ENS 52631: Difference between revisions
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ENS Event | |
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07:56 Mar 23, 2017 | |
Title | High Pressure Core Spray Declared Inoperable |
Event Description | River Bend Station personnel declared the High Pressure Core Spray (HPCS) system inoperable at 0256 on 3/23/2017.
During performance of the HPCS Pump and Valve Operability Test, the operators observed an unusual system response after E22-MOVF023 (HPCS Test Return to the Suppression Pool) was stroked closed. A field check showed that the key that connects the E22-MOVF023 valve stem to the anti-rotation device had become dislodged. E22-MOVF023 is a Primary Containment Isolation Valve (PCIV) and is designed to close automatically on an ECCS [Emergency Core Cooling System] initiation signal to ensure that injection flow is directed to the reactor vessel. Technical Specification (TS) 3.6.1.3 requires that containment penetrations associated with an inoperable PCIV be isolated. E22-MOVF023 was declared inoperable at 0028. Operators were unable to close or demonstrate that E22-MOVF023 was fully closed as required by TS 3.6.1.3 and proceeded to isolate the associated containment penetration by closing other system valves. This action was completed at 0320. The net effect of the actions taken to isolate the containment penetration is that HPCS is inoperable as of 0256. This results in 14 day LCO. The licensee has notified the NRC Resident Inspector.
The Event Time was 0028 CDT rather than 0256 CDT. "The scheduled surveillance test of the high pressure core spray system was initiated at 2355 CDT on March 22, and the pump was secured at 0028 CDT on March 23. The inspection of the HPCS test return valve to the suppression pool occurred at 0050 CDT, and it was at that point that an apparent malfunction of the valve had occurred to the extent that it did not appear to be able to perform its safety function to close upon receipt of a design basis system initiation signal. Thus, the event time for this condition would be more accurately defined as 0028 CDT. Notified R4DO (James Drake) via e-mail. |
Where | |
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River Bend Louisiana (NRC Region 4) | |
Reporting | |
10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | |
Time - Person (Reporting Time:+-0.53 h-0.0221 days <br />-0.00315 weeks <br />-7.25994e-4 months <br />) | |
Opened: | Tim Gates 07:24 Mar 23, 2017 |
NRC Officer: | Karl Diederich |
Last Updated: | Mar 23, 2017 |
52631 - NRC Website
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Unit 1 | |
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Reactor critical | Critical |
Scram | No |
Before | Power Operation (100 %) |
After | Power Operation (100 %) |