ENS 44906: Difference between revisions

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| event date = 03/13/2009 21:51 CDT
| event date = 03/13/2009 21:51 CDT
| last update date = 03/14/2009
| last update date = 03/14/2009
| title = Feedwater Regulating Valve Failure Leads To Manual Reactor Trip
| title = Feedwater Regulating Valve Failure Leads to Manual Reactor Trip
| event text = At 2151 CDT on 3/13/2009 with plant power at 84% following securing of the 2P-1A Main Feedwater Pump at 1934 due to bearing degradation, Unit 2 experienced a failure of the 'B' Main Feedwater Regulating Valve 2CV-0740 which caused 2E-24B Steam Generator level to lower. At 2151, with 2E-24B Steam Generator level at approximately 25% control room staff manually tripped the reactor anticipating an automatic trip at 22% steam generator level.  Emergency Feedwater Actuation System automatically actuated at 22% steam generator level and responded to restore level to the normal post-trip levels. All Control Element Assemblies (rods) Inserted on the reactor trip.
| event text = At 2151 CDT on 3/13/2009 with plant power at 84% following securing of the 2P-1A Main Feedwater Pump at 1934 due to bearing degradation, Unit 2 experienced a failure of the 'B' Main Feedwater Regulating Valve 2CV-0740 which caused 2E-24B Steam Generator level to lower. At 2151, with 2E-24B Steam Generator level at approximately 25% control room staff manually tripped the reactor anticipating an automatic trip at 22% steam generator level.  Emergency Feedwater Actuation System automatically actuated at 22% steam generator level and responded to restore level to the normal post-trip levels. All Control Element Assemblies (rods) Inserted on the reactor trip.
No safeties or relief valves opened after the trip.  The plant is in its normal shutdown electrical line-up.  Steam generator level is being maintained with emergency feedwater and decay heat is being dumped to the main condenser.
No safeties or relief valves opened after the trip.  The plant is in its normal shutdown electrical line-up.  Steam generator level is being maintained with emergency feedwater and decay heat is being dumped to the main condenser.

Latest revision as of 21:12, 1 March 2018

ENS 44906 +/-
Where
Arkansas Nuclear Entergy icon.png
Arkansas (NRC Region 4)
Reporting
10 CFR 50.72(b)(3)(iv)(A), System Actuation

10 CFR 50.72(b)(2)(iv)(B), RPS Actuation

10 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release
Time - Person (Reporting Time:+-0.8 h-0.0333 days <br />-0.00476 weeks <br />-0.0011 months <br />)
Opened: Rex Knight
02:03 Mar 14, 2009
NRC Officer: Mark Abramovitz
Last Updated: Mar 14, 2009
44906 - NRC Website
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