ENS 40522: Difference between revisions
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StriderTol (talk | contribs) (Created page by program invented by Mark Hawes) |
StriderTol (talk | contribs) (Created page by program invented by StriderTol) |
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| event date = 02/15/2004 15:19 CST | | event date = 02/15/2004 15:19 CST | ||
| last update date = 02/16/2004 | | last update date = 02/16/2004 | ||
| title = Automatic Reactor Trip | | title = Automatic Reactor Trip with Auxiliary Feedwater Actuation | ||
| event text = The following information was received from the licensee via facsimile: | | event text = The following information was received from the licensee via facsimile: | ||
At 1519 [CDT] on 2-15-04, the plant was at 20 power, increasing load. During the transfer from the bypass feedwater regulating valves to the main feedwater regulating valves, the main turbine tripped due to a P-14 S/G Hi-Hi level signal. The P-14 signal also caused a Feedwater Isolation Signal (FWIS), which resulted in a Motor Driven Aux Feedwater Actuation (MDAFAS), and Steam Generator Blowdown Isolation Signal. | At 1519 [CDT] on 2-15-04, the plant was at 20 power, increasing load. During the transfer from the bypass feedwater regulating valves to the main feedwater regulating valves, the main turbine tripped due to a P-14 S/G Hi-Hi level signal. The P-14 signal also caused a Feedwater Isolation Signal (FWIS), which resulted in a Motor Driven Aux Feedwater Actuation (MDAFAS), and Steam Generator Blowdown Isolation Signal. | ||
Latest revision as of 21:24, 1 March 2018
| Where | |
|---|---|
| Callaway Missouri (NRC Region 4) | |
| Reporting | |
| 10 CFR 50.72(b)(2)(iv)(B), RPS Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
| Time - Person (Reporting Time:+-1.02 h-0.0425 days <br />-0.00607 weeks <br />-0.0014 months <br />) | |
| Opened: | Hope Bradley 20:18 Feb 15, 2004 |
| NRC Officer: | Howie Crouch |
| Last Updated: | Feb 16, 2004 |
| 40522 - NRC Website
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