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{{#Wiki_filter:* *
{{#Wiki_filter:~-JI consumers
* consumers Power company General Offices: 212 West Michigan Avenue, Jackson, Michigan 49201
* Power company General Offices: 212 West Michigan Avenue, Jackson, Michigan 49201
* Area Code 517 788-0550 May 21, 1976 Mr James G. Keppler . Office of Inspection Enforcement Region ITI US Nuclear Regulatory Com.mission 799 Roosevelt Road Glen Ellyn, IL 60137 DOCKET 50-255, LICENSE DPR-20 ... PALISADES PLANT -ER:.._76-13 DISCHARGE ABOVE 5°F LIMIT Attached is a reportable occurrence which relates to the Palisades Plant, This occurrence involves the discharge of cooling water above the 5°F limit and has been classified as a prompt reportable event. David A, Bixel Assistant Nuclear Licensing Administrator  
* Area Code 517 788-0550 May 21, 1976 Mr James G. Keppler .
' . : .. ..r r\ _.. . . .
Office of Inspection Enforcement Region ITI US Nuclear Regulatory Com.mission 799 Roosevelt Road Glen Ellyn, IL 60137 DOCKET 50-255, LICENSE DPR-20 ...
* *
PALISADES PLANT - ER:.._76-13 DISCHARGE ABOVE 5°F LIMIT
* LICENSEE EVENT REPOR
* Attached is a reportable occurrence which relates to the Palisades Plant, This occurrence involves the discharge of cooling water above the 5°F limit and has been classified as a prompt reportable event.
* Palisades CONTROL BLOCK: ._I __.____...l__.l___.l_..1  
David A, Bixel Assistant Nuclear Licensing Administrator
...........
*                                                              :. ..r r\ ' .
1 (PLEASE PRINT ALL REQUIRED INFORMATION]
                                                                          ~
UC EN SEE NAME @El jl-11 rlPI AILI ii 7 B 9 14 REPORT 1 6 LICENSE NUMBER 10101-10101010101-10101 15 25 LICENSE TYPE 14111111111 26 30 EVENT DATE EVENT TYPE I o 111 31 32 REPORT DATE @IT]coN'T  
                                                                            .*~~ ,'~.~ ~\_.. :*~i.,,;
* ..... I __.___.I 7 B 57 5B Gj' REPORT SOURCE NUMBER lol 51 ol-1 01215151 lol5IOl717161 1015121111161 59 60 61 BB 69 74 75 BO EVENT DESCRIPTION lol2l !During start-up/shutdown of the plant cooling towers on May 7 and May 9, 1976, I 7 B 9 BO IPl3f I four events occurred which resulted in discharging water above the 5°F limit. On I 7 89 00 lol41 I two of these occasions the 500 million Btu/h limit was exceeded.
                                                                                              . ~\..
Most discharges I 7 89 . 00 lol51 I occurred at 6°F over the limit. One event discharged at iv30°F over limit for 10 I 7 89. 80 lolsl f minutes and averaged 18°F over limit. I 7 8 9 PRME BO SYSTEM CAUSE CODE -CODE COMPONENT CODE COMPONENT SUPPi.ER @01HIFI W l.zlzlzlzlzlzl 7 8 9 10 11 12 17 w 43 CAUSE DESCRIPTION COMPONENT MANUFACTURER I z I z I z I z I 44 47 VIOLATION Lx..I 48 lolal I During plant start-up following the first refueling outage a cooling tower had to 7 8 9 . 10101 lbe removed from service to'repair .a leaking condenser tube. The events occurred 7 8 9 IT@] I related to this process or to that involving placing of the cooling towers in* 7 8 9 FACILITY METHOD OF STATUS % POWER OTHER STATUS DISCOVERY DISCOVERY DESCRIPTION Em L£J I I I NA I w I NA 7 8 9 10 12 13 44 45 46 FORM OF ACTIVITY CONTENT rn RELEASED OF RELEASE AMOUNT OF ACTIVITY I LOCATION OF RELEASE w WI NA NA 7 8 9 10 11 44 45 PERSONNEL EXPOSURES
* LICENSEE EVENT REPOR*
* NUMBER TYPE DESCRIPTION ololol w 7 8 9 11 12 13 'v PERS'ONNEL INJURIES NUMBER DESCRIPTION
CONTROL BLOCK: ._I__.____...l__.l___.l_..1...........1 Palisades (PLEASE PRINT ALL REQUIRED INFORMATION]
[iEl 1010101 NA 7 8 9 11 12 PROBABLE CONSEQUENCES None 7 8 9 LOSS OR DAMAGE TO FACILITY TYPE DESCRIPTION
1                            6 UCEN SEE                                                                               LICENSE              EVENT NAME                               LICENSE NUMBER                                      TYPE                TYPE
[2]], NA 7 8 9 10 PUBLICITY
      @El   jl-11 rlPI AILI             ii     10101-10101010101-10101                                   14111111111                I o 111 7    B9                              14    15                                                   25   26                   30   31     32 REPORT   REPORT
[ill] NA 7 8 9 I 80 I BO I BO 80 80 80 80 80 80 80
      @IT]coN'T *I.....__.___.I     Gj'     SOURCE
* ADDITIONAL FACTORS I (Contd From Cause) service. NPDES limits were not exceeded. 7 8 9 We are reviewing this I 80 EJfil I occurrence in relation to present licensing action involving operation of the I 7 . 8 9 cooling towers. BO}}
                                                ~
DOCK~ NUMBER lol 51 ol-1 01215151 EVENT DATE lol5IOl717161 REPORT DATE 1015121111161 7    B          57        5B      59     60     61                                     BB   69                       74   75                     BO EVENT DESCRIPTION lol2l !During start-up/shutdown of the plant cooling towers on May 7 and May 9, 1976,                                                                 I 7   B 9                                                                                                                                             BO IPl3f I four events occurred which resulted in discharging water above the 5°F limit.                                                             On   I 7     89                                                                                                                                               00 lol41   I two of these occasions the 500 million Btu/h limit was exceeded. Most discharges                                                             I 7     89                                                                     .                                                                       00 lol51   I occurred at 6°F over the limit. One event discharged at iv30°F over limit for 10                                                             I 7   89.                                                                                                                                             80 lolsl f minutes and averaged 18°F over limit.                                                                                                           I 7     8 9                                                                   PRME                                                                       BO SYSTEM       CAUSE                                     COMPONENT                COMPONENT CODE     -   CODE             COMPONENT CODE               SUPPi.ER             MANUFACTURER          VIOLATION 7
    @01HIFI 8 9 10 W
11 l.zlzlzlzlzlzl 12                     17 w 43 Iz I z I z 44 IzI 47 Lx..I 48 CAUSE DESCRIPTION 7
lolal I During plant start-up following the first refueling outage a cooling tower had to 8 9                                                                                                                                             80 I
  . 10101 lbe removed from service to'repair .a leaking condenser tube.                                                   The events occurred               I 7     8 9                                                                                                                                             BO IT@] I related to this process or to that involving placing of the cooling towers                                                           in*       I 7     8 9                                                                                                                                             BO FACILITY                                                             METHOD OF DISCOVERY DESCRIPTION w
STATUS             % POWER               OTHER STATUS               DISCOVERY Em8 7
L£J 9              10 I I 12I      13 NA                   I 44     45 I
46 NA 80 FORM OF ACTIVITY       CONTENT RELEASED       OF RELEASE         AMOUNT OF ACTIVITY                                               LOCATION OF RELEASE rn w 7     8       9 WI 10 11 NA                      I 44       45 NA 80 PERSONNEL EXPOSURES
* NUMBER           TYPE     DESCRIPTION 7
    ~I ololol 8 9               11 w12    13                                                                                             'v             80 PERS'ONNEL INJURIES NUMBER           DESCRIPTION
[iEl     1010101                                                                 NA 7     8 9                 11   12                                                                                                                       80 PROBABLE CONSEQUENCES
    ~                None 7     8 9                                                                                                                                               80 LOSS OR DAMAGE TO FACILITY TYPE       DESCRIPTION
[2)), ~                                                                        NA 7     8 9         10                                                                                                                                   80 PUBLICITY
[ill]                           NA 7     8 9                                                                                                                                               80 ADDITIONAL FACTORS
*   ~      I   (Contd From Cause) service.                     NPDES limits were not exceeded.                           We are reviewing this           I 7    8 9                                                                                                                                              80 EJfil I occurrence               in relation to present licensing action involving operation of the                                                     I 7 .8 9       cooling towers.                                                                                                                           BO}}

Latest revision as of 03:35, 17 March 2020

Licensee Event Report ER-76-013, Discharge of Cooling Water Above 5oF Limit
ML18352A342
Person / Time
Site: Palisades Entergy icon.png
Issue date: 05/21/1976
From: Bixel D
Consumers Power Co
To: James Keppler
NRC/RGN-III
References
LER 1976-013-00
Download: ML18352A342 (2)


Text

~-JI consumers

  • Power company General Offices: 212 West Michigan Avenue, Jackson, Michigan 49201
  • Area Code 517 788-0550 May 21, 1976 Mr James G. Keppler .

Office of Inspection Enforcement Region ITI US Nuclear Regulatory Com.mission 799 Roosevelt Road Glen Ellyn, IL 60137 DOCKET 50-255, LICENSE DPR-20 ...

PALISADES PLANT - ER:.._76-13 DISCHARGE ABOVE 5°F LIMIT

  • Attached is a reportable occurrence which relates to the Palisades Plant, This occurrence involves the discharge of cooling water above the 5°F limit and has been classified as a prompt reportable event.

David A, Bixel Assistant Nuclear Licensing Administrator

  • :. ..r r\ ' .

~

.*~~ ,'~.~ ~\_.. :*~i.,,;

. ~\..

  • LICENSEE EVENT REPOR*

CONTROL BLOCK: ._I__.____...l__.l___.l_..1...........1 Palisades (PLEASE PRINT ALL REQUIRED INFORMATION]

1 6 UCEN SEE LICENSE EVENT NAME LICENSE NUMBER TYPE TYPE

@El jl-11 rlPI AILI ii 10101-10101010101-10101 14111111111 I o 111 7 B9 14 15 25 26 30 31 32 REPORT REPORT

@IT]coN'T *I.....__.___.I Gj' SOURCE

~

DOCK~ NUMBER lol 51 ol-1 01215151 EVENT DATE lol5IOl717161 REPORT DATE 1015121111161 7 B 57 5B 59 60 61 BB 69 74 75 BO EVENT DESCRIPTION lol2l !During start-up/shutdown of the plant cooling towers on May 7 and May 9, 1976, I 7 B 9 BO IPl3f I four events occurred which resulted in discharging water above the 5°F limit. On I 7 89 00 lol41 I two of these occasions the 500 million Btu/h limit was exceeded. Most discharges I 7 89 . 00 lol51 I occurred at 6°F over the limit. One event discharged at iv30°F over limit for 10 I 7 89. 80 lolsl f minutes and averaged 18°F over limit. I 7 8 9 PRME BO SYSTEM CAUSE COMPONENT COMPONENT CODE - CODE COMPONENT CODE SUPPi.ER MANUFACTURER VIOLATION 7

@01HIFI 8 9 10 W

11 l.zlzlzlzlzlzl 12 17 w 43 Iz I z I z 44 IzI 47 Lx..I 48 CAUSE DESCRIPTION 7

lolal I During plant start-up following the first refueling outage a cooling tower had to 8 9 80 I

. 10101 lbe removed from service to'repair .a leaking condenser tube. The events occurred I 7 8 9 BO IT@] I related to this process or to that involving placing of the cooling towers in* I 7 8 9 BO FACILITY METHOD OF DISCOVERY DESCRIPTION w

STATUS  % POWER OTHER STATUS DISCOVERY Em8 7

L£J 9 10 I I 12I 13 NA I 44 45 I

46 NA 80 FORM OF ACTIVITY CONTENT RELEASED OF RELEASE AMOUNT OF ACTIVITY LOCATION OF RELEASE rn w 7 8 9 WI 10 11 NA I 44 45 NA 80 PERSONNEL EXPOSURES

  • NUMBER TYPE DESCRIPTION 7

~I ololol 8 9 11 w12 13 'v 80 PERS'ONNEL INJURIES NUMBER DESCRIPTION

[iEl 1010101 NA 7 8 9 11 12 80 PROBABLE CONSEQUENCES

~ None 7 8 9 80 LOSS OR DAMAGE TO FACILITY TYPE DESCRIPTION

[2)), ~ NA 7 8 9 10 80 PUBLICITY

[ill] NA 7 8 9 80 ADDITIONAL FACTORS

  • ~ I (Contd From Cause) service. NPDES limits were not exceeded. We are reviewing this I 7 8 9 80 EJfil I occurrence in relation to present licensing action involving operation of the I 7 .8 9 cooling towers. BO