ENS 51899
ENS Event | |
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03:29 May 3, 2016 | |
Title | High Pressure Core Spray System Inoperable Due to a Control Room Chiller Trip |
Event Description | At 2229 [CDT] on 05-02-2016, River Bend Station declared the High Pressure Core Spray system INOPERABLE in accordance with Technical Specification 3.8.9, Condition E (Declare High Pressure Core Spray System and Standby Service Water System Pump 2C inoperable immediately) due to Division 1 Control Room Air Conditioning System HVK-CHL1C being INOPERABLE due to a trip of the chiller on high inboard bearing temperature.
Actions taken to exit the LCO: Alternated divisions of Control Room Air Conditioning System to Division 2 HVK-CHL1D in service and Division 1 HVK-CHL1A in standby. The licensee notified the NRC Resident Inspector.
Supplement: An operability evaluation has been performed based on system operating procedures in place at the time of this event, and on calculations regarding heat-up rates of the spaces served by the main control room air conditioning system. Operating procedures already in place on May 2 specified the operator actions required to restore the air conditioning system to service following the unanticipated trip of a chiller. The normal shift complement was on duty at the time of the event, and could have provided an adequate number of operators to accomplish this task. The operability evaluation made no new assumptions regarding availability of operators. The manual actions to be performed for the start of an alternate chiller following a trip of an in-service chiller system have been determined to require 2.15 hours1.736111e-4 days <br />0.00417 hours <br />2.480159e-5 weeks <br />5.7075e-6 months <br />, based on ANSI 58.8 guidance. (ANSI/ANS 58.8, Time Response Design Criteria for Nuclear Safety Related Operator Actions, provides the industry guidance In this regard.) Calculations of building heat-up rates have demonstrated that the loss of the air conditioning system can be sustained for 19 hours2.199074e-4 days <br />0.00528 hours <br />3.141534e-5 weeks <br />7.2295e-6 months <br /> before temperatures in the rooms containing the Division 3 electrical equipment that support operability of the HPCS system exceed their maximum allowable ambient value. Based on the conclusions of the operability evaluation, the trip of the 'C' HVK chiller on May 2 had no actual adverse effect on the ability of the electrical distribution systems in the main control building to support the safety function of the HPCS system. Event Notification 51899 is hereby withdrawn. The licensee has notified the NRC Resident Inspector. Notified R4DO (Rollins). |
Where | |
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River Bend Louisiana (NRC Region 4) | |
Reporting | |
10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | |
Time - Person (Reporting Time:+-1.65 h-0.0688 days <br />-0.00982 weeks <br />-0.00226 months <br />) | |
Opened: | Danny James 01:50 May 3, 2016 |
NRC Officer: | Vince Klco |
Last Updated: | Jun 22, 2016 |
51899 - NRC Website
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Unit 1 | |
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Reactor critical | Critical |
Scram | No |
Before | Power Operation (100 %) |
After | Power Operation (100 %) |