Information Notice 2011-02, Operator Performance Issues Involving Reactivity Management at Nuclear Power Plants: Difference between revisions

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| issue date = 01/31/2011
| issue date = 01/31/2011
| title = Operator Performance Issues Involving Reactivity Management at Nuclear Power Plants
| title = Operator Performance Issues Involving Reactivity Management at Nuclear Power Plants
| author name = Blount T B
| author name = Blount T
| author affiliation = NRC/NRR/DPR
| author affiliation = NRC/NRR/DPR
| addressee name =  
| addressee name =  
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{{#Wiki_filter:ML101810282 UNITED STATES NUCLEAR REGULATORY COMMISSION OFFICE OF NUCLEAR REACTOR REGULATION WASHINGTON, DC 20555-001 January 31, 2011 NRC INFORMATION NOTICE 2011-02: OPERATOR PERFORMANCE ISSUES INVOLVING REACTIVITY MANAGEMENT AT NUCLEAR POWER PLANTS
{{#Wiki_filter:UNITED STATES
 
NUCLEAR REGULATORY COMMISSION
 
OFFICE OF NUCLEAR REACTOR REGULATION
 
WASHINGTON, DC 20555-001 January 31, 2011 NRC INFORMATION NOTICE 2011-02:                 OPERATOR PERFORMANCE ISSUES
 
INVOLVING REACTIVITY MANAGEMENT AT
 
NUCLEAR POWER PLANTS


==ADDRESSEES==
==ADDRESSEES==
All holders of operating licenses for nuclear power reactors under the provisions of Title 10 of the Code of Federal Regulations (10 CFR) Part 50, "Domestic Licensing of Production and Utilization Facilities," except those who have permanently ceased operations and have certified that fuel has been permanently removed from the reactor.
All holders of operating licenses for nuclear power reactors under the provisions of Title 10 of
 
the Code of Federal Regulations (10 CFR) Part 50, Domestic Licensing of Production and
 
Utilization Facilities, except those who have permanently ceased operations and have certified
 
that fuel has been permanently removed from the reactor.


==PURPOSE==
==PURPOSE==
The U.S. Nuclear Regulatory Commission (NRC) is issuing this information notice (IN) to inform addressees of events involving deficiencies with reactivity management planning and
The U.S. Nuclear Regulatory Commission (NRC) is issuing this information notice (IN) to inform
 
addressees of events involving deficiencies with reactivity management planning and
 
implementation. The NRC expects recipients to review the information for applicability to their
 
facilities and to consider actions, as appropriate, to avoid similar problems. Suggestions
 
contained in this IN are not NRC requirements; therefore, no specific action or written response


implementation.  The NRC expects recipients to review the information for applicability to their facilities and to consider actions, as appropriate, to avoid similar problems.  Suggestions contained in this IN are not NRC requirements; therefore, no specific action or written response is required.
is required.


==DESCRIPTION OF CIRCUMSTANCES==
==DESCRIPTION OF CIRCUMSTANCES==


===Callaway Plant===
===Callaway Plant===
  During a Callaway Plant shutdown in October 2003, the control room operators did not
During a Callaway Plant shutdown in October 2003, the control room operators did not
 
effectively control core reactivity during low-power operations. The event began on the morning
 
of October 20, 2003, when the Callaway Plant experienced an inverter failure on a
 
safety-related bus that put the unit in a 24-hour technical specification action to restore the
 
inverter or be in Mode 3 (hot standby) within the next 6 hours. The next morning, because the
 
inverter had not yet been restored, operators initiated a plant shutdown at approximately
 
10 percent per hour. With the main turbine on line and with turbine bypass valves closed, operators attempted to stabilize the plant at approximately 8-percent power. Per procedure, operators opened the turbine drain valves, which increased main steam flow, reducing reactor
 
coolant temperature and adding positive reactivity. At the same time, negative reactivity was
 
being inserted by xenon buildup, decreasing reactor power. The net effect was that reactor
 
coolant temperature decreased by approximately 10 degrees Fahrenheit over a half-hour
 
period. Operators did not withdraw control rods or dilute boron concentration to stabilize reactor
 
power or reactor coolant temperature. As a result of the lowering reactor coolant temperature, pressurizer level lowered enough to cause letdown to isolate. In addition, reactor coolant
 
temperature decreased below the technical specification required minimum temperature while
 
critical for several minutes. In response to the lowering reactor coolant temperature, the
 
operators manually tripped the main turbine with power at approximately 5 percent. Upon
 
tripping the main turbine, the turbine bypass valves controlled steam pressure, causing reactor
 
coolant temperature and pressurizer level to return to normal. Tripping the main turbine
 
reduced main steam flow, increasing reactor coolant temperature and adding negative
 
reactivity, which together with the addition of negative reactivity by xenon buildup, caused the
 
reactor to become subcritical. Operators did not insert the control rods until almost 2 hours after
 
the reactor became subcritical.
 
A subsequent review of this plant shutdown found that control room operators did not effectively
 
control reactivity to maintain the reactor in the desired condition during low-power operations by
 
properly anticipating, controlling, and responding to changing plant parameters. Operators did
 
not use control rods or boron concentrationtwo means that operators can use to directly
 
control the amount and timing of reactivity changesto adjust for reactivity changes by xenon
 
buildup and reactor coolant temperature changes. Specifically, reactivity was not effectively
 
controlled in that (1) operators did not sufficiently anticipate and compensate for xenon buildup
 
when they attempted to stabilize and hold the plant at approximately 8 percent power which
 
caused reactor coolant temperature to continue to decrease below the technical specification
 
required minimum temperature for criticality; (2) operators did not shut down the reactor in a
 
deliberate manner (e.g., by inserting control rod banks), but rather the reactor became
 
subcritical by xenon buildup and by the increase in reactor coolant temperature resulting from
 
the operators manually tripping the main turbine; and, (3) operators did not insert control rods
 
for nearly 2 hours after the reactor became subcritical. Fully inserting control rods provides
 
assurance that the reactor remains shut down (regardless of reactor coolant temperature or
 
xenon concentration). Notwithstanding, the NRC determined the delay in completing the
 
shutdown by inserting the control rods did not result in an unsafe reactor condition.
 
Operator performance in not effectively controlling reactivity was attributable, in part, to
 
weaknesses with management oversight, training, and procedural guidance. The pre-evolution
 
practice session using the simulator did not cover plant operations below 10-percent power and
 
did not include operation after the point where the operators tripped the main turbine. The
 
reactivity management plan did not address the possibility that the expected reactivity change
 
from tripping the main turbine together with the xenon buildup could cause the reactor to
 
become subcritical. The licensees initial post-shutdown review did not identify and evaluate the
 
atypical manner that the reactor became subcritical. This omission delayed application of the
 
lessons learned to operator qualification and requalification training and significantly delayed
 
procedure changes to address weaknesses in operator control of reactivity during low-power
 
operation. This event is also discussed in Callaway PlantNRC Integrated Inspection Report
 
05000483/2007003, dated August 2, 2007, which can be found on the NRCs public Web site in
 
the Agencywide Documents Access and Management System (ADAMS) under Accession
 
No. ML072140876.


effectively control core reactivity during low-power operations.  The event began on the morning of October 20, 2003, when the Callaway Plant experienced an inverter failure on a safety-related bus that put the unit in a 24-hour technical specification action to restore the inverter or be in Mode 3 (hot standby) within the next 6 hours.  The next morning, because the inverter had not yet been restored, operators initiated a plant shutdown at approximately
===River Bend Station===
On March 8, 2008, with River Bend Station at 25-percent power, control room operators were


10 percent per hour.  With the main turbine on line and with turbine bypass valves closed, operators attempted to stabilize the plant at approximately 8-percent power.  Per procedure, operators opened the turbine drain valves, which increased main steam flow, reducing reactor coolant temperature and adding positive reactivity.  At the same time, negative reactivity was being inserted by xenon buildup, decreasing reactor power. The net effect was that reactor coolant temperature decreased by approximately 10 degrees Fahrenheit over a half-hour period.  Operators did not withdraw control rods or dilute boron concentration to stabilize reactor
withdrawing control rods to increase reactor power. The operating procedure for plant startup


power or reactor coolant temperature.  As a result of the lowering reactor coolant temperature, pressurizer level lowered enough to cause letdown to isolate.  In addition, reactor coolant temperature decreased below the technical specification required minimum temperature while critical for several minutes.  In response to the lowering reactor coolant temperature, the operators manually tripped the main turbine with power at approximately 5 percent.  Upon tripping the main turbine, the turbine bypass valves controlled steam pressure, causing reactor coolant temperature and pressurizer level to return to normal.  Tripping the main turbine
directs operators to withdraw control rods using a withdrawal sequence specified in a reactivity


reduced main steam flow, increasing reactor coolant temperature and adding negative reactivity, which together with the addition of negative reactivity by xenon buildup, caused the reactor to become subcritical. Operators did not insert the control rods until almost 2 hours after the reactor became subcritical.
control plan that is provided to them by licensee reactor engineering. However, the dedicated


A subsequent review of this plant shutdown found that control room operators did not effectively control reactivity to maintain the reactor in the desired condition during low-power operations by properly anticipating, controlling, and responding to changing plant parameters.  Operators did not use control rods or boron concentration-two means that operators can use to directly control the amount and timing of reactivity changes-to adjust for reactivity changes by xenon buildup and reactor coolant temperature changes. Specifically, reactivity was not effectively controlled in that (1) operators did not sufficiently anticipate and compensate for xenon buildup when they attempted to stabilize and hold the plant at approximately 8 percent power which caused reactor coolant temperature to continue to decrease below the technical specification required minimum temperature for criticality; (2) operators did not shut down the reactor in a deliberate manner (e.g., by inserting control rod banks), but rather the reactor became subcritical by xenon buildup and by the increase in reactor coolant temperature resulting from
reactor operator at the controls stated an incorrect target position when reading aloud a rod movement step in the reactivity control plan. As a result, this operator individually withdrew six


the operators manually tripping the main turbine; and, (3) operators did not insert control rods for nearly 2 hours after the reactor became subcritical.  Fully inserting control rods provides assurance that the reactor remains shut down (regardless of reactor coolant temperature or xenon concentration).  Notwithstanding, the NRC determined the delay in completing the shutdown by inserting the control rods did not result in an unsafe reactor condition.
consecutive rods to position 24 rather than the target position 20 specified in the reactivity


Operator performance in not effectively controlling reactivity was attributable, in part, to weaknesses with management oversight, training, and procedural guidance. The pre-evolution practice session using the simulator did not cover plant operations below 10-percent power and did not include operation after the point where the operators tripped the main turbine.  The
control plan. The dedicated peer-check reactor operator did not identify that the stated target


reactivity management plan did not address the possibility that the expected reactivity change from tripping the main turbine together with the xenon buildup could cause the reactor to become subcritical.  The licensee's initial post-shutdown review did not identify and evaluate the atypical manner that the reactor became subcritical.  This omission delayed application of the lessons learned to operator qualification and requalification training and significantly delayed
position was incorrect because he could not readily see the reactivity control plan that was


procedure changes to address weaknesses in operator control of reactivity during low-power operation. This event is also discussed in "Callaway Plant-NRC Integrated Inspection Report 05000483/2007003," dated August 2, 2007, which can be found on the NRC's public Web site in the Agencywide Documents Access and Management System (ADAMS) under Accession No. ML072140876.  River Bend Station
resting on the lap of the reactor operator at the controls. The operator at the controls halted the


On March 8, 2008, with River Bend Station at 25-percent power, control room operators were withdrawing control rods to increase reactor power.  The operating procedure for plant startup directs operators to withdraw control rods using a withdrawal sequence specified in a reactivity control plan that is provided to them by licensee reactor engineering.  However, the dedicated
withdrawal of the seventh rod at position 18 after the dedicated peer-check reactor operator


reactor operator at the controls stated an incorrect target position when reading aloud a rod movement step in the reactivity control plan.  As a result, this operator individually withdrew six consecutive rods to position 24 rather than the target position 20 specified in the reactivity control plan.  The dedicated peer-check reactor operator did not identify that the stated target
identified the error. The licensee determined that the reactor operator at the controls and the


position was incorrect because he could not readily see the reactivity control plan that was resting on the lap of the reactor operator at the controls.  The operator at the controls halted the withdrawal of the seventh rod at position 18 after the dedicated peer-check reactor operator identified the error.  The licensee determined that the reactor operator at the controls and the peer-checker did not follow the procedures to prevent human performance errors and that the
peer-checker did not follow the procedures to prevent human performance errors and that the


senior reactor operator did not maintain effective oversight of the activity. Additional information is available in "River Bend Station-NRC Integrated Inspection Report 05000458/2008002," dated May 9, 2008 (ADAMS Accession No. ML081300838).  Diablo Canyon Power Plant, Unit 2 In August 2009, Diablo Canyon Power Plant Unit 2 was shut down in order to troubleshoot and
senior reactor operator did not maintain effective oversight of the activity. Additional information


repair a main transformer bushing.  In preparation for the shutdown, the control room operators performed simulator training on a ramp downpower using a draft copy of a ramp plan provided via e-mail by reactor engineering.  Before the actual shutdown, a revised ramp plan was provided by reactor engineering, approved by the operations manager, and issued in the shift orders. This revised ramp plan was also e-mailed to all shift members. The oncoming shift
is available in River Bend StationNRC Integrated Inspection Report 05000458/2008002, dated May 9, 2008 (ADAMS Accession No. ML081300838).


foreman and shift manager did not review the approved ramp plan located in the shift orders nor did they review the ramp plan as part of the reactivity brief.  Operators began the ramp downpower using the original (unapproved) draft ramp plan.  After the first 2 hours of the downpower, the control room operator questioned plant conditions that were inconsistent with the simulator scenario and contacted the reactor engineer.  The reactor engineer provided a
===Diablo Canyon Power Plant, Unit 2===
In August 2009, Diablo Canyon Power Plant Unit 2 was shut down in order to troubleshoot and


copy of the approved ramp plan.  No reactivity manipulations outside of the approved plan had been made. Operators continued the downpower using the approved ramp plan.
repair a main transformer bushing. In preparation for the shutdown, the control room operators


The licensee performed an apparent cause evaluation and determined that the shift foreman did not validate that the ramp plan in use was the same as the one that the operations manager had
performed simulator training on a ramp downpower using a draft copy of a ramp plan provided


approved. Licensee corrective actions included revising existing procedures to require validation of the ramp plan by the shift foreman and shift manager during the reactivity briefing.  This event is also discussed in "Diablo Canyon Power Plant-NRC Integrated Inspection Report 05000275/2009005 and 05000323/2009005," dated February 3, 2010 (ADAMS Accession No. ML100341199).  Arkansas Nuclear One
via e-mail by reactor engineering. Before the actual shutdown, a revised ramp plan was


On April 25, 2010, following the completion of a refueling outage, Arkansas Nuclear One, Unit 1 was at approximately 20-percent reactor power determined by heat balance (approximately 30-percent reactor power indicated on nuclear instrumentation (NI)) and holding to allow instrumentation and controls (I&C) technicians to calibrate the NI, which involves adjusting the gain on the NI excore detectors so that NI indicated reactor power level matches the reactor power determined by heat balance.  To prevent the integrated control system (ICS) from automatically moving control rods in response to the changing input of NI reactor power level from the gain adjustment, the calibration procedure first directs a control room operator to place the control rod station in manual.  The I&C technician who was implementing the procedure
provided by reactor engineering, approved by the operations manager, and issued in the shift


stated to a control room operator, "We are ready to place ICS to manual.The control room operator responded, "ICS is in manual."  However, this exchange did not result in the operator placing the control rod station in manual and it remained in automatic.  When I&C technicians subsequently adjusted the gain on the NIs, control rods automatically withdrew for
orders. This revised ramp plan was also e-mailed to all shift members. The oncoming shift


approximately 38 seconds and resulted in an automatic reactor trip because of high reactor power (49.55 percent NI indicated reactor power) and high RCS pressure.  The rapid event succession did not afford operators time to complete diagnosis of the rod withdrawal and initiate manual corrective action.
foreman and shift manager did not review the approved ramp plan located in the shift orders nor


The causes of the event included failure to follow the NI calibration procedure, miscommunication between the I&C technician and the reactor operator, failure to conduct a pre-job brief, and lack of supervisory oversight. Additional information is available in "Arkansas Nuclear One-NRC Integrated Inspection Report 05000313/2010003 and 05000368/2010003," dated August 5, 2010 (ADAMS Accession No. ML102180209).
did they review the ramp plan as part of the reactivity brief. Operators began the ramp
 
downpower using the original (unapproved) draft ramp plan. After the first 2 hours of the
 
downpower, the control room operator questioned plant conditions that were inconsistent with
 
the simulator scenario and contacted the reactor engineer. The reactor engineer provided a
 
copy of the approved ramp plan. No reactivity manipulations outside of the approved plan had
 
been made. Operators continued the downpower using the approved ramp plan.
 
The licensee performed an apparent cause evaluation and determined that the shift foreman did
 
not validate that the ramp plan in use was the same as the one that the operations manager had
 
approved. Licensee corrective actions included revising existing procedures to require
 
validation of the ramp plan by the shift foreman and shift manager during the reactivity briefing.
 
This event is also discussed in Diablo Canyon Power PlantNRC Integrated Inspection Report
 
05000275/2009005 and 05000323/2009005, dated February 3, 2010 (ADAMS Accession
 
No. ML100341199).
 
===Arkansas Nuclear One===
On April 25, 2010, following the completion of a refueling outage, Arkansas Nuclear One, Unit 1 was at approximately 20-percent reactor power determined by heat balance (approximately
 
30-percent reactor power indicated on nuclear instrumentation (NI)) and holding to allow
 
instrumentation and controls (I&C) technicians to calibrate the NI, which involves adjusting the
 
gain on the NI excore detectors so that NI indicated reactor power level matches the reactor
 
power determined by heat balance. To prevent the integrated control system (ICS) from
 
automatically moving control rods in response to the changing input of NI reactor power level
 
from the gain adjustment, the calibration procedure first directs a control room operator to place
 
the control rod station in manual. The I&C technician who was implementing the procedure
 
stated to a control room operator, We are ready to place ICS to manual. The control room operator responded, ICS is in manual. However, this exchange did not result in the operator
 
placing the control rod station in manual and it remained in automatic. When I&C technicians
 
subsequently adjusted the gain on the NIs, control rods automatically withdrew for
 
approximately 38 seconds and resulted in an automatic reactor trip because of high reactor
 
power (49.55 percent NI indicated reactor power) and high RCS pressure. The rapid event
 
succession did not afford operators time to complete diagnosis of the rod withdrawal and initiate
 
manual corrective action.
 
The causes of the event included failure to follow the NI calibration procedure, miscommunication between the I&C technician and the reactor operator, failure to conduct a
 
pre-job brief, and lack of supervisory oversight. Additional information is available in Arkansas
 
Nuclear OneNRC Integrated Inspection Report 05000313/2010003 and 05000368/2010003, dated August 5, 2010 (ADAMS Accession No. ML102180209).


==BACKGROUND==
==BACKGROUND==
The following are related NRC generic communications:  
The following are related NRC generic communications:
*      NRC IN 92-39, Unplanned Return to Criticality during Reactor Shutdown, dated
 
May 13, 1992, discussed events involving unplanned returns to criticality caused by the
 
cooldown of the reactor coolant system during reactor shutdowns (ADAMS Accession


* NRC IN 92-39, "Unplanned Return to Criticality during Reactor Shutdown," dated May 13, 1992, discussed events involving unplanned returns to criticality caused by the cooldown of the reactor coolant system during reactor shutdowns (ADAMS Accession No. ML031200314).
No. ML031200314).


* NRC IN 96-69, "Operator Actions Affecting Reactivity," dated December 20, 1996, highlighted several events in which poor command and control during reactivity evolutions have led to unanticipated and unintended plant conditions (ADAMS Accession No. ML031050475).
*       NRC IN 96-69, Operator Actions Affecting Reactivity, dated December 20, 1996, highlighted several events in which poor command and control during reactivity


* NRC IN 97-62, "Unrecognized Reactivity Addition During Plant Shutdown," dated August 6, 1997, discussed an incident in which a reactor operator inserted control rods to bring the reactor subcritical and then promptly withdrew the rods in order to take the
evolutions have led to unanticipated and unintended plant conditions (ADAMS
 
Accession No. ML031050475).
 
*       NRC IN 97-62, Unrecognized Reactivity Addition During Plant Shutdown, dated
 
August 6, 1997, discussed an incident in which a reactor operator inserted control rods
 
to bring the reactor subcritical and then promptly withdrew the rods in order to take the


reactor to the critical (ADAMS Accession No. ML031050177).
reactor to the critical (ADAMS Accession No. ML031050177).
Line 87: Line 289:
One of the most important responsibilities of an on-duty licensed reactor operator and senior
One of the most important responsibilities of an on-duty licensed reactor operator and senior


reactor operator is reactivity management in order to maintain the reactor in the desired condition, consistent with plant technical specifications, by properly anticipating, controlling, and responding to changing plant parameters. Reactivity management involves establishing and implementing procedures for operators to use in determining the effects on reactivity of plant changes, and to operate the controls associated with plant equipment that could affect
reactor operator is reactivity management in order to maintain the reactor in the desired
 
condition, consistent with plant technical specifications, by properly anticipating, controlling, and
 
responding to changing plant parameters. Reactivity management involves establishing and
 
implementing procedures for operators to use in determining the effects on reactivity of plant
 
changes, and to operate the controls associated with plant equipment that could affect
 
reactivity. Before conducting planned evolutions involving reactivity changes (e.g., power
 
decreases and increases), although there is no specific NRC requirement to do so, many
 
licensee reactor engineering staffs prepare a reactivity management plan that helps control
 
room operators maintain the reactor in the desired condition by providing expected plant
 
responses and expected alarms. Required training is expected to give licensed operators an
 
understanding of facility operating characteristics during steady-state and transient conditions, including causes and effects of temperature, pressure, coolant chemistry, and load changes, as well as, operating limitations and their bases. Licensee post-transient reviews are important for
 
determining the cause of transients or unexpected plant responses and for taking corrective
 
actions, such as procedure changes and training, to prevent recurrence.


reactivity.  Before conducting planned evolutions involving reactivity changes (e.g., power decreases and increases), although there is no specific NRC requirement to do so, many licensee reactor engineering staffs prepare a reactivity management plan that helps control room operators maintain the reactor in the desired condition by providing expected plant responses and expected alarms.  Required training is expected to give licensed operators an understanding of facility operating characteristics during steady-state and transient conditions, including causes and effects of temperature, pressure, coolant chemistry, and load changes, as well as, operating limitations and their bases.  Licensee post-transient reviews are important for determining the cause of transients or unexpected plant responses and for taking corrective actions, such as procedure changes and training, to prevent recurrence.
During one of the events discussed above, after the reactor became subcritical through xenon


During one of the events discussed above, after the reactor became subcritical through xenon buildup and a reactor coolant temperature increase, operators delayed inserting control rods for nearly 2 hours.  NRC IN 92-39 discusses an event in which, after the operators brought the reactor subcritical by inserting control rods, an inadvertent unplanned return to criticality
buildup and a reactor coolant temperature increase, operators delayed inserting control rods for


occurred because operators delayed actions to continue inserting control rods while changing shifts. Although not specifically required, licensees may consider revising procedures and training operators so that, after the reactor becomes subcritical, the operators will proceed without delay to insert control rods or add boron to ensure the reactor remains shut down.
nearly 2 hours. NRC IN 92-39 discusses an event in which, after the operators brought the
 
reactor subcritical by inserting control rods, an inadvertent unplanned return to criticality
 
occurred because operators delayed actions to continue inserting control rods while changing
 
shifts. Although not specifically required, licensees may consider revising procedures and
 
training operators so that, after the reactor becomes subcritical, the operators will proceed
 
without delay to insert control rods or add boron to ensure the reactor remains shut down.


==CONTACT==
==CONTACT==
This IN requires no specific action or written response. Please direct any questions about this matter to the technical contact listed below or to the appropriate Office of Nuclear Reactor Regulation project manager.
This IN requires no specific action or written response. Please direct any questions about this
 
matter to the technical contact listed below or to the appropriate Office of Nuclear Reactor
 
Regulation project manager.


/RA/ by TMcGinty for
/RA/ by TMcGinty for


Thomas B. Blount, Acting Director Division of Policy and Rulemaking Office of Nuclear Reactor Regulation
Thomas B. Blount, Acting Director
 
Division of Policy and Rulemaking
 
Office of Nuclear Reactor Regulation


===Technical Contact:===
===Technical Contact:===
Geoffrey Miller    817-860-8141 geoffrey.miller@nrc.gov


Note: NRC generic communications may be found on the NRC public Web site, http://www.nrc.gov, under Electronic Reading Room/Document Collections.
===Geoffrey Miller===
                        817-860-8141 geoffrey.miller@nrc.gov
 
Note: NRC generic communications may be found on the NRC public Web site, http://www.nrc.gov, under Electronic Reading Room/Document Collections.
 
ML101810282 OFFICE    BC:DRP:R-IV            Tech Editor          IOLB:DIRS              BC:IOLB:DIRS
 
NAME      GMiller                CHsu                LVick                  JMcHale
 
DATE      12/1/10 (e-mail)        9/4/10 (e-mail)      12/8/10 (e-mail)      12/8/10 (e-mail)
OFFICE    D:DIRS                  BC:SRXB:DSS          OGC(NLO)              OEGIB/DRA/RES
 
NAME      FBrown                  AUlses              DRoth                  LCriscione
 
Non-Concur
 
DATE      1/20/2011              12/13/10            12/14/10 (e-mail)      12/15/10
OFFICE    LA:PGCB:NRR            PM:PGCB:NRR          BC:PGCB:NRR            D:DPR:NRR


ML101810282 OFFICE BC:DRP:R-IV Tech Editor IOLB:DIRS BC:IOLB:DIRS NAME GMiller CHsu LVick JMcHale DATE 12/1/10 (e-mail) 9/4/10 (e-mail) 12/8/10 (e-mail) 12/8/10 (e-mail) OFFICE D:DIRS BC:SRXB:DSS OGC(NLO) OEGIB/DRA/RES NAME FBrown AUlses DRoth LCriscione Non-Concur DATE 1/20/2011 12/13/10 12/14/10 (e-mail) 12/15/10 OFFICE LA:PGCB:NRR PM:PGCB:NRR BC:PGCB:NRR D:DPR:NRR NAME CHawes DBeaulieu SRosenberg TBlount (TMcGinty for) OFFICE 01/25/2011 (e-mail) 1/20/2011 1/26/2011 1/31/2011}}
NAME     CHawes                 DBeaulieu           SRosenberg             TBlount (TMcGinty for)
OFFICE   01/25/2011 (e-mail)     1/20/2011           1/26/2011             1/31/2011}}


{{Information notice-Nav}}
{{Information notice-Nav}}

Latest revision as of 17:35, 13 November 2019

Operator Performance Issues Involving Reactivity Management at Nuclear Power Plants
ML101810282
Person / Time
Issue date: 01/31/2011
From: Blount T
Division of Policy and Rulemaking
To:
Beaulieu, D P, NRR/DPR, 415-3243
References
IN-11-002
Download: ML101810282 (6)


UNITED STATES

NUCLEAR REGULATORY COMMISSION

OFFICE OF NUCLEAR REACTOR REGULATION

WASHINGTON, DC 20555-001 January 31, 2011 NRC INFORMATION NOTICE 2011-02: OPERATOR PERFORMANCE ISSUES

INVOLVING REACTIVITY MANAGEMENT AT

NUCLEAR POWER PLANTS

ADDRESSEES

All holders of operating licenses for nuclear power reactors under the provisions of Title 10 of

the Code of Federal Regulations (10 CFR) Part 50, Domestic Licensing of Production and

Utilization Facilities, except those who have permanently ceased operations and have certified

that fuel has been permanently removed from the reactor.

PURPOSE

The U.S. Nuclear Regulatory Commission (NRC) is issuing this information notice (IN) to inform

addressees of events involving deficiencies with reactivity management planning and

implementation. The NRC expects recipients to review the information for applicability to their

facilities and to consider actions, as appropriate, to avoid similar problems. Suggestions

contained in this IN are not NRC requirements; therefore, no specific action or written response

is required.

DESCRIPTION OF CIRCUMSTANCES

Callaway Plant

During a Callaway Plant shutdown in October 2003, the control room operators did not

effectively control core reactivity during low-power operations. The event began on the morning

of October 20, 2003, when the Callaway Plant experienced an inverter failure on a

safety-related bus that put the unit in a 24-hour technical specification action to restore the

inverter or be in Mode 3 (hot standby) within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />. The next morning, because the

inverter had not yet been restored, operators initiated a plant shutdown at approximately

10 percent per hour. With the main turbine on line and with turbine bypass valves closed, operators attempted to stabilize the plant at approximately 8-percent power. Per procedure, operators opened the turbine drain valves, which increased main steam flow, reducing reactor

coolant temperature and adding positive reactivity. At the same time, negative reactivity was

being inserted by xenon buildup, decreasing reactor power. The net effect was that reactor

coolant temperature decreased by approximately 10 degrees Fahrenheit over a half-hour

period. Operators did not withdraw control rods or dilute boron concentration to stabilize reactor

power or reactor coolant temperature. As a result of the lowering reactor coolant temperature, pressurizer level lowered enough to cause letdown to isolate. In addition, reactor coolant

temperature decreased below the technical specification required minimum temperature while

critical for several minutes. In response to the lowering reactor coolant temperature, the

operators manually tripped the main turbine with power at approximately 5 percent. Upon

tripping the main turbine, the turbine bypass valves controlled steam pressure, causing reactor

coolant temperature and pressurizer level to return to normal. Tripping the main turbine

reduced main steam flow, increasing reactor coolant temperature and adding negative

reactivity, which together with the addition of negative reactivity by xenon buildup, caused the

reactor to become subcritical. Operators did not insert the control rods until almost 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> after

the reactor became subcritical.

A subsequent review of this plant shutdown found that control room operators did not effectively

control reactivity to maintain the reactor in the desired condition during low-power operations by

properly anticipating, controlling, and responding to changing plant parameters. Operators did

not use control rods or boron concentrationtwo means that operators can use to directly

control the amount and timing of reactivity changesto adjust for reactivity changes by xenon

buildup and reactor coolant temperature changes. Specifically, reactivity was not effectively

controlled in that (1) operators did not sufficiently anticipate and compensate for xenon buildup

when they attempted to stabilize and hold the plant at approximately 8 percent power which

caused reactor coolant temperature to continue to decrease below the technical specification

required minimum temperature for criticality; (2) operators did not shut down the reactor in a

deliberate manner (e.g., by inserting control rod banks), but rather the reactor became

subcritical by xenon buildup and by the increase in reactor coolant temperature resulting from

the operators manually tripping the main turbine; and, (3) operators did not insert control rods

for nearly 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> after the reactor became subcritical. Fully inserting control rods provides

assurance that the reactor remains shut down (regardless of reactor coolant temperature or

xenon concentration). Notwithstanding, the NRC determined the delay in completing the

shutdown by inserting the control rods did not result in an unsafe reactor condition.

Operator performance in not effectively controlling reactivity was attributable, in part, to

weaknesses with management oversight, training, and procedural guidance. The pre-evolution

practice session using the simulator did not cover plant operations below 10-percent power and

did not include operation after the point where the operators tripped the main turbine. The

reactivity management plan did not address the possibility that the expected reactivity change

from tripping the main turbine together with the xenon buildup could cause the reactor to

become subcritical. The licensees initial post-shutdown review did not identify and evaluate the

atypical manner that the reactor became subcritical. This omission delayed application of the

lessons learned to operator qualification and requalification training and significantly delayed

procedure changes to address weaknesses in operator control of reactivity during low-power

operation. This event is also discussed in Callaway PlantNRC Integrated Inspection Report 05000483/2007003, dated August 2, 2007, which can be found on the NRCs public Web site in

the Agencywide Documents Access and Management System (ADAMS) under Accession

No. ML072140876.

River Bend Station

On March 8, 2008, with River Bend Station at 25-percent power, control room operators were

withdrawing control rods to increase reactor power. The operating procedure for plant startup

directs operators to withdraw control rods using a withdrawal sequence specified in a reactivity

control plan that is provided to them by licensee reactor engineering. However, the dedicated

reactor operator at the controls stated an incorrect target position when reading aloud a rod movement step in the reactivity control plan. As a result, this operator individually withdrew six

consecutive rods to position 24 rather than the target position 20 specified in the reactivity

control plan. The dedicated peer-check reactor operator did not identify that the stated target

position was incorrect because he could not readily see the reactivity control plan that was

resting on the lap of the reactor operator at the controls. The operator at the controls halted the

withdrawal of the seventh rod at position 18 after the dedicated peer-check reactor operator

identified the error. The licensee determined that the reactor operator at the controls and the

peer-checker did not follow the procedures to prevent human performance errors and that the

senior reactor operator did not maintain effective oversight of the activity. Additional information

is available in River Bend StationNRC Integrated Inspection Report 05000458/2008002, dated May 9, 2008 (ADAMS Accession No. ML081300838).

Diablo Canyon Power Plant, Unit 2

In August 2009, Diablo Canyon Power Plant Unit 2 was shut down in order to troubleshoot and

repair a main transformer bushing. In preparation for the shutdown, the control room operators

performed simulator training on a ramp downpower using a draft copy of a ramp plan provided

via e-mail by reactor engineering. Before the actual shutdown, a revised ramp plan was

provided by reactor engineering, approved by the operations manager, and issued in the shift

orders. This revised ramp plan was also e-mailed to all shift members. The oncoming shift

foreman and shift manager did not review the approved ramp plan located in the shift orders nor

did they review the ramp plan as part of the reactivity brief. Operators began the ramp

downpower using the original (unapproved) draft ramp plan. After the first 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> of the

downpower, the control room operator questioned plant conditions that were inconsistent with

the simulator scenario and contacted the reactor engineer. The reactor engineer provided a

copy of the approved ramp plan. No reactivity manipulations outside of the approved plan had

been made. Operators continued the downpower using the approved ramp plan.

The licensee performed an apparent cause evaluation and determined that the shift foreman did

not validate that the ramp plan in use was the same as the one that the operations manager had

approved. Licensee corrective actions included revising existing procedures to require

validation of the ramp plan by the shift foreman and shift manager during the reactivity briefing.

This event is also discussed in Diablo Canyon Power PlantNRC Integrated Inspection Report 05000275/2009005 and 05000323/2009005, dated February 3, 2010 (ADAMS Accession

No. ML100341199).

Arkansas Nuclear One

On April 25, 2010, following the completion of a refueling outage, Arkansas Nuclear One, Unit 1 was at approximately 20-percent reactor power determined by heat balance (approximately

30-percent reactor power indicated on nuclear instrumentation (NI)) and holding to allow

instrumentation and controls (I&C) technicians to calibrate the NI, which involves adjusting the

gain on the NI excore detectors so that NI indicated reactor power level matches the reactor

power determined by heat balance. To prevent the integrated control system (ICS) from

automatically moving control rods in response to the changing input of NI reactor power level

from the gain adjustment, the calibration procedure first directs a control room operator to place

the control rod station in manual. The I&C technician who was implementing the procedure

stated to a control room operator, We are ready to place ICS to manual. The control room operator responded, ICS is in manual. However, this exchange did not result in the operator

placing the control rod station in manual and it remained in automatic. When I&C technicians

subsequently adjusted the gain on the NIs, control rods automatically withdrew for

approximately 38 seconds and resulted in an automatic reactor trip because of high reactor

power (49.55 percent NI indicated reactor power) and high RCS pressure. The rapid event

succession did not afford operators time to complete diagnosis of the rod withdrawal and initiate

manual corrective action.

The causes of the event included failure to follow the NI calibration procedure, miscommunication between the I&C technician and the reactor operator, failure to conduct a

pre-job brief, and lack of supervisory oversight. Additional information is available in Arkansas

Nuclear OneNRC Integrated Inspection Report 05000313/2010003 and 05000368/2010003, dated August 5, 2010 (ADAMS Accession No. ML102180209).

BACKGROUND

The following are related NRC generic communications:

  • NRC IN 92-39, Unplanned Return to Criticality during Reactor Shutdown, dated

May 13, 1992, discussed events involving unplanned returns to criticality caused by the

cooldown of the reactor coolant system during reactor shutdowns (ADAMS Accession

No. ML031200314).

  • NRC IN 96-69, Operator Actions Affecting Reactivity, dated December 20, 1996, highlighted several events in which poor command and control during reactivity

evolutions have led to unanticipated and unintended plant conditions (ADAMS

Accession No. ML031050475).

  • NRC IN 97-62, Unrecognized Reactivity Addition During Plant Shutdown, dated

August 6, 1997, discussed an incident in which a reactor operator inserted control rods

to bring the reactor subcritical and then promptly withdrew the rods in order to take the

reactor to the critical (ADAMS Accession No. ML031050177).

DISCUSSION

One of the most important responsibilities of an on-duty licensed reactor operator and senior

reactor operator is reactivity management in order to maintain the reactor in the desired

condition, consistent with plant technical specifications, by properly anticipating, controlling, and

responding to changing plant parameters. Reactivity management involves establishing and

implementing procedures for operators to use in determining the effects on reactivity of plant

changes, and to operate the controls associated with plant equipment that could affect

reactivity. Before conducting planned evolutions involving reactivity changes (e.g., power

decreases and increases), although there is no specific NRC requirement to do so, many

licensee reactor engineering staffs prepare a reactivity management plan that helps control

room operators maintain the reactor in the desired condition by providing expected plant

responses and expected alarms. Required training is expected to give licensed operators an

understanding of facility operating characteristics during steady-state and transient conditions, including causes and effects of temperature, pressure, coolant chemistry, and load changes, as well as, operating limitations and their bases. Licensee post-transient reviews are important for

determining the cause of transients or unexpected plant responses and for taking corrective

actions, such as procedure changes and training, to prevent recurrence.

During one of the events discussed above, after the reactor became subcritical through xenon

buildup and a reactor coolant temperature increase, operators delayed inserting control rods for

nearly 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />. NRC IN 92-39 discusses an event in which, after the operators brought the

reactor subcritical by inserting control rods, an inadvertent unplanned return to criticality

occurred because operators delayed actions to continue inserting control rods while changing

shifts. Although not specifically required, licensees may consider revising procedures and

training operators so that, after the reactor becomes subcritical, the operators will proceed

without delay to insert control rods or add boron to ensure the reactor remains shut down.

CONTACT

This IN requires no specific action or written response. Please direct any questions about this

matter to the technical contact listed below or to the appropriate Office of Nuclear Reactor

Regulation project manager.

/RA/ by TMcGinty for

Thomas B. Blount, Acting Director

Division of Policy and Rulemaking

Office of Nuclear Reactor Regulation

Technical Contact:

Geoffrey Miller

817-860-8141 geoffrey.miller@nrc.gov

Note: NRC generic communications may be found on the NRC public Web site, http://www.nrc.gov, under Electronic Reading Room/Document Collections.

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