verification
              less than or equal to 27*F. The licensee initiated PIP 2-C97-2014-to
that the intermediate ceck doors be closed and free of frost
              investigate this incident.
accumulation.
              On June 18. after repairing the containment airlock, ice was removed
The TS Bases also states that impairment by ice, frost.
              from the three intermediate deck doors. The cause of the ice buildup
or debris is considered to render the doors inoperable, but capable of
              was found to be the failure of heat tracing on an ice condenser air
opening.
              handling fan drain line, which prevented adequate draining of defrost
Based on this, the inspector concluded that operations
              condensate. The heat tracing was subsequently repaired. The licensee
personnel had failed to declare the three doors inopera]le and follow
                                                                            Enclosure 2
the Action Statement of TS 3.6.5.3.a when the problem was initially
                                                                        -
identified. This action statement allowed power operation to continue
for up to 14 days provided ice bed temperature was monitored at least
once per four hours and the maximum ice bed temperature was maintained
less than or equal to 27*F.
The licensee initiated PIP 2-C97-2014-to
investigate this incident.
On June 18. after repairing the containment airlock, ice was removed
from the three intermediate deck doors.
The cause of the ice buildup
was found to be the failure of heat tracing on an ice condenser air
handling fan drain line, which prevented adequate draining of defrost
condensate. The heat tracing was subsequently repaired. The licensee
Enclosure 2
-


,
,
                                    3
3
determined during activities to remove the ice that all three doors were
i
i
  determined during activities to remove the ice that all three doors were
l
l not blocked to the extent that would have prevented their opening during
not blocked to the extent that would have prevented their opening during
a LOCA.
The inspector also noted that the ice bed monitoring system was
'
'
  a LOCA. The inspector also noted that the ice bed monitoring system was
operational during the period that ice was on the doors and control room
  operational during the period that ice was on the doors and control room
annunciator alarms would have alerted the operators of anomalous ice bed
  annunciator alarms would have alerted the operators of anomalous ice bed
temperatures. Therefore, the ins)ector considered the safety
  temperatures. Therefore, the ins)ector considered the safety
consequences of this incident to )e minimal.
  consequences of this incident to )e minimal.
The inspector reviewed Operations Management Procedure (OMP) 2-29.
  The inspector reviewed Operations Management Procedure (OMP) 2-29.
Technical Specifications Action Item Log. Step 3.4 requires that non-
  Technical Specifications Action Item Log. Step 3.4 requires that non-
compliance with a Limiting Condition For Operation requiring operation
  compliance with a Limiting Condition For Operation requiring operation
in a TS Action Statement, be logged in TSAll.
  in a TS Action Statement, be logged in TSAll. The ins)ector determined
The ins)ector determined
  that a TSAll entry was not logged for this condition w1en ice was
that a TSAll entry was not logged for this condition w1en ice was
  identified on the doors rendering them inoperable. The failure to
identified on the doors rendering them inoperable.
  declare the doors inoperable and enter a TSAll entry for t % applicable
The failure to
  TS Action Statement in accordance with OMP 2-29 was identitied as a
declare the doors inoperable and enter a TSAll entry for t % applicable
  Violation of TS 6.8.1. Procedures and Programs. This failure to follow
TS Action Statement in accordance with OMP 2-29 was identitied as a
  procedures constitutes a violation of minor significance and is being
Violation of TS 6.8.1. Procedures and Programs. This failure to follow
  treated as a Non-Cited Violation (NCV). consistent with Section IV of
procedures constitutes a violation of minor significance and is being
  the NRL Enforcement Policy. This item is identified as NCV 50 414/97-
treated as a Non-Cited Violation (NCV). consistent with Section IV of
  09 01:   Failure to Declare Ice Condenser Intermediate Deck Doors
the NRL Enforcement Policy. This item is identified as NCV 50 414/97-
  Inoperable and Log Appropriate TSAll Entry.
09 01:
  Auxiliary Shutdown Panel Volume Control Tank (VCT) Instrumentation Drift
Failure to Declare Ice Condenser Intermediate Deck Doors
  During a walkdown of the four Motor Driven Auxiliary Feedwater Shutdown
Inoperable and Log Appropriate TSAll Entry.
  Panels, the inspector identified that three of the four VCT level
Auxiliary Shutdown Panel Volume Control Tank (VCT) Instrumentation Drift
  indications were not reading accurately. There is one VCT gauge on each
During a walkdown of the four Motor Driven Auxiliary Feedwater Shutdown
  Shutdown Panel. Gauge indications differed from control room
Panels, the inspector identified that three of the four VCT level
  indications by as much as 20 percent level. The ins)ector alerted
indications were not reading accurately.
  operations-personnel to-the problem and noted that t1ey were very
There is one VCT gauge on each
  responsive in initiating corrective actions. Due to subsequent problems
Shutdown Panel. Gauge indications differed from control room
  in calibrating the gauges and unavailability of like parts, engineering
indications by as much as 20 percent level.
  modifications were developed and implemented to replace the gauges with
The ins)ector alerted
  more accurate models. Based on discussions with Instrumentation and
operations-personnel to-the problem and noted that t1ey were very
  Electrical (IAE) personnel, it was indicated that most likely, the
responsive in initiating corrective actions.
  gauges had drifted out of accuracy over a long period of-time.
Due to subsequent problems
  The inspector reviewed periodic surveillance test procedures associated
in calibrating the gauges and unavailability of like parts, engineering
  with verifying Shutdown Panel instrumentation indications. VCT level
modifications were developed and implemented to replace the gauges with
  was not among the indications checked periodically. The inspector
more accurate models.
  noted. however, that VCT level was not required by TS to be o)erable
Based on discussions with Instrumentation and
  from the Shutdown Panels. However, the VCT indication could )e
Electrical (IAE) personnel, it was indicated that most likely, the
  potentially used during operation from the Shutdown Panels. It was also
gauges had drifted out of accuracy over a long period of-time.
  apparent that-there had been opportunities to have identified the gauge
The inspector reviewed periodic surveillance test procedures associated
  output drift during the periodic surveillances of other Shutdown Panel
with verifying Shutdown Panel instrumentation indications.
  instrumentation.
VCT level
                                                                Enclosure 2
was not among the indications checked periodically.
The inspector
noted. however, that VCT level was not required by TS to be o)erable
from the Shutdown Panels.
However, the VCT indication could )e
potentially used during operation from the Shutdown Panels.
It was also
apparent that-there had been opportunities to have identified the gauge
output drift during the periodic surveillances of other Shutdown Panel
instrumentation.
Enclosure 2


  _________ __- _ _                           .
_________ __- _ _
                                                            -
.
l                                                             4
-
                          Unit 2 Power Rance Channel NI-42 Soare Window Illuminated
l
                          On June 27. 1997, the day after Unit 2 tripped on low Reactor Coolant
4
                          System flow, the inspector noticed an annunciator window on the Nuclear
Unit 2 Power Rance Channel NI-42 Soare Window Illuminated
                          Instrument (N1) 42 Power Range drawer that was illuminated. The
On June 27. 1997, the day after Unit 2 tripped on low Reactor Coolant
                          annunciator window was labeled " spare" and appeared to serve no
System flow, the inspector noticed an annunciator window on the Nuclear
                          function. The inspector questioned the control room operators about the
Instrument (N1) 42 Power Range drawer that was illuminated.
                          illuminated window. The window apparently first illuminated following
The
                          the trip; however, the operators were not aware that the window was
annunciator window was labeled " spare" and appeared to serve no
                          illuminated, nor the reason for the condition. Based on subsequent
function.
                          discussions with reactor engineering personnel, the inspector learned
The inspector questioned the control room operators about the
                          that this spare annunciator window was previously used as the negative
illuminated window. The window apparently first illuminated following
                          rate trip indication light. During the previous refueling outage. this
the trip; however, the operators were not aware that the window was
                          trip function was isolated from the reactor protection logic, the
illuminated, nor the reason for the condition.
                          modification that implemented the rate trip change was supposed to have
Based on subsequent
                          removed the bulb from these windows on all of the N1 drawers. .It was
discussions with reactor engineering personnel, the inspector learned
                          believed that the bulb in the NI-42 drawer was removed, but may have
that this spare annunciator window was previously used as the negative
                          been reinstalled by lAE personnel by mistake during subsequent NI
rate trip indication light. During the previous refueling outage. this
                          maintenance activities following the refueling outage. The light was
trip function was isolated from the reactor protection logic, the
                          extinguished once the rate trip function was reset and the bulb. removed.
modification that implemented the rate trip change was supposed to have
                          The licensee initiated a PIP to address this problem.
removed the bulb from these windows on all of the N1 drawers. .It was
                          TS Loaaina Error for Trackina Containment Airlock Door Seal Surveillance
believed that the bulb in the NI-42 drawer was removed, but may have
                          lRR
been reinstalled by lAE personnel by mistake during subsequent NI
                          On July 11, 1997, during review of the Unit 2 TSAIL. the inspector
maintenance activities following the refueling outage. The light was
                          noticed an incorrect entry that was made on July 9. The entry was for
extinguished once the rate trip function was reset and the bulb. removed.
                          tracking a TS required 72 hour airlock door seal test following opening
The licensee initiated a PIP to address this problem.
                          of the airlock door on July 9. The time required for the test to be
TS Loaaina Error for Trackina Containment Airlock Door Seal Surveillance
                          performed was listed in TSAIL as July 16 instead of July 12. The
lRR
                          inspector discussed the error with operations personnel who corrected
On July 11, 1997, during review of the Unit 2 TSAIL. the inspector
                          the entry. It was also indicated that the seal test was scheduled to be
noticed an incorrect entry that was made on July 9.
                          performed that same day. Based on this, the inspector determined the
The entry was for
                          test would not have been missed even though the TSAll was incorrect.
tracking a TS required 72 hour airlock door seal test following opening
                          The inspector was concerned that the TSAll error had not been identified
of the airlock door on July 9.
                          over the two previous two days that the problem existed.
The time required for the test to be
                          Individually, the above problems had little actual safety consequences.
performed was listed in TSAIL as July 16 instead of July 12.
                          however, in the aggregate represented the need for greater attention to
The
                          detail and questioning attitude by operations personnel during the
inspector discussed the error with operations personnel who corrected
                          performance of routine activities.
the entry.
                    01.2 Unit 2 Reactor Trio on low Reactor Coolant System Flow-
It was also indicated that the seal test was scheduled to be
                      a.   Insoection Scope (71707. 937,01).
performed that same day.
                          On June 26 a Unit 2 reactor trip from 100% power occurred when the 2B
Based on this, the inspector determined the
                          Reactor Coolant Pump (RCP) tripped and caused a loss of flow signal in
test would not have been missed even though the TSAll was incorrect.
                          the associated loop. The inspector discussed the unit trip with
The inspector was concerned that the TSAll error had not been identified
                          engineering, operations and maintenance personnel, as well as reviewed
over the two previous two days that the problem existed.
                          the associated electrical diagrams. Unit Trip Report and Pl? 2-C97-2221.
Individually, the above problems had little actual safety consequences.
                                                                                        Enclosure 2
however, in the aggregate represented the need for greater attention to
detail and questioning attitude by operations personnel during the
performance of routine activities.
01.2 Unit 2 Reactor Trio on low Reactor Coolant System Flow-
a.
Insoection Scope (71707. 937,01).
On June 26 a Unit 2 reactor trip from 100% power occurred when the 2B
Reactor Coolant Pump (RCP) tripped and caused a loss of flow signal in
the associated loop. The inspector discussed the unit trip with
engineering, operations and maintenance personnel, as well as reviewed
the associated electrical diagrams. Unit Trip Report and Pl? 2-C97-2221.
Enclosure 2


l                                       5
l
i b, Observations and Findinas
5
i
b,
Observations and Findinas
On June 21. a negative leg ground was detected on ron vital distribution
i
i
!
!
    On June 21. a negative leg ground was detected on ron vital distribution
bus 2CDB.
    bus 2CDB.   The ground subsequently was traced to tre 125 VDC control
The ground subsequently was traced to tre 125 VDC control
l   power circuit of breaker 2T6 6. On June 26. the b"eaker was opened to
l
power circuit of breaker 2T6 6.
On June 26. the b"eaker was opened to
facilitate troubleshooting the cause of the ground.
The Instrument and
'
'
    facilitate troubleshooting the cause of the ground. The Instrument and      .
Electrical (IAE) technicians noticed that the breaker failure initiation
    Electrical (IAE) technicians noticed that the breaker failure initiation     l
l
    relay in 2TB 6 control cubicle was chattering, but continued with their     i
.
    troubleshooting activities. Shortly thereafter, a reactor trip
relay in 2TB 6 control cubicle was chattering, but continued with their
    occurred.
i
    The licensee determined that. the source of the ground fault was the
troubleshooting activities.
    breaker pushbutton, a Cutler-Hammer E30 model,     lhe pushbutton had       '
Shortly thereafter, a reactor trip
    failed and created a negative leg-to ground fault on 2CDB. The
occurred.
    pushbutton internals had changed state when 2TB 6 was tripped open
The licensee determined that. the source of the ground fault was the
    during troubleshooting, introducing a fault path to the positive leg.
breaker pushbutton, a Cutler-Hammer E30 model,
    Noise from the cabinet ground was induced through the switch and the
lhe pushbutton had
    breaker failure initiation relay (94B) coil, causing it to chatter and
'
    eventually actuate to trip the incoming breaker on the short bus of 2TB.
failed and created a negative leg-to ground fault on 2CDB. The
    The auto close function of the 2TB tie breaker was blocked by a lockout
pushbutton internals had changed state when 2TB 6 was tripped open
    rela
during troubleshooting, introducing a fault path to the positive leg.
    bus,y, and the bus de-energized. The 2B RCP. which is supplied from the
Noise from the cabinet ground was induced through the switch and the
          tripped, and the subsequent low flow in the B loop caused a reactor
breaker failure initiation relay (94B) coil, causing it to chatter and
    trip.
eventually actuate to trip the incoming breaker on the short bus of 2TB.
    The inspector discussed the reactor trip with operations and engineering
The auto close function of the 2TB tie breaker was blocked by a lockout
    personnel to determine if the root cause involved a human error. The
rela
    chattering of the relay, generated when 2TB 6 was opened, could have
bus,y, and the bus de-energized. The 2B RCP. which is supplied from the
    been stop)ed if the IAE technicians had reclosed the breaker when they
tripped, and the subsequent low flow in the B loop caused a reactor
    noticed tlat relay chattering. However, they did not understand what
trip.
    was causing the chattering at the time. The inspector concluded that
The inspector discussed the reactor trip with operations and engineering
    the IAE technicians responded appropriately by leaving the breaker in
personnel to determine if the root cause involved a human error. The
    the opened position since the cause and impact of the relay chattering
chattering of the relay, generated when 2TB 6 was opened, could have
    were not understood.
been stop)ed if the IAE technicians had reclosed the breaker when they
    The inspector inquired about the time delay between ground detection
noticed tlat relay chattering.
    (identified on a Saturday) and troubleshooting activities (initiated the
However, they did not understand what
    following Wednesday).     l.icensee personnel indicated that Single Point Of
was causing the chattering at the time.
    Contact (SPOC) technicians were not trained and qualified to use the
The inspector concluded that
    ground chasing equipment. As a result a'stempts to locate the ground
the IAE technicians responded appropriately by leaving the breaker in
    could not be made until the following Monday when a trained IAE
the opened position since the cause and impact of the relay chattering
    technician would be available. Also, priority status was not associated
were not understood.
    with troubleshooting the ground indication early in the week. In
The inspector inquired about the time delay between ground detection
    addition, the inspector determined that only two techniciant on site
(identified on a Saturday) and troubleshooting activities (initiated the
    were fully qualified to use the ground-chasing equipment to locate the
following Wednesday).
    source of a ground, and that_one of those technicians had been offsite
l.icensee personnel indicated that Single Point Of
    since February and was not scheduled to return until October of this
Contact (SPOC) technicians were not trained and qualified to use the
    year. A shortage of trained personnel available to perform the
ground chasing equipment.
    troubleshooting contributed to the delay. At the end of the ins)ection
As a result a'stempts to locate the ground
    period, the delay in investigating the ground, associated contri)uting
could not be made until the following Monday when a trained IAE
    factors, and appropriate corrective actions were not addressed within
technician would be available. Also, priority status was not associated
    the licensee's corrective action program.
with troubleshooting the ground indication early in the week.
                                                                    Enclosure 2
In
addition, the inspector determined that only two techniciant on site
were fully qualified to use the ground-chasing equipment to locate the
source of a ground, and that_one of those technicians had been offsite
since February and was not scheduled to return until October of this
year. A shortage of trained personnel available to perform the
troubleshooting contributed to the delay.
At the end of the ins)ection
period, the delay in investigating the ground, associated contri)uting
factors, and appropriate corrective actions were not addressed within
the licensee's corrective action program.
Enclosure 2


.
.
                                            6
6
        The unit was restarted on June 28 after trip list activities were
The unit was restarted on June 28 after trip list activities were
        performed and minor equipment problems were corrected. The licensee is         '
performed and minor equipment problems were corrected. The licensee is
        planning to document the reactor trip in a Licensee Event Report.
'
l   c.   Conclusions
planning to document the reactor trip in a Licensee Event Report.
        The inspector concluded that root cause evaluations of the reactor trip
l
        were adequately performed.     The cause of the tt!p did not involve human
c.
        error or non conservative decision making. The protective relaying
Conclusions
        associated with the short bus of 2TB functioned as designed. The
The inspector concluded that root cause evaluations of the reactor trip
        inspector determined that, although the delay in troubleshooting
were adequately performed.
        activities to locate the source of the ground did not affect the outcome
The cause of the tt!p did not involve human
          (reactor trip), challenges existed in the following areas: (1)
error or non conservative decision making. The protective relaying
        associating appropriate priority to locating ground indications in a
associated with the short bus of 2TB functioned as designed. The
        timely manner, and (2) ensuring that trained personnel are avullable to
inspector determined that, although the delay in troubleshooting
        troubleshoot ground indications. At the end of the inspection period,
activities to locate the source of the ground did not affect the outcome
        efforts to address the delay, understand its causes, and identify
(reactor trip), challenges existed in the following areas: (1)
        corrective actions were not evident in the licensee's corrective action
associating appropriate priority to locating ground indications in a
        program.
timely manner, and (2) ensuring that trained personnel are avullable to
troubleshoot ground indications. At the end of the inspection period,
efforts to address the delay, understand its causes, and identify
corrective actions were not evident in the licensee's corrective action
program.
'
'
  01.3 Unit 2 Downoower in Response to Generator Outout Breaker Trouble
01.3 Unit 2 Downoower in Response to Generator Outout Breaker Trouble
    a.   insoection Scone (71707)
a.
        On July 2. Unit 2 control room operators received a generator breaker
insoection Scone (71707)
        trouble alarm and identified a continuous decrease in minimum close air
On July 2. Unit 2 control room operators received a generator breaker
          3ressure on 28 Main G2nerator Power Circuit Breaker (PCB). Operators
trouble alarm and identified a continuous decrease in minimum close air
        Jegan a rapid load reduction, and the PCB automatically tripped after
3ressure on 28 Main G2nerator Power Circuit Breaker (PCB). Operators
        reactor power reached 50%. The inspector reviewed PIP 2 C97 2177 and
Jegan a rapid load reduction, and the PCB automatically tripped after
        discussed the downpower and associated equipment failure with licensee
reactor power reached 50%.
        personnel.
The inspector reviewed PIP 2 C97 2177 and
    b.   Observations and Findinos
discussed the downpower and associated equipment failure with licensee
        On July 2, the Main Generator PCB 2B Trouble annunciator alarmed in the
personnel.
        control room. Control room operators determined that there was a
b.
        continuous decrease in air 3ressure on the 28 Main Generator PCB,
Observations and Findinos
        indicating an approach to 11e minimum air pressure is required to open
On July 2, the Main Generator PCB 2B Trouble annunciator alarmed in the
        the breaker. Air
control room.
      ' the resulting arc. pressure is required
Control room operators determined that there was a
                              Since the           to openofthe
continuous decrease in air 3ressure on the 28 Main Generator PCB,
                                          safety function     thebreaker andtodissipate
indicating an approach to 11e minimum air pressure is required to open
                                                                  PCB was     open, it
the breaker. Air
        was designed to automatically open before the minimum pressure required
' the resulting arc. pressure is required to open the breaker and dissipate
        for this function is reached.     The minimum tri
Since the safety function of the PCB was to open, it
        Generator PCB 2B is between 446 and 452 psig. p pressure on Main
was designed to automatically open before the minimum pressure required
        To preclude an automatic turbine runback on the potential automatic
for this function is reached.
        opening of the PCB operators began a rapid load reduction, The PCB
The minimum tri
        automatically tripped after reactor power reached 50%. No overcurrent
Generator PCB 2B is between 446 and 452 psig. p pressure on Main
        alarms were received on Main Transformer 2A.
To preclude an automatic turbine runback on the potential automatic
        The license deternJned that a solenoid (or )ilot) valve associated with           I
opening of the PCB operators began a rapid load reduction, The PCB
automatically tripped after reactor power reached 50%.
No overcurrent
alarms were received on Main Transformer 2A.
The license deternJned that a solenoid (or )ilot) valve associated with
I
the air sup)1y to a:1 three main generator )CB poles had failed,
s
s
        the air sup)1y to a:1 three main generator )CB poles had failed,
rendering t1e air system unable to deliver air to the breaker.
        rendering t1e air system unable to deliver air to the breaker.
Normally, the solenoid valve receives signals from the breaker poles to
        Normally, the solenoid valve receives signals from the breaker poles to
Enclosure 2
                                                                          Enclosure 2
V
                                                V


7
i
i
                                            7
supply air to them. When the air pressure on any pole reaches
,
,
        supply air to them. When the air pressure on any pole reaches
a> proximately 485 psi.-a pressure switch actuates and the solenoid valve
        a> proximately 485 psi.-a pressure switch actuates and the solenoid valve
sluttles to pneumatically control a regulator that delivers air to the
        sluttles to pneumatically control a regulator that delivers air to the
breaker poles. When air pressure is restored to 500 psi the signal
        breaker poles. When air pressure is restored to 500 psi the signal
from the pole to the solenoid is terminated.
'
'
        from the pole to the solenoid is terminated.
Station PIP 2-C97-2177 documented the root cause of the solenoid
        Station PIP 2-C97-2177 documented the root cause of the solenoid
failure.
        failure. The failed solenoid was new and had been installed during the
The failed solenoid was new and had been installed during the
        April 1997 refueling outage. The component failure was attributed to a
April 1997 refueling outage.
        deformed nylon bushing. The valve had been assembled to compensate for
The component failure was attributed to a
        the defect which initially allowed the valve to operate as designed.
deformed nylon bushing.
        However, the valve's internal components drifted from their assembled
The valve had been assembled to compensate for
        positions over time and eventually were unable to engage with the
the defect which initially allowed the valve to operate as designed.
        valve's lower assembly, thereby preventing air flow to the poles.
However, the valve's internal components drifted from their assembled
        To address the potential that newly purchased solenoid valves could be
positions over time and eventually were unable to engage with the
        installed with problems, the licensee had revised procedure
valve's lower assembly, thereby preventing air flow to the poles.
        IP/0/B/4974/01, Main Generator PCB Maintenance. - Revision 5 of the
To address the potential that newly purchased solenoid valves could be
        procedure included a Note between Steps 10.3.7 and 10.3.8. The-Note
installed with problems, the licensee had revised procedure
        read: "If pilot valve is replaced, ensure pilot valve has been
IP/0/B/4974/01, Main Generator PCB Maintenance. - Revision 5 of the
        disassembled and inspected for pro >er assembly and components. or
procedure included a Note between Steps 10.3.7 and 10.3.8. The-Note
        rebuilt prior to installation." T1e inspector verified that this
read: "If pilot valve is replaced, ensure pilot valve has been
        procedure change had been made,
disassembled and inspected for pro>er assembly and components. or
    c.   Conclusions
rebuilt prior to installation." T1e inspector verified that this
        The inspector concluded that control room operators were effective in
procedure change had been made,
          )recluding a turbine runback by reducing reactor power to 50% before the
c.
          3CB opened. The licensee's root cause evaluation was detailed and
Conclusions
        actions to prevent recurrence were adequate.
The inspector concluded that control room operators were effective in
  01.4 Lower Containment Air Temoerature Exceeded for Short Duration
)recluding a turbine runback by reducing reactor power to 50% before the
    a.   Insnection Stone (71707)
3CB opened.
        On June 30. the licensee was performing maintenance on the Unit 2
The licensee's root cause evaluation was detailed and
        Lower Containment Ventilation Units (LCVUs). While the 2A and 20
actions to prevent recurrence were adequate.
        LCVUs were out of service, the lower containment temperature
01.4 Lower Containment Air Temoerature Exceeded for Short Duration
        increased to 117.4'F. The inspector reviewed apalicable operating
a.
        procedures. TS. the FSAR, tagout requirements, tie innage work
Insnection Stone (71707)
        schedule, and PIP 2 C97-2127. The inspector also discussed the
On June 30. the licensee was performing maintenance on the Unit 2
        -issue with operations, engineering and work control personnel.
Lower Containment Ventilation Units (LCVUs). While the 2A and 20
    b.   Observations-and Findinas
LCVUs were out of service, the lower containment temperature
        During normal operation. the Containment Chilled Water (YV)
increased to 117.4'F. The inspector reviewed apalicable operating
        chillers service various containment loads including the LCt!Us and
procedures. TS. the FSAR, tagout requirements, tie innage work
        the Reactor Coolant Pump (RCP) Motor Air Coolers. 0_n June 30,
schedule, and PIP 2 C97-2127.
        preventive maintenance (PM) and electrical motor testing were
The inspector also discussed the
        scheduled for the 2A and 20 LCVUs. The 2A LCVU was removed from
-issue with operations, engineering and work control personnel.
                                                                      Enclosure 2
b.
Observations-and Findinas
During normal operation. the Containment Chilled Water (YV)
chillers service various containment loads including the LCt!Us and
the Reactor Coolant Pump (RCP) Motor Air Coolers.
0_n June 30,
preventive maintenance (PM) and electrical motor testing were
scheduled for the 2A and 20 LCVUs. The 2A LCVU was removed from
Enclosure 2


                                                                                                                      I
I
                                                                                                                      !
!
                                                                                                                        l
l
                                                              8
8
                                                                                                                        l
l
  service first. After the PM for the 2A LCVU was completed, but                                                         i
service first.
before motor testing was completed, operations personnel decided
After the PM for the 2A LCVU was completed, but
to remove the 2D LCVU for PM.                               The 2D LCVU was removed from                             ,
i
service at 10:55 a.m.             While both LCVUs were out of service, lower
before motor testing was completed, operations personnel decided
containment temperature increased. To compensate for the
to remove the 2D LCVU for PM.
temperature increase, control room operators adjusted the
The 2D LCVU was removed from
o)eration of the remaining inservice LCVUs (2B and 2C) from
,
  "iormal" to "High Speed." and then to " Max Cool." However, for a                                                       !
service at 10:55 a.m.
brief period of time lower containment temperature had exceeded
While both LCVUs were out of service, lower
the high high temperature Operator Aid Computer (0AC) alarm
containment temperature increased.
setpoint of 115.6'F and the adjusted TS limit of 117.2*F.
To compensate for the
ultimately reaching 117.4'F. Lower containment temperature was                                                       ,
temperature increase, control room operators adjusted the
                                                                                                                      '
o)eration of the remaining inservice LCVUs (2B and 2C) from
above 117'F for approximately 3 minutes before it was restored to
"iormal" to "High Speed." and then to " Max Cool." However, for a
within TS limits. The Action required by TS 3.6.1.5 was to
brief period of time lower containment temperature had exceeded
                                                                                                                        ,
the high high temperature Operator Aid Computer (0AC) alarm
                                                                                                                        i
setpoint of 115.6'F and the adjusted TS limit of 117.2*F.
restore the air temperature to within the limits within 8 hours or
ultimately reaching 117.4'F.
be in at least hot standby within the next 6 hours. Since the
Lower containment temperature was
                                                                                                                        .
',
                                                                                                                      !
above 117'F for approximately 3 minutes before it was restored to
bich lower containment temperature existed for only a few minutes.                                                   -
within TS limits.
th6 licensee was in compliance with the TS action.                                                                   .
The Action required by TS 3.6.1.5 was to
At anroximately 11:10 a.m., operations personnel decided to post)one
,
the M on the 2D LCVU. recall the associated tags and return the _CVU to
i
service until the 2A LCVU was restored to operation. While operators                                                 i
restore the air temperature to within the limits within 8 hours or
.
be in at least hot standby within the next 6 hours. Since the
!
bich lower containment temperature existed for only a few minutes.
-
th6 licensee was in compliance with the TS action.
.
At anroximately 11:10 a.m., operations personnel decided to post)one
the M on the 2D LCVU. recall the associated tags and return the _CVU to
service until the 2A LCVU was restored to operation.
While operators
i
were returning the 2D LCVU to service and all three LCVUs to normal
were returning the 2D LCVU to service and all three LCVUs to normal
alignment, the YV chillers in service (A and C) trip >ed on low flow.
alignment, the YV chillers in service (A and C) trip>ed on low flow.
Based on a review of the circumstances surrounding t1e trip of the A and                                             ,
Based on a review of the circumstances surrounding t1e trip of the A and
,
C YV chillers, the inspector discerned that the following took place.
C YV chillers, the inspector discerned that the following took place.
When the B and C LCVUs were taken to " Max Cool" in an effort to reduce                                               !
When the B and C LCVUs were taken to " Max Cool" in an effort to reduce
lower containment temperature, the flow control valves in the chiller
!
loop fully opened as designed, and thermostatic control of,the chilled
lower containment temperature, the flow control valves in the chiller
loop fully opened as designed, and thermostatic control of,the chilled
water supply was lost. When operations subsequently restored the D LCVU
water supply was lost. When operations subsequently restored the D LCVU
to service and returned the LCVUs to normal operation, thermostatic                                                     i
to service and returned the LCVUs to normal operation, thermostatic
control of the flow control valves was reinstated. The existing
i
control of the flow control valves was reinstated.
The existing
temperature caused the flow control valves to throttle closed, and the
temperature caused the flow control valves to throttle closed, and the
chillers tripped on low load. Normal alignment with the A and B YV
chillers tripped on low load.
Normal alignment with the A and B YV
chillers was established within 30 minutes of the chiller trips. The C
chillers was established within 30 minutes of the chiller trips. The C
YV chiller had also been restarted, but tripped after running for 10
YV chiller had also been restarted, but tripped after running for 10
minutes.             Shortly thereafter, containment temperatures were restored to
minutes.
Shortly thereafter, containment temperatures were restored to
normal levels.
normal levels.
Operations surveillance procedure PT/1/A/4600/02A. Mode 1 Periodic
Operations surveillance procedure PT/1/A/4600/02A. Mode 1 Periodic
Surveillance Items. Enclosure-13.1. Periodic Surveillance Items Data,
Surveillance Items. Enclosure-13.1. Periodic Surveillance Items Data,
approved January 23, 1997, provides surveillance acceptance criteria in                                               -
approved January 23, 1997, provides surveillance acceptance criteria in
-
accordance with the lower containment temperature limits imposed by TS
accordance with the lower containment temperature limits imposed by TS
3.6.1.5. Lower containment minimum and maximum air temperature limits
3.6.1.5.
Lower containment minimum and maximum air temperature limits
are based on the average inlet temperatures of the operating LCVUs.
are based on the average inlet temperatures of the operating LCVUs.
Temperature readings associated with non running LCVUs provide
Temperature readings associated with non running LCVUs provide
indication of static air temperature and therefore, are not used to
indication of static air temperature and therefore, are not used to
determine average containment air temperature.                               Therefore. temperature
determine average containment air temperature.
Therefore. temperature
':mits are adjusted conservatively as a function of uncertainty (because
':mits are adjusted conservatively as a function of uncertainty (because
of the reduced sample size) in generalizing local indications to average
of the reduced sample size) in generalizing local indications to average
                                                                                          Enclosure 2
Enclosure 2
                                                                                                                      1
1
      ..-._..__ ,,
..-._..__ ,,
                  -
,a..
                              ,a..
._-..,....,--...--m.__-
                              -
-
                                    ._-..,....,--...--m.__-     -
- - _ _ - _ . . _ .
                                                                                    -      - - _ _ - _ . . _ . . .-m.
.
.-m.
-
-
-


                                  9
9
containment air temperature. As the number of LCVUs in service
containment air temperature. As the number of LCVUs in service
decreases, the temperature limit decreases (becomes more conservative).
decreases, the temperature limit decreases (becomes more conservative).
Line 618: Line 778:
described in the FSAR is designed to maintain a maximum
described in the FSAR is designed to maintain a maximum
temperature of 120*F in the lower compartment during rnrmal plant
temperature of 120*F in the lower compartment during rnrmal plant
operation. During normal operation, three units (each providing
operation.
During normal operation, three units (each providing
33.3% capacity) are in service, and one unit is on standby.
33.3% capacity) are in service, and one unit is on standby.
Technical Specification Interpretation 3.6.1.5 states that                   3
3
                                                                            !
Technical Specification Interpretation 3.6.1.5 states that
!
containment air temperature can be maintained with one active
containment air temperature can be maintained with one active
component out-of-service (i.e., three LCVUs in service).
component out-of-service (i.e., three LCVUs in service).
Based upon a review of the FSAR and TS as well as discussions
Based upon a review of the FSAR and TS as well as discussions
with on-shift operators, the inspector determined that the                   4
with on-shift operators, the inspector determined that the
4
decision to remove the D LCVU from service while preventive
decision to remove the D LCVU from service while preventive
maintenance (PM)s on the A LCVU were ongoing was non conservative
maintenance (PM)s on the A LCVU were ongoing was non conservative
Line 634: Line 797:
which controls the configuration of the LCVUs. The procedure did not
which controls the configuration of the LCVUs. The procedure did not
provide adequate guidance to address the impact of removing two LVCus
provide adequate guidance to address the impact of removing two LVCus
from service on lower containment temperature. Operations Management
from service on lower containment temperature.
Operations Management
Procedure 2-18. Tagout Removal and Restoration Procedure. Revision 46.
Procedure 2-18. Tagout Removal and Restoration Procedure. Revision 46.
Responsibility 4.8. states that the person placing or removing tag (s)
Responsibility 4.8. states that the person placing or removing tag (s)
shall check procedures affected and any outstanding tagouts associated
shall check procedures affected and any outstanding tagouts associated
with that procedure / system for any adverse effects. Because the adverse
with that procedure / system for any adverse effects.
Because the adverse
impact of removing 2 LCVUs from service was not addressed in the
impact of removing 2 LCVUs from service was not addressed in the
procedure, this responsibility could not be effectively realized.
procedure, this responsibility could not be effectively realized.
  n addition, procedure OP/2/A/6450/01 did not address the interaction
n addition, procedure OP/2/A/6450/01 did not address the interaction
between LCVU operation and integrated Containment Ventilation (VV)
between LCVU operation and integrated Containment Ventilation (VV)
Systems. Step 2.7.3 of OP/2/A/6450/01. Enclosure 4.12. LCVU Additional
Systems.
Step 2.7.3 of OP/2/A/6450/01. Enclosure 4.12. LCVU Additional
Cooling and YV Chiller Trip Prevention directs the operator to ensure
Cooling and YV Chiller Trip Prevention directs the operator to ensure
that three LCVUs are in the " NORM" position. The performance of this
that three LCVUs are in the " NORM" position. The performance of this
step caused the A and C YV chillers to trip. Procedure
step caused the A and C YV chillers to trip.
slowly reduce the demand on the system was not provided,       guidance
Procedure
                                                          nor was a     to
slowly reduce the demand on the system was not provided, guidance to
nor was a
precaution or note provided to warn of the potential to induce a chiller
precaution or note provided to warn of the potential to induce a chiller
trip as a function of load demand changes.
trip as a function of load demand changes.
Line 655: Line 822:
Enclosure 4.2. Lower Containment Ventilation Unit Startup and Normal
Enclosure 4.2. Lower Containment Ventilation Unit Startup and Normal
Operation, provided procedural guidance for starting up the system by
Operation, provided procedural guidance for starting up the system by
placing three LCVUs in operation. Enclosure 4.7. Lower Containment
placing three LCVUs in operation.
Enclosure 4.7. Lower Containment
Ventilation Unit Shutdown provides procedural guidance for shutdown of
Ventilation Unit Shutdown provides procedural guidance for shutdown of
the system by placing all four LCVU switches in the OFF position.
the system by placing all four LCVU switches in the OFF position.
                                                              Enclosure 2
Enclosure 2
                                                -
-


l
l
                                              10
10
          However, no procedural guidance existed for stopping an individual LCVU
However, no procedural guidance existed for stopping an individual LCVU
          and subsequently restarting it or making other required alignment
and subsequently restarting it or making other required alignment
          changes needed to facilitate the performance of the PM. The inspector
changes needed to facilitate the performance of the PM. The inspector
          recognized that this lack of procedural guidance was unrelated to the
recognized that this lack of procedural guidance was unrelated to the
lower co'itainment temperature increase and the YV chiller trips.
l
The inspector also identified a minor discrepancy in the planned
l
l
          lower co'itainment temperature increase and the YV chiller trips.
innage work schedule.
          The inspector also identified a minor discrepancy in the planned
The 2A LCVU had two work items planned to
l        innage work schedule.   The 2A LCVU had two work items planned to
be worked which included a PM and electrical motor testing.
          be worked which included a PM and electrical motor testing.     The
The
          PM on the 2A LCVU was scheduled to be completed at 12:00 p.m. on
PM on the 2A LCVU was scheduled to be completed at 12:00 p.m. on
          June 30, 1997. The motor electrical testing on the 2A LCVU was
June 30, 1997.
          scheduled to be completed at 1:00 p.m. on June 30. The PM on the
The motor electrical testing on the 2A LCVU was
          20 LCVU was scheduled to commence at 12:00 p.m. on June 30.
scheduled to be completed at 1:00 p.m. on June 30.
          immediately following the scheduled completion of the PM on the 2A
The PM on the
          LCVU.
20 LCVU was scheduled to commence at 12:00 p.m. on June 30.
                  This schedule allowed both the A and 0 LCVUs to be out of
immediately following the scheduled completion of the PM on the 2A
          service for 1 hour, which was non conservative and not in
LCVU.
          accordance with the alignment described in the FSAR.
This schedule allowed both the A and 0 LCVUs to be out of
    c.   Conclusions
service for 1 hour, which was non conservative and not in
          The inspector concluded that the decision to deviate from the
accordance with the alignment described in the FSAR.
          preferred normal alignment of LCVU operation to support planned
c.
          maintenance exhibited non conservative work scheduling and
Conclusions
          operator judgement. As a result. lower containment temperature
The inspector concluded that the decision to deviate from the
          increased slightly above the adjusted TS limit for a brief period
preferred normal alignment of LCVU operation to support planned
          of time. However, temperatures were reduced below the adjusted TS
maintenance exhibited non conservative work scheduling and
          limit within 8 hours as required by the TS action requirement.
operator judgement.
          Therefore, exceeding the lower containment air temperature on
As a result. lower containment temperature
          plant equipment had minor safety significance and did not pose a
increased slightly above the adjusted TS limit for a brief period
          threat to safety related equipment. The LCVU operating procedures
of time.
          did not address the adverse impact of removing two LCVUs from
However, temperatures were reduced below the adjusted TS
          service. simultaneously. nor did the procedure address the
limit within 8 hours as required by the TS action requirement.
          interaction between LCVU operation and integrated containment
Therefore, exceeding the lower containment air temperature on
          ventilation systems. These procedural inadequacies constituh a
plant equipment had minor safety significance and did not pose a
          violation of TS 6.8.1. Procedures and Programs. This failure
threat to safety related equipment. The LCVU operating procedures
          constitutes a violation of minor significance and is being treated
did not address the adverse impact of removing two LCVUs from
          as a NCV. consistent with Section IV of the NRC Enforcement
service. simultaneously. nor did the procedure address the
          Policy.   This item is identified as NCV 50-414/97-09-02:
interaction between LCVU operation and integrated containment
          Inadequate LCVU Operating Procedure.
ventilation systems. These procedural inadequacies constituh a
  08
violation of TS 6.8.1. Procedures and Programs. This failure
        ,
constitutes a violation of minor significance and is being treated
          Hiscellaneous Operations Issues (92901)
as a NCV. consistent with Section IV of the NRC Enforcement
  08.1   (Closed) Un.reigh.ed_Ltem (URI) 50-413.414/94-13-02: Emergency Operating
Policy.
          Procedure (EOP) 50.59 Evaluations Not Reviewed by Nuclear Safety Review
This item is identified as NCV 50-414/97-09-02:
          Board (NSRB) as Required by TS
Inadequate LCVU Operating Procedure.
          This item was related to an apparent failure to meet the TS requirement
08
          for the NSRB to review 50.59 evaluations for E0P changes. The
Hiscellaneous Operations Issues (92901)
          inspector's review determined that the re
,
          being appropriately reviewed by the NSRBThe  quired 50.59 evaluations
08.1
                                                            licensee's             were
(Closed) Un.reigh.ed_Ltem (URI) 50-413.414/94-13-02:
                                                                      procedures had
Emergency Operating
                                                                          Enclosure 2
Procedure (EOP) 50.59 Evaluations Not Reviewed by Nuclear Safety Review
Board (NSRB) as Required by TS
This item was related to an apparent failure to meet the TS requirement
for the NSRB to review 50.59 evaluations for E0P changes. The
inspector's review determined that the re
being appropriately reviewed by the NSRB quired 50.59 evaluations were
The licensee's procedures had
Enclosure 2


  __-_______ __-_ - _ _ - .
__-_______ __-_ - _ _ - .
                                                      11
11
  been inconsistent in defining the 10 CFR 50.59 screening evaluation and
been inconsistent in defining the 10 CFR 50.59 screening evaluation and
  the 10 CFR 50.59 Unreviewed aafety Question (US0) evaluation. The TS
the 10 CFR 50.59 Unreviewed aafety Question (US0) evaluation. The TS
  requirement was intended for the NSRB to review the 10 CFR 50.59 U50
requirement was intended for the NSRB to review the 10 CFR 50.59 U50
  evaluations. Nuclear Site Procedure NS0-209, 10 CFR 50.59 Evaluations.
evaluations. Nuclear Site Procedure NS0-209, 10 CFR 50.59 Evaluations.
  Revision 6. was revised after 1994 to clearly define the two
Revision 6. was revised after 1994 to clearly define the two
  evaluations. The licensee initiated a change to NSD 703. Administrative
evaluations. The licensee initiated a change to NSD 703. Administrative
  Instruction for Station Procedures, to clearly distinguish on the
Instruction for Station Procedures, to clearly distinguish on the
  procedure change process documentation whether the evaluation performed
procedure change process documentation whether the evaluation performed
  was a screening evaluation or an USQ evaluation. The inspector reviewed
was a screening evaluation or an USQ evaluation. The inspector reviewed
three US0 evaluations for E0P changes and verified the US0 evaluation
,
,
' three US0 evaluations for E0P changes and verified the US0 evaluation
'
had been sent to the NSRB_for review. A 1995 evaluation had been
i
i
  had been sent to the NSRB_for review. A 1995 evaluation had been
reviewed and two 1997 evaluations were scheduled for review at the next
  reviewed and two 1997 evaluations were scheduled for review at the next
  NSRB meeting. The inspector concluded that this issue was adequately
;
;
  resolved and the TS requirements had been met by the licensee.
NSRB meeting.
  During the invettigation of the above issue, the inspector reviewed
The inspector concluded that this issue was adequately
  a) proximately 20 examp',cs of 10 CFR 50.59 screening evaluations for E0P
resolved and the TS requirements had been met by the licensee.
  c1anges and identified a deficiency in the licensee's procedure
During the invettigation of the above issue, the inspector reviewed
  implementation of this activity. Specifically, the justifications for
a) proximately 20 examp',cs of 10 CFR 50.59 screening evaluations for E0P
  the screening questions were inadequate in many changes.                     The
c1anges and identified a deficiency in the licensee's procedure
  justifications were inadequate in that they only repeated the screening
implementation of this activity.
  question as a negative statement. NSD 209, 10 CFR 50.59 Evaluations.
Specifically, the justifications for
  Revision 5. required the doca,3ntation of justification for responses to
the screening questions were inadequate in many changes.
  50.59 screening questions. It further stated that justifications should
The
  be complete enough so that an independent reviewer cculd come to the
justifications were inadequate in that they only repeated the screening
  same conclusion. The following E0P change 50.59 screening evaluations
question as a negative statement. NSD 209, 10 CFR 50.59 Evaluations.
  were inadequate and did not meet the applicable procedure requirements:
Revision 5. required the doca,3ntation of justification for responses to
  o                         EP/2/A/5000/FR 1.2 dated November 17, 1995
50.59 screening questions.
  e                          EP/1/A/5000/FR-1.1 dated September 19. 1996
It further stated that justifications should
  *                         OF/1/A/6350/08 dated February 28. 1996
be complete enough so that an independent reviewer cculd come to the
  e                          EP/2/A/5000/F-0 dated March 26, 1997
same conclusion.
  e                         EP/1/A/5000/FR H.1 dated August 16, 1996
The following E0P change 50.59 screening evaluations
  *                          EP/1/A/5000/FR-H.1 dated January 30, 1995
were inadequate and did not meet the applicable procedure requirements:
  This failure to follow NSD 209 for 10 CFR 50.59 screening evaluations,
o
  is identified as the first example of Violation (VIO) 50 413.414/9/-09-
EP/2/A/5000/FR 1.2 dated November 17, 1995
  04:                       Failure to Follow Procedure. The inspector did not identify any
EP/1/A/5000/FR-1.1 dated September 19. 1996
  US0 condition related to the inadequate 50.59 screening evaluations.
e
  The inspector noted that the 50.59 screening evaluations for E0P changes
*
  were performed by the Operations organization. Previous inspections of
OF/1/A/6350/08 dated February 28. 1996
  50.59 evaluation performance have concluded that the Engineering
EP/2/A/5000/F-0 dated March 26, 1997
  organization performed to a high standard in this area for 50.59
e
  evaluations related to modifications. Although both organizations
EP/1/A/5000/FR H.1 dated August 16, 1996
                                                                                  Enclosure 2
e
EP/1/A/5000/FR-H.1 dated January 30, 1995
*
This failure to follow NSD 209 for 10 CFR 50.59 screening evaluations,
is identified as the first example of Violation (VIO) 50 413.414/9/-09-
04:
Failure to Follow Procedure. The inspector did not identify any
US0 condition related to the inadequate 50.59 screening evaluations.
The inspector noted that the 50.59 screening evaluations for E0P changes
were performed by the Operations organization.
Previous inspections of
50.59 evaluation performance have concluded that the Engineering
organization performed to a high standard in this area for 50.59
evaluations related to modifications.
Although both organizations
Enclosure 2


                                          12
12
        receive the same training and use the same procedures. Operation's
receive the same training and use the same procedures. Operation's
        performance in this activity was deficient as previously noted. The
performance in this activity was deficient as previously noted. The
        inspector reviewed a 1997 50.59 USO evaluation for an E0P change.   This
inspector reviewed a 1997 50.59 USO evaluation for an E0P change.
        evaluation was good in that it included a well detailed justification
This
        for responses to the USQ evaluation questions. This indicated that the
evaluation was good in that it included a well detailed justification
for responses to the USQ evaluation questions.
This indicated that the
>
>
        Operations deficient performance was related only to the 50.59 screening
Operations deficient performance was related only to the 50.59 screening
        evaluations.
evaluations.
                                    II. Maintenance
II. Maintenance
l
l
  M1   Conduct of Maintenance
M1
Conduct of Maintenance
1
1
  M1.1 Electrical Flash Durinn Breaker Preventive Maintem nte
M1.1 Electrical Flash Durinn Breaker Preventive Maintem nte
    a. Inspection Stone (62707)
a.
        The inspector reviewed the circumstances and the licensee's corrective
Inspection Stone (62707)
        actions associated with an electrical flash that occurred inside a 600
The inspector reviewed the circumstances and the licensee's corrective
        Volt non safety-related breaker cubicle while periodic breaker PM was
actions associated with an electrical flash that occurred inside a 600
        being performed. The electrical flash resulted in a minor personnel
Volt non safety-related breaker cubicle while periodic breaker PM was
        injury and extensive damage to the breaker cubicle.
being performed. The electrical flash resulted in a minor personnel
    b. Observations and Findinas
injury and extensive damage to the breaker cubicle.
        On June 3. 1997, an Instrumentation and Electrical (IAE) technician was
b.
        aerforming PM on 600 Volt breakers 2MXM-F09C and 2MXM-F090.   These
Observations and Findinas
        areakers supplied power to two Unit 2 ice condenser refrigeration air
On June 3. 1997, an Instrumentation and Electrical (IAE) technician was
        handling fans. The PM activity involved testing the overcurrent
aerforming PM on 600 Volt breakers 2MXM-F09C and 2MXM-F090.
        protective devices associated with the breakers. The technician had
These
        removed breaker F09C from its cubicle and was in the process of removing
areakers supplied power to two Unit 2 ice condenser refrigeration air
        breaker F090 from its cubicle. While removing F090, an electrical ficsh
handling fans. The PM activity involved testing the overcurrent
        occurred in the F09C cubicle, which was located directly above F09D.
protective devices associated with the breakers.
        The technician received minor facial burns. but was not seriously
The technician had
        injured. Breaker F09C was electrically welded in its cubicle as a
removed breaker F09C from its cubicle and was in the process of removing
        result of the electrical fault, The inspector responded to the breaker
breaker F090 from its cubicle. While removing F090, an electrical ficsh
        work location and noted good licensee immediate actions in response to
occurred in the F09C cubicle, which was located directly above F09D.
        the incident. These actions included terminati'     11 PM work, roping
The technician received minor facial burns. but was not seriously
        off the area for personnel safety consideratior . nd initiating a
injured.
        Failure Investigative Process (FIP) to determine the root cause of the
Breaker F09C was electrically welded in its cubicle as a
        electrical fav a.
result of the electrical fault,
        On June 6, 1997. Motor Control Center 2MXM was de energized, and the
The inspector responded to the breaker
        breaker cubicle for F09C inspected. The damage to the bus was minimal;
work location and noted good licensee immediate actions in response to
        however, the stabs for F09C were badly damaged and recuired replacement.
the incident. These actions included terminati'
        Both breakers F09C and F09D were repaired, tested, anc returned to
11 PM work, roping
        service. The inspector attended the PORC meeting conducted to discuss
off the area for personnel safety consideratior .
        the repair plans and noted that management performed a thorough review
nd initiating a
        of the plans with good discussions on the impact of the work planned on
Failure Investigative Process (FIP) to determine the root cause of the
        the plant. The repairs were completed without incident.
electrical fav a.
                                                                      Enclosure 2
On June 6, 1997. Motor Control Center 2MXM was de energized, and the
breaker cubicle for F09C inspected.
The damage to the bus was minimal;
however, the stabs for F09C were badly damaged and recuired replacement.
Both breakers F09C and F09D were repaired, tested, anc returned to
service.
The inspector attended the PORC meeting conducted to discuss
the repair plans and noted that management performed a thorough review
of the plans with good discussions on the impact of the work planned on
the plant. The repairs were completed without incident.
Enclosure 2


  _____               -
_____
                                                13
-
              The FlP team was thorough in their investigations and determined that
13
              the stabs b? hind breaker F09C had come in contact with the energized
The FlP team was thorough in their investigations and determined that
              bus.   Since the breaker power connecting cables had been determed and
the stabs b? hind breaker F09C had come in contact with the energized
              left untaped in the bottom of the breaker cubicle. an electrical ground
bus.
              path was created when the cables were re energized. The FIP determined
Since the breaker power connecting cables had been determed and
              the method for racking the breaker out in the maintenance position was
left untaped in the bottom of the breaker cubicle. an electrical ground
              inadequate.   In the maintenance position a lock tab on the front of the
path was created when the cables were re energized. The FIP determined
              breaker cubicle had been used to position the breaker away from the bus;
the method for racking the breaker out in the maintenance position was
l             however this method did not provide sufficient distance between the bus
inadequate.
              and stabs. While this method had not resulted in any problems in the
In the maintenance position a lock tab on the front of the
              past, the result of having two breakers in the maintenance position,
breaker cubicle had been used to position the breaker away from the bus;
              located one above the other, created an even smaller bus / stab distance
l
              that resulted in electrical flash over.
however this method did not provide sufficient distance between the bus
              As a result of the FlP investigations, instrumentation procedures
and stabs. While this method had not resulted in any problems in the
              governing work on 600 Volt breakers were revised to change the method of
past, the result of having two breakers in the maintenance position,
              racking out these breakers for maintenance. Instead of using the lock
located one above the other, created an even smaller bus / stab distance
              tab, procedures directed that a padlock be placed on the breaker or the
that resulted in electrical flash over.
              bteaker be removed completely to ensure adequate stab / bus distance is
As a result of the FlP investigations, instrumentation procedures
              maintained. In addition, IAE personnel involved with breaker work were
governing work on 600 Volt breakers were revised to change the method of
              to be provided training on this new method of racking 600 Volt breakers
racking out these breakers for maintenance.
              out to the maintenance position.
Instead of using the lock
        c.   Conclusions
tab, procedures directed that a padlock be placed on the breaker or the
              The inspector concluded that the FlP team was thorough in investigating
bteaker be removed completely to ensure adequate stab / bus distance is
              the cause of the electrical flash. The root cause evaluation revealed
maintained.
              configuration weaknesses in the method of locking out 600 Volt breaker
In addition, IAE personnel involved with breaker work were
              cubicles to the maintenance position. The inspector determined that the
to be provided training on this new method of racking 600 Volt breakers
              licensee adecuately implemented corrective actions to prevent recurrence
out to the maintenance position.
              of this incicent.
c.
        M1.2 'Jngdeounte Leak Rate lest of Unit 2 Containment Isolation Valve
Conclusions
        a,   insoection Scope (40500. 61726. 62707)
The inspector concluded that the FlP team was thorough in investigating
              On June 4,1997, the licensee identified that Unit 2 containment
the cause of the electrical flash.
              isolation valve 2NV 874 had not been properly Type C leak rate tested in
The root cause evaluation revealed
              accordance with 10 CFR 50. Appendix J during the previous. refueling
configuration weaknesses in the method of locking out 600 Volt breaker
              outage. On June 6. the valve was properly tested and failed the Type C
cubicles to the maintenance position. The inspector determined that the
              leak rate test. -The valve disc was replaced, and the valve was
licensee adecuately implemented corrective actions to prevent recurrence
              successfully tested on June 7. The licensee submitted LER 50 414/97-004
of this incicent.
            . to document the inadecuate leak cate test conducted during the outage.
M1.2 'Jngdeounte Leak Rate lest of Unit 2 Containment Isolation Valve
              The inspector reviewec the circumstances associated with the inadequate
a,
              testing, attended PORC meetings to discuss retesting valve 2NV-874
insoection Scope (40500. 61726. 62707)
              online, witnessed aspects of the June 6 retest, reviewed leak rate test
On June 4,1997, the licensee identified that Unit 2 containment
              results, and discussed the incident with engineering and Operations Test
isolation valve 2NV 874 had not been properly Type C leak rate tested in
              Group (OTG) personnel,
accordance with 10 CFR 50. Appendix J during the previous. refueling
                                                                            Enclosure 2
outage.
                                                                  _           -
On June 6. the valve was properly tested and failed the Type C
leak rate test. -The valve disc was replaced, and the valve was
successfully tested on June 7.
The licensee submitted LER 50 414/97-004
. to document the inadecuate leak cate test conducted during the outage.
The inspector reviewec the circumstances associated with the inadequate
testing, attended PORC meetings to discuss retesting valve 2NV-874
online, witnessed aspects of the June 6 retest, reviewed leak rate test
results, and discussed the incident with engineering and Operations Test
Group (OTG) personnel,
Enclosure 2
_
-


i
i
                                      14
14
  b. Observations and Findinas
b.
    On &ne 4.1997 the OTG Suaervisor was conducting a procedure
Observations and Findinas
    completion verification of Jnit 2 Periodic Test (PT) procedure
On &ne 4.1997 the OTG Suaervisor was conducting a procedure
    PT/2/A/4200/01C. Containment Isolation Valve t.eak Rate Test. This
completion verification of Jnit 2 Periodic Test (PT) procedure
    procedure had been performed during the previous refueling outage in
PT/2/A/4200/01C. Containment Isolation Valve t.eak Rate Test.
This
procedure had been performed during the previous refueling outage in
1
1
    April 1997. During the review, the supervisor idcntified that Step
April 1997. During the review, the supervisor idcntified that Step
    2.2.3 of Enclosure 13.7. Penetration No. M228 Type C 1.eak Rate Test had
2.2.3 of Enclosure 13.7. Penetration No. M228 Type C 1.eak Rate Test had
    been marked "Not Applicable'' by the OTG technician performing the test.
been marked "Not Applicable'' by the OTG technician performing the test.
                                                                                ,
I
                                                                                I
,
    resulting in the step not being performed. This step required test vent     I
resulting in the step not being performed. This step required test vent
    flow path valve 2NV 873 to be opened while testing inside containment
I
    isolation check valve 2NV 874 (associated with the Standby Makeup System   '
flow path valve 2NV 873 to be opened while testing inside containment
    flowpath to the reactor coolant pump seals). Without an open test vent
isolation check valve 2NV 874 (associated with the Standby Makeup System
    flowpath, the leak rate test on 2NV 874 had been invalid.
'
    The inspector verified that appropriate actions were implemented upon
flowpath to the reactor coolant pump seals). Without an open test vent
    identification of the invalid lea ( rate test. These actions included
flowpath, the leak rate test on 2NV 874 had been invalid.
    2NV 874 being declared inoperable and in accordance with TS 3.6.3, the
The inspector verified that appropriate actions were implemented upon
    outboard containment isolation valve (2NV 872A) in the penetration was
identification of the invalid lea ( rate test. These actions included
    closed and power was removed from the valve operator within four hours.
2NV 874 being declared inoperable and in accordance with TS 3.6.3,
    The inspector attended the June 5 and 6 PORC meetings conducted to
the
    discuss activities to retest 2NV-874. Management thoroughly discussed
outboard containment isolation valve (2NV 872A) in the penetration was
    the impact on the plant with testing the valve while online. In
closed and power was removed from the valve operator within four hours.
    addition engineering developed a special leak rate test procedure and a
The inspector attended the June 5 and 6 PORC meetings conducted to
    detailed briefing package explaining the necessary actions for
discuss activities to retest 2NV-874.
    controlling the retest activities.
Management thoroughly discussed
    On June 6. the inspector witnessed aspects of the leak rate test on 2NV-
the impact on the plant with testing the valve while online.
    874. The inspector noted that testing was well controll?d and performed
In
    in accordance with the test procedure.- The valve was not able to be-
addition engineering developed a special leak rate test procedure and a
    pressurized and resulted in-a failed leak rate test. Valve maintenance
detailed briefing package explaining the necessary actions for
    was performed resulting in replacement of the valve disc and disc
controlling the retest activities.
    spring. A subsequent leak rate test was performed following the
On June 6. the inspector witnessed aspects of the leak rate test on 2NV-
    maintenance activity. The inspector reviewed the results of this
874. The inspector noted that testing was well controll?d and performed
    testing which verified that leakage was within acceptable limits.
in accordance with the test procedure.- The valve was not able to be-
    Following successful testing 2NV 874 was declared operable and the
pressurized and resulted in-a failed leak rate test.
    penetration was returned to its normal configuration,
Valve maintenance
  c.   n
was performed resulting in replacement of the valve disc and disc
    C_Qn.clusions
spring. A subsequent leak rate test was performed following the
    The inspector concluded the identification by the OTG Supervisor of a
maintenance activity.
    procedure discrepancy that resulted in an invalid leak rate test of nD-
The inspector reviewed the results of this
    874 was an example of good questioning attitude. The PORN performed a
testing which verified that leakage was within acceptable limits.
    thorough review of subsequent activities to properly perform the leak
Following successful testing 2NV 874 was declared operable and the
    rate test. Good engineering support was )rovided, both in developing a
penetration was returned to its normal configuration,
    leak rate test procedure and briefing paccage for the evolution.
C_Qn.clusions
    The inspector noted that the procedure completion review was not
c.
    performed by the OTG Supervisor following actual completion of all
n
    testing or prior to plant startup from the refueling outage. Since this
The inspector concluded the identification by the OTG Supervisor of a
                                                                  Enclosure 2
procedure discrepancy that resulted in an invalid leak rate test of nD-
            _ _ _ _
874 was an example of good questioning attitude. The PORN performed a
                                                                              -
thorough review of subsequent activities to properly perform the leak
rate test. Good engineering support was )rovided, both in developing a
leak rate test procedure and briefing paccage for the evolution.
The inspector noted that the procedure completion review was not
performed by the OTG Supervisor following actual completion of all
testing or prior to plant startup from the refueling outage.
Since this
Enclosure 2
_ _ _ _
-


  . . - _ .     __-         --_           ---           - -             -   - - . . - - _-                   _.
. . - _ .
                                                      15
__-
l                   was the only review that was recuired following test procedure
--_
                    completion, the inspector consicered the review untimely. Had this
---
                    review been completed prior to plant startup, this problem may have been
- -
                    identified and corrected arior to the unit entering a mode recuiring
-
                    containment integrity. T1e failure to open test vent valve 2hV-873
- - . . - - _-
                    during/4200/01C
_.
                    PT/2/A              was identified as a violation of TS 6.8.1.           leak
15
                                                                                          This    rate testing of
l
                                                                                                issue
was the only review that was recuired following test procedure
                    is identified as Violation E0-414/97-09 03: Failure to Follow Procedure
completion, the inspector consicered the review untimely.
                    Results in Invalid Local Leak Rate Test of Valve 2NV 874.
Had this
            M8     Miscellaneous Maintenance Issues (92902.
review been completed prior to plant startup, this problem may have been
l           M8.1 (Closed) VIO 50 413. 414/97-01-01: Failure to Include all Structures.
identified and corrected arior to the unit entering a mode recuiring
                    S stems and Components in the Scope of the Maintenance Rule as Required
containment integrity.
                    b 10 CFR 50.65
T1e failure to open test vent valve 2hV-873
                    This violation was identified when the inspectors determined that the
during/4200/01C was identified as a violation of TS 6.8.1. leak rate testing of  
                    licensee had incorrectly excluded a number of structures. systems and
PT/2/A
                    components from the scope of the Maintenance Rule. The licensee
This issue
                    acknowledged the violation and issued a Problem Investigation Process
is identified as Violation E0-414/97-09 03:
;                  (PIP) report PIP No. 0 C97-0419. to document correctivo actions taken
Failure to Follow Procedure
!                   and, track the progress made in addressing the issues. The systems
Results in Invalid Local Leak Rate Test of Valve 2NV 874.
                    affected included Nuclear Sampling (NM). Main Steam to Auxiliary
M8
                    Equi) ment (SA). Auxiliary Building Chilled Water (YN) and Ice Condenser
Miscellaneous Maintenance Issues (92902.
l
M8.1 (Closed) VIO 50 413. 414/97-01-01: Failure to Include all Structures.
S stems and Components in the Scope of the Maintenance Rule as Required
b 10 CFR 50.65
This violation was identified when the inspectors determined that the
licensee had incorrectly excluded a number of structures. systems and
components from the scope of the Maintenance Rule.
The licensee
acknowledged the violation and issued a Problem Investigation Process
(PIP) report PIP No. 0 C97-0419. to document correctivo actions taken
;
!
and, track the progress made in addressing the issues.
The systems
affected included Nuclear Sampling (NM). Main Steam to Auxiliary
Equi) ment (SA). Auxiliary Building Chilled Water (YN) and Ice Condenser
l
l
Hitti Pins (NF).
Following a review by the site Expert Panel these
'
'
                    Hitti Pins (NF). Following a review by the site Expert Panel these
systems or components were added to the scope of the Maintenance Rule.
                    systems or components were added to the scope of the Maintenance Rule.
Corrective actions taken or planned included a review of the 239
                    Corrective actions taken or planned included a review of the 239
functions that had been excluded from the Maintenance Rule scope. This
'
'
                    functions that had been excluded from the Maintenance Rule scope. This
review was scheduled for completion in December 1997.- and will be
                    review was scheduled for completion in December 1997.- and will be
documented in PIP No. 0-C97-0419,
                    documented in PIP No. 0-C97-0419, In addition, structures and functions
In addition, structures and functions
                    excluded from the Maintenance Rule will be reviewed for Generic Scoping
excluded from the Maintenance Rule will be reviewed for Generic Scoping
                    applicability. The due date for this review is also December 1997. The
applicability. The due date for this review is also December 1997. The
                    inspectors concluded the licensee's corrective actions were appropriate.
inspectors concluded the licensee's corrective actions were appropriate.
,
,
            M8.2. (Closed V10 50-413.414/97 01-04: Failure to implement the Requirements
M8.2. (Closed V10 50-413.414/97 01-04: Failure to implement the Requirements
                    of (a)(1) and (a)(2) of the Maintenance Rule
of (a)(1) and (a)(2) of the Maintenance Rule
l                   This violation was identified when the inspectors determined that the
l
l                   licensee was using Forced Outage Rate (FOR) instead of Unplanned
This violation was identified when the inspectors determined that the
l                  Capability loss Factor (UCLF) as a Plant Level Performance Criteria for
l
'                  monitoring A2 systs....; 3er 10 CFR 50.65. The concern was that FOR was
licensee was using Forced Outage Rate (FOR) instead of Unplanned
                    not as sensitive as UC F in detecting declining performance in some
                    systems.
                    The licensee acknowledged the violation and took appropriate action to
                    correct the problem. The licensee incorporated the Plant Transient
                    Criteria as part of the Forced Outage Criteria. This combination of
                    criteria was intended to provide appropriate equivalent defense in depth
                    monitoring as the Unplanned Capability Loss Factor. A Plant level
                                                                                          Enclosure 2
l
l
                                                      ._                               -       --       -
Capability loss Factor (UCLF) as a Plant Level Performance Criteria for
!
monitoring A2 systs....; 3er 10 CFR 50.65. The concern was that FOR was
'
not as sensitive as UC F in detecting declining performance in some
systems.
The licensee acknowledged the violation and took appropriate action to
correct the problem.
The licensee incorporated the Plant Transient
Criteria as part of the Forced Outage Criteria. This combination of
criteria was intended to provide appropriate equivalent defense in depth
monitoring as the Unplanned Capability Loss Factor. A Plant level
Enclosure 2
l
.
-
..
._
.
--
-
--
-


                                                                                          1
1
;
;
                                              16
16
l
l
            Performance Criteria called Plant Transients, which defined unacceptable
Performance Criteria called Plant Transients, which defined unacceptable
            performance was added to Engineering Directives Manual (EDM)-210 as Rev.
performance was added to Engineering Directives Manual (EDM)-210 as Rev.
i
i
4.
The inspectors concluded the licensee's corrective actions were
'
appropriate.
M8.3 (Closed) Insoector Followuo item (IFI) 50 413.414/97-01-02: Followup and
'
'
            4.    The inspectors concluded the licensee's corrective actions were
Review of Licensee Procedure to implement the Requirements of (a)(1) and
            appropriate.                                                                  l
(a)(2) of the Maintenance Rule after issuance of Regulatory Guide 1.160,
                                                                                          I
Rev.2
      M8.3 (Closed) Insoector Followuo item (IFI) 50 413.414/97-01-02: Followup and
EDM-210." Requirements for Monitoring the Effectiveness of Maintenance
                                                                                          '
            Review of Licensee Procedure to implement the Requirements of (a)(1) and
            (a)(2) of the Maintenance Rule after issuance of Regulatory Guide 1.160,
            Rev.2
i
i
            EDM-210." Requirements for Monitoring the Effectiveness of Maintenance
at Nuclear Power Plants or the Maintenance Rule " Rev. 5.
            at Nuclear Power Plants or the Maintenance Rule " Rev. 5. revised the
revised the
            definition of Maintenance such that it was now in agreement with
definition of Maintenance such that it was now in agreement with
            Regulatory Guide 1.160. Rev. 2, dated March 1997. Revision 5 of the EDM
Regulatory Guide 1.160. Rev. 2, dated March 1997.
            now considers any operator action performed in support of Maintenance as
Revision 5 of the EDM
            a Maintenance Preventable Function Failure (MPff) candidate. In
now considers any operator action performed in support of Maintenance as
            addition, the flow gra)h of Appendix A to the subject EDM, were revised
a Maintenance Preventable Function Failure (MPff) candidate.
            for clarity. One of tie two was revised from Vendor Error to Off-site
In
            Vendor Services while the other from Operations or Plant configuration
addition, the flow gra)h of Appendix A to the subject EDM, were revised
            control to Operation or Plant Configuration Control not associated with
for clarity.
            a maintenance activity. The inspectors concluded the licensee's
One of tie two was revised from Vendor Error to Off-site
Vendor Services while the other from Operations or Plant configuration
control to Operation or Plant Configuration Control not associated with
a maintenance activity.
The inspectors concluded the licensee's
i
i
            corrective actions were appropriate.
corrective actions were appropriate.
      M8.4 (Closed) IFT 50-413.414/97-OL-01 Followup on Licensee Actions to
M8.4 (Closed) IFT 50-413.414/97-OL-01 Followup on Licensee Actions to
            Provide Performance Criteria for Structures After Resolution of this
Provide Performance Criteria for Structures After Resolution of this
            Issue
Issue
            EDM-210. " Requirements for Monitoring the Effectiveness of Maintenance
EDM-210. " Requirements for Monitoring the Effectiveness of Maintenance
:           at Nuclear Power Plants or the Maintenance Rule." Rev. 5. changed the
:
            3erformance criteria for all Maintenance Rule structures to comply with
at Nuclear Power Plants or the Maintenance Rule." Rev. 5. changed the
            legulatory Guide 1.160. Rev. 2. This criteria applies to both risk and
3erformance criteria for all Maintenance Rule structures to comply with
            non-risk significant Maintenance Rule structures.
legulatory Guide 1.160. Rev. 2.
            EDM 410. " Ins)ection Program for Civil Engineering Structures and
This criteria applies to both risk and
            Components." Rev. 1. dated June 16, 1997, is the controlling document
non-risk significant Maintenance Rule structures.
            for monitoring and assessing civil engineering structures and' components
EDM 410. " Ins)ection Program for Civil Engineering Structures and
            to the requirements of 10 CFR 50.65 and Regulatory Guide 1.160,.Rev. 2.
Components." Rev. 1. dated June 16, 1997, is the controlling document
            dated March 1997. It provides examination guidelines, acceptance
for monitoring and assessing civil engineering structures and' components
            criteria and documentation requirements. As such. Catawba civil
to the requirements of 10 CFR 50.65 and Regulatory Guide 1.160,.Rev. 2.
dated March 1997. It provides examination guidelines, acceptance
criteria and documentation requirements.
As such. Catawba civil
,
,
            engineering was responsible for implementing the ins)ection program for
engineering was responsible for implementing the ins)ection program for
l           structures and components. The inspectors reviewed EDM-410. Rev. 1 for
l
            content and adequacy. The inspectors noted that the procedure provided
structures and components.
            adequate guidelines and the acceptance criteria contained within,
The inspectors reviewed EDM-410. Rev. 1 for
            followed Regulatory Guide 1.160. Rev. 2 guidelines for acceptable and
content and adequacy.
.           unacceptable performance criteria.
The inspectors noted that the procedure provided
adequate guidelines and the acceptance criteria contained within,
followed Regulatory Guide 1.160. Rev. 2 guidelines for acceptable and
.
unacceptable performance criteria.
l
l
l
l          Through discussions and document review, the inspectors ascertained that
Through discussions and document review, the inspectors ascertained that
            the inspection program for structures was adequately administered and
the inspection program for structures was adequately administered and
            implemented. Responsible engineers had received training and were
implemented.
            familiar with Maintenance Rule requirements as they applied to their
Responsible engineers had received training and were
            area of responsibility.
familiar with Maintenance Rule requirements as they applied to their
area of responsibility.
5
5
                                                                          Enclosure 2
Enclosure 2
L ___ _--       _ . _ _      _.         .. . _ __..     _   _ _        _  __   , /
L
___
_--
.
.
..
.
..
_
_
__
,
/


_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _                                                 __               - _ __               _________
_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _
                                                                                      17
__
                                                  At the close of this inspection. 39 structures had been inspected and an
- _ __
                                                  additional 120 were scheduled for inspection by year's end. Ins)ection
_ _ _ _ _ _ _ _ _
                                                  per the revised EDMs -210 and -410 commenced on July 1, 1997.                 T1e
17
                                                  inspectors reviewed the licensee's classroom training material. ES-CN-
At the close of this inspection. 39 structures had been inspected and an
                                                  97-21. used to cormiunicate Regulatory Guide 1.160. Rev. 2 guidelines.
additional 120 were scheduled for inspection by year's end.
                                                  Training of personnel was held between June 9 and 18. 1997. The
Ins)ection
                                                  inspectors concluded the licensee's corrective actions were ap]ropriate.
per the revised EDMs -210 and -410 commenced on July 1, 1997.
                                                                              III. Enaineerina
T1e
                                          El     Conduct of Engineering
inspectors reviewed the licensee's classroom training material. ES-CN-
                                          El.1 Primary and Secondary Thermal Power DiscreDancy
97-21. used to cormiunicate Regulatory Guide 1.160. Rev. 2 guidelines.
                                            a. -Insoection Stone (37551)
Training of personnel was held between June 9 and 18. 1997.
                                                  On July 15 the licensee discovered a discrepancy of approximately 0.6%
The
                                                  between the Unit 2 primary and secondary thermal power indications.
inspectors concluded the licensee's corrective actions were ap]ropriate.
                                                  Secondary thermal
III. Enaineerina
                                                  was reduced to 99.7%)power
El
                                                                          andwas  immediately
Conduct of Engineering
                                                                                a FIP  team was reduced
El.1 Primary and Secondary Thermal Power DiscreDancy
                                                                                                    initiated to   to determine
a. -Insoection Stone (37551)
                                                                                                                      99.3% (reactor
On July 15 the licensee discovered a discrepancy of approximately 0.6%
                                                                                                                                  the power
between the Unit 2 primary and secondary thermal power indications.
                                                  cause of the discreaancy. The inspector attended management briefings
Secondary thermal
                                                  by the FIP team mem)ers on the progress of their investigation: reviewed
was reduced to 99. power was immediately reduced to 99.3% (reactor power
                                                  associated TS and TS Interpretations: and discussed the issue with
7%) and a FIP team was initiated to determine the
                                                  Operations. Engineering and Maintenance personnel.
cause of the discreaancy. The inspector attended management briefings
                                            b.   Observations and Findinas
by the FIP team mem)ers on the progress of their investigation: reviewed
                                                  On July 15. Operations personnel were notified by the reactor
associated TS and TS Interpretations: and discussed the issue with
                                                  engineering group that there was a 0.6% discrepancy between primary and
Operations. Engineering and Maintenance personnel.
                                                  secondary thermal power indications, and that actual thermal Jower might
b.
                                                  be greater than the secondary thermal power (the designated tiermal
Observations and Findinas
                                                  power best estimate) indication. The reactor engineering group
On July 15. Operations personnel were notified by the reactor
                                                  discovered, during a routine review of secondary plant parameters, that
engineering group that there was a 0.6% discrepancy between primary and
                                                  primary thermal power had slowly increased over time since the Unit 2
secondary thermal power indications, and that actual thermal Jower might
                                                  restart from the April 1997 refueling outage. A FIP team was initiated
be greater than the secondary thermal power (the designated tiermal
                                                  to determine the cause of the discrepancy, and control room operators
power best estimate) indication. The reactor engineering group
                                                  decreased reactor aower to 99.3%. Tae reactor was operated at 99.3%
discovered, during a routine review of secondary plant parameters, that
                                                  power until the FI) team could determine the cause of the discrepancy.
primary thermal power had slowly increased over time since the Unit 2
                                                  The FIP team determined, during the course of their investigation, that
restart from the April 1997 refueling outage.
                                                  theT,Yto586.9F.
A FIP team was initiated
                                                  587.3              indication had responded
to determine the cause of the discrepancy, and control room operators
                                                                        Operations  been drifting   downward T,,,
decreased reactor aower to 99.3%. Tae reactor was operated at 99.3%
                                                                                                by decreasing            since May 11, 1997, from
power until the FI) team could determine the cause of the discrepancy.
                                                                                                                            to minimize
The FIP team determined, during the course of their investigation, that
                                                  the T * /T error. Lowering T,,, caused the reactor to increase AT to
theT,Yto586.9F. indication had been drifting downward since May 11, 1997, from
                                                  maint'aIn,r,,actorpowerequaltosecondarypower.
587.3
                                                            e                                                    The drift in the T,,,
Operations responded by decreasing T,,, to minimize
                                                  indication resulted in changes in T       Tm T,,, and AT but did not
the T * /T
                                                  cause a change in indicated or actud3 primary and secondary thermal
error.
                                                  power. Although the FIP team could not attribute this indication drift
Lowering T,,, caused the reactor to increase AT to
                                                  to the primary / secondary thermal power indication discrepancy they
maint'aIn,r,,actorpowerequaltosecondarypower. The drift in the T,,,
                                                  determined that a degraded 7300 process card was responsible for the
e
                                                                                                                              Enclosure 2
indication resulted in changes in T
                                                                                                _.               .   -                   . - . . _ .
Tm
T,,, and AT but did not
cause a change in indicated or actud3 primary and secondary thermal
power.
Although the FIP team could not attribute this indication drift
to the primary / secondary thermal power indication discrepancy they
determined that a degraded 7300 process card was responsible for the
Enclosure 2
.
.
-
.
-
. . _ .


                                                                                          }
}
                                                                                          l
18
                                  18
drift and initiated plans to have the card replaced after the root cause
drift and initiated plans to have the card replaced after the root cause
of the power indication discrepancy was identified.
of the power indication discrepancy was identified.
The FIP team also determined that indicated feedwater flow had decreased
The FIP team also determined that indicated feedwater flow had decreased
while steam flow had remained constant. This was attributed to
while steam flow had remained constant.
feedwater venturi defouling as a function of the new cycle (restart from
This was attributed to
feedwater venturi defouling as a function of the new cycle (restart from
the April refueling outage was in early May). the recent reactor trip
the April refueling outage was in early May). the recent reactor trip
(June 26), and was the recent rapid downpower (July 2). The result of
(June 26), and was the recent rapid downpower (July 2). The result of
defouling was a decrease in indicated feedwater flow with a
defouling was a decrease in indicated feedwater flow with a
consequential decrease in indicated secondary thermal                 Operations
consequential decrease in indicated secondary thermal
maintains secondary Thermal Power Best Estimate (TPBE) power.
maintains secondary Thermal Power Best Estimate (TPBE) power. Operations
                                                          near 100% by
near 100% by
periodically opening flow control valves, which in turn causes primary
periodically opening flow control valves, which in turn causes primary
power to increase to maintain T
power to increase to maintain T
defouling caused an increase in.,,   for and
defouling caused an increase in.,, for 100% power level. The gradual
                                  actual 100%   power level.
actual and indicated primary thermal
                                              indicated       The
power, as well as actual secondary thermal power.
                                                        primary       gradual
However, the
                                                                  thermal
power, as well as actual secondary thermal power. However, the
resultant discrepancy between indicated and actual secondary thermal
resultant discrepancy between indicated and actual secondary thermal
)ower accounted for approximately 0.10% to 0.15% of the 0.6% discrepancy
)ower accounted for approximately 0.10% to 0.15% of the 0.6% discrepancy
)etween primary and secondary indicated thermal power.
)etween primary and secondary indicated thermal power.
The major contributor (0.3% to 0.4%) to the discreaancy between primary
The major contributor (0.3% to 0.4%) to the discreaancy between primary
and secondary thermal power was determined by the IP team on July 16 as
and secondary thermal power was determined by the
IP team on July 16 as
hot leg streaming. According to Westinghouse, hot leg streaming refers
hot leg streaming. According to Westinghouse, hot leg streaming refers
to the inability to accurately characterize bulk hot leg temperature.
to the inability to accurately characterize bulk hot leg temperature.
The licensee examined data from the Unit 2 Beginning of C.rcle and
The licensee examined data from the Unit 2 Beginning of C.rcle and
identified changes in the behavior of this phenomenon from previous
identified changes in the behavior of this phenomenon from previous
cycles. S)ecifically. calculations revealed that indicated Tw had
cycles.
S)ecifically. calculations revealed that indicated Tw had
increased ay 0.2*F and caused indicated primary thermal power to
increased ay 0.2*F and caused indicated primary thermal power to
increase. As discussed above these changes were originally masked by
increase.
the decrease in primary tem                                                             -
As discussed above these changes were originally masked by
T,,,/T,,, as a function of T,,,peratures   accompanying the decrease in
the decrease in primary tem
                              indication drift.
T,,,/T,,, as a function of T,,,peratures accompanying the decrease in
-
indication drift.
Hot leg streaming has occurred in previous cycles on both units and has
Hot leg streaming has occurred in previous cycles on both units and has
resulted in as high as a 1.0% difference between primary and secondary
resulted in as high as a 1.0% difference between primary and secondary
Line 1,132: Line 1,434:
error to warrant adjustment via the Reactor Coolant System (RCS)
error to warrant adjustment via the Reactor Coolant System (RCS)
Temperature Calibration Procedure, which is run quarterly. The OPAT and
Temperature Calibration Procedure, which is run quarterly. The OPAT and
OTAT trip strings remained within their TS limits. In addition, the
OTAT trip strings remained within their TS limits.
In addition, the
nuclear instrumentation system is calibrated to secondary thermal power,
nuclear instrumentation system is calibrated to secondary thermal power,
so the associated overpower trip setpoints were unaffected.
so the associated overpower trip setpoints were unaffected.
                                                                Enclosure 2
Enclosure 2
                                                                                          ,
,
                                                                _,
_,
                                                                    -
-.-.-.c.
                                                                        -.-.-.c. _. ---
. ---
-


                  _ _ _ _ - _ _ _ _ - - - - _ _ _ _ - - - - -
_ _ _ _
                                                                - - - - - -
- _ _ _ _
                                                                                            -
- - - - _ _ _ _ - - - -
                                                              19
-
            Reactor Power was increased to 99.5% on July 16 and the degraded T,q
- - - - - -
            card was replaced on July 17. The inspector attended the prejob brief
-
            for the card replacement and observed the work activity in the control
19
            room. The replacement was successfully completed within less than 1
Reactor Power was increased to 99.5% on July 16 and the degraded T,q
            hour and without incidence. At the end of the inspection period, the
card was replaced on July 17.
3a         license was considering either performina periodic manual calculations
The inspector attended the prejob brief
            to the correct the thermal power aiscrepancy, or conducting a full
for the card replacement and observed the work activity in the control
            calorimetric to account for the deviation.
room. The replacement was successfully completed within less than 1
        c. Conclusiqn_q
hour and without incidence.
                                                                                              ,
At the end of the inspection period, the
*          The inspector concluded that the licensee's identification of the
3a
E           thermal power discrepancy exhibited attention to detail and a thm
license was considering either performina periodic manual calculations
            review of plant data. Actions to initiate a FlP team to invr a
to the correct the thermal power aiscrepancy, or conducting a full
g           root cause were appropriate, and steps to reduce reactor po'
calorimetric to account for the deviation.
            discrepancy was understood were conservative and indicative
c.
            positive nuclear safety ethic. Replacement of the faulty T,             ,a was
Conclusiqn_q
            well-planned. coordinated and controlled, and executed in an expeditious
,
            manner.
The inspector concluded that the licensee's identification of the
      E2   Engineering Support of Facilities and Equipment
*
    .
E
      E2.1 Review of Corrective Actions
thermal power discrepancy exhibited attention to detail and a thm
        a. Inspedjon Scooe (37550. 92903)
review of plant data. Actions to initiate a FlP team to invr
            The inspector reviewed Engineering corrective actions to resolve open
g
            itens identified during the development of the station Design Base
root cause were appropriate, and steps to reduce reactor po'
            Documents (DBDs) and findings from Self-initiated Technical Audits
a
            (SITAs). Also reviewed were the licensee's actions to address a 10 CFR
discrepancy was understood were conservative and indicative
            Part 21 issue related to a defective Emergency Diesel Generator (EDG)
positive nuclear safety ethic.
            intake / exhaust valve spring. Anplicable regulatory requirements
Replacement of the faulty T,
            included 10 CFR 50 Appendix B. ESAR. Technical Specifications and
,a was
            implementing licensee procedures.
well-planned. coordinated and controlled, and executed in an expeditious
        b. Observations and Findinos
manner.
            DS_Qs
E2
            Developed between 1990 and 1994. DBDs consolidated design and licensing
Engineering Support of Facilities and Equipment
            documentation for selected station systems and programs. The ]rocedure
.
            guidance for development and maintenance of DBDs was provided ay
E2.1 Review of Corrective Actions
            Enoineering Directives Manual . EDM-170. Design Specifications, revision
a.
Inspedjon Scooe (37550. 92903)
The inspector reviewed Engineering corrective actions to resolve open
itens identified during the development of the station Design Base
Documents (DBDs) and findings from Self-initiated Technical Audits
(SITAs).
Also reviewed were the licensee's actions to address a 10 CFR
Part 21 issue related to a defective Emergency Diesel Generator (EDG)
intake / exhaust valve spring. Anplicable regulatory requirements
included 10 CFR 50 Appendix B. ESAR. Technical Specifications and
implementing licensee procedures.
b.
Observations and Findinos
DS_Qs
Developed between 1990 and 1994. DBDs consolidated design and licensing
documentation for selected station systems and programs. The ]rocedure
guidance for development and maintenance of DBDs was provided
ay
Enoineering Directives Manual . EDM-170. Design Specifications, revision
5.
Open items were evaluhed for operability during the DBD development
'
'
            5. Open items were evaluhed for operability during the DBD development
and Licensee Event Reports (LERs) initiated as required.
            and Licensee Event Reports (LERs) initiated as required. EDM-170
EDM-170
            required the remaining items to be entered into the Problem
required the remaining items to be entered into the Problem
            Investigation Process (PIP) for tracking and resolution. Additionally,
Investigation Process (PIP) for tracking and resolution. Additionally,
            the l u ensee's February 10. 1997. response to the 10 CFR 50.54f letter
the l u ensee's February 10. 1997. response to the 10 CFR 50.54f letter
            related to the Adequacy and Availability of Design Basis Information.
related to the Adequacy and Availability of Design Basis Information.
  P         stated that DBD open items woeli be ente 1 4 into the PIP for trackir.g
P
N          and resolution.
4
                                                                                Enclosure 2
N
  .
stated that DBD open items woeli be ente 1
                                                                            Mi
into the PIP for trackir.g
and resolution.
Enclosure 2
.
Mi


                                  20
20
TM inspector reviewed the resolution of open item in the Reactor
TM inspector reviewed the resolution of open item in the Reactor
coolant System DBD to sample the adecuacy of item resolution activity.
coolant System DBD to sample the adecuacy of item resolution activity.
Approximately 20 items were evaluatec to verify that the PIP and
Approximately 20 items were evaluatec to verify that the PIP and
interfacing station programs evaluated and resolved the open item
interfacing station programs evaluated and resolved the open item
issues.   The items were adequately resolved.
issues.
The items were adequately resolved.
An independent industry audit of Catawba in late 1996, identified as a
An independent industry audit of Catawba in late 1996, identified as a
finding the numerous lon9-term unresolved DBD open items. The response
finding the numerous lon9-term unresolved DBD open items. The response
to the finding was to initiate a blanket PIP (PIP 0-C97-0595 dated
to the finding was to initiate a blanket PIP (PIP 0-C97-0595 dated
March 5,1997) to cover the systems with the identified open items.
March 5,1997) to cover the systems with the identified open items.
Line 1,207: Line 1,536:
PIP corrective actions established a schedule to resolve and close the
PIP corrective actions established a schedule to resolve and close the
referenced DBD open items by September 1. 1997,
referenced DBD open items by September 1. 1997,
During this inspection, the inspector identified additional E       'en
During this inspection, the inspector identified additional E
'en
items which were not entered into the PIP process nor incluau .d the
items which were not entered into the PIP process nor incluau .d the
blanket PIP. The open items.were included in DBD CNS-1435.00-0002. Post
blanket PIP. The open items.were included in DBD CNS-1435.00-0002. Post
Fire Safe Shutdown, revision 4. and DBD CNS-1465.00-00-0018. Station
Fire Safe Shutdown, revision 4. and DBD CNS-1465.00-00-0018. Station
Blackout (SBO) Rule, revision 2. Although not entered into the PIP
Blackout (SBO) Rule, revision 2.
3rocess. the licensee provided meeti g documentation indicating the Post
Although not entered into the PIP
rire Safe Shutdown open items were being evaluated. These items were
3rocess. the licensee provided meeti g documentation indicating the Post
rire Safe Shutdown open items were being evaluated.
These items were
identified by a November 1995 electrical post fire shutdown review
identified by a November 1995 electrical post fire shutdown review
performeo after the initial DBD development and entered into the DBD by
performeo after the initial DBD development and entered into the DBD by
revision 4 at that time. There was no c: :umented evaluation of
revision 4 at that time. There was no c: :umented evaluation of
o)erability   or A
o)erability or A
tie PIP process.ppendix     R commitments
tie PIP process.ppendix R commitments which would have been addressed by
                    Following             which
Following the inspector's identification of this issue
                                the inspector's   would haveof
                                                identification been
                                                                this addressed
                                                                    issue     by
the licensee initiated PIP 0-C97-1918 to track resolution of these open
the licensee initiated PIP 0-C97-1918 to track resolution of these open
items. The inspector identified no significant safety concerns related
items.
The inspector identified no significant safety concerns related
to the open items reviewed. This failure to follow procedure for
to the open items reviewed. This failure to follow procedure for
resolution of DBD open items is identified as the second example of
resolution of DBD open items is identified as the second example of
Violation 50-413.414/97-09-04: Failure to Follow Procedure.
Violation 50-413.414/97-09-04: Failure to Follow Procedure.
                                                                                  *
*
SITAS
SITAS
The ins)ector reviewed a recently comp'eted SITA report dated June 11.
The ins)ector reviewed a recently comp'eted SITA report dated June 11.
1997, w11ch reviewed the adequacy of resolution of SITA findings. The
1997, w11ch reviewed the adequacy of resolution of SITA findings.
The
scope of the audit was good in that it reviewed the resolution of 80
scope of the audit was good in that it reviewed the resolution of 80
findings from four previous SITAs. The depth of the audit was good in
findings from four previous SITAs. The depth of the audit was good in
Line 1,248: Line 1,578:
maintenance procedure. A defective spring was identified at Catawba in
maintenance procedure. A defective spring was identified at Catawba in
1996. The spring was replaced. analyzed, and sent to the vendor for
1996. The spring was replaced. analyzed, and sent to the vendor for
                                                                                  '
'
                                                              Encloture 2
Encloture 2
                .                                                       _
.
_


    ._.           _ _ _ _       ..     ..
._.
                                                          .       .   ..   .
_ _ _ _
                                                                              .       ..
..
                                                  21
..
              further analysis.     The licensee's respon.e to the notice on this issue
.
              was appropriate,
.
          c. Conclusions
..
              Resolution of DBD open items was generally adequate in that no safety
.
              significant issues were identifieo in the open items. A violation was
.
              identified for failure to follow licensee procedure requirements to
..
              enter open DBD open items into the station PIP process for tracking and
21
.            resolution. The audit of SITA corrective actions demonstrated that the
further analysis.
              licensee was aggressively following SITA findings and is identified as a
The licensee's respon.e to the notice on this issue
              strength in corrective action performance. Additionally, the licensee
was appropriate,
              adequately addressed the EDG 10 CFR Part 21 issue related to potentially
c.
              defective intake / exhaust springs.
Conclusions
        E3   Engineering Procedures and Documentation
Resolution of DBD open items was generally adequate in that no safety
        E3.1 Chanaes. Tests. and Exneriments Performed in Accordance With
significant issues were identifieo in the open items. A violation was
              10 CFR 50.59 (thru December 31. 1996)
identified for failure to follow licensee procedure requirements to
          a. Insoection Scone (37551)
enter open DBD open items into the station PIP process for tracking and
                                                                                          '
resolution.
The audit of SITA corrective actions demonstrated that the
.
licensee was aggressively following SITA findings and is identified as a
strength in corrective action performance. Additionally, the licensee
adequately addressed the EDG 10 CFR Part 21 issue related to potentially
defective intake / exhaust springs.
E3
Engineering Procedures and Documentation
E3.1 Chanaes. Tests. and Exneriments Performed in Accordance With
10 CFR 50.59 (thru December 31. 1996)
a.
Insoection Scone (37551)
'
f
f
              By letter dated March 31, 1997. Duke Power Company (the licer.see)
By letter dated March 31, 1997. Duke Power Company (the licer.see)
              submitted its annual summary of all changes, tests, and experiments,
submitted its annual summary of all changes, tests, and experiments,
              which were completed under the provisions of 10 CF,150.59 for the period
which were completed under the provisions of 10 CF,150.59 for the period
              through December 31. 1996. The licensee's March 31, 1997, summary
through December 31. 1996. The licensee's March 31, 1997, summary
              included approximately 380 changes made during the subject period. The
included approximately 380 changes made during the subject period. The
              inspector evaluated these changes against the p,avisions of the
inspector evaluated these changes against the p,avisions of the
              regulation.
regulation.
                                                                                          <
<
          b. Observations and Findinas
b.
              In accordance with 10 CFR 50.59, a licensee may:     (1) make changes in
Observations and Findinas
              the facility as described in the safety analysis report, (2) make
In accordance with 10 CFR 50.59, a licensee may:
              changes -in the procedures as described in the safety analysis report,
(1) make changes in
              and (3) corduct tests or experiments not described in the safety
the facility as described in the safety analysis report, (2) make
              analysis report, without prior Commission approval, unless the change
changes -in the procedures as described in the safety analysis report,
              involvy a changc in the Technical Specifications or an Unreviewed
and (3) corduct tests or experiments not described in the safety
              Safety duestion (US0). The regulation defines an US0 as a proposed
analysis report, without prior Commission approval, unless the change
              action that: (a) may increase the probability of occurrence or
involvy a changc in the Technical Specifications or an Unreviewed
              consequences of an accident or malfunction of equipment important to
Safety duestion (US0). The regulation defines an US0 as a proposed
              safety previously evaluated in the safety analysis report, or (b) may
action that:
              create a possibility for an accident or malfunction of a different type
(a) may increase the probability of occurrence or
              than any previously evaluated in the safety analysis report or (c) may
consequences of an accident or malfunction of equipment important to
              reduce the margin of safety as defined in the basis for any Technical
safety previously evaluated in the safety analysis report, or (b) may
              Specification.
create a possibility for an accident or malfunction of a different type
              The inspector reviewed the licensee's current (dated March 10. 1997)
than any previously evaluated in the safety analysis report or (c) may
              version of Nuclear System Directive 209. "10 CFR 50.59 Evaluations."
reduce the margin of safety as defined in the basis for any Technical
              which is patterned after NSAC-125. " Guidelines for 10 CFR 50.59 Safety
Specification.
                                                                              Enclosure 2
The inspector reviewed the licensee's current (dated March 10. 1997)
  .
version of Nuclear System Directive 209. "10 CFR 50.59 Evaluations."
which is patterned after NSAC-125. " Guidelines for 10 CFR 50.59 Safety
Enclosure 2
.


      _ _ _ _         _-- __       --
_ _ _ _
                                        22
_--
Evaluations." June 1989. This document requires that changes be
__
--
22
Evaluations." June 1989.
This document requires that changes be
evaluated against the appropriate Final Safety Analysis Report (FSAR).
evaluated against the appropriate Final Safety Analysis Report (FSAR).
Technical Specifications, end NRC Safety Evaluation Report sections to
Technical Specifications, end NRC Safety Evaluation Report sections to
determine if there is need for revision.         Specifically, the criteria
determine if there is need for revision.
specified by 10 CFR 50.59 are broken down into seven (7) questions. For
Specifically, the criteria
specified by 10 CFR 50.59 are broken down into seven (7) questions.
For
a change to be qualified for 10 CFR 50.59, the answers to all seven
a change to be qualified for 10 CFR 50.59, the answers to all seven
questions must be "no". Based on review of this document, and the
questions must be "no".
Based on review of this document, and the
review of the licensee's 10 CFR 50.59 evaluations. the inspector
review of the licensee's 10 CFR 50.59 evaluations. the inspector
concluded that the licensee's directive appropriately reflects the
concluded that the licensee's directive appropriately reflects the
Line 1,320: Line 1,674:
this review, the inspector selected the following changes for more
this review, the inspector selected the following changes for more
detailed review onsite:
detailed review onsite:
e             Exempt Changes:
e
              Exempt Change CE-3176
Exempt Changes:
              Exempt Change CE-3705
Exempt Change CE-3176
              Exempt Change CE-3759
Exempt Change CE-3705
              Exempt Change CE-4745
Exempt Change CE-3759
              Exempt Charge CE-4746
Exempt Change CE-4745
              Exempt Change CE-4821
Exempt Charge CE-4746
              Exempt Change CE-4822
Exempt Change CE-4821
              Exempt Change CE-7416
Exempt Change CE-4822
              Exempt Change CE-7977
Exempt Change CE-7416
              Exempt Change CE-8126
Exempt Change CE-7977
              Exempt Change CE-8182
Exempt Change CE-8126
              Exempt Change CE-8245
Exempt Change CE-8182
              Exempt Change CE-8410
Exempt Change CE-8245
              Exempt Change CE-61008
Exempt Change CE-8410
              Exempt Change CE-61162
Exempt Change CE-61008
e            Miscellaneous Changes:
Exempt Change CE-61162
              SIMULATE (a computer code) Version 4
Miscellaneous Changes:
*             Modifications:
e
              NSM CN-11371
SIMULATE (a computer code) Version 4
              NSM CN-20396
*
o            0:?rable But Degraded Evaluations:
Modifications:
              PIF 2-C97-0157
NSM CN-11371
              PIP 2-096-3250
NSM CN-20396
e            Operability Evaluations:
0:?rable But Degraded Evaluations:
                                                                    Enclosure 2
o
                                        _
PIF 2-C97-0157
                                                                                ~
PIP 2-096-3250
Operability Evaluations:
e
Enclosure 2
_
~


  . - _ _ _ _ _ _ _ _ _ _ - _ -
. - _ _ _ _ _ _ _ _ _ _ - _ -
                                                              23
23
                                Operability Evaluation dated 2/15/94
Operability Evaluation dated 2/15/94
                                Operability Evaluation dated 2/18/94
Operability Evaluation dated 2/18/94
                                Operability Evaluation dated 6/28/94
Operability Evaluation dated 6/28/94
  e                             Procedure Channes:
e
                                OP/1/A/6200/11
Procedure Channes:
                                AM/2/A/5100/07
OP/1/A/6200/11
                                OP/2/B/6200/33. Change 4 Rev. 4
AM/2/A/5100/07
                                OP/1/A/6550/14
OP/2/B/6200/33. Change 4 Rev. 4
                                PT/1/B/4700/82
OP/1/A/6550/14
  The ins ector determined that these changes were correctly evaluated
PT/1/B/4700/82
  under t e provisions of 10 CFR 50.59
The ins ector determined that these changes were correctly evaluated
  During the in-office and onsite reviews, the inspector made a number of
under t e provisions of 10 CFR 50.59
  observations and has communicated them to licensee personnel:
During the in-office and onsite reviews, the inspector made a number of
  *                              The use of nuke-specific system identifiers in the annual summary
observations and has communicated them to licensee personnel:
                                (which is submitted to the NRC and is thus available to the
The use of n ke-specific system identifiers in the annual summary
*
u
(which is submitted to the NRC and is thus available to the
public) is discouraged unless the licensee provides a key in the
l
l
summary. These identifiers do not bear any apparent correlation
l
to the actual systems (e.g. , NC = reactor coolant system. KC =
l
l
                                public) is discouraged unless the licensee provides a key in the
component cooling system, etc..).
l                                summary. These identifiers do not bear any apparent correlation
The inspector made a similar
l                                to the actual systems (e.g. , NC = reactor coolant system. KC =
observation on the summary submitted on March 2~. 1996 (see
l                                component cooling system, etc..). The inspector made a similar
Inspection Report 50-413.414/96-10).
                                observation on the summary submitted on March 2~. 1996 (see
                                Inspection Report 50-413.414/96-10).
'
'
  o                              The licensee's corresponding revision of the UFSAR. per 10 CFR
The licensee's corresponding revision of the UFSAR. per 10 CFR
                                50.71. lags behind 10 CFR 50.59 evaluations. The next u)date of
o
                                the UFSAR. scheduled for late 1997. should capture all tie changes
50.71. lags behind 10 CFR 50.59 evaluations.
                                that are within the scope of the UFSAR.
The next u)date of
  e                              While the licensee had acceptably evaluated all the changes
the UFSAR. scheduled for late 1997. should capture all tie changes
                                audited by the inspector, a number of them eppeared in the summary
that are within the scope of the UFSAR.
                                with insufficient information for a reader to even determine what
While the licensee had acceptably evaluated all the changes
                                system was involved, or what change was made. The inspector
e
                                recommended a several-sentence description. identifying the
audited by the inspector, a number of them eppeared in the summary
                                system, the component, and the nature of the change, and
with insufficient information for a reader to even determine what
                                accompanied by a several-sentence evaluation. Despite this
system was involved, or what change was made.
                                problem with the summary, the evaluations were found to be
The inspector
                                thorough and in compliance with 10 CFR 50.59. The licensee was
recommended a several-sentence description. identifying the
                                aware of this aroblem with the summary and has initiated actions
system, the component, and the nature of the change, and
                                to correct suc1 weakness by revising its guidance document. NSD
accompanied by a several-sentence evaluation.
                                209 (see Problem Investigation Process Form 0-C97-2027. dated June
Despite this
                                19. 1997).
problem with the summary, the evaluations were found to be
  *                              The term " Exempt Changes" may cause confusion in the context of 10
thorough and in compliance with 10 CFR 50.59.
                                CFR 50.59.   It is a term internal to the licensee's docunentation.
The licensee was
                                It pertains to changes that "do not require the Modification
aware of this aroblem with the summary and has initiated actions
                                                                                          Enclosure 2
to correct suc1 weakness by revising its guidance document. NSD
209 (see Problem Investigation Process Form 0-C97-2027. dated June
19. 1997).
The term " Exempt Changes" may cause confusion in the context of 10
*
CFR 50.59.
It is a term internal to the licensee's docunentation.
It pertains to changes that "do not require the Modification
Enclosure 2


                            - _ _ _ _
- _ _ _ _
                                                                                  1
1
                                                                                  b
b
                                                  24
24
              Program controls for configuration management and therefore are
Program controls for configuration management and therefore are
              specifically exempted from the requirements to process an
specifically exempted from the requirements to process an
              editorial NM or NSM." According to licensee personnel, an " exempt
editorial NM or NSM." According to licensee personnel, an " exempt
              change" is essentially a minor change.
change" is essentially a minor change.
        e    The summary contained a significant number of errors, which stated
The summary contained a significant number of errors, which stated
              the opposite of the actual facts. For example, test procedure
e
              TT/1/A/9200/88 states "there are Unreviewed Safety Questions
the opposite of the actual facts.
              associated with this test procedure" when the onsite evaluation
For example, test procedure
              shows that there was no unreviewed safety question. The licensee
TT/1/A/9200/88 states "there are Unreviewed Safety Questions
              submitted a letter on July 9, 1997, correcting such errors.
associated with this test procedure" when the onsite evaluation
    c. Crnclusions
shows that there was no unreviewed safety question.
        Based on in-office review of the licensee's March 31, 1997, annual
The licensee
        summary on 10 CFR 50.59 changes, onsite review of the licensee's 10 CFR
submitted a letter on July 9, 1997, correcting such errors.
        50.59 evaluatius, and audit of the licensee's 3rocedures, the inspector
c.
        concluded that the licensee had complied with t1e provisions of the
Crnclusions
        regulation for the changes listed in the annual summary.
Based on in-office review of the licensee's March 31, 1997, annual
summary on 10 CFR 50.59 changes, onsite review of the licensee's 10 CFR
50.59 evaluatius, and audit of the licensee's 3rocedures, the inspector
concluded that the licensee had complied with t1e provisions of the
regulation for the changes listed in the annual summary.
l
l
                                          IV. Plant Suocort
IV. Plant Suocort
  R1     Radiological Protection and Chemistry Controls
R1
  R1.1 Tours of the Radiolooical Control Area (RCA) (71750)
Radiological Protection and Chemistry Controls
        The inspectors periodically toured the RCA during the inspection period.
R1.1 Tours of the Radiolooical Control Area (RCA) (71750)
t        Radiological control practices were observed and discussed with
The inspectors periodically toured the RCA during the inspection period.
Radiological control practices were observed and discussed with
t
!
!
        radiological control personnel, including RCA entry and exit, survey
radiological control personnel, including RCA entry and exit, survey
        postings locked high radiation areas, and radiological area material
postings
        conditions. The inspector concluded that radiological control practices
locked high radiation areas, and radiological area material
        were proper.
conditions.
                                      V. Management Meetinas
The inspector concluded that radiological control practices
  X1     Exit Meeting Summary
were proper.
  The inspectors ) resented the inspection results to members of licensee
V. Management Meetinas
  management at t1e conclusion of the inspection on July 11 and July 23. 1997.
X1
  The licensee acknowledged the findings presented. No proprietary information
Exit Meeting Summary
  was identified. Dissenting comments were not received from the licensee.
The inspectors ) resented the inspection results to members of licensee
                                                                      Enclosure 2
management at t1e conclusion of the inspection on July 11 and July 23. 1997.
The licensee acknowledged the findings presented.
No proprietary information
was identified.
Dissenting comments were not received from the licensee.
Enclosure 2


          _ - _ _ _ . - - - _
_ - _ _ _ . - - - _
                                                                                  .,
-.
                              -.     -
-
                                  t
.,
                                                    25
t
                                    PARTIAL LIST OF PERSONS CONTACTED
25
  Licensee
PARTIAL LIST OF PERSONS CONTACTED
  Bhatnager. A. . Operations Su>erintendent
Licensee
  Birch. M. . Safety Assurance ianager
Bhatnager. A. . Operations Su>erintendent
  Coy., S., Radiation Protection Manager
Birch. M. . Safety Assurance ianager
  Forbes. J., Engineering Manager
Coy., S., Radiation Protection Manager
  Jones. R.. Station Manager
Forbes. J., Engineering Manager
  Harrall. T., Instrument and Electrical Maintenance Superintendent
Jones. R.. Station Manager
  Kelly. C.. Mainteriance Manager
Harrall. T., Instrument and Electrical Maintenance Superintendent
  Kimball . D. , Safety Review Group Manager
Kelly. C.. Mainteriance Manager
  Kitlan. M., Regulatory Compliance Manager
Kimball . D. , Safety Review Group Manager
Kitlan. M., Regulatory Compliance Manager
'
'
  Nicholson. K., Compliance Specialist
Nicholson. K., Compliance Specialist
  Peterson. G., Catawba Site Vice-President
Peterson. G., Catawba Site Vice-President
  Tower. D., Regulatory Compliance
Tower. D., Regulatory Compliance
l
l
                                                                                      ,
,
4
4
                                                                      Enclosure 2
Enclosure 2
                                                                                    u
u


                _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ - _                     __
_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ - _
                                                                                            26
__
                                                                              INSPECTION PROCEDURES USED
26
  IP 37551:   Onsite Engineering
INSPECTION PROCEDURES USED
  IP 40500:   Effectiveness of Licensee Controls in Identifying. Resolving, and
IP 37551:
              Preventing Problems                                                                                                   i
Onsite Engineering
  IP 61726:   Surveillance Observation
IP 40500:
  IP 37550:   Engineering
Effectiveness of Licensee Controls in Identifying. Resolving, and
  IP 62707:   Maintenance Observation
i
  IP 71707:   Plant Operations
Preventing Problems
  IP 71750:   Plant Support Activitia
IP 61726:
  IP 92901:   Followup - Operations
Surveillance Observation
  IP 92902:   Followup - Maintenance
IP 37550:
  IP 92903:   Followup - Engineering
Engineering
  IP 93702:   Prompt Onsite Respense to Events
IP 62707:
                                                                        ITEMS OPENED, CLOSED, AND DISCUSSED
Maintenance Observation
  Opened
IP 71707:
Plant Operations
IP 71750:
Plant Support Activitia
IP 92901:
Followup - Operations
IP 92902:
Followup - Maintenance
IP 92903:
Followup - Engineering
IP 93702:
Prompt Onsite Respense to Events
ITEMS OPENED, CLOSED, AND DISCUSSED
Opened
i
i
  50-414/97-09-01                                                           NCV         Failure to Declare Ice Condenser
50-414/97-09-01
                                                                                          Intermediate Deck Doors Inoperable and Log
NCV
                                                                                        Appropriate TSAIL Entry (Section C1.1)
Failure to Declare Ice Condenser
  50-414/97-09-02                                                           NCV           Inadequate Lower Containment Ventilation
Intermediate Deck Doors Inoperable and Log
                                                                                        Unit Operating Procedure (Section 01.4)
Appropriate TSAIL Entry (Section C1.1)
50-414/97-09-02
NCV
Inadequate Lower Containment Ventilation
Unit Operating Procedure (Section 01.4)
'
'
  50-414/97-09-03                                                           VIO         Failure to Follow Procedure Results in
50-414/97-09-03
                                                                                          Invalid Local Leak Rate Test of Valve 2NV-
VIO
                                                                                        874 (Section M1.2)
Failure to Follow Procedure Results in
  50-413.414/97-09-04                                                       VIO         Failure to Follow Procedure - Two Examples
Invalid Local Leak Rate Test of Valve 2NV-
                                                                                          (Sections 08.1. E2.1)
874 (Section M1.2)
  Closed
50-413.414/97-09-04
  50-413.414/97-01-01                                                       VIO         Failure to Include All Structures Systems
VIO
                                                                                        and Components in the Scope of the
Failure to Follow Procedure - Two Examples
                                                                                        Maintenance Rule as Required by 10 CFR
(Sections 08.1. E2.1)
                                                                                        50.65(b) (Section M8.1)
Closed
  50-414.414/97-01-02                                                       IFI         Followup and review of licensee procedure
50-413.414/97-01-01
                                                                                        to implement the requirements of (a)(1)
VIO
                                                                                        and (a)(2) of the Maintenance Rule after
Failure to Include All Structures Systems
                                                                                        issuance of Revision 2 of Regulatory Guide
and Components in the Scope of the
                                                                                        1.160 (Section M8.3)
Maintenance Rule as Required by 10 CFR
  50-413.414/97-01-03                                                       IFl         Followup on Licensee Actions to Provide
50.65(b) (Section M8.1)
                                                                                        Performance Criteria for Structures After
50-414.414/97-01-02
                                                                                        Resolution of this Issue (Section M8.4)
IFI
                                                                                                                        Enclosure 2
Followup and review of licensee procedure
to implement the requirements of (a)(1)
and (a)(2) of the Maintenance Rule after
issuance of Revision 2 of Regulatory Guide
1.160 (Section M8.3)
50-413.414/97-01-03
IFl
Followup on Licensee Actions to Provide
Performance Criteria for Structures After
Resolution of this Issue (Section M8.4)
Enclosure 2


- _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _                         _
- _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _
                                                                                                                  27
_
                                                                        50-413.414/97-01-04         VIO       Failure to implement the requirements of
27
                                                                                                              (a)(1) and (a)(2) of the Maintenance Rule
50-413.414/97-01-04
                                                                                                              (Section M3.2)
VIO
                                                                        50 413.414/94-13-02         URI       Emergency Operating Procedure 50.59
Failure to implement the requirements of
                                                                                                              Evaluations Not Reviewed by Nuclear Safety
(a)(1) and (a)(2) of the Maintenance Rule
                                                                                                  '
(Section M3.2)
                                                                                                              Review Board as Required by TS (Section     l
50 413.414/94-13-02
                                                                                                              08.1)
URI
Emergency Operating Procedure 50.59
Evaluations Not Reviewed by Nuclear Safety
Review Board as Required by TS (Section
l
'
08.1)
<
<
l                                                                                                       List of Acronyms
l
!                                                                       CFR   -
List of Acronyms
                                                                                    Code of Federal Fagulations
!
                                                                        DBD   -
CFR
                                                                                    Design Basis Documents
Code of Federal Fagulations
                                                                        EDG   -
-
                                                                                    Emergency Diesel Generator
DBD
                                                                        EDM   -
Design Basis Documents
                                                                                    Engineering Directives Manual
-
                                                                        E0P   -
EDG
                                                                                    Emergency Operating Procedure
Emergency Diesel Generator
                                                                        FIP   -
-
                                                                                    Failure Investigative Process
EDM
                                                                        FSAR -
Engineering Directives Manual
                                                                                    Final Safety Analysis Report
-
                                                                        IAE   -
E0P
                                                                                    Instrument and Electrical
Emergency Operating Procedure
                                                                        IFI   -
-
                                                                                    Inspector Followup Iten
FIP
                                                                        IST   -
Failure Investigative Process
                                                                                    Inservice Testing
-
                                                                        LCVU -
FSAR
                                                                                    Lower Containment Ventilation Unit
Final Safety Analysis Report
                                                                        LER   -
-
                                                                                    Licensee Event Report
IAE
                                                                        LLRT -
-
                                                                                    Local Leak Rate Test
Instrument and Electrical
                                                                        MPFF -
IFI
                                                                                    Maintenance Preventable Function Failure
-
                                                                        NCV   -
Inspector Followup Iten
                                                                                    Non Cited Violation
IST
                                                                        NM   -
Inservice Testing
                                                                                    Nuclear Sampling
-
                                                                        NRC   -
LCVU
                                                                                    Nuclear Regulatory Commission
Lower Containment Ventilation Unit
                                                                        NSD   -
-
                                                                                    Nuclear Site Directive
LER
                                                                        NSRB -
-
                                                                                    Nuclear Safety Review Board
Licensee Event Report
                                                                        DAC   -
LLRT
                                                                                    Operator Aid Com] uter
Local Leak Rate Test
                                                                        POR   -
-
                                                                                    Public Document Room
MPFF
                                                                        PIP   -
Maintenance Preventable Function Failure
                                                                                    Problem Investigation Process
-
                                                                        PM   -
NCV
                                                                                    Preventive Maintenance
Non Cited Violation
                                                                        asig -
-
                                                                                    Pounds Per Square Inch Gauge
NM
                                                                        RCA   -
Nuclear Sampling
                                                                                    Radiologically Controlled Area
-
                                                                        RCP   -
NRC
                                                                                    Reactor Coolant Pump
Nuclear Regulatory Commission
                                                                        RCS   -
-
                                                                                    Reactor Coolant System
NSD
                                                                        RG   -
-
                                                                                    Regulatory Guide
Nuclear Site Directive
                                                                        SA   --
NSRB
                                                                                    Main Steam to Auxiliary Equipment
Nuclear Safety Review Board
                                                                        SB0   -
-
                                                                                    Station Blackout Role
DAC
                                                                        SITA -     Self Initiated Technical Audit
Operator Aid Com] uter
                                                                        SPOC -
-
                                                                                    Single Point of Contact
POR
                                                                        TPBE -     Thermal Power Best Estimate
-
                                                                        TS   -
Public Document
                                                                                    Technical Specifications
Room
                                                                        TSAIL -     Tech Spec' Action Item Log
PIP
                                                                        UCLF -     Unplanned Capability loss Factor
-
                                                                        UFSAR -     Updated Final Safety Analysis Report
Problem Investigation Process
                                                                                                                                              Enclosure 2
PM
                                                                                                                                                          _
-
Preventive Maintenance
asig
Pounds Per Square Inch Gauge
-
RCA
-
Radiologically Controlled Area
RCP
-
Reactor Coolant Pump
RCS
Reactor Coolant System
-
RG
-
Regulatory Guide
SA
--
Main Steam to Auxiliary Equipment
SB0
-
Station Blackout Role
SITA -
Self Initiated Technical Audit
SPOC
Single Point of Contact
-
TPBE -
Thermal Power Best Estimate
TS
-
Technical Specifications
TSAIL -
Tech Spec' Action Item Log
UCLF -
Unplanned Capability loss Factor
UFSAR -
Updated Final Safety Analysis Report
Enclosure 2
_


                                    28
28
  URI- -
URI-
          Unresolved Item-
-
  USO -
Unresolved Item-
          Unreviewed Safety Question
USO
  VDC' -
Unreviewed Safety Question
          Volts direct current
-
                .
VDC'
  VIO -
Volts direct current
          Violation
-
  -VV   -
.
          Containment Ventilation
VIO
  WO   -
Violation
          Work Order
-
  YN   -
-VV
          Auxiliary Building Chilled Water
Containment Ventilation
-
WO
Work Order
-
YN
Auxiliary Building Chilled Water
-
l
l
                                          Enclosure 2
Enclosure 2
                                                      _
_
}}
}}

Latest revision as of 14:29, 23 May 2025

Insp Repts 50-413/97-09 & 50-414/97-09 on 970608-0719. Violations Noted.Major Areas Inspected:Aspects of Licensee Operations,Maint,Engineering & Plant Support
ML20210N734
Person / Time
Site: Catawba  
Issue date: 08/18/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20210N708 List:
References
50-413-97-09, 50-413-97-9, 50-414-97-09, 50-414-97-9, NUDOCS 9708260105
Download: ML20210N734 (32)


See also: IR 05000413/1997009

Text

.

. . . . . . . _ ,

Notice of Violation

3

withholding of such material, you muit tpecifically identify the portions of

your response that you seek to have witkield and provide in detail the bases

l

for your claim of withholding (e.g., explain why the disclosure of information

'

will create an unwarranted invasion of personal privacy or provide the

confidential commercial or financial information).

If safeguards information

,

l

1s necessary to provide an acceptable response, please provide the level of

protection described in 10 CFR 73.21.

Dated at Atlanta, Georgia

this 18th day of August, 1997

l

Enclosure 1

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.

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1

U. S. NUCLEAR REGULATORY COMMISSION

REGION 11

Docket Nos:

50-413, 50 414

License Nos:

NPF-35. NPF-52

Report Nos..

50-413/97 09. 50 414/97-09

Licensee:

Duke Power Company

Facility:

Catawba Nuclear Station. Units 1 and 2

Location:

422 South Church Street

l

Charlotte. NC 28242

Dates:

June 8 - July 19, 1997

Inspectors:

J. Zeiler. Acting Senior Resident inspector

R. L. Franovich, Resident inspector

M. Giles. Resident inspector (In Training)

N. Economos Region 11 Inspector (Sections M8.1. 2. 3. 4)

R. M. Moore. Region 11 Inspector (Sections 08.1. E2.1 )

Approved by:

S. M. Shaeffer. Acting Chief

Reactor Projects Branch 1

Division of Reactor Projects

l

I

Enclosure 2

9708260105 970818

PDR

ADOCK 05000413

0

PDR

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EXECUTIVE SUMMARY

Catawba Nuclear Station. Units 1 & 2

NRC Inspection Report 50 413/97-09, 50 414/97 09

This integrated inspection included aspects of licensee operations.

maintenance, engineering, and plant support.

The report covers a 6-week

period of resident ins)ection; in addition, it includes the results of

announced inspections ay Regional reactor safety inspectors.

Doerations

A Non Cited Violation (NCV) was identified for failure to declare three

e

ice condenser intermediate deck doors inoperable and log an associated

Technical Specification Action item Log entry after identifying ice

buildup on the doors.

This item along with several other minor human

performance weaknesses indicated a need for greater attention to detail

and questioning attitude by operations personnel during the performance

of routine activities (Section 01.1).

The root cause evaluations of a reactor coolant pump trip and subsequent

e

reactor trip were adequatel

involve human error or non y performed. The cause of the trip did not

conservative decision making.

The protective

relaying associated with the short bus of 2TB functioned as designed.

However, a delay in troubleshooting activities to locate the source of

the associated ground indicated that the ground received a low priority

status in the work schedule and that trained personnel were not readily

available to troubleshoot ground indications in a timely manner (Section

w.2).

Control room operators were effective in precluding a turbine runback by

reducing reactor power to 50% before the 28 Main Generator Power Circuit

Breaker opened on low air pressure.

The licensee's root cause

evaluation was detailed, and actions to prevent recurrence were

considered adequate (Section 01.3).

The decision to deviate from the preferred normal alignment of

Lower Containment Ventilation Unit (LCVU) operation to support

planned maintenance exhibited non-conservative work scheduling and

operatorjudgement.

This resulted in lower containment air

temperature increasing slightly above the adjusted Technical

Specification limit for a brief period of time.

The LCVU

operating procedures did not address the adverse impact of

removing two LCVUs from service simultaneously, nor did the

procedure address the interaction between LCVU operation and

integrated containment ventilation systems.

These procedural

inadequacies were identified as a NCV (Section 01.4).

A violation (first example) for failure to follow procedure was

identified related to Operations failure to adequately document 10 CFR 50.59 screening evaluations (Section 08.1).

Enclosure 2

_ _ _ _ _

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

2

Maintenance

A Failure In!estigation Process (FIP) team was thorough in investigating

e

the cause of an electrical flash in a 600 Volt breaker cubicle

associated with Motor Control Center 2MXM. The root cause indicated

configuration and procedure weaknesses in the method of locking out 600

Volt breaker cubicles to the maintenance position.

Adaquate corrective

actions to prevent recurrence of this incident were implemented (Section

M1.1).

The licensee's identification of a technician's failure to follow a leak

e

rate test procedure that resulted in an invaild test of valve 2NV-874

during the previous refueling outage was an example of good questioning

attitude: however, the procedure completion review was untimely.

The

Plant Operations Review Committee performed a thorough review of

subsequent activities to aroperly retest the valve.

Good engineering

support was arovided, bot 1 in developing a leak rate test procedure and

briefing paccage for the evolution.

The failure to follow the leak rate

test procedure was identified as a Violation (Section M1.2).

Enaineerina

The licensee's identification of a discrepancy between primary and

e

secondary thermal power indication exhibited attention to detail in the

review of plant data.

Actions to initiate a FIP team to investigate the

root cause were appropriate and steps to reduce reactor power until the

discrepancy was understood were conservative.

Replacement of a faulty

T,,, card was well-planned, coordinated and controlled and executed in

an expediticas manner (Section El.1).

Resolution of Design Base Document (DBD) open items was generally

o

adequate.

However, a violation (second example) for failure to follow

procedure was identified related to Engineering's failure to enter DBD

open items into the Problem identification Process as required by

procedure and stated in the licensee's response to the Des'.gn Basis

50.54f letter (Section E2.1).

The licensee's corrective action audit that assessed the resolution of

e

Self-N iated Technical Audit findings was identified as a strength in

correc " ve action performance (Section E2.1).

The licensee adequately addressed the Emergency Diesel Generator 10 CFR

e

Part 21 issue related to potentially defective intake / exhaust springs

(Section E2.1).

Based on in-office review of the licensee *s March 31, 1997, annual

summary on 10 CFR 50.59 changes, onsite review of the licensee's 10 CFR 50.59 evaluations, and audit of the licensee's procedures, the inspector

concluded that the licensee had complied with t1e provisions of the

regulation for the changes listed in the annual summary (Section E3.1).

Enclosure 2

-

,

3

Plant Suncort

Radiological control practices observed during the inspection period

e

were considered to b(. proper (Section R1.1).

l

l

Enclosure 2

,

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_

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

I

Reoort Details

Summary of Plant Status

,

Unit 1 operated at or near 100% power during the inspection period.

l

On June 26, a Unit 2 reactor trip occurred on low Reactor Coolant System loop

l

flow as a result of an electrical ground fault which de energized the

i

electrical bus that powers the "2B' Reactor Coolant Pump (RCP).

The unit was

returned to 100% power operation on June 29.

Power was reduce 1 to 50% on July

2 to preclude a turbine trip / reactor trip u)on the anticipated failure of

Main Generator Power Circuit Breaker (PCB) 23.

A solenoid (or pilot) valve

'

associated with the air supply to all three main generator PCB poles had

failed, rendering the air system unable to deliver air to the breaker. The

solenoid valve was replaced, and the unit was returned to 100% power the

following day.

Reactor power was reduced to 99.3% on July 15 in response to a

discrepancy between primary and secondary thermal power indications.

The

discrepancy was attributed to feedwater venturi defouling and hot leg

streaming, and did not reflect an actual temperature difference. The unit

returned to 100% power on July 17 and operated at or near 100% power for the

remainder of the inspection period.

Review of UDdated Final Safety Analysis Report (UFSAR) Commitm_gn_t1

While performing inspections discussed in this report, the inspector reviewed

the applicable portions of the UFSAR that were related to the areas ins)ected.

The inspector verified that the UFSAR wording was consistent with the o) served

plant practices, procedures, and/or parameters.

I. Operations

01

Conduct of Operations

01.1 General Comments (71707)

The inspector conducted frequent control room tours to verify proper

staffing operator attentiveness and communications. and adherence to

approved )rocedures.

The inspector attended daily operations turnover

and Site )irection meetings to maintain awareness of overall plant

operations.

Operator logs were reviewed to verify operational safety

and compliance with Technical Specifications (TS).

Instrumentation,

computer indications, and safety system lineups were periodically

reviewed from the Control Room to assess o)erability.

Plant tours were

conducted to observe equipment status and

Jousekeeping.

Problem

Identification Process (PIP) reports were routinely reviewed to assure

that potential safety concerns and equipment problems were reported and-

resolved,

in general, the conduct of operations was professional and safety

conscious. Good )lant equipment material conditions ar.d housekee ing

were noted througaout the report period.

However, as addressed b low,

sevcral minor operator human performance deficiencies were identified

Enclosure 2

_ _ _ _ _ _ _

.

,

2

involving a failure to enter a TS Action Statement, failure to identify

equipment status anomalies, and failure to properly document a Technical

Specification Action item Log (TSAIL) entry.

Failure to Declare Unit 2 Ice Condenser Intermediate Deck Doors

inoDerable and Enter ADolicable TS Action Statement

On June 17 at 2:38 p.m., while performing the weekly TS surveillance on

the intermediate deck doors the licensee identified that three doors

had ice buildup (reported to be less than one half inch thick). The

function of these doors is to open during a des.gn basis accident to

ensure that the containment loss Of Coolant Accident (LOCA) atmos)here

l

would be diverted through the ice condenser.

Upon discovery of t1e ice,

a test procedure discrepancy was entered and a work request was

initiated to remove the ice.

However, work to remove the ice or

investigate the extent of the impact on the door opening function was

not initiated due to problems with personnel accessing containment

through the containment airlock door.

Later that night, the oncoming

Shift Work Manager became aware of the previces day's problem and

-contacted engineering personnel to perform an operability evaluation of

the condition.

The following morning, the inspector reviewed the

results of this evaluation.

The evaluation concluded that the " ice

condenser" was operable.

This was based primarily-on a previous McGuire

Nuclear Station analysis that showed up to one-third of the intermediate

deck doors could fail to open and there would still be enough ice

condenser flow area for LOCA heat removal.

The inspector determined the

evaluation focused to narrowly on the ice condenser system operability

and failed to adequately evaluate the operability of the intermediate

deck doors, especially with regard to consideration of information in

the applicable TS and Bases.

TS 3.6.5.3 requires the intermediate deck doors be operable in Modes 1-

4.

TS Surveillance Recuirement 4.6.5.3.2 requires a 7-day verification

that the intermediate ceck doors be closed and free of frost

accumulation.

The TS Bases also states that impairment by ice, frost.

or debris is considered to render the doors inoperable, but capable of

opening.

Based on this, the inspector concluded that operations

personnel had failed to declare the three doors inopera]le and follow

the Action Statement of TS 3.6.5.3.a when the problem was initially

identified. This action statement allowed power operation to continue

for up to 14 days provided ice bed temperature was monitored at least

once per four hours and the maximum ice bed temperature was maintained

less than or equal to 27*F.

The licensee initiated PIP 2-C97-2014-to

investigate this incident.

On June 18. after repairing the containment airlock, ice was removed

from the three intermediate deck doors.

The cause of the ice buildup

was found to be the failure of heat tracing on an ice condenser air

handling fan drain line, which prevented adequate draining of defrost

condensate. The heat tracing was subsequently repaired. The licensee

Enclosure 2

-

,

3

determined during activities to remove the ice that all three doors were

i

l

not blocked to the extent that would have prevented their opening during

a LOCA.

The inspector also noted that the ice bed monitoring system was

'

operational during the period that ice was on the doors and control room

annunciator alarms would have alerted the operators of anomalous ice bed

temperatures. Therefore, the ins)ector considered the safety

consequences of this incident to )e minimal.

The inspector reviewed Operations Management Procedure (OMP) 2-29.

Technical Specifications Action Item Log. Step 3.4 requires that non-

compliance with a Limiting Condition For Operation requiring operation

in a TS Action Statement, be logged in TSAll.

The ins)ector determined

that a TSAll entry was not logged for this condition w1en ice was

identified on the doors rendering them inoperable.

The failure to

declare the doors inoperable and enter a TSAll entry for t % applicable

TS Action Statement in accordance with OMP 2-29 was identitied as a

Violation of TS 6.8.1. Procedures and Programs. This failure to follow

procedures constitutes a violation of minor significance and is being

treated as a Non-Cited Violation (NCV). consistent with Section IV of

the NRL Enforcement Policy. This item is identified as NCV 50 414/97-

09 01:

Failure to Declare Ice Condenser Intermediate Deck Doors

Inoperable and Log Appropriate TSAll Entry.

Auxiliary Shutdown Panel Volume Control Tank (VCT) Instrumentation Drift

During a walkdown of the four Motor Driven Auxiliary Feedwater Shutdown

Panels, the inspector identified that three of the four VCT level

indications were not reading accurately.

There is one VCT gauge on each

Shutdown Panel. Gauge indications differed from control room

indications by as much as 20 percent level.

The ins)ector alerted

operations-personnel to-the problem and noted that t1ey were very

responsive in initiating corrective actions.

Due to subsequent problems

in calibrating the gauges and unavailability of like parts, engineering

modifications were developed and implemented to replace the gauges with

more accurate models.

Based on discussions with Instrumentation and

Electrical (IAE) personnel, it was indicated that most likely, the

gauges had drifted out of accuracy over a long period of-time.

The inspector reviewed periodic surveillance test procedures associated

with verifying Shutdown Panel instrumentation indications.

VCT level

was not among the indications checked periodically.

The inspector

noted. however, that VCT level was not required by TS to be o)erable

from the Shutdown Panels.

However, the VCT indication could )e

potentially used during operation from the Shutdown Panels.

It was also

apparent that-there had been opportunities to have identified the gauge

output drift during the periodic surveillances of other Shutdown Panel

instrumentation.

Enclosure 2

_________ __- _ _

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l

4

Unit 2 Power Rance Channel NI-42 Soare Window Illuminated

On June 27. 1997, the day after Unit 2 tripped on low Reactor Coolant

System flow, the inspector noticed an annunciator window on the Nuclear

Instrument (N1) 42 Power Range drawer that was illuminated.

The

annunciator window was labeled " spare" and appeared to serve no

function.

The inspector questioned the control room operators about the

illuminated window. The window apparently first illuminated following

the trip; however, the operators were not aware that the window was

illuminated, nor the reason for the condition.

Based on subsequent

discussions with reactor engineering personnel, the inspector learned

that this spare annunciator window was previously used as the negative

rate trip indication light. During the previous refueling outage. this

trip function was isolated from the reactor protection logic, the

modification that implemented the rate trip change was supposed to have

removed the bulb from these windows on all of the N1 drawers. .It was

believed that the bulb in the NI-42 drawer was removed, but may have

been reinstalled by lAE personnel by mistake during subsequent NI

maintenance activities following the refueling outage. The light was

extinguished once the rate trip function was reset and the bulb. removed.

The licensee initiated a PIP to address this problem.

TS Loaaina Error for Trackina Containment Airlock Door Seal Surveillance

lRR

On July 11, 1997, during review of the Unit 2 TSAIL. the inspector

noticed an incorrect entry that was made on July 9.

The entry was for

tracking a TS required 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> airlock door seal test following opening

of the airlock door on July 9.

The time required for the test to be

performed was listed in TSAIL as July 16 instead of July 12.

The

inspector discussed the error with operations personnel who corrected

the entry.

It was also indicated that the seal test was scheduled to be

performed that same day.

Based on this, the inspector determined the

test would not have been missed even though the TSAll was incorrect.

The inspector was concerned that the TSAll error had not been identified

over the two previous two days that the problem existed.

Individually, the above problems had little actual safety consequences.

however, in the aggregate represented the need for greater attention to

detail and questioning attitude by operations personnel during the

performance of routine activities.

01.2 Unit 2 Reactor Trio on low Reactor Coolant System Flow-

a.

Insoection Scope (71707. 937,01).

On June 26 a Unit 2 reactor trip from 100% power occurred when the 2B

Reactor Coolant Pump (RCP) tripped and caused a loss of flow signal in

the associated loop. The inspector discussed the unit trip with

engineering, operations and maintenance personnel, as well as reviewed

the associated electrical diagrams. Unit Trip Report and Pl? 2-C97-2221.

Enclosure 2

l

5

i

b,

Observations and Findinas

On June 21. a negative leg ground was detected on ron vital distribution

i

!

bus 2CDB.

The ground subsequently was traced to tre 125 VDC control

l

power circuit of breaker 2T6 6.

On June 26. the b"eaker was opened to

facilitate troubleshooting the cause of the ground.

The Instrument and

'

Electrical (IAE) technicians noticed that the breaker failure initiation

l

.

relay in 2TB 6 control cubicle was chattering, but continued with their

i

troubleshooting activities.

Shortly thereafter, a reactor trip

occurred.

The licensee determined that. the source of the ground fault was the

breaker pushbutton, a Cutler-Hammer E30 model,

lhe pushbutton had

'

failed and created a negative leg-to ground fault on 2CDB. The

pushbutton internals had changed state when 2TB 6 was tripped open

during troubleshooting, introducing a fault path to the positive leg.

Noise from the cabinet ground was induced through the switch and the

breaker failure initiation relay (94B) coil, causing it to chatter and

eventually actuate to trip the incoming breaker on the short bus of 2TB.

The auto close function of the 2TB tie breaker was blocked by a lockout

rela

bus,y, and the bus de-energized. The 2B RCP. which is supplied from the

tripped, and the subsequent low flow in the B loop caused a reactor

trip.

The inspector discussed the reactor trip with operations and engineering

personnel to determine if the root cause involved a human error. The

chattering of the relay, generated when 2TB 6 was opened, could have

been stop)ed if the IAE technicians had reclosed the breaker when they

noticed tlat relay chattering.

However, they did not understand what

was causing the chattering at the time.

The inspector concluded that

the IAE technicians responded appropriately by leaving the breaker in

the opened position since the cause and impact of the relay chattering

were not understood.

The inspector inquired about the time delay between ground detection

(identified on a Saturday) and troubleshooting activities (initiated the

following Wednesday).

l.icensee personnel indicated that Single Point Of

Contact (SPOC) technicians were not trained and qualified to use the

ground chasing equipment.

As a result a'stempts to locate the ground

could not be made until the following Monday when a trained IAE

technician would be available. Also, priority status was not associated

with troubleshooting the ground indication early in the week.

In

addition, the inspector determined that only two techniciant on site

were fully qualified to use the ground-chasing equipment to locate the

source of a ground, and that_one of those technicians had been offsite

since February and was not scheduled to return until October of this

year. A shortage of trained personnel available to perform the

troubleshooting contributed to the delay.

At the end of the ins)ection

period, the delay in investigating the ground, associated contri)uting

factors, and appropriate corrective actions were not addressed within

the licensee's corrective action program.

Enclosure 2

.

6

The unit was restarted on June 28 after trip list activities were

performed and minor equipment problems were corrected. The licensee is

'

planning to document the reactor trip in a Licensee Event Report.

l

c.

Conclusions

The inspector concluded that root cause evaluations of the reactor trip

were adequately performed.

The cause of the tt!p did not involve human

error or non conservative decision making. The protective relaying

associated with the short bus of 2TB functioned as designed. The

inspector determined that, although the delay in troubleshooting

activities to locate the source of the ground did not affect the outcome

(reactor trip), challenges existed in the following areas: (1)

associating appropriate priority to locating ground indications in a

timely manner, and (2) ensuring that trained personnel are avullable to

troubleshoot ground indications. At the end of the inspection period,

efforts to address the delay, understand its causes, and identify

corrective actions were not evident in the licensee's corrective action

program.

'

01.3 Unit 2 Downoower in Response to Generator Outout Breaker Trouble

a.

insoection Scone (71707)

On July 2. Unit 2 control room operators received a generator breaker

trouble alarm and identified a continuous decrease in minimum close air

3ressure on 28 Main G2nerator Power Circuit Breaker (PCB). Operators

Jegan a rapid load reduction, and the PCB automatically tripped after

reactor power reached 50%.

The inspector reviewed PIP 2 C97 2177 and

discussed the downpower and associated equipment failure with licensee

personnel.

b.

Observations and Findinos

On July 2, the Main Generator PCB 2B Trouble annunciator alarmed in the

control room.

Control room operators determined that there was a

continuous decrease in air 3ressure on the 28 Main Generator PCB,

indicating an approach to 11e minimum air pressure is required to open

the breaker. Air

' the resulting arc. pressure is required to open the breaker and dissipate

Since the safety function of the PCB was to open, it

was designed to automatically open before the minimum pressure required

for this function is reached.

The minimum tri

Generator PCB 2B is between 446 and 452 psig. p pressure on Main

To preclude an automatic turbine runback on the potential automatic

opening of the PCB operators began a rapid load reduction, The PCB

automatically tripped after reactor power reached 50%.

No overcurrent

alarms were received on Main Transformer 2A.

The license deternJned that a solenoid (or )ilot) valve associated with

I

the air sup)1y to a:1 three main generator )CB poles had failed,

s

rendering t1e air system unable to deliver air to the breaker.

Normally, the solenoid valve receives signals from the breaker poles to

Enclosure 2

V

7

i

supply air to them. When the air pressure on any pole reaches

,

a> proximately 485 psi.-a pressure switch actuates and the solenoid valve

sluttles to pneumatically control a regulator that delivers air to the

breaker poles. When air pressure is restored to 500 psi the signal

from the pole to the solenoid is terminated.

'

Station PIP 2-C97-2177 documented the root cause of the solenoid

failure.

The failed solenoid was new and had been installed during the

April 1997 refueling outage.

The component failure was attributed to a

deformed nylon bushing.

The valve had been assembled to compensate for

the defect which initially allowed the valve to operate as designed.

However, the valve's internal components drifted from their assembled

positions over time and eventually were unable to engage with the

valve's lower assembly, thereby preventing air flow to the poles.

To address the potential that newly purchased solenoid valves could be

installed with problems, the licensee had revised procedure

IP/0/B/4974/01, Main Generator PCB Maintenance. - Revision 5 of the

procedure included a Note between Steps 10.3.7 and 10.3.8. The-Note

read: "If pilot valve is replaced, ensure pilot valve has been

disassembled and inspected for pro>er assembly and components. or

rebuilt prior to installation." T1e inspector verified that this

procedure change had been made,

c.

Conclusions

The inspector concluded that control room operators were effective in

)recluding a turbine runback by reducing reactor power to 50% before the

3CB opened.

The licensee's root cause evaluation was detailed and

actions to prevent recurrence were adequate.

01.4 Lower Containment Air Temoerature Exceeded for Short Duration

a.

Insnection Stone (71707)

On June 30. the licensee was performing maintenance on the Unit 2

Lower Containment Ventilation Units (LCVUs). While the 2A and 20

LCVUs were out of service, the lower containment temperature

increased to 117.4'F. The inspector reviewed apalicable operating

procedures. TS. the FSAR, tagout requirements, tie innage work

schedule, and PIP 2 C97-2127.

The inspector also discussed the

-issue with operations, engineering and work control personnel.

b.

Observations-and Findinas

During normal operation. the Containment Chilled Water (YV)

chillers service various containment loads including the LCt!Us and

the Reactor Coolant Pump (RCP) Motor Air Coolers.

0_n June 30,

preventive maintenance (PM) and electrical motor testing were

scheduled for the 2A and 20 LCVUs. The 2A LCVU was removed from

Enclosure 2

I

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8

l

service first.

After the PM for the 2A LCVU was completed, but

i

before motor testing was completed, operations personnel decided

to remove the 2D LCVU for PM.

The 2D LCVU was removed from

,

service at 10:55 a.m.

While both LCVUs were out of service, lower

containment temperature increased.

To compensate for the

temperature increase, control room operators adjusted the

o)eration of the remaining inservice LCVUs (2B and 2C) from

"iormal" to "High Speed." and then to " Max Cool." However, for a

brief period of time lower containment temperature had exceeded

the high high temperature Operator Aid Computer (0AC) alarm

setpoint of 115.6'F and the adjusted TS limit of 117.2*F.

ultimately reaching 117.4'F.

Lower containment temperature was

',

above 117'F for approximately 3 minutes before it was restored to

within TS limits.

The Action required by TS 3.6.1.5 was to

,

i

restore the air temperature to within the limits within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> or

.

be in at least hot standby within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />. Since the

!

bich lower containment temperature existed for only a few minutes.

-

th6 licensee was in compliance with the TS action.

.

At anroximately 11:10 a.m., operations personnel decided to post)one

the M on the 2D LCVU. recall the associated tags and return the _CVU to

service until the 2A LCVU was restored to operation.

While operators

i

were returning the 2D LCVU to service and all three LCVUs to normal

alignment, the YV chillers in service (A and C) trip>ed on low flow.

Based on a review of the circumstances surrounding t1e trip of the A and

,

C YV chillers, the inspector discerned that the following took place.

When the B and C LCVUs were taken to " Max Cool" in an effort to reduce

!

lower containment temperature, the flow control valves in the chiller

loop fully opened as designed, and thermostatic control of,the chilled

water supply was lost. When operations subsequently restored the D LCVU

to service and returned the LCVUs to normal operation, thermostatic

i

control of the flow control valves was reinstated.

The existing

temperature caused the flow control valves to throttle closed, and the

chillers tripped on low load.

Normal alignment with the A and B YV

chillers was established within 30 minutes of the chiller trips. The C

YV chiller had also been restarted, but tripped after running for 10

minutes.

Shortly thereafter, containment temperatures were restored to

normal levels.

Operations surveillance procedure PT/1/A/4600/02A. Mode 1 Periodic

Surveillance Items. Enclosure-13.1. Periodic Surveillance Items Data,

approved January 23, 1997, provides surveillance acceptance criteria in

-

accordance with the lower containment temperature limits imposed by TS 3.6.1.5.

Lower containment minimum and maximum air temperature limits

are based on the average inlet temperatures of the operating LCVUs.

Temperature readings associated with non running LCVUs provide

indication of static air temperature and therefore, are not used to

determine average containment air temperature.

Therefore. temperature

':mits are adjusted conservatively as a function of uncertainty (because

of the reduced sample size) in generalizing local indications to average

Enclosure 2

1

..-._..__ ,,

,a..

._-..,....,--...--m.__-

-

- - _ _ - _ . . _ .

.

.-m.

-

-

-

9

containment air temperature. As the number of LCVUs in service

decreases, the temperature limit decreases (becomes more conservative).

With two LCVUs running. the lower containment TS limit of 120*F was

adjusted to 117.2'F.

The Containment Lower Compartment Ventilation Subsystem as

described in the FSAR is designed to maintain a maximum

temperature of 120*F in the lower compartment during rnrmal plant

operation.

During normal operation, three units (each providing

33.3% capacity) are in service, and one unit is on standby.

3

Technical Specification Interpretation 3.6.1.5 states that

!

containment air temperature can be maintained with one active

component out-of-service (i.e., three LCVUs in service).

Based upon a review of the FSAR and TS as well as discussions

with on-shift operators, the inspector determined that the

4

decision to remove the D LCVU from service while preventive

maintenance (PM)s on the A LCVU were ongoing was non conservative

and caused lower containment temperature to exceed the adjusted TS

limit.

The inspector also determined that problems existed with procedure

OP/2/A/6450/01. Containment Ventilation Systems. dated June 15. 1994,

which controls the configuration of the LCVUs. The procedure did not

provide adequate guidance to address the impact of removing two LVCus

from service on lower containment temperature.

Operations Management

Procedure 2-18. Tagout Removal and Restoration Procedure. Revision 46.

Responsibility 4.8. states that the person placing or removing tag (s)

shall check procedures affected and any outstanding tagouts associated

with that procedure / system for any adverse effects.

Because the adverse

impact of removing 2 LCVUs from service was not addressed in the

procedure, this responsibility could not be effectively realized.

n addition, procedure OP/2/A/6450/01 did not address the interaction

between LCVU operation and integrated Containment Ventilation (VV)

Systems.

Step 2.7.3 of OP/2/A/6450/01. Enclosure 4.12. LCVU Additional

Cooling and YV Chiller Trip Prevention directs the operator to ensure

that three LCVUs are in the " NORM" position. The performance of this

step caused the A and C YV chillers to trip.

Procedure

slowly reduce the demand on the system was not provided, guidance to

nor was a

precaution or note provided to warn of the potential to induce a chiller

trip as a function of load demand changes.

The inspector also noted that no procedure guidance was available for

swapping between running and_non running LCVU units. OP/2/A/6450/01.

Enclosure 4.2. Lower Containment Ventilation Unit Startup and Normal

Operation, provided procedural guidance for starting up the system by

placing three LCVUs in operation.

Enclosure 4.7. Lower Containment

Ventilation Unit Shutdown provides procedural guidance for shutdown of

the system by placing all four LCVU switches in the OFF position.

Enclosure 2

-

l

10

However, no procedural guidance existed for stopping an individual LCVU

and subsequently restarting it or making other required alignment

changes needed to facilitate the performance of the PM. The inspector

recognized that this lack of procedural guidance was unrelated to the

lower co'itainment temperature increase and the YV chiller trips.

l

The inspector also identified a minor discrepancy in the planned

l

innage work schedule.

The 2A LCVU had two work items planned to

be worked which included a PM and electrical motor testing.

The

PM on the 2A LCVU was scheduled to be completed at 12:00 p.m. on

June 30, 1997.

The motor electrical testing on the 2A LCVU was

scheduled to be completed at 1:00 p.m. on June 30.

The PM on the

20 LCVU was scheduled to commence at 12:00 p.m. on June 30.

immediately following the scheduled completion of the PM on the 2A

LCVU.

This schedule allowed both the A and 0 LCVUs to be out of

service for 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />, which was non conservative and not in

accordance with the alignment described in the FSAR.

c.

Conclusions

The inspector concluded that the decision to deviate from the

preferred normal alignment of LCVU operation to support planned

maintenance exhibited non conservative work scheduling and

operator judgement.

As a result. lower containment temperature

increased slightly above the adjusted TS limit for a brief period

of time.

However, temperatures were reduced below the adjusted TS

limit within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> as required by the TS action requirement.

Therefore, exceeding the lower containment air temperature on

plant equipment had minor safety significance and did not pose a

threat to safety related equipment. The LCVU operating procedures

did not address the adverse impact of removing two LCVUs from

service. simultaneously. nor did the procedure address the

interaction between LCVU operation and integrated containment

ventilation systems. These procedural inadequacies constituh a

violation of TS 6.8.1. Procedures and Programs. This failure

constitutes a violation of minor significance and is being treated

as a NCV. consistent with Section IV of the NRC Enforcement

Policy.

This item is identified as NCV 50-414/97-09-02:

Inadequate LCVU Operating Procedure.

08

Hiscellaneous Operations Issues (92901)

,

08.1

(Closed) Un.reigh.ed_Ltem (URI) 50-413.414/94-13-02:

Emergency Operating

Procedure (EOP) 50.59 Evaluations Not Reviewed by Nuclear Safety Review

Board (NSRB) as Required by TS

This item was related to an apparent failure to meet the TS requirement

for the NSRB to review 50.59 evaluations for E0P changes. The

inspector's review determined that the re

being appropriately reviewed by the NSRB quired 50.59 evaluations were

The licensee's procedures had

Enclosure 2

__-_______ __-_ - _ _ - .

11

been inconsistent in defining the 10 CFR 50.59 screening evaluation and

the 10 CFR 50.59 Unreviewed aafety Question (US0) evaluation. The TS

requirement was intended for the NSRB to review the 10 CFR 50.59 U50

evaluations. Nuclear Site Procedure NS0-209, 10 CFR 50.59 Evaluations.

Revision 6. was revised after 1994 to clearly define the two

evaluations. The licensee initiated a change to NSD 703. Administrative

Instruction for Station Procedures, to clearly distinguish on the

procedure change process documentation whether the evaluation performed

was a screening evaluation or an USQ evaluation. The inspector reviewed

three US0 evaluations for E0P changes and verified the US0 evaluation

,

'

had been sent to the NSRB_for review. A 1995 evaluation had been

i

reviewed and two 1997 evaluations were scheduled for review at the next

NSRB meeting.

The inspector concluded that this issue was adequately

resolved and the TS requirements had been met by the licensee.

During the invettigation of the above issue, the inspector reviewed

a) proximately 20 examp',cs of 10 CFR 50.59 screening evaluations for E0P

c1anges and identified a deficiency in the licensee's procedure

implementation of this activity.

Specifically, the justifications for

the screening questions were inadequate in many changes.

The

justifications were inadequate in that they only repeated the screening

question as a negative statement. NSD 209, 10 CFR 50.59 Evaluations.

Revision 5. required the doca,3ntation of justification for responses to

50.59 screening questions.

It further stated that justifications should

be complete enough so that an independent reviewer cculd come to the

same conclusion.

The following E0P change 50.59 screening evaluations

were inadequate and did not meet the applicable procedure requirements:

o

EP/2/A/5000/FR 1.2 dated November 17, 1995

EP/1/A/5000/FR-1.1 dated September 19. 1996

e

OF/1/A/6350/08 dated February 28. 1996

EP/2/A/5000/F-0 dated March 26, 1997

e

EP/1/A/5000/FR H.1 dated August 16, 1996

e

EP/1/A/5000/FR-H.1 dated January 30, 1995

This failure to follow NSD 209 for 10 CFR 50.59 screening evaluations,

is identified as the first example of Violation (VIO) 50 413.414/9/-09-

04:

Failure to Follow Procedure. The inspector did not identify any

US0 condition related to the inadequate 50.59 screening evaluations.

The inspector noted that the 50.59 screening evaluations for E0P changes

were performed by the Operations organization.

Previous inspections of

50.59 evaluation performance have concluded that the Engineering

organization performed to a high standard in this area for 50.59

evaluations related to modifications.

Although both organizations

Enclosure 2

12

receive the same training and use the same procedures. Operation's

performance in this activity was deficient as previously noted. The

inspector reviewed a 1997 50.59 USO evaluation for an E0P change.

This

evaluation was good in that it included a well detailed justification

for responses to the USQ evaluation questions.

This indicated that the

>

Operations deficient performance was related only to the 50.59 screening

evaluations.

II. Maintenance

l

M1

Conduct of Maintenance

1

M1.1 Electrical Flash Durinn Breaker Preventive Maintem nte

a.

Inspection Stone (62707)

The inspector reviewed the circumstances and the licensee's corrective

actions associated with an electrical flash that occurred inside a 600

Volt non safety-related breaker cubicle while periodic breaker PM was

being performed. The electrical flash resulted in a minor personnel

injury and extensive damage to the breaker cubicle.

b.

Observations and Findinas

On June 3. 1997, an Instrumentation and Electrical (IAE) technician was

aerforming PM on 600 Volt breakers 2MXM-F09C and 2MXM-F090.

These

areakers supplied power to two Unit 2 ice condenser refrigeration air

handling fans. The PM activity involved testing the overcurrent

protective devices associated with the breakers.

The technician had

removed breaker F09C from its cubicle and was in the process of removing

breaker F090 from its cubicle. While removing F090, an electrical ficsh

occurred in the F09C cubicle, which was located directly above F09D.

The technician received minor facial burns. but was not seriously

injured.

Breaker F09C was electrically welded in its cubicle as a

result of the electrical fault,

The inspector responded to the breaker

work location and noted good licensee immediate actions in response to

the incident. These actions included terminati'

11 PM work, roping

off the area for personnel safety consideratior .

nd initiating a

Failure Investigative Process (FIP) to determine the root cause of the

electrical fav a.

On June 6, 1997. Motor Control Center 2MXM was de energized, and the

breaker cubicle for F09C inspected.

The damage to the bus was minimal;

however, the stabs for F09C were badly damaged and recuired replacement.

Both breakers F09C and F09D were repaired, tested, anc returned to

service.

The inspector attended the PORC meeting conducted to discuss

the repair plans and noted that management performed a thorough review

of the plans with good discussions on the impact of the work planned on

the plant. The repairs were completed without incident.

Enclosure 2

_____

-

13

The FlP team was thorough in their investigations and determined that

the stabs b? hind breaker F09C had come in contact with the energized

bus.

Since the breaker power connecting cables had been determed and

left untaped in the bottom of the breaker cubicle. an electrical ground

path was created when the cables were re energized. The FIP determined

the method for racking the breaker out in the maintenance position was

inadequate.

In the maintenance position a lock tab on the front of the

breaker cubicle had been used to position the breaker away from the bus;

l

however this method did not provide sufficient distance between the bus

and stabs. While this method had not resulted in any problems in the

past, the result of having two breakers in the maintenance position,

located one above the other, created an even smaller bus / stab distance

that resulted in electrical flash over.

As a result of the FlP investigations, instrumentation procedures

governing work on 600 Volt breakers were revised to change the method of

racking out these breakers for maintenance.

Instead of using the lock

tab, procedures directed that a padlock be placed on the breaker or the

bteaker be removed completely to ensure adequate stab / bus distance is

maintained.

In addition, IAE personnel involved with breaker work were

to be provided training on this new method of racking 600 Volt breakers

out to the maintenance position.

c.

Conclusions

The inspector concluded that the FlP team was thorough in investigating

the cause of the electrical flash.

The root cause evaluation revealed

configuration weaknesses in the method of locking out 600 Volt breaker

cubicles to the maintenance position. The inspector determined that the

licensee adecuately implemented corrective actions to prevent recurrence

of this incicent.

M1.2 'Jngdeounte Leak Rate lest of Unit 2 Containment Isolation Valve

a,

insoection Scope (40500. 61726. 62707)

On June 4,1997, the licensee identified that Unit 2 containment

isolation valve 2NV 874 had not been properly Type C leak rate tested in

accordance with 10 CFR 50. Appendix J during the previous. refueling

outage.

On June 6. the valve was properly tested and failed the Type C

leak rate test. -The valve disc was replaced, and the valve was

successfully tested on June 7.

The licensee submitted LER 50 414/97-004

. to document the inadecuate leak cate test conducted during the outage.

The inspector reviewec the circumstances associated with the inadequate

testing, attended PORC meetings to discuss retesting valve 2NV-874

online, witnessed aspects of the June 6 retest, reviewed leak rate test

results, and discussed the incident with engineering and Operations Test

Group (OTG) personnel,

Enclosure 2

_

-

i

14

b.

Observations and Findinas

On &ne 4.1997 the OTG Suaervisor was conducting a procedure

completion verification of Jnit 2 Periodic Test (PT) procedure

PT/2/A/4200/01C. Containment Isolation Valve t.eak Rate Test.

This

procedure had been performed during the previous refueling outage in

1

April 1997. During the review, the supervisor idcntified that Step

2.2.3 of Enclosure 13.7. Penetration No. M228 Type C 1.eak Rate Test had

been marked "Not Applicable by the OTG technician performing the test.

I

,

resulting in the step not being performed. This step required test vent

I

flow path valve 2NV 873 to be opened while testing inside containment

isolation check valve 2NV 874 (associated with the Standby Makeup System

'

flowpath to the reactor coolant pump seals). Without an open test vent

flowpath, the leak rate test on 2NV 874 had been invalid.

The inspector verified that appropriate actions were implemented upon

identification of the invalid lea ( rate test. These actions included

2NV 874 being declared inoperable and in accordance with TS 3.6.3,

the

outboard containment isolation valve (2NV 872A) in the penetration was

closed and power was removed from the valve operator within four hours.

The inspector attended the June 5 and 6 PORC meetings conducted to

discuss activities to retest 2NV-874.

Management thoroughly discussed

the impact on the plant with testing the valve while online.

In

addition engineering developed a special leak rate test procedure and a

detailed briefing package explaining the necessary actions for

controlling the retest activities.

On June 6. the inspector witnessed aspects of the leak rate test on 2NV-

874. The inspector noted that testing was well controll?d and performed

in accordance with the test procedure.- The valve was not able to be-

pressurized and resulted in-a failed leak rate test.

Valve maintenance

was performed resulting in replacement of the valve disc and disc

spring. A subsequent leak rate test was performed following the

maintenance activity.

The inspector reviewed the results of this

testing which verified that leakage was within acceptable limits.

Following successful testing 2NV 874 was declared operable and the

penetration was returned to its normal configuration,

C_Qn.clusions

c.

n

The inspector concluded the identification by the OTG Supervisor of a

procedure discrepancy that resulted in an invalid leak rate test of nD-

874 was an example of good questioning attitude. The PORN performed a

thorough review of subsequent activities to properly perform the leak

rate test. Good engineering support was )rovided, both in developing a

leak rate test procedure and briefing paccage for the evolution.

The inspector noted that the procedure completion review was not

performed by the OTG Supervisor following actual completion of all

testing or prior to plant startup from the refueling outage.

Since this

Enclosure 2

_ _ _ _

-

. . - _ .

__-

--_

---

- -

-

- - . . - - _-

_.

15

l

was the only review that was recuired following test procedure

completion, the inspector consicered the review untimely.

Had this

review been completed prior to plant startup, this problem may have been

identified and corrected arior to the unit entering a mode recuiring

containment integrity.

T1e failure to open test vent valve 2hV-873

during/4200/01C was identified as a violation of TS 6.8.1. leak rate testing of

PT/2/A

This issue

is identified as Violation E0-414/97-09 03:

Failure to Follow Procedure

Results in Invalid Local Leak Rate Test of Valve 2NV 874.

M8

Miscellaneous Maintenance Issues (92902.

l

M8.1 (Closed) VIO 50 413. 414/97-01-01: Failure to Include all Structures.

S stems and Components in the Scope of the Maintenance Rule as Required

b 10 CFR 50.65

This violation was identified when the inspectors determined that the

licensee had incorrectly excluded a number of structures. systems and

components from the scope of the Maintenance Rule.

The licensee

acknowledged the violation and issued a Problem Investigation Process

(PIP) report PIP No. 0 C97-0419. to document correctivo actions taken

!

and, track the progress made in addressing the issues.

The systems

affected included Nuclear Sampling (NM). Main Steam to Auxiliary

Equi) ment (SA). Auxiliary Building Chilled Water (YN) and Ice Condenser

l

Hitti Pins (NF).

Following a review by the site Expert Panel these

'

systems or components were added to the scope of the Maintenance Rule.

Corrective actions taken or planned included a review of the 239

functions that had been excluded from the Maintenance Rule scope. This

'

review was scheduled for completion in December 1997.- and will be

documented in PIP No. 0-C97-0419,

In addition, structures and functions

excluded from the Maintenance Rule will be reviewed for Generic Scoping

applicability. The due date for this review is also December 1997. The

inspectors concluded the licensee's corrective actions were appropriate.

,

M8.2. (Closed V10 50-413.414/97 01-04: Failure to implement the Requirements

of (a)(1) and (a)(2) of the Maintenance Rule

l

This violation was identified when the inspectors determined that the

l

licensee was using Forced Outage Rate (FOR) instead of Unplanned

l

Capability loss Factor (UCLF) as a Plant Level Performance Criteria for

!

monitoring A2 systs....; 3er 10 CFR 50.65. The concern was that FOR was

'

not as sensitive as UC F in detecting declining performance in some

systems.

The licensee acknowledged the violation and took appropriate action to

correct the problem.

The licensee incorporated the Plant Transient

Criteria as part of the Forced Outage Criteria. This combination of

criteria was intended to provide appropriate equivalent defense in depth

monitoring as the Unplanned Capability Loss Factor. A Plant level

Enclosure 2

l

.

-

..

._

.

--

-

--

-

1

16

l

Performance Criteria called Plant Transients, which defined unacceptable

performance was added to Engineering Directives Manual (EDM)-210 as Rev.

i

4.

The inspectors concluded the licensee's corrective actions were

'

appropriate.

M8.3 (Closed) Insoector Followuo item (IFI) 50 413.414/97-01-02: Followup and

'

Review of Licensee Procedure to implement the Requirements of (a)(1) and

(a)(2) of the Maintenance Rule after issuance of Regulatory Guide 1.160,

Rev.2

EDM-210." Requirements for Monitoring the Effectiveness of Maintenance

i

at Nuclear Power Plants or the Maintenance Rule " Rev. 5.

revised the

definition of Maintenance such that it was now in agreement with

Regulatory Guide 1.160. Rev. 2, dated March 1997.

Revision 5 of the EDM

now considers any operator action performed in support of Maintenance as

a Maintenance Preventable Function Failure (MPff) candidate.

In

addition, the flow gra)h of Appendix A to the subject EDM, were revised

for clarity.

One of tie two was revised from Vendor Error to Off-site

Vendor Services while the other from Operations or Plant configuration

control to Operation or Plant Configuration Control not associated with

a maintenance activity.

The inspectors concluded the licensee's

i

corrective actions were appropriate.

M8.4 (Closed) IFT 50-413.414/97-OL-01 Followup on Licensee Actions to

Provide Performance Criteria for Structures After Resolution of this

Issue

EDM-210. " Requirements for Monitoring the Effectiveness of Maintenance

at Nuclear Power Plants or the Maintenance Rule." Rev. 5. changed the

3erformance criteria for all Maintenance Rule structures to comply with

legulatory Guide 1.160. Rev. 2.

This criteria applies to both risk and

non-risk significant Maintenance Rule structures.

EDM 410. " Ins)ection Program for Civil Engineering Structures and

Components." Rev. 1. dated June 16, 1997, is the controlling document

for monitoring and assessing civil engineering structures and' components

to the requirements of 10 CFR 50.65 and Regulatory Guide 1.160,.Rev. 2.

dated March 1997. It provides examination guidelines, acceptance

criteria and documentation requirements.

As such. Catawba civil

,

engineering was responsible for implementing the ins)ection program for

l

structures and components.

The inspectors reviewed EDM-410. Rev. 1 for

content and adequacy.

The inspectors noted that the procedure provided

adequate guidelines and the acceptance criteria contained within,

followed Regulatory Guide 1.160. Rev. 2 guidelines for acceptable and

.

unacceptable performance criteria.

l

l

Through discussions and document review, the inspectors ascertained that

the inspection program for structures was adequately administered and

implemented.

Responsible engineers had received training and were

familiar with Maintenance Rule requirements as they applied to their

area of responsibility.

5

Enclosure 2

L

___

_--

.

.

..

.

..

_

_

__

,

/

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

__

- _ __

_ _ _ _ _ _ _ _ _

17

At the close of this inspection. 39 structures had been inspected and an

additional 120 were scheduled for inspection by year's end.

Ins)ection

per the revised EDMs -210 and -410 commenced on July 1, 1997.

T1e

inspectors reviewed the licensee's classroom training material. ES-CN-

97-21. used to cormiunicate Regulatory Guide 1.160. Rev. 2 guidelines.

Training of personnel was held between June 9 and 18. 1997.

The

inspectors concluded the licensee's corrective actions were ap]ropriate.

III. Enaineerina

El

Conduct of Engineering

El.1 Primary and Secondary Thermal Power DiscreDancy

a. -Insoection Stone (37551)

On July 15 the licensee discovered a discrepancy of approximately 0.6%

between the Unit 2 primary and secondary thermal power indications.

Secondary thermal

was reduced to 99. power was immediately reduced to 99.3% (reactor power

7%) and a FIP team was initiated to determine the

cause of the discreaancy. The inspector attended management briefings

by the FIP team mem)ers on the progress of their investigation: reviewed

associated TS and TS Interpretations: and discussed the issue with

Operations. Engineering and Maintenance personnel.

b.

Observations and Findinas

On July 15. Operations personnel were notified by the reactor

engineering group that there was a 0.6% discrepancy between primary and

secondary thermal power indications, and that actual thermal Jower might

be greater than the secondary thermal power (the designated tiermal

power best estimate) indication. The reactor engineering group

discovered, during a routine review of secondary plant parameters, that

primary thermal power had slowly increased over time since the Unit 2

restart from the April 1997 refueling outage.

A FIP team was initiated

to determine the cause of the discrepancy, and control room operators

decreased reactor aower to 99.3%. Tae reactor was operated at 99.3%

power until the FI) team could determine the cause of the discrepancy.

The FIP team determined, during the course of their investigation, that

theT,Yto586.9F. indication had been drifting downward since May 11, 1997, from

587.3

Operations responded by decreasing T,,, to minimize

the T * /T

error.

Lowering T,,, caused the reactor to increase AT to

maint'aIn,r,,actorpowerequaltosecondarypower. The drift in the T,,,

e

indication resulted in changes in T

Tm

T,,, and AT but did not

cause a change in indicated or actud3 primary and secondary thermal

power.

Although the FIP team could not attribute this indication drift

to the primary / secondary thermal power indication discrepancy they

determined that a degraded 7300 process card was responsible for the

Enclosure 2

.

.

-

.

-

. . _ .

}

18

drift and initiated plans to have the card replaced after the root cause

of the power indication discrepancy was identified.

The FIP team also determined that indicated feedwater flow had decreased

while steam flow had remained constant.

This was attributed to

feedwater venturi defouling as a function of the new cycle (restart from

the April refueling outage was in early May). the recent reactor trip

(June 26), and was the recent rapid downpower (July 2). The result of

defouling was a decrease in indicated feedwater flow with a

consequential decrease in indicated secondary thermal

maintains secondary Thermal Power Best Estimate (TPBE) power. Operations

near 100% by

periodically opening flow control valves, which in turn causes primary

power to increase to maintain T

defouling caused an increase in.,, for 100% power level. The gradual

actual and indicated primary thermal

power, as well as actual secondary thermal power.

However, the

resultant discrepancy between indicated and actual secondary thermal

)ower accounted for approximately 0.10% to 0.15% of the 0.6% discrepancy

)etween primary and secondary indicated thermal power.

The major contributor (0.3% to 0.4%) to the discreaancy between primary

and secondary thermal power was determined by the

IP team on July 16 as

hot leg streaming. According to Westinghouse, hot leg streaming refers

to the inability to accurately characterize bulk hot leg temperature.

The licensee examined data from the Unit 2 Beginning of C.rcle and

identified changes in the behavior of this phenomenon from previous

cycles.

S)ecifically. calculations revealed that indicated Tw had

increased ay 0.2*F and caused indicated primary thermal power to

increase.

As discussed above these changes were originally masked by

the decrease in primary tem

T,,,/T,,, as a function of T,,,peratures accompanying the decrease in

-

indication drift.

Hot leg streaming has occurred in previous cycles on both units and has

resulted in as high as a 1.0% difference between primary and secondary

thermal power. To account for this, an adjustment factor in the OAC

calculation corrects the discrepancy.

The FIP team concluded that sea:dary thermal power had always been

accurately and correctly indicated, and that primary thermal power

indication did not reflect an actual increase in power level above TS

limits. The inspector discussed the impact of the primary thermal power

indication on Reactor Protection System setpoints and functions.

According to the reactor engineering group, the venturi defouling and

hot leg streaming factors did not constitute a sufficient temperature

error to warrant adjustment via the Reactor Coolant System (RCS)

Temperature Calibration Procedure, which is run quarterly. The OPAT and

OTAT trip strings remained within their TS limits.

In addition, the

nuclear instrumentation system is calibrated to secondary thermal power,

so the associated overpower trip setpoints were unaffected.

Enclosure 2

,

_,

-.-.-.c.

. ---

-

_ _ _ _

- _ _ _ _

- - - - _ _ _ _ - - - -

-

- - - - - -

-

19

Reactor Power was increased to 99.5% on July 16 and the degraded T,q

card was replaced on July 17.

The inspector attended the prejob brief

for the card replacement and observed the work activity in the control

room. The replacement was successfully completed within less than 1

hour and without incidence.

At the end of the inspection period, the

3a

license was considering either performina periodic manual calculations

to the correct the thermal power aiscrepancy, or conducting a full

calorimetric to account for the deviation.

c.

Conclusiqn_q

,

The inspector concluded that the licensee's identification of the

E

thermal power discrepancy exhibited attention to detail and a thm

review of plant data. Actions to initiate a FlP team to invr

g

root cause were appropriate, and steps to reduce reactor po'

a

discrepancy was understood were conservative and indicative

positive nuclear safety ethic.

Replacement of the faulty T,

,a was

well-planned. coordinated and controlled, and executed in an expeditious

manner.

E2

Engineering Support of Facilities and Equipment

.

E2.1 Review of Corrective Actions

a.

Inspedjon Scooe (37550. 92903)

The inspector reviewed Engineering corrective actions to resolve open

itens identified during the development of the station Design Base

Documents (DBDs) and findings from Self-initiated Technical Audits

(SITAs).

Also reviewed were the licensee's actions to address a 10 CFR Part 21 issue related to a defective Emergency Diesel Generator (EDG)

intake / exhaust valve spring. Anplicable regulatory requirements

included 10 CFR 50 Appendix B. ESAR. Technical Specifications and

implementing licensee procedures.

b.

Observations and Findinos

DS_Qs

Developed between 1990 and 1994. DBDs consolidated design and licensing

documentation for selected station systems and programs. The ]rocedure

guidance for development and maintenance of DBDs was provided

ay

Enoineering Directives Manual . EDM-170. Design Specifications, revision

5.

Open items were evaluhed for operability during the DBD development

'

and Licensee Event Reports (LERs) initiated as required.

EDM-170

required the remaining items to be entered into the Problem

Investigation Process (PIP) for tracking and resolution. Additionally,

the l u ensee's February 10. 1997. response to the 10 CFR 50.54f letter

related to the Adequacy and Availability of Design Basis Information.

P

4

N

stated that DBD open items woeli be ente 1

into the PIP for trackir.g

and resolution.

Enclosure 2

.

Mi

20

TM inspector reviewed the resolution of open item in the Reactor

coolant System DBD to sample the adecuacy of item resolution activity.

Approximately 20 items were evaluatec to verify that the PIP and

interfacing station programs evaluated and resolved the open item

issues.

The items were adequately resolved.

An independent industry audit of Catawba in late 1996, identified as a

finding the numerous lon9-term unresolved DBD open items. The response

to the finding was to initiate a blanket PIP (PIP 0-C97-0595 dated

March 5,1997) to cover the systems with the identified open items.

Many of these open items were not previously in the PIP process. The

PIP corrective actions established a schedule to resolve and close the

referenced DBD open items by September 1. 1997,

During this inspection, the inspector identified additional E

'en

items which were not entered into the PIP process nor incluau .d the

blanket PIP. The open items.were included in DBD CNS-1435.00-0002. Post

Fire Safe Shutdown, revision 4. and DBD CNS-1465.00-00-0018. Station

Blackout (SBO) Rule, revision 2.

Although not entered into the PIP

3rocess. the licensee provided meeti g documentation indicating the Post

rire Safe Shutdown open items were being evaluated.

These items were

identified by a November 1995 electrical post fire shutdown review

performeo after the initial DBD development and entered into the DBD by

revision 4 at that time. There was no c: :umented evaluation of

o)erability or A

tie PIP process.ppendix R commitments which would have been addressed by

Following the inspector's identification of this issue

the licensee initiated PIP 0-C97-1918 to track resolution of these open

items.

The inspector identified no significant safety concerns related

to the open items reviewed. This failure to follow procedure for

resolution of DBD open items is identified as the second example of

Violation 50-413.414/97-09-04: Failure to Follow Procedure.

SITAS

The ins)ector reviewed a recently comp'eted SITA report dated June 11.

1997, w11ch reviewed the adequacy of resolution of SITA findings.

The

scope of the audit was good in that it reviewed the resolution of 80

findings from four previous SITAs. The depth of the audit was good in

that corrective act ans were verified through the extent of station

programs (e.g. . PIP work requests, modification etc. .) involved in the

resolution. The findings were well defined and demonstrated an

independent and objective audit. Corrective actions for the findings

hcd not yet been developed.

EDG 10 CFR Part 21 Notice

The inspector ruiewed the licensee's actions to address a Cooper

Industries 10 CFR Part 21 notice regarding potentially defective EDG

intake / exhaust valve springs which was applicable to Catawba. The

notice was initiated in 1991 and revised on May 1. 1997. The licensee

had included an inspection for the spring defect into the EDG

maintenance procedure. A defective spring was identified at Catawba in

1996. The spring was replaced. analyzed, and sent to the vendor for

'

Encloture 2

.

_

._.

_ _ _ _

..

..

.

.

..

.

.

..

21

further analysis.

The licensee's respon.e to the notice on this issue

was appropriate,

c.

Conclusions

Resolution of DBD open items was generally adequate in that no safety

significant issues were identifieo in the open items. A violation was

identified for failure to follow licensee procedure requirements to

enter open DBD open items into the station PIP process for tracking and

resolution.

The audit of SITA corrective actions demonstrated that the

.

licensee was aggressively following SITA findings and is identified as a

strength in corrective action performance. Additionally, the licensee

adequately addressed the EDG 10 CFR Part 21 issue related to potentially

defective intake / exhaust springs.

E3

Engineering Procedures and Documentation

E3.1 Chanaes. Tests. and Exneriments Performed in Accordance With

10 CFR 50.59 (thru December 31. 1996)

a.

Insoection Scone (37551)

'

f

By letter dated March 31, 1997. Duke Power Company (the licer.see)

submitted its annual summary of all changes, tests, and experiments,

which were completed under the provisions of 10 CF,150.59 for the period

through December 31. 1996. The licensee's March 31, 1997, summary

included approximately 380 changes made during the subject period. The

inspector evaluated these changes against the p,avisions of the

regulation.

<

b.

Observations and Findinas

In accordance with 10 CFR 50.59, a licensee may:

(1) make changes in

the facility as described in the safety analysis report, (2) make

changes -in the procedures as described in the safety analysis report,

and (3) corduct tests or experiments not described in the safety

analysis report, without prior Commission approval, unless the change

involvy a changc in the Technical Specifications or an Unreviewed

Safety duestion (US0). The regulation defines an US0 as a proposed

action that:

(a) may increase the probability of occurrence or

consequences of an accident or malfunction of equipment important to

safety previously evaluated in the safety analysis report, or (b) may

create a possibility for an accident or malfunction of a different type

than any previously evaluated in the safety analysis report or (c) may

reduce the margin of safety as defined in the basis for any Technical

Specification.

The inspector reviewed the licensee's current (dated March 10. 1997)

version of Nuclear System Directive 209. "10 CFR 50.59 Evaluations."

which is patterned after NSAC-125. " Guidelines for 10 CFR 50.59 Safety

Enclosure 2

.

_ _ _ _

_--

__

--

22

Evaluations." June 1989.

This document requires that changes be

evaluated against the appropriate Final Safety Analysis Report (FSAR).

Technical Specifications, end NRC Safety Evaluation Report sections to

determine if there is need for revision.

Specifically, the criteria

specified by 10 CFR 50.59 are broken down into seven (7) questions.

For

a change to be qualified for 10 CFR 50.59, the answers to all seven

questions must be "no".

Based on review of this document, and the

review of the licensee's 10 CFR 50.59 evaluations. the inspector

concluded that the licensee's directive appropriately reflects the

criteria of this regulation and that. if followed accordingly, should

ensure that a change would be correctly performed under this regulation.

The inspector performed an in-office review of the licensee's summary to

determine the nature and safety significance of each change. Through

this review, the inspector selected the following changes for more

detailed review onsite:

e

Exempt Changes:

Exempt Change CE-3176

Exempt Change CE-3705

Exempt Change CE-3759

Exempt Change CE-4745

Exempt Charge CE-4746

Exempt Change CE-4821

Exempt Change CE-4822

Exempt Change CE-7416

Exempt Change CE-7977

Exempt Change CE-8126

Exempt Change CE-8182

Exempt Change CE-8245

Exempt Change CE-8410

Exempt Change CE-61008

Exempt Change CE-61162

Miscellaneous Changes:

e

SIMULATE (a computer code) Version 4

Modifications:

NSM CN-11371

NSM CN-20396

0:?rable But Degraded Evaluations:

o

PIF 2-C97-0157

PIP 2-096-3250

Operability Evaluations:

e

Enclosure 2

_

~

. - _ _ _ _ _ _ _ _ _ _ - _ -

23

Operability Evaluation dated 2/15/94

Operability Evaluation dated 2/18/94

Operability Evaluation dated 6/28/94

e

Procedure Channes:

OP/1/A/6200/11

AM/2/A/5100/07

OP/2/B/6200/33. Change 4 Rev. 4

OP/1/A/6550/14

PT/1/B/4700/82

The ins ector determined that these changes were correctly evaluated

under t e provisions of 10 CFR 50.59

During the in-office and onsite reviews, the inspector made a number of

observations and has communicated them to licensee personnel:

The use of n ke-specific system identifiers in the annual summary

u

(which is submitted to the NRC and is thus available to the

public) is discouraged unless the licensee provides a key in the

l

l

summary. These identifiers do not bear any apparent correlation

l

to the actual systems (e.g. , NC = reactor coolant system. KC =

l

component cooling system, etc..).

The inspector made a similar

observation on the summary submitted on March 2~. 1996 (see

Inspection Report 50-413.414/96-10).

'

The licensee's corresponding revision of the UFSAR. per 10 CFR

o

50.71. lags behind 10 CFR 50.59 evaluations.

The next u)date of

the UFSAR. scheduled for late 1997. should capture all tie changes

that are within the scope of the UFSAR.

While the licensee had acceptably evaluated all the changes

e

audited by the inspector, a number of them eppeared in the summary

with insufficient information for a reader to even determine what

system was involved, or what change was made.

The inspector

recommended a several-sentence description. identifying the

system, the component, and the nature of the change, and

accompanied by a several-sentence evaluation.

Despite this

problem with the summary, the evaluations were found to be

thorough and in compliance with 10 CFR 50.59.

The licensee was

aware of this aroblem with the summary and has initiated actions

to correct suc1 weakness by revising its guidance document. NSD

209 (see Problem Investigation Process Form 0-C97-2027. dated June

19. 1997).

The term " Exempt Changes" may cause confusion in the context of 10

CFR 50.59.

It is a term internal to the licensee's docunentation.

It pertains to changes that "do not require the Modification

Enclosure 2

- _ _ _ _

1

b

24

Program controls for configuration management and therefore are

specifically exempted from the requirements to process an

editorial NM or NSM." According to licensee personnel, an " exempt

change" is essentially a minor change.

The summary contained a significant number of errors, which stated

e

the opposite of the actual facts.

For example, test procedure

TT/1/A/9200/88 states "there are Unreviewed Safety Questions

associated with this test procedure" when the onsite evaluation

shows that there was no unreviewed safety question.

The licensee

submitted a letter on July 9, 1997, correcting such errors.

c.

Crnclusions

Based on in-office review of the licensee's March 31, 1997, annual

summary on 10 CFR 50.59 changes, onsite review of the licensee's 10 CFR 50.59 evaluatius, and audit of the licensee's 3rocedures, the inspector

concluded that the licensee had complied with t1e provisions of the

regulation for the changes listed in the annual summary.

l

IV. Plant Suocort

R1

Radiological Protection and Chemistry Controls

R1.1 Tours of the Radiolooical Control Area (RCA) (71750)

The inspectors periodically toured the RCA during the inspection period.

Radiological control practices were observed and discussed with

t

!

radiological control personnel, including RCA entry and exit, survey

postings

locked high radiation areas, and radiological area material

conditions.

The inspector concluded that radiological control practices

were proper.

V. Management Meetinas

X1

Exit Meeting Summary

The inspectors ) resented the inspection results to members of licensee

management at t1e conclusion of the inspection on July 11 and July 23. 1997.

The licensee acknowledged the findings presented.

No proprietary information

was identified.

Dissenting comments were not received from the licensee.

Enclosure 2

_ - _ _ _ . - - - _

-.

-

.,

t

25

PARTIAL LIST OF PERSONS CONTACTED

Licensee

Bhatnager. A. . Operations Su>erintendent

Birch. M. . Safety Assurance ianager

Coy., S., Radiation Protection Manager

Forbes. J., Engineering Manager

Jones. R.. Station Manager

Harrall. T., Instrument and Electrical Maintenance Superintendent

Kelly. C.. Mainteriance Manager

Kimball . D. , Safety Review Group Manager

Kitlan. M., Regulatory Compliance Manager

'

Nicholson. K., Compliance Specialist

Peterson. G., Catawba Site Vice-President

Tower. D., Regulatory Compliance

l

,

4

Enclosure 2

u

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ - _

__

26

INSPECTION PROCEDURES USED

IP 37551:

Onsite Engineering

IP 40500:

Effectiveness of Licensee Controls in Identifying. Resolving, and

i

Preventing Problems

IP 61726:

Surveillance Observation

IP 37550:

Engineering

IP 62707:

Maintenance Observation

IP 71707:

Plant Operations

IP 71750:

Plant Support Activitia

IP 92901:

Followup - Operations

IP 92902:

Followup - Maintenance

IP 92903:

Followup - Engineering

IP 93702:

Prompt Onsite Respense to Events

ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

i

50-414/97-09-01

NCV

Failure to Declare Ice Condenser

Intermediate Deck Doors Inoperable and Log

Appropriate TSAIL Entry (Section C1.1)

50-414/97-09-02

NCV

Inadequate Lower Containment Ventilation

Unit Operating Procedure (Section 01.4)

'

50-414/97-09-03

VIO

Failure to Follow Procedure Results in

Invalid Local Leak Rate Test of Valve 2NV-

874 (Section M1.2)

50-413.414/97-09-04

VIO

Failure to Follow Procedure - Two Examples

(Sections 08.1. E2.1)

Closed

50-413.414/97-01-01

VIO

Failure to Include All Structures Systems

and Components in the Scope of the

Maintenance Rule as Required by 10 CFR 50.65(b) (Section M8.1)

50-414.414/97-01-02

IFI

Followup and review of licensee procedure

to implement the requirements of (a)(1)

and (a)(2) of the Maintenance Rule after

issuance of Revision 2 of Regulatory Guide 1.160 (Section M8.3)

50-413.414/97-01-03

IFl

Followup on Licensee Actions to Provide

Performance Criteria for Structures After

Resolution of this Issue (Section M8.4)

Enclosure 2

- _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

_

27

50-413.414/97-01-04

VIO

Failure to implement the requirements of

(a)(1) and (a)(2) of the Maintenance Rule

(Section M3.2)

50 413.414/94-13-02

URI

Emergency Operating Procedure 50.59

Evaluations Not Reviewed by Nuclear Safety

Review Board as Required by TS (Section

l

'

08.1)

<

l

List of Acronyms

!

CFR

Code of Federal Fagulations

-

DBD

Design Basis Documents

-

EDG

Emergency Diesel Generator

-

EDM

Engineering Directives Manual

-

E0P

Emergency Operating Procedure

-

FIP

Failure Investigative Process

-

FSAR

Final Safety Analysis Report

-

IAE

-

Instrument and Electrical

IFI

-

Inspector Followup Iten

IST

Inservice Testing

-

LCVU

Lower Containment Ventilation Unit

-

LER

-

Licensee Event Report

LLRT

Local Leak Rate Test

-

MPFF

Maintenance Preventable Function Failure

-

NCV

Non Cited Violation

-

NM

Nuclear Sampling

-

NRC

Nuclear Regulatory Commission

-

NSD

-

Nuclear Site Directive

NSRB

Nuclear Safety Review Board

-

DAC

Operator Aid Com] uter

-

POR

-

Public Document

Room

PIP

-

Problem Investigation Process

PM

-

Preventive Maintenance

asig

Pounds Per Square Inch Gauge

-

RCA

-

Radiologically Controlled Area

RCP

-

Reactor Coolant Pump

RCS

Reactor Coolant System

-

RG

-

Regulatory Guide

SA

--

Main Steam to Auxiliary Equipment

SB0

-

Station Blackout Role

SITA -

Self Initiated Technical Audit

SPOC

Single Point of Contact

-

TPBE -

Thermal Power Best Estimate

TS

-

Technical Specifications

TSAIL -

Tech Spec' Action Item Log

UCLF -

Unplanned Capability loss Factor

UFSAR -

Updated Final Safety Analysis Report

Enclosure 2

_

28

URI-

-

Unresolved Item-

USO

Unreviewed Safety Question

-

VDC'

Volts direct current

-

.

VIO

Violation

-

-VV

Containment Ventilation

-

WO

Work Order

-

YN

Auxiliary Building Chilled Water

-

l

Enclosure 2

_