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| | issue date = 03/31/1995 | | | issue date = 03/31/1995 |
| | title = Application for Amends to Licenses DPR-58 & DPR-74.Amends Would Modify TS 3/4.6.1.7 to Allow Limited Purge Operation in Modes 1,2,3 & 4 for Pressure Control,Alara & Respirable Air Quality Considerations | | | title = Application for Amends to Licenses DPR-58 & DPR-74.Amends Would Modify TS 3/4.6.1.7 to Allow Limited Purge Operation in Modes 1,2,3 & 4 for Pressure Control,Alara & Respirable Air Quality Considerations |
| | author name = FITZPATRICK E | | | author name = Fitzpatrick E |
| | author affiliation = INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG | | | author affiliation = INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG |
| | addressee name = | | | addressee name = |
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| | document type = OPERATING LICENSES-APPLIATION TO AMEND-RENEW EXISTING, TEXT-LICENSE APPLICATIONS & PERMITS | | | document type = OPERATING LICENSES-APPLIATION TO AMEND-RENEW EXISTING, TEXT-LICENSE APPLICATIONS & PERMITS |
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| {{#Wiki_filter:PR.ICDR.IMY''CELERATEDRIDSPROCESSING)REGULATORYINFORMATIONDISTRIBUTIONSYSTEM(RIDS)ACCESSIONNBR:9504060198DOC.DATE:95/03/31NOTARIZED:YESDOCKETFACIL:50-315DonaldC.CookNuclearPowerPlant,Unit1,IndianaM0500031550-316DonaldC.CookNuclearPowerPlant,Unit2,IndianaM05000316AUTH.NAMEAUTHORAFFILIATIONFITZPATRICK,E.IndianaMichiganPowerCo.(formerlyIndiana&MichiganEleRECIP.NAMERECIPIENTAFFILIATIONDocumentControlBranch(DocumentControlDesk)SUBZECT:ApplicationforamendstolicensesDPR-58&DPR-74.Amends.wouldmodifyTS3/4.6.1.7toallowlimitedpurgeoperationinmodes1,2,3&4forpressurecontrol,ALARA&respirableairqualityconsiderations.DISTRIBUTIONCODE:A001DCOPIESRECEIVED:LTRENCLSIZE:TITLE:ORSubmittal:GeneralDistributionNOTES:RECIPIENTIDCODE/NAMEPD3-1LAHICKMAN,ZINTERNAL~FILECENTER~01'RR/DRCH/HICBNRR/DSSA/SRXBOGC/HDS2EXTERNAL:NOACCOPIESLTTRENCL111111111110RECIPIENTIDCODE/NAMEPD3-1PDNMSS/DWM/LLDPNRR/DSSA/SPLBNUDOCS-ABSTRACTNRCPDRCOPIESLTTRENCL1122111111NOTETOALL"RIDS'ECIPIENTS:PLEASEHELPUSTOREDUCEWASTE!CONTACTTHEDOCUMENTCONTROLDESK,ROOMPI-37(EXT.504-2083)TOELIMINATEYOURNAMEFROMDISTRIBUTIONLISTSFORDOCUMENTSYOUDON'TNEEDlTOTALNUMBEROFCOPIESREQUIRED:LTTR13ENCL12 fll indianaMichiganPowerCompanyP.O.Box16631Columbus,OH43216i4arch31,1995AEP:NRC:1185DocketNos.:50-31550-316U.S.NuclearRegulatoryCommissionATTN:DocumentControlDeskWashington,D.C.20555Gentlemen:DonaldC.CookNuclearPlantUnits1and2PROPOSEDAMENDMENTTOTECHNICALSPECIFICATIONSECTION3/4.6.1.7FORCONTAINMENTPURGEREQUIREMENTSandThisletteranditsattachmentsconstituteanapplicationforamendmenttotheTechnicalSpecifications(T/Ss)forDonaldC.CookNuclearPlantUnits1and2.Specifically,weareproposingtomodifyT/Ss3/4.6.1.7,ContainmentVentilationSystem,anditsassociatedBases,toallowlimited(240hoursannually)purgeoperationinMODES1,2,3,and4forpressurecontrol,ALARAandrespirableairqualityconsiderations.Theproposedchangeswillenhanceourabilitytousethecontainmentpurgesystemtoreduceunnecessaiyhardshipsonplantpersonnelperformingactivitiesincontainment.Additionally,anincreaseinallowablepurgetimeisbeingrequestedtoaddressimprovementsinplantoperationsandcapacityfactors.Attachment1providesadetaileddescriptionoftheproposedchanges,thejustificationforthechanges,andou'rdeterminationofnosignificanthazardsconsiderationperformedpursuantto10CFR50.92.Attachment2containstheexistingT/Spagesmarkedtoreflecttheproposedchanges.Attachment3containstherevisedT/Spages.Webelievetheproposedchangeswillnotresultin(1)asignificantincreasein.theamounts,andnosignificantchangeinthetypesofanyeffluentthatmaybereleasedoffsite,or(2)asignificantincreaseinindividualorcumulativeoccupationalradiationexposure.TheseproposedchangeshavebeenreviewedbythePlantNuclearSafetyReviewCommitteeandtheNuclearSafetyandDesignReviewCommittee.',9504060198950331PDRADDCK05000315PPDR'l) | | {{#Wiki_filter:R.ICDR.IMY' P'CELERATED RIDS PROCESSING) |
| ~,s)f9f U.S.NuclearRegulatoryCommissionPage2AEP:NRC:1185Incompliancewiththerequirementsof10CFR50.91(b)(l),copiesofthisletteranditsattachmentshavebeentransmittedtotheMichiganPublicServiceCommissionandtotheMichiganDepartmentofPublicHealth.Sincerely,E.E.FitptrickVicePresidentSWORNTOANDSUBSCRIBEDBEFOREMETHIS~4~~DAYOFQQ~~I~1995/0NotaPublicMyCommissionExpires:~P-$'$'hAttachmentsCC:A.A.BlindG.CharnoffJ.B.MartinNFEMSectionChiefNRCResidentInspector-BridgmanJ.R.Padgett ATTACHMENT1TOAEP:NRC:1185DESCRIPTIONANDJUSTIFICATIONOFCHANGES10CFR50.92ANALYSISFORCHANGESTOTHEDONALDC.COOKNUCLEARPLANTUNITS1AND2TECHNICALSPECIFICATIONS C~wI~w~g~ | | REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS) |
| Attachment1toAEP:NRC:1185Page1I.ESCRIPTIONOFCHANGESTheproposedamendmenttoTechnicalSpecifications(T/Ss)3/4.6.1.7makesthefollowingspecificchangestotheCookNuclearPlantUnits1and2T/Ss:T/S3/4.6.1.7A.RevisestheLimitingConditionforOperationforspecification3/4.6.1.7(onpage3/46-9a)toredefinetheconditionsinwhichitispermissibletooperatethecontainmentpurgesystemwheninMODES1,2,3,and4.TheproposedLimitingConditionforOperationwouldbemodifiedtoread:"Thecontainmentpurgesupplyandexhaustisolationvalvesshallbeclosedexceptwhenoperationofthecontainmentpurgesystemisrequiredfor;pressurecontrol,ALARA,andrespirableairqualityconsiderationsforpersonnelentryandforsurveillancetestingandmaintenanceactivities."B.RevisetheBasesforspecification3/4.6.1.7(pageB3/46-2a)toreflecttheactivitieswhichallowpurginginMODES1,2,3,and4,asdefinedabove.Additionalchangestothebaseswillinclude,1)increasingtheallowablepurgetimefrom200to240hours,2)addingareferencetotheabilityofthepurgeisolationvalvestocloseagainstLOCAforces,therebyassuring10CFR100guidelinesaremaintained,and3)deleting"**"notescorrectedduringpreviousamendments.IX.JUSTIFICATIONFORCHANGEST/S3/4.6.1.7WeproposetochangethewordinginboththeLimitingConditionForOperationandtheBasesofT/S3/4.6.1.7toallowlimitedcontainmentpurgingwhileinMODES1,2,3,and4forreasonsotherthan"safetyrelatedreasons."Ascurrentlywritten,.useofthecontainmentpurgesystemduringMODES1,2,3,and4islimitedto"safetyrelatedreasons."Thesearedefinedas"theneedtoimprovecontainmentworkingconditions,e.g.,reduceairborneactivity,toperformsurveillanceand/ormaintenanceonasafety-relatedsystemorpieceofequipment."Additionally,purgeoperationislimitedto200hours,perthetechnicalspecificationbases.Therestrictivenessofthiswordingresultsinunnecessaryhardshiptooperators,maintenancetechnicians,instrumenttechnicians,andotherplantworkersperformingroutinetasksincontainment.Forexample,maintenanceactivitiesrelatedtotheuppercontainment
| | ACCESSION NBR:9504060198 DOC.DATE: 95/03/31 NOTARIZED: YES DOCKET FACIL:50-315 Donald C. Cook Nuclear Power Plant, Unit 1, Indiana M 05000315 50-316 Donald C. Cook Nuclear Power Plant, Unit 2, Indiana M 05000316 AUTH. NAME AUTHOR AFFILIATION FITZPATRICK,E. Indiana Michigan Power Co. (formerly Indiana & Michigan Ele RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk) |
| -aIne Attachment1toAEP:NRC:1185Page2ventilationsystemsandtheglycolfloorcoolingsystemrepresentrequiredactivitiesonequipmentwhichisnotcharacterizedas"safetyrelated."Achangetothespecificationwouldallowthelimiteduseofcontainmentpurgetoaddressadverseenvironmentalconditions(i.e.,temperature,humidity,and/orpressure),ALARAconcerns,andtoassurethatrespirableairqualityismaintained.Itshouldbenotedthattheuseofthepurgesystemtosupporttheaboveactivitieswouldberestrictedtooccasionswhentheexistingairfiltrationandtemperaturecontrolsystemswerenotsufficienttoprovideacontainmentatmospheresupportiveofworkingconditions.AnadditionalchangetoT/S3/4.6.1.7istoincreasethecurrentpurgelimitof200hoursperyearto240hours.Theoriginaltimelimitwascalculatedbasedonaunitcapacityfactorof77X.Asaresultoflongeroperatingcyclesandimprovedplantperformance,theCookNuclearPlantcapacityfactorisnowforecastedtobe93X.Utilizingthesamecalculationwhichestablishedthe200hourlimit,andincreasingthecapacityfactorto93Xyieldsavalueof240hours.ThisincreasedtimeallotmentreflectstheadditionaltimetheunitwillremaininMODES1,2,3,and4witha93Kcapacityfactor.Asstatedinthetechnicalspecificationbases,thecontainmentpurgesystematCookNuclearPlanthasbeendesignedinaccordancewithNRCBranchTechnicalPositionCBS6-4,Rev.1,anddemonstratedtobecapableofclosureagainstthedynamicforcesassociatedwithalossofcoolantaccident.Thepurgevalveswillreceiveacontainmentventilationisolationsignalonbothasafetyinjectionandhighradiationsignalsandclosewithin5seconds.InaccordancewiththeaboveBranchTechnicalPosition,thepotentialsiteboundarydoseswerecalculatedbasedontheoriginalanalysisusedtodeterminetheradiologicalconsequencesofalossofcoolantaccident.Theresultsofthisanalysisindicatedatotalthyroiddoseof165remforthe0-2hoursiteboundarydoseandawholebodydoseof9.32rem.Sincephysicalchangeswillnotresultfromtheproposedamendment,thesiteboundarydoesguidelinesof10CFR100(300remthyroidand25remwholebody)willnotbeexceededintheeventofanaccidentduringcontainmentpurgingoperations.Theadditionof40hoursofallowableannualpurgetimewillnotresultinasignificantincreaseintheamountofeffluentreleased.TheOffsiteDoseCalculationManual(ODCM)ensuresthatthedoserateatanytimeattheSITEBOUNDARYfromgaseouseffluentfromallunitsonthesitewillbewithintheannualdoselimitsofAppendixB,Table2,Column1of10CFR20forUNRESTRICTEDAREAS.Thesespecificationswillbestrictlyadheredtoduringanyreleaseviathepurgepathway. | | SUBZECT: Application for amends to licenses DPR-58 & DPR-74.Amends |
| Attachment1toAEP:NRC:1185Page3Inconclusion,webelievethattheproposedtechnicalspecificationswillnotaffectsystemcapabilityorintroduceanewordifferentmodeofpurgesystemoperationnotpreviouslyaddressedintheaboveanalysis.III.10CFR5092CRITERIAPer10CFR50.92,aproposedchangedoesnotinvolveasignificanthazardsconsiderationifthechangedoesnot:involveasignificantincreaseintheprobabilityorconsequencesofanaccidentpreviouslyevaluated,2.createthepossibilityofanewordifferentkindofaccidentfromanyaccidentpreviouslyevaluated,or3.involveasignificantreductioninamarginofsafety.CriteronThepurposeofthisamendmentistoallowflexibilityintheuseofthecontainmentpurgesystemduringMODES1,2,3,and4.Theuseofthissystemduringthesemodesofoperationhaspreviouslybeenapproved(AmendmentNo.66).Therefore,thisamendmentrequestdoesnotinvolvea,significantincreaseintheprobabilityorconsequencesofanaccidentpreviouslyevaluatedbecausetheproposedchange'otheT/Ssdoesnotaffecttheassumptions,parameters,orresultsofanyUFSARaccidentanalysis.Basedontheexistingsystemdesignanddemonstratedclosurecapabilityitisconcludedthattheproposedchangesdonotmodifytheresponseofthecontainmentduringadesignbasisaccident.Theproposedamendmentdoesnotaddormodifyanyexistingequipment.Basedontheseconsiderations,itisconcludedthatthechangesdonotinvolveasignificantincreaseintheprobabilityorconsequencesofanaccidentpreviouslyevaluated.Criterion2Theproposedchangedoesnotinvolvephysicalchangestotheplantorchangesintheplantoperatingconfiguration.Thus,itisconcludedthattheproposedchangedoesnotcreatethepossibilityofanewordifferentkindofaccidentfromanyaccidentpreviouslyevaluated.
| | . would modify TS 3/4.6.1.7 to allow limited purge operation in modes 1,2,3 & 4 for pressure control,ALARA & respirable air quality considerations. |
| Attachment1toAEP:NRC:1185Page4Criterion3Themarginforsafetypresentlyprovidedisnotreducedbytheproposedchange.Asdiscussedpreviously,thecontainmentpurgevalveshavebeendesignedanddemonstratedcapableofclosureagainstthedynamicforcesresultingfromalossofcoolantaccident.Theproposedamendmentdoesnotimpacttheabilityofthepurgevalvestoperformtheirintended.function(i.e.achieveclosure)intheeventofanaccident.Basedontheseconsiderations,itisconcludedthatthechangesdonotinvolveasignificantreductioninamarginofsafety.IV.CONCLUSIONInconclusion,webelievethattheproposedchangedoesnotinvolvesignificanthazardsconsiderationsbecause,asdemonstratedinthepreviousdiscussions,operationoftheCookNuclearPlantinaccordancewiththechangeswouldnot:involveasignificantincreaseintheprobabilityorconsequencesofanaccidentpreviouslyevaluated,2.createthepossibilityofanewordifferentkindofaccidentfromanyaccidentpreviouslyevaluated,or3.involveasignificantreductioninamarginofsafety.
| | DISTRIBUTION CODE: A001D COPIES RECEIVED:LTR ENCL SIZE: |
| ATTACHMENT2TOAEP:NRC:1185EXISTINGTECHNICALSPECIFICATIONPAGESMARKEDTOREFLECTPROPOSEDCHANGES 4\~}}
| | TITLE: OR Submittal: General Distribution NOTES: |
| | RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD3-1 LA 1 1 PD3-1 PD 1 1 HICKMAN,Z 1 1 INTERNAL~FILE CENTER 1 1 NMS S/DWM/LLDP 2 2 |
| | ~01'RR/DRCH/HICB 1 1 NRR/DSSA/SPLB 1 1 NRR/DSSA/SRXB 1 1 NUDOCS-ABSTRACT 1 1 OGC/HDS2 1 0 EXTERNAL: NOAC NRC PDR 1 1 NOTE TO ALL"RIDS'ECIPIENTS: |
| | PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM PI-37 (EXT. 504-2083 ) TO ELIMINATEYOUR NAME FROM DISTRIBUTIONLISTS FOR DOCUMENTS YOU DON'T NEEDl TOTAL NUMBER OF COPIES REQUIRED: LTTR 13 ENCL 12 |
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| | indiana Michigan Power Company P.O. Box 16631 Columbus, OH 43216 i4arch 31, 1995 AEP:NRC:1185 Docket Nos.: 50-315 50-316 U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D. C. 20555 Gentlemen: |
| | Donald C. Cook Nuclear Plant Units 1 and 2 PROPOSED AMENDMENT TO TECHNICAL SPECIFICATION SECTION 3/4.6.1.7 FOR CONTAINMENT PURGE REQUIREMENTS and This letter and its attachments constitute an application for amendment to the Technical Specifications (T/Ss) for Donald C. Cook Nuclear Plant Units 1 and 2. Specifically, we are proposing to modify T/Ss 3/4.6.1.7, Containment Ventilation System, and its associated Bases, to allow limited (240 hours annually) purge operation in MODES 1, 2, 3, and 4 for pressure control, ALARA and respirable air quality considerations. The proposed changes will enhance our ability to use the containment purge system to reduce unnecessaiy hardships on plant personnel performing activities in containment. Additionally, an increase in allowable purge time is being requested to address improvements in plant operations and capacity factors. |
| | Attachment 1 provides a detailed description of the proposed changes, the justification for the changes, and ou'r determination of no significant hazards consideration performed pursuant to 10 CFR 50.92. Attachment 2 contains the existing T/S pages marked to reflect the proposed changes. Attachment 3 contains the revised T/S pages. |
| | We believe the proposed changes will not result in (1) a significant increase in .the amounts, and no significant change in the types of any effluent that may be released offsite, or (2) a significant increase in individual or cumulative occupational radiation exposure. |
| | These proposed changes have been reviewed by the Plant Nuclear Safety Review Committee and the Nuclear Safety and Design Review Committee. |
| | ', 9504060198 950331 PDR ADDCK 05000315 'l ) |
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| | U. S. Nuclear Regulatory Commission AEP:NRC:1185 Page 2 In compliance with the requirements of 10 CFR 50.91(b)(l), copies of this letter and its attachments have been transmitted to the Michigan Public Service Commission and to the Michigan Department of Public Health. |
| | Sincerely, E. E. Fit p trick Vice President SWORN TO AND SUBSCRIBED BEFORE ME THIS ~4~~ DAY OF QQ~~I~1995 |
| | /0 Nota Public My Commission Expires:~P-$ '$'h Attachments CC: A. A. Blind G. Charnoff J. B. Martin NFEM Section Chief NRC Resident Inspector - Bridgman J. R. Padgett |
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| | ATTACHMENT 1 TO AEP:NRC:1185 DESCRIPTION AND JUSTIFICATION OF CHANGES 10 CFR 50.92 ANALYSIS FOR CHANGES TO THE DONALD C. COOK NUCLEAR PLANT UNITS 1 AND 2 TECHNICAL SPECIFICATIONS |
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| | to AEP:NRC:1185 Page 1 I. ESCRIPTION OF CHANGES The proposed amendment to Technical Specifications (T/Ss) 3/4.6.1.7 makes the following specific changes to the Cook Nuclear Plant Units 1 and 2 T/Ss: |
| | T/S 3/4.6.1.7 A. Revises the Limiting Condition for Operation for specification 3/4.6.1.7 (on page 3/4 6-9a) to redefine the conditions in which it is permissible to operate the containment purge system when in MODES 1, 2, 3, and 4. The proposed Limiting Condition for Operation would be modified to read: |
| | "The containment purge supply and exhaust isolation valves shall be closed except when operation of the containment purge system is required for; pressure control, ALARA, and respirable air quality considerations for personnel entry and for surveillance testing and maintenance activities." |
| | B. Revise the Bases for specification 3/4.6.1.7 (page B 3/4 6-2a) to reflect the activities which allow purging in MODES 1, 2, 3, and 4, as defined above. Additional changes to the bases will include, 1) increasing the allowable purge time from 200 to 240 hours, 2) adding a reference to the ability of the purge isolation valves to close against LOCA forces, thereby assuring 10 CFR 100 guidelines are maintained, and 3) deleting |
| | "**" notes corrected during previous amendments. |
| | IX. JUSTIFICATION FOR CHANGES T/S 3/4.6.1.7 We propose to change the wording in both the Limiting Condition For Operation and the Bases of T/S 3/4.6.1.7 to allow limited containment purging while in MODES 1, 2, 3, and 4 for reasons other than "safety related reasons." |
| | As currently written,. use of the containment purge system during MODES 1, 2, 3, and 4 is limited to "safety related reasons." These are defined as "the need to improve containment working conditions, e.g., reduce airborne activity, to perform surveillance and/or maintenance on a safety-related system or piece of equipment." |
| | Additionally, purge operation is limited to 200 hours, per the technical specification bases. |
| | The restrictiveness of this wording results in unnecessary hardship to operators, maintenance technicians, instrument technicians, and other plant workers performing routine tasks in containment. For example, maintenance activities related to the upper containment |
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| | to AEP:NRC:1185 Page 2 ventilation systems and the glycol floor cooling system represent required activities on equipment which is not characterized as "safety related." |
| | A change to the specification would allow the limited use of containment purge to address adverse environmental conditions (i.e., |
| | temperature, humidity, and/or pressure), ALARA concerns, and to assure that respirable air quality is maintained. It should be noted that the use of the purge system to support the above activities would be restricted to occasions when the existing air filtration and temperature control systems were not sufficient to provide a containment atmosphere supportive of working conditions. |
| | An additional change to T/S 3/4.6.1.7 is to increase the current purge limit of 200 hours per year to 240 hours. The original time limit was calculated based on a unit capacity factor of 77X. As a result of longer operating cycles and improved plant performance, the Cook Nuclear Plant capacity factor is now forecasted to be 93X. |
| | Utilizing the same calculation which established the 200 hour limit, and increasing the capacity factor to 93X yields a value of 240 hours. This increased time allotment reflects the additional time the unit will remain in MODES 1, 2, 3, and 4 with a 93K capacity factor. |
| | As stated in the technical specification bases, the containment purge system at Cook Nuclear Plant has been designed in accordance with NRC Branch Technical Position CBS 6-4, Rev. 1, and demonstrated to be capable of closure against the dynamic forces associated with a loss of coolant accident. The purge valves will receive a containment ventilation isolation signal on both a safety injection and high radiation signals and close within 5 seconds. In accordance with the above Branch Technical Position, the potential site boundary doses were calculated based on the original analysis used to determine the radiological consequences of a loss of coolant accident. The results of this analysis indicated a total thyroid dose of 165 rem for the 0-2 hour site boundary dose and a whole body dose of 9.32 rem. Since physical changes will not result from the proposed amendment, the site boundary does guidelines of 10 CFR 100 (300 rem thyroid and 25 rem whole body) will not be exceeded in the event of an accident during containment purging operations. |
| | The addition of 40 hours of allowable annual purge time will not result in a significant increase in the amount of effluent released. |
| | The Offsite Dose Calculation Manual (ODCM) ensures that the dose rate at any time at the SITE BOUNDARY from gaseous effluent from all units on the site will be within the annual dose limits of Appendix B, Table 2, Column 1 of 10 CFR 20 for UNRESTRICTED AREAS. These specifications will be strictly adhered to during any release via the purge pathway. |
| | to AEP:NRC:1185 Page 3 In conclusion, we believe that the proposed technical specifications will not affect system capability or introduce a new or different mode of purge system operation not previously addressed in the above analysis. |
| | III. 10 CFR 50 92 CRITERIA Per 10 CFR 50.92, a proposed change does not involve a significant hazards consideration if the change does not: |
| | involve a significant increase in the probability or consequences of an accident previously evaluated, |
| | : 2. create the possibility of a new or different kind of accident from any accident previously evaluated, or |
| | : 3. involve a significant reduction in a margin of safety. |
| | Criter on The purpose of this amendment is to allow flexibility in the use of the containment purge system during MODES 1, 2, 3, and 4. The use of this system during these modes of operation has previously been approved (Amendment No. 66). Therefore, this amendment request does not involve a ,significant increase in the probability or consequences of an accident previously evaluated because the proposed change 'o the T/Ss does not affect the assumptions, parameters, or results of any UFSAR accident analysis. Based on the existing system design and demonstrated closure capability it is concluded that the proposed changes do not modify the response of the containment during a design basis accident. The proposed amendment does not add or modify any existing equipment. Based on these considerations, it is concluded that the changes do not involve a significant increase in the probability or consequences of an accident previously evaluated. |
| | Criterion 2 The proposed change does not involve physical changes to the plant or changes in the plant operating configuration. Thus, it is concluded that the proposed change does not create the possibility of a new or different kind of accident from any accident previously evaluated. |
| | to AEP:NRC:1185 Page 4 Criterion 3 The margin for safety presently provided is not reduced by the proposed change. As discussed previously, the containment purge valves have been designed and demonstrated capable of closure against the dynamic forces resulting from a loss of coolant accident. The proposed amendment does not impact the ability of the purge valves to perform their intended .function (i.e. achieve closure) in the event of an accident. Based on these considerations, it is concluded that the changes do not involve a significant reduction in a margin of safety. |
| | IV. CONCLUSION In conclusion, we believe that the proposed change does not involve significant hazards considerations because, as demonstrated in the previous discussions, operation of the Cook Nuclear Plant in accordance with the changes would not: |
| | involve a significant increase in the probability or consequences of an accident previously evaluated, |
| | : 2. create the possibility of a new or different kind of accident from any accident previously evaluated, or |
| | : 3. involve a significant reduction in a margin of safety. |
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| | ATTACHMENT 2 TO AEP:NRC:1185 EXISTING TECHNICAL SPECIFICATION PAGES MARKED TO REFLECT PROPOSED CHANGES |
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Category:OPERATING LICENSES-APPLIATION TO AMEND-RENEW EXISTING
MONTHYEARML17335A5551999-10-12012 October 1999 Application for Amends to Licenses DPR-58 & DPR-74,revising TS Surveillance Requirement 4.6.2.2.d for Spray Additive Sys to Relocate Details Associated with Acceptance Criteria & Test Parameters to Associated TS Bases ML17335A5591999-10-11011 October 1999 Supplement to Application for Amends to Licenses DPR-58 & DPR-74,replacing Correct TS Pages Inadvertently Included in 990923 Submittal.Attached Pages Also Include Appropriate Administrative Changes ML17335A5411999-10-0101 October 1999 Application for Amends to Licenses DPR-58 & DPR-74,revising Containment Recirculation Sump Water Inventory.Calculation & non-proprietary WCAP-15302 Rept Also Encl ML17326A1571999-09-23023 September 1999 Application for Amends to Licenses DPR-58 & DPR-74,involving Movement of Loads in Excess of Design Basis Seismic Capability of Auxiliary Bldg Load Handling Equipment & Structures ML17326A1421999-09-17017 September 1999 Application for Amends to Licenses DPR-58 & DPR-74,to Allow Credit of Rod Cluster Control Assemblies for Cold Leg Large Break LOCA Subcriticality.Ts Pages & non-proprietary Versions of WCAP-15246 Encl.Proprietary Version Withheld ML17326A1161999-09-10010 September 1999 Application for Amends to Licenses DPR-58 & DPR-74,revising TS Surveillance Requirement 4.4.7,TS Tables 4.4-3,3.4-1 & TS Surveillance Requirement 4.11.2.2 Re RCS & Gas Storage Tank Sampling ML17326A0921999-08-17017 August 1999 Application for Amend to License DPR-58,to Change TS 3/4.4.5 & Bases for TS 3/4.4.5,3/4.4.6.2 & 3/4.4.8 to Remove voltage-based Repair Criteria,F* Repair Criteria & Sleeving Methodologies from Unit 1 TS & Clarify Bases Sections ML17325B6041999-05-21021 May 1999 Application for Amends to Licenses DPR-58 & DPR-74,revising Limitations of Positive Reactivity Additions in Several TS Action Statements ML17325B5511999-04-19019 April 1999 Application for Amends to Licenses DPR-58 & DPR-74,revising TS 3/4.8.1.2, Electrical Power Systems & Associated Bases to Provide one-time Extension of 18-month Surveillance Interval for Specific SRs ML17335A3661998-12-0303 December 1998 Application for Amends to Licenses DPR-58 & DPR-74,adding TS for Distributed Ignition Sys ML17335A3631998-12-0303 December 1998 Application for Amend to License DPR-58,revising TS 3/4.7.7, Sealed Source Contamination & Associated Bases to Address Testing Requirements for Fission Detectors ML17335A3591998-12-0303 December 1998 Application for Amends to Licenses DPR-58 & DPR-74,making Administrative Changes to Remove Obsolete Info,To Provide Consistency Between Units 1 & 2,to Provide Consistency with Std Tech Specs,To Provide Clarification & to Correct Typos ML17335A3561998-12-0303 December 1998 Application for Amends to Licenses DPR-58 & DPR-74,revising TS 4.6.5.1, Ice Condenser,Ice Bed & Associated Bases to Reflect Max Ice Condenser Flow Channel Blockage Assumed in Accident Analyses ML17335A2631998-10-0808 October 1998 Application for Amends to Licenses DPR-58 & DPR-74,revising TS Containment Sys Bases 3/4.6.1.4 Re Internal Pressure & 3/4.6.1.5 Re Air Temp ML17335A2761998-10-0808 October 1998 Application for Amends to Licenses DPR-58 & DPR-74,placing Tighter Restrictions on Amount of Time RWST Water Level Instrumentation Can Be Out of Svc Before Compensatory Actions Are Required ML17335A2671998-10-0808 October 1998 Application for Amends to Licenses DPR-58 & DPR-74,revising TS 3.4.1.3, RCS - Shutdown & Associated Bases to Provide Separate Requirements for Modes 4 & 5 with Loops Filled & Mode 5 with Loops Not Filled ML17335A2311998-09-14014 September 1998 Application for Amends to Licenses DPR-58 & DPR-74,changing Runout Limits for Safety Injection Pump to 675 Gpm Unless Pump Is Specifically Tested to Higher Flow Rate Not Exceeding 700 Gpm ML17335A1901998-08-28028 August 1998 Application for Amend to License DPR-58,requesting Extension of SG Surveillance,Which TSs Require to Be Performed on or Before 990408,until End of Current Refuel Cycle Currently Scheduled for Mar 2000.W/assessment of SG Degradation & TSs ML17334A7471998-06-10010 June 1998 Application for Amends to Licenses DPR-54 & DPR-78,changing Implementation Date to Reduce Boric Acid Concentration in Boric Acid Storage Sys.Attachment 1 to Ltr Contains Description of Proposed Change & Justification for Change ML17334B7011998-03-0303 March 1998 Application for Amends to TS for Licenses DPR-58 & DPR-74, Removing Word Immediately from Unit 1 Hydrogen Recombiner Surveillance Requirement 4.6.4.2.b.4 & Revising Plants TS 3/4.6.4 Bases ML17334B6561997-10-0808 October 1997 Application for Amends to Licenses DPR-58 & DPR-78,changing TSs 3/4.6.5 & 3/4.5.5 to Increase Both Minimum Required Ice Mass Per Ice Basket & Total Minimum Required Ice Mass. Proprietary Summary of Sump Inventory Calculations,Encl ML17333B0431997-09-19019 September 1997 Application for Amends to Licenses DPR-58 & DPR-74,deleting Requirement for Automatic Valve Closure Feature on RHR Sys Suction from RCS ML17333A9831997-08-11011 August 1997 Application for Amends to Licenses DPR-58 & DPR-74,allowing Filling of ECCS Accumulators W/O Declaring ECCS Equipment Inoperable ML17335A2101997-08-0101 August 1997 Application for Amends to Licenses DPR-58 & DPR-74,deleting Wording When Secondary Steam Supply Pressure Is Greater than 310 Psig from TS ML17333A8281997-03-26026 March 1997 Application for Amends to Licenses DPR-58 & DPR-74, Modifying TS 4.7.5.1.e.2 Which Describes Control Room Ventilation Sys Autostart Functions ML17333A8311997-03-26026 March 1997 Application for Amends to Licenses DPR-58 & DPR-74,changing Grammatical Correction to Wording of Unit 2 TS 3.4.8,Action a for Modes 1,2 & 3 & Returning Frequency Requirement to TS 4.7.1.2.c & 4.7.1.2.d That Was Inadvertently Deleted ML17333A7121996-12-20020 December 1996 Application for Amends to Licenses DPR-58 & DPR-74, Requesting Rev of Reactor Coolant Pump Flywheel Insp Frequency ML17334B5941996-07-11011 July 1996 Application for Amends to Licenses DPR-58 & DPR-74,revising TS to Support Operation of Unit 2 at Increased Core Rated Thermal Power of 3,588 Mwt.Rev 1 to WCAP-14489, ...Unit 2 3,600 Mwt Uprating Program Licensing Rept Encl ML17334B5901996-06-19019 June 1996 Application for Amend to License DPR-58,addressing Applicable Requirements of NRC GL 95-05, Voltage-Based Repair Criteria for Repair of Westinghouse SG Tubes Affected by Outside Diameter Stress Corrosion Cracking. ML17334B5891996-06-11011 June 1996 Application for Amends to Licenses DPR-58 & DPR-74,removing TSs Certain Requirements for Administrative Controls,Related to QA Requirements,Per Administrative Ltr 96-05 ML17333A4201996-04-0808 April 1996 Application for Amends to Licenses DPR-58 & DPR-74,moving TS 4.0.4 Exemption Statement for MSSVs Into Section 4.7.1.1 ML17333A3551996-03-12012 March 1996 Application for Amend to License DPR-74,removing TSs Re Shutdown & Control Rod Position Indication While in Modes 3, 4 & 5 ML17334B5751996-02-29029 February 1996 Application for Amends to Licenses DPR-58 & DPR-74,revising TS to Reduce Boric Acid Concentration in Boric Acid Storage Sys from Approx 12 Percent to Approx 4 Percent by Weight. Technical Rept Presenting Justificaion for Changes Encl ML17334B5741996-02-26026 February 1996 Application for Amends to Licenses DPR-58 & DPR-74,modifying TS 5.6.2 to Increase Current Limit on Nominal Fuel Assembly Enrichment for New,Westinghouse - Fabricated Fuel Stored in New Fuel Storage Racks ML17333A3201996-02-22022 February 1996 Application for Amends to Licenses DPR-58 & DPR-74,proposing to Remove Requirement That Operations Superintendent Must Hold or Have Held Sol at Plant or Similar Reactor ML17333A3151996-02-22022 February 1996 Application for Amends to Licenses DPR-58 & DPR-74,modifying Table 4.8-1,DG Test Schedule by Ref Rg 1.9,Rev 3 Rather than Rg 1.108,Rev 1 Criteria for Determination of Valid DG Test ML17333A2641996-01-12012 January 1996 Application for Amends to Licenses DPR-58 & DPR-74,modifying TS Section 4.4.11 to Eliminate SR Demonstrating Operability of Emergency Power Supply for Pressurizer PORVs & Block Valves ML17333A2391995-12-19019 December 1995 Application for Amends to Licenses DPR-58 & DPR-74,modifying TS 3/4.6.1.2,3/4.6.1.3,3/4.6.1.6 & 3/4.6.1.6 to Require Types A,B & C Tests (Overall Integrated & Local Containment Leakage Rate) to Be Performed Per 10CFR50,App J Option B ML17332B0111995-11-10010 November 1995 Application for Amends to Licenses DPR-58 & DPR-74,revising Ts,By Modifying Surveillance Testing of EDG During Refueling & Normal Operations ML17332A9971995-10-20020 October 1995 Application for Amends to Licenses DPR-58 & DPR-74,proposing to Add Exemption to TS 4.0.4 in Surveillance Requirements for MSIV ML17332A9111995-08-0606 August 1995 Application for Amends to Licenses DPR-58 & DPR-74,informing That Licensee Has 45 Days from Date of Issuance to Implement Amend Unless Otherwise Specified ML17334B5561995-08-0404 August 1995 Application for Exigent Amend to License DPR-58,modifying TS 4.4.5.4 & 4.4.5.5 for Repair of Hybrid Expansion Joint Sleeved SG Tubes.Proprietary W Rept WCAP-14446, Repair...Of Hybrid Expansion Joint...Tubes Encl.W Rept Withheld ML17332A8271995-06-30030 June 1995 Application for Amends to Licenses DPR-58 & DPR-74,changing TS Section 5.3.1 to Allow Fuel Reconstitution,Per GL 90-02, Suppl 1 ML17334B5501995-06-20020 June 1995 License Amend Request to Licenses DPR-58 & DPR-74,to Remove Requirements for Fire Protection Systems from Licenses & Guidance in GL 86-10,GL 88-12 & GL 93-07 ML17332A7991995-06-15015 June 1995 Application for Amends to Licenses DPR-58 & DPR-74,revising TS 4.8.1.1.2.e.7 to Reduce Duration of Surveillance Testing for EDGs During Refueling Operations from 24 H to 8 H ML17334B5481995-05-26026 May 1995 Application for Amends to Licenses DPR-58 & DPR-74.Amends Would Support Operation of Unit 1 at SG Tube Plugging Levels Up to 30%,make One Unit 1 TS More Nearly Like Corresponding Unit 2 TS & Maintain Consistency of Unit 2 Criteria ML17334B5461995-05-26026 May 1995 Application for Amends to Licenses DPR-58 & DPR-74,modifying Tech Specs 3/4.3.1 (Reactor Trip Sys Instrumentation) & 3/4.3.2 (ESFAS Instrumentation) & Bases to Relocate Tables of Response Time Limits to Ufsar,Per GL 93-08 ML17332A7661995-05-25025 May 1995 Application for Amends to Licenses DPR-58 & DPR-74.Amends Would Incorporate Cycle & Burnup Dependent Peaking Factor Penalty ML17332A7741995-05-25025 May 1995 Application for Amends to Licenses DPR-58 & DPR-74,modifying TS 5.3.1 to Allow Fuel Reconstitution,Per GL 90-02,Suppl 1 ML17332A7771995-05-25025 May 1995 Application for Amends to Licenses DPR-58 & DPR-74,modifying TS Table 4.3-2 to Change Main Steam Line Isolation Valve Manual Actuation Sys Surveillance Frequency from Monthly to Quarterly 1999-09-23
[Table view] Category:TEXT-LICENSE APPLICATIONS & PERMITS
MONTHYEARML17335A5551999-10-12012 October 1999 Application for Amends to Licenses DPR-58 & DPR-74,revising TS Surveillance Requirement 4.6.2.2.d for Spray Additive Sys to Relocate Details Associated with Acceptance Criteria & Test Parameters to Associated TS Bases ML17335A5591999-10-11011 October 1999 Supplement to Application for Amends to Licenses DPR-58 & DPR-74,replacing Correct TS Pages Inadvertently Included in 990923 Submittal.Attached Pages Also Include Appropriate Administrative Changes ML17335A5411999-10-0101 October 1999 Application for Amends to Licenses DPR-58 & DPR-74,revising Containment Recirculation Sump Water Inventory.Calculation & non-proprietary WCAP-15302 Rept Also Encl ML17326A1571999-09-23023 September 1999 Application for Amends to Licenses DPR-58 & DPR-74,involving Movement of Loads in Excess of Design Basis Seismic Capability of Auxiliary Bldg Load Handling Equipment & Structures ML17326A1421999-09-17017 September 1999 Application for Amends to Licenses DPR-58 & DPR-74,to Allow Credit of Rod Cluster Control Assemblies for Cold Leg Large Break LOCA Subcriticality.Ts Pages & non-proprietary Versions of WCAP-15246 Encl.Proprietary Version Withheld ML17326A1161999-09-10010 September 1999 Application for Amends to Licenses DPR-58 & DPR-74,revising TS Surveillance Requirement 4.4.7,TS Tables 4.4-3,3.4-1 & TS Surveillance Requirement 4.11.2.2 Re RCS & Gas Storage Tank Sampling ML17326A0921999-08-17017 August 1999 Application for Amend to License DPR-58,to Change TS 3/4.4.5 & Bases for TS 3/4.4.5,3/4.4.6.2 & 3/4.4.8 to Remove voltage-based Repair Criteria,F* Repair Criteria & Sleeving Methodologies from Unit 1 TS & Clarify Bases Sections ML17325B6041999-05-21021 May 1999 Application for Amends to Licenses DPR-58 & DPR-74,revising Limitations of Positive Reactivity Additions in Several TS Action Statements ML17325B5511999-04-19019 April 1999 Application for Amends to Licenses DPR-58 & DPR-74,revising TS 3/4.8.1.2, Electrical Power Systems & Associated Bases to Provide one-time Extension of 18-month Surveillance Interval for Specific SRs ML17335A3661998-12-0303 December 1998 Application for Amends to Licenses DPR-58 & DPR-74,adding TS for Distributed Ignition Sys ML17335A3631998-12-0303 December 1998 Application for Amend to License DPR-58,revising TS 3/4.7.7, Sealed Source Contamination & Associated Bases to Address Testing Requirements for Fission Detectors ML17335A3591998-12-0303 December 1998 Application for Amends to Licenses DPR-58 & DPR-74,making Administrative Changes to Remove Obsolete Info,To Provide Consistency Between Units 1 & 2,to Provide Consistency with Std Tech Specs,To Provide Clarification & to Correct Typos ML17335A3561998-12-0303 December 1998 Application for Amends to Licenses DPR-58 & DPR-74,revising TS 4.6.5.1, Ice Condenser,Ice Bed & Associated Bases to Reflect Max Ice Condenser Flow Channel Blockage Assumed in Accident Analyses ML17335A2631998-10-0808 October 1998 Application for Amends to Licenses DPR-58 & DPR-74,revising TS Containment Sys Bases 3/4.6.1.4 Re Internal Pressure & 3/4.6.1.5 Re Air Temp ML17335A2761998-10-0808 October 1998 Application for Amends to Licenses DPR-58 & DPR-74,placing Tighter Restrictions on Amount of Time RWST Water Level Instrumentation Can Be Out of Svc Before Compensatory Actions Are Required ML17335A2671998-10-0808 October 1998 Application for Amends to Licenses DPR-58 & DPR-74,revising TS 3.4.1.3, RCS - Shutdown & Associated Bases to Provide Separate Requirements for Modes 4 & 5 with Loops Filled & Mode 5 with Loops Not Filled ML17335A2311998-09-14014 September 1998 Application for Amends to Licenses DPR-58 & DPR-74,changing Runout Limits for Safety Injection Pump to 675 Gpm Unless Pump Is Specifically Tested to Higher Flow Rate Not Exceeding 700 Gpm ML17335A1901998-08-28028 August 1998 Application for Amend to License DPR-58,requesting Extension of SG Surveillance,Which TSs Require to Be Performed on or Before 990408,until End of Current Refuel Cycle Currently Scheduled for Mar 2000.W/assessment of SG Degradation & TSs ML17334A7471998-06-10010 June 1998 Application for Amends to Licenses DPR-54 & DPR-78,changing Implementation Date to Reduce Boric Acid Concentration in Boric Acid Storage Sys.Attachment 1 to Ltr Contains Description of Proposed Change & Justification for Change ML17334B7011998-03-0303 March 1998 Application for Amends to TS for Licenses DPR-58 & DPR-74, Removing Word Immediately from Unit 1 Hydrogen Recombiner Surveillance Requirement 4.6.4.2.b.4 & Revising Plants TS 3/4.6.4 Bases ML17334B6561997-10-0808 October 1997 Application for Amends to Licenses DPR-58 & DPR-78,changing TSs 3/4.6.5 & 3/4.5.5 to Increase Both Minimum Required Ice Mass Per Ice Basket & Total Minimum Required Ice Mass. Proprietary Summary of Sump Inventory Calculations,Encl ML17333B0431997-09-19019 September 1997 Application for Amends to Licenses DPR-58 & DPR-74,deleting Requirement for Automatic Valve Closure Feature on RHR Sys Suction from RCS ML17333A9831997-08-11011 August 1997 Application for Amends to Licenses DPR-58 & DPR-74,allowing Filling of ECCS Accumulators W/O Declaring ECCS Equipment Inoperable ML17335A2101997-08-0101 August 1997 Application for Amends to Licenses DPR-58 & DPR-74,deleting Wording When Secondary Steam Supply Pressure Is Greater than 310 Psig from TS ML17333A8281997-03-26026 March 1997 Application for Amends to Licenses DPR-58 & DPR-74, Modifying TS 4.7.5.1.e.2 Which Describes Control Room Ventilation Sys Autostart Functions ML17333A8311997-03-26026 March 1997 Application for Amends to Licenses DPR-58 & DPR-74,changing Grammatical Correction to Wording of Unit 2 TS 3.4.8,Action a for Modes 1,2 & 3 & Returning Frequency Requirement to TS 4.7.1.2.c & 4.7.1.2.d That Was Inadvertently Deleted ML17333A7121996-12-20020 December 1996 Application for Amends to Licenses DPR-58 & DPR-74, Requesting Rev of Reactor Coolant Pump Flywheel Insp Frequency ML17334B5941996-07-11011 July 1996 Application for Amends to Licenses DPR-58 & DPR-74,revising TS to Support Operation of Unit 2 at Increased Core Rated Thermal Power of 3,588 Mwt.Rev 1 to WCAP-14489, ...Unit 2 3,600 Mwt Uprating Program Licensing Rept Encl ML17334B5901996-06-19019 June 1996 Application for Amend to License DPR-58,addressing Applicable Requirements of NRC GL 95-05, Voltage-Based Repair Criteria for Repair of Westinghouse SG Tubes Affected by Outside Diameter Stress Corrosion Cracking. ML17334B5891996-06-11011 June 1996 Application for Amends to Licenses DPR-58 & DPR-74,removing TSs Certain Requirements for Administrative Controls,Related to QA Requirements,Per Administrative Ltr 96-05 ML17333A4201996-04-0808 April 1996 Application for Amends to Licenses DPR-58 & DPR-74,moving TS 4.0.4 Exemption Statement for MSSVs Into Section 4.7.1.1 ML17333A3551996-03-12012 March 1996 Application for Amend to License DPR-74,removing TSs Re Shutdown & Control Rod Position Indication While in Modes 3, 4 & 5 ML17334B5751996-02-29029 February 1996 Application for Amends to Licenses DPR-58 & DPR-74,revising TS to Reduce Boric Acid Concentration in Boric Acid Storage Sys from Approx 12 Percent to Approx 4 Percent by Weight. Technical Rept Presenting Justificaion for Changes Encl ML17334B5741996-02-26026 February 1996 Application for Amends to Licenses DPR-58 & DPR-74,modifying TS 5.6.2 to Increase Current Limit on Nominal Fuel Assembly Enrichment for New,Westinghouse - Fabricated Fuel Stored in New Fuel Storage Racks ML17333A3201996-02-22022 February 1996 Application for Amends to Licenses DPR-58 & DPR-74,proposing to Remove Requirement That Operations Superintendent Must Hold or Have Held Sol at Plant or Similar Reactor ML17333A3151996-02-22022 February 1996 Application for Amends to Licenses DPR-58 & DPR-74,modifying Table 4.8-1,DG Test Schedule by Ref Rg 1.9,Rev 3 Rather than Rg 1.108,Rev 1 Criteria for Determination of Valid DG Test ML17333A2641996-01-12012 January 1996 Application for Amends to Licenses DPR-58 & DPR-74,modifying TS Section 4.4.11 to Eliminate SR Demonstrating Operability of Emergency Power Supply for Pressurizer PORVs & Block Valves ML17333A2391995-12-19019 December 1995 Application for Amends to Licenses DPR-58 & DPR-74,modifying TS 3/4.6.1.2,3/4.6.1.3,3/4.6.1.6 & 3/4.6.1.6 to Require Types A,B & C Tests (Overall Integrated & Local Containment Leakage Rate) to Be Performed Per 10CFR50,App J Option B ML17332B0111995-11-10010 November 1995 Application for Amends to Licenses DPR-58 & DPR-74,revising Ts,By Modifying Surveillance Testing of EDG During Refueling & Normal Operations ML17332A9971995-10-20020 October 1995 Application for Amends to Licenses DPR-58 & DPR-74,proposing to Add Exemption to TS 4.0.4 in Surveillance Requirements for MSIV ML17332A9111995-08-0606 August 1995 Application for Amends to Licenses DPR-58 & DPR-74,informing That Licensee Has 45 Days from Date of Issuance to Implement Amend Unless Otherwise Specified ML17334B5561995-08-0404 August 1995 Application for Exigent Amend to License DPR-58,modifying TS 4.4.5.4 & 4.4.5.5 for Repair of Hybrid Expansion Joint Sleeved SG Tubes.Proprietary W Rept WCAP-14446, Repair...Of Hybrid Expansion Joint...Tubes Encl.W Rept Withheld ML17332A8271995-06-30030 June 1995 Application for Amends to Licenses DPR-58 & DPR-74,changing TS Section 5.3.1 to Allow Fuel Reconstitution,Per GL 90-02, Suppl 1 ML17334B5501995-06-20020 June 1995 License Amend Request to Licenses DPR-58 & DPR-74,to Remove Requirements for Fire Protection Systems from Licenses & Guidance in GL 86-10,GL 88-12 & GL 93-07 ML17332A7991995-06-15015 June 1995 Application for Amends to Licenses DPR-58 & DPR-74,revising TS 4.8.1.1.2.e.7 to Reduce Duration of Surveillance Testing for EDGs During Refueling Operations from 24 H to 8 H ML17334B5481995-05-26026 May 1995 Application for Amends to Licenses DPR-58 & DPR-74.Amends Would Support Operation of Unit 1 at SG Tube Plugging Levels Up to 30%,make One Unit 1 TS More Nearly Like Corresponding Unit 2 TS & Maintain Consistency of Unit 2 Criteria ML17334B5461995-05-26026 May 1995 Application for Amends to Licenses DPR-58 & DPR-74,modifying Tech Specs 3/4.3.1 (Reactor Trip Sys Instrumentation) & 3/4.3.2 (ESFAS Instrumentation) & Bases to Relocate Tables of Response Time Limits to Ufsar,Per GL 93-08 ML17332A7661995-05-25025 May 1995 Application for Amends to Licenses DPR-58 & DPR-74.Amends Would Incorporate Cycle & Burnup Dependent Peaking Factor Penalty ML17332A7741995-05-25025 May 1995 Application for Amends to Licenses DPR-58 & DPR-74,modifying TS 5.3.1 to Allow Fuel Reconstitution,Per GL 90-02,Suppl 1 ML17332A7771995-05-25025 May 1995 Application for Amends to Licenses DPR-58 & DPR-74,modifying TS Table 4.3-2 to Change Main Steam Line Isolation Valve Manual Actuation Sys Surveillance Frequency from Monthly to Quarterly 1999-09-23
[Table view] |
Text
R.ICDR.IMY' P'CELERATED RIDS PROCESSING)
REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
ACCESSION NBR:9504060198 DOC.DATE: 95/03/31 NOTARIZED: YES DOCKET FACIL:50-315 Donald C. Cook Nuclear Power Plant, Unit 1, Indiana M 05000315 50-316 Donald C. Cook Nuclear Power Plant, Unit 2, Indiana M 05000316 AUTH. NAME AUTHOR AFFILIATION FITZPATRICK,E. Indiana Michigan Power Co. (formerly Indiana & Michigan Ele RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)
SUBZECT: Application for amends to licenses DPR-58 & DPR-74.Amends
. would modify TS 3/4.6.1.7 to allow limited purge operation in modes 1,2,3 & 4 for pressure control,ALARA & respirable air quality considerations.
DISTRIBUTION CODE: A001D COPIES RECEIVED:LTR ENCL SIZE:
TITLE: OR Submittal: General Distribution NOTES:
RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD3-1 LA 1 1 PD3-1 PD 1 1 HICKMAN,Z 1 1 INTERNAL~FILE CENTER 1 1 NMS S/DWM/LLDP 2 2
~01'RR/DRCH/HICB 1 1 NRR/DSSA/SPLB 1 1 NRR/DSSA/SRXB 1 1 NUDOCS-ABSTRACT 1 1 OGC/HDS2 1 0 EXTERNAL: NOAC NRC PDR 1 1 NOTE TO ALL"RIDS'ECIPIENTS:
PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM PI-37 (EXT. 504-2083 ) TO ELIMINATEYOUR NAME FROM DISTRIBUTIONLISTS FOR DOCUMENTS YOU DON'T NEEDl TOTAL NUMBER OF COPIES REQUIRED: LTTR 13 ENCL 12
fl l
indiana Michigan Power Company P.O. Box 16631 Columbus, OH 43216 i4arch 31, 1995 AEP:NRC:1185 Docket Nos.: 50-315 50-316 U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D. C. 20555 Gentlemen:
Donald C. Cook Nuclear Plant Units 1 and 2 PROPOSED AMENDMENT TO TECHNICAL SPECIFICATION SECTION 3/4.6.1.7 FOR CONTAINMENT PURGE REQUIREMENTS and This letter and its attachments constitute an application for amendment to the Technical Specifications (T/Ss) for Donald C. Cook Nuclear Plant Units 1 and 2. Specifically, we are proposing to modify T/Ss 3/4.6.1.7, Containment Ventilation System, and its associated Bases, to allow limited (240 hours0.00278 days <br />0.0667 hours <br />3.968254e-4 weeks <br />9.132e-5 months <br /> annually) purge operation in MODES 1, 2, 3, and 4 for pressure control, ALARA and respirable air quality considerations. The proposed changes will enhance our ability to use the containment purge system to reduce unnecessaiy hardships on plant personnel performing activities in containment. Additionally, an increase in allowable purge time is being requested to address improvements in plant operations and capacity factors.
Attachment 1 provides a detailed description of the proposed changes, the justification for the changes, and ou'r determination of no significant hazards consideration performed pursuant to 10 CFR 50.92. Attachment 2 contains the existing T/S pages marked to reflect the proposed changes. Attachment 3 contains the revised T/S pages.
We believe the proposed changes will not result in (1) a significant increase in .the amounts, and no significant change in the types of any effluent that may be released offsite, or (2) a significant increase in individual or cumulative occupational radiation exposure.
These proposed changes have been reviewed by the Plant Nuclear Safety Review Committee and the Nuclear Safety and Design Review Committee.
', 9504060198 950331 PDR ADDCK 05000315 'l )
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U. S. Nuclear Regulatory Commission AEP:NRC:1185 Page 2 In compliance with the requirements of 10 CFR 50.91(b)(l), copies of this letter and its attachments have been transmitted to the Michigan Public Service Commission and to the Michigan Department of Public Health.
Sincerely, E. E. Fit p trick Vice President SWORN TO AND SUBSCRIBED BEFORE ME THIS ~4~~ DAY OF QQ~~I~1995
/0 Nota Public My Commission Expires:~P-$ '$'h Attachments CC: A. A. Blind G. Charnoff J. B. Martin NFEM Section Chief NRC Resident Inspector - Bridgman J. R. Padgett
ATTACHMENT 1 TO AEP:NRC:1185 DESCRIPTION AND JUSTIFICATION OF CHANGES 10 CFR 50.92 ANALYSIS FOR CHANGES TO THE DONALD C. COOK NUCLEAR PLANT UNITS 1 AND 2 TECHNICAL SPECIFICATIONS
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to AEP:NRC:1185 Page 1 I. ESCRIPTION OF CHANGES The proposed amendment to Technical Specifications (T/Ss) 3/4.6.1.7 makes the following specific changes to the Cook Nuclear Plant Units 1 and 2 T/Ss:
T/S 3/4.6.1.7 A. Revises the Limiting Condition for Operation for specification 3/4.6.1.7 (on page 3/4 6-9a) to redefine the conditions in which it is permissible to operate the containment purge system when in MODES 1, 2, 3, and 4. The proposed Limiting Condition for Operation would be modified to read:
"The containment purge supply and exhaust isolation valves shall be closed except when operation of the containment purge system is required for; pressure control, ALARA, and respirable air quality considerations for personnel entry and for surveillance testing and maintenance activities."
B. Revise the Bases for specification 3/4.6.1.7 (page B 3/4 6-2a) to reflect the activities which allow purging in MODES 1, 2, 3, and 4, as defined above. Additional changes to the bases will include, 1) increasing the allowable purge time from 200 to 240 hours0.00278 days <br />0.0667 hours <br />3.968254e-4 weeks <br />9.132e-5 months <br />, 2) adding a reference to the ability of the purge isolation valves to close against LOCA forces, thereby assuring 10 CFR 100 guidelines are maintained, and 3) deleting
"**" notes corrected during previous amendments.
IX. JUSTIFICATION FOR CHANGES T/S 3/4.6.1.7 We propose to change the wording in both the Limiting Condition For Operation and the Bases of T/S 3/4.6.1.7 to allow limited containment purging while in MODES 1, 2, 3, and 4 for reasons other than "safety related reasons."
As currently written,. use of the containment purge system during MODES 1, 2, 3, and 4 is limited to "safety related reasons." These are defined as "the need to improve containment working conditions, e.g., reduce airborne activity, to perform surveillance and/or maintenance on a safety-related system or piece of equipment."
Additionally, purge operation is limited to 200 hours0.00231 days <br />0.0556 hours <br />3.306878e-4 weeks <br />7.61e-5 months <br />, per the technical specification bases.
The restrictiveness of this wording results in unnecessary hardship to operators, maintenance technicians, instrument technicians, and other plant workers performing routine tasks in containment. For example, maintenance activities related to the upper containment
-a I n e
to AEP:NRC:1185 Page 2 ventilation systems and the glycol floor cooling system represent required activities on equipment which is not characterized as "safety related."
A change to the specification would allow the limited use of containment purge to address adverse environmental conditions (i.e.,
temperature, humidity, and/or pressure), ALARA concerns, and to assure that respirable air quality is maintained. It should be noted that the use of the purge system to support the above activities would be restricted to occasions when the existing air filtration and temperature control systems were not sufficient to provide a containment atmosphere supportive of working conditions.
An additional change to T/S 3/4.6.1.7 is to increase the current purge limit of 200 hours0.00231 days <br />0.0556 hours <br />3.306878e-4 weeks <br />7.61e-5 months <br /> per year to 240 hours0.00278 days <br />0.0667 hours <br />3.968254e-4 weeks <br />9.132e-5 months <br />. The original time limit was calculated based on a unit capacity factor of 77X. As a result of longer operating cycles and improved plant performance, the Cook Nuclear Plant capacity factor is now forecasted to be 93X.
Utilizing the same calculation which established the 200 hour0.00231 days <br />0.0556 hours <br />3.306878e-4 weeks <br />7.61e-5 months <br /> limit, and increasing the capacity factor to 93X yields a value of 240 hours0.00278 days <br />0.0667 hours <br />3.968254e-4 weeks <br />9.132e-5 months <br />. This increased time allotment reflects the additional time the unit will remain in MODES 1, 2, 3, and 4 with a 93K capacity factor.
As stated in the technical specification bases, the containment purge system at Cook Nuclear Plant has been designed in accordance with NRC Branch Technical Position CBS 6-4, Rev. 1, and demonstrated to be capable of closure against the dynamic forces associated with a loss of coolant accident. The purge valves will receive a containment ventilation isolation signal on both a safety injection and high radiation signals and close within 5 seconds. In accordance with the above Branch Technical Position, the potential site boundary doses were calculated based on the original analysis used to determine the radiological consequences of a loss of coolant accident. The results of this analysis indicated a total thyroid dose of 165 rem for the 0-2 hour site boundary dose and a whole body dose of 9.32 rem. Since physical changes will not result from the proposed amendment, the site boundary does guidelines of 10 CFR 100 (300 rem thyroid and 25 rem whole body) will not be exceeded in the event of an accident during containment purging operations.
The addition of 40 hours4.62963e-4 days <br />0.0111 hours <br />6.613757e-5 weeks <br />1.522e-5 months <br /> of allowable annual purge time will not result in a significant increase in the amount of effluent released.
The Offsite Dose Calculation Manual (ODCM) ensures that the dose rate at any time at the SITE BOUNDARY from gaseous effluent from all units on the site will be within the annual dose limits of Appendix B, Table 2, Column 1 of 10 CFR 20 for UNRESTRICTED AREAS. These specifications will be strictly adhered to during any release via the purge pathway.
to AEP:NRC:1185 Page 3 In conclusion, we believe that the proposed technical specifications will not affect system capability or introduce a new or different mode of purge system operation not previously addressed in the above analysis.
III. 10 CFR 50 92 CRITERIA Per 10 CFR 50.92, a proposed change does not involve a significant hazards consideration if the change does not:
involve a significant increase in the probability or consequences of an accident previously evaluated,
- 2. create the possibility of a new or different kind of accident from any accident previously evaluated, or
- 3. involve a significant reduction in a margin of safety.
Criter on The purpose of this amendment is to allow flexibility in the use of the containment purge system during MODES 1, 2, 3, and 4. The use of this system during these modes of operation has previously been approved (Amendment No. 66). Therefore, this amendment request does not involve a ,significant increase in the probability or consequences of an accident previously evaluated because the proposed change 'o the T/Ss does not affect the assumptions, parameters, or results of any UFSAR accident analysis. Based on the existing system design and demonstrated closure capability it is concluded that the proposed changes do not modify the response of the containment during a design basis accident. The proposed amendment does not add or modify any existing equipment. Based on these considerations, it is concluded that the changes do not involve a significant increase in the probability or consequences of an accident previously evaluated.
Criterion 2 The proposed change does not involve physical changes to the plant or changes in the plant operating configuration. Thus, it is concluded that the proposed change does not create the possibility of a new or different kind of accident from any accident previously evaluated.
to AEP:NRC:1185 Page 4 Criterion 3 The margin for safety presently provided is not reduced by the proposed change. As discussed previously, the containment purge valves have been designed and demonstrated capable of closure against the dynamic forces resulting from a loss of coolant accident. The proposed amendment does not impact the ability of the purge valves to perform their intended .function (i.e. achieve closure) in the event of an accident. Based on these considerations, it is concluded that the changes do not involve a significant reduction in a margin of safety.
IV. CONCLUSION In conclusion, we believe that the proposed change does not involve significant hazards considerations because, as demonstrated in the previous discussions, operation of the Cook Nuclear Plant in accordance with the changes would not:
involve a significant increase in the probability or consequences of an accident previously evaluated,
- 2. create the possibility of a new or different kind of accident from any accident previously evaluated, or
- 3. involve a significant reduction in a margin of safety.
ATTACHMENT 2 TO AEP:NRC:1185 EXISTING TECHNICAL SPECIFICATION PAGES MARKED TO REFLECT PROPOSED CHANGES
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