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{{#Wiki_filter:e .*.-o Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038 Salem Generating Station U.S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555  
{{#Wiki_filter:e
.*.-o PS~G Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038 Salem Generating Station flay 11, 1989 U.S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555


==Dear Sir:==
==Dear Sir:==
MONTHLY OPERATING REPORT SALEM NO. 1 DOCKET NO. 50-272 flay 11, 1989 In compliance with Section 6.9.1.6, Reporting Requirements for the Salem Technical Specifications, the original copy of the monthly operating reports for the month of April 1989 are being sent to you. RH: sl Average Daily Unit Power Level Operating Data Report Unit Shutdowns and Power Reductions Safety Related Maintenance Major Plant Modification Operating Summary Refueling Information L. K. Miller General Manager -Salem Operations cc: Mr. William T. Russell Regional Administrator USNRC Region I 631 Park Avenue King of Prussia, PA 19406 Enclosures 8-l-7.R4 -----")*-*4(")
 
*,=_,"=' **
MONTHLY OPERATING REPORT SALEM NO. 1 DOCKET NO. 50-272 In compliance with Section 6.9.1.6, Reporting Requirements for the Salem Technical Specifications, the original copy of the monthly operating reports for the month of April 1989 are being sent to you.
):"*1:i::::*:( .,:. -.. , 'JI""
Average Daily Unit Power Level Operating Data Report Unit Shutdowns and Power Reductions Safety Related Maintenance Major Plant Modification Operating Summary Refueling Information sk~
o5otu272 R PDC The Energy People ff14 'l I 95-2189 (SM) 12-88 Completed by Month APRIL .e AVERAGE DAILY UNIT POWER LEVEL Art Orticelle 1989 Docket No. Unit Name Date Telephone Extension Day Average Daily Power Level Day Average Daily (MWe-NET) (MWe-NET) 1 0 17 0 2 0 18 0 3 0 19 0 4 0 20 0 5 0 21 0 6 0 22 0 7 0 23 0 8 0 24 0 9 0 25 0 10 0 26 0 11 0 27 0 12 0 28 0 13 0 29 0 14 0 30 0 15 0 31 16 0 P. 8.1-7 Rl 50-272 Salem # 1 5-09-89 609-935-6000 4451 Power Level j,G'*:f OPERATING DATA REPORT Completed by Pell White Operating Status Docket No .50-272 Date:
L. K. Miller General Manager -
Telephone:
Salem Operations RH: sl cc:       Mr. William T. Russell Regional Administrator USNRC Region I 631 Park Avenue King of Prussia, PA 19406 Enclosures 8-l-7.R4
935-6000 Extension:
                          - :=~*:')(- ):"*1:i::::*:(
: 1. Unit Name Salem No. 1 Notes 2. Reporting Period April 1989 3. Licensed Thermal Power (MWt) 3411 4. Nameplate Rating (Gross MWe) 1170 5. Design Electrical Rating (Net MWe) 1115 6. Maximum Dependable Capacity(Gross MWe)1149 7. Maximum Dependable Capacity (Net MWe) 1106 8. If Changes Occur in Capacity Ratings (items 3 through 7) since Last Report, Give Reason N/A
                                      - - - ")*-*4(").,:. -      ..**, (l~.'JI""
: 9. Power Level to Which Restricted, if any (Net MWe) N/A
                                                            *,=_,"='      ~A
: 10. Reasons for Restrictions, if any N/A
                            ~b~-              ~fiocK        o5otu272 R                                                PDC The Energy People                                                                               ff14
: 11. Hours in Reporting Period 12. No. of Hrs. Reactor was Critical 13. Reactor Reserve Shutdown Hrs. 14. Hours Generator On-Line 15. Unit Reserve Shutdown Hours 16. Gross Thermal Energy Generated (MWH) 17. Gross Elec. Energy Generated (MWH) 18. Net Elec. Energy Generated (MWH) 19. Unit Service Factor 20. Unit Availability Factor 21. Unit Capacity Factor (using MDC Net) 22. Unit Capacity Factor (using DER Net) 2 3. Unit Forced Outage Rate This Month Year to Date 719 2879 0 1862.33 0 0 0 1811.75 0 0 0 6106848 0 2039200 -4020 1945095 0 62.9 0 62.9 0 61.1 0 60.6 0 12.2 Cumulative 103752 66 494. 53 0 64 447. 65 0 201543640.4 66986380 63751219 62.1 62.1 55.6 55.1 22.1 24. Shutdowns scheduled over next 6 months (type, date and duration of each) NONE 25*. If shutdown at end of Report Period, Estimated Date of Startup: Unit currently in 8th refueling outage scheduled start date May 26, 1989. 8-l-7.R2 Completed by No. Date 0071 4-01-89 0071 4-01-89 007 1 4-01-89 1 F: Forced S: Scheduled HNIT SHUTDOWN AND POWER REDUCTIONS Docket No.50-272 REPORT MONTH APRIL 1989 Unit Name Date Telephone Extension Salem No.I Art Orticelle Method of Duration Shutting License Type Hours Reason Down Event 1 s s s 2 Reactor 719 c 4 719 c 4 719 c 4 2 Reason A-Equipment Failure-explain B-Maintenance or Test C-Refue ling D-Regulatory Restriction Report ------------------E-Operator Training & Licensing Exam F-Administrative G-Operational Error-explain H-Other-explain System Code 4 CA HA HA 3 Method 1-Man ua 1 Component C od*e 5 VESSEL GENERA TURBIN 2-Manual Scram. 3-Automatic Scram. 4-Continuation of Previous Outage 5-Load Reduction 9-0ther 5-09-89 609-935-6000 4451 Cause and Corrective Action to Prevent Recurrence NUCLEAR REACTOR OVERHAUL GENERATOR MAJOR OVERHAUL MAJOR TURBINE OVERHAUL 4 Exhibit G Instructions for tion of Data Entry Sheets for Licensee Event Report (LER) File (NUREG 0161) 5 Salem as Source WO NO 890125071 890330094 890330112 890410160 890413128 890425105 PSE&G SALEM GENERATING STATION SAFETY RELATED WORK ORDER LOG SALEM UNIT 1 UNIT EQUIPMENT IDENTIFICATION 1 EMERG. AIR COMPRESSOR FAILURE DESCRIPTION:
                                                                                                      'l I 95-2189 (SM) 12-88
#1 EMERG. AIR COMPRESSOR OIL LEAK / REPLACE GASKET. 1 lSAll 8 FAILURE DESCRIPTION:
 
FAILED LEAK RATE TEST/MARK NO. A-157. INSPECT. 1 lSAll 9 "FAILURE DESCRIPTION:
                                                  .e AVERAGE DAILY UNIT POWER LEVEL Docket No. 50-272 Unit Name   Salem # 1 Date       5-09-89 Completed by    Art Orticelle                    Telephone  609-935-6000 Extension   4451 Month    APRIL 1989 Day Average Daily Power Level             Day Average Daily Power Level (MWe-NET)                                 (MWe-NET) 1           0                                 17           0 2           0                                 18           0 3           0                                 19           0 4           0                                 20           0 5           0                                 21           0 6           0                                 22           0 7           0                                 23           0 8           0                                 24           0 9           0                                 25           0 10         0                                 26           0 11         0                                 27           0 12         0                                 28           0 13         0                                 29           0 14         0                                 30           0 15         0                                 31 16         0 P. 8.1-7 Rl j,G'*:f
FAILED LEAK RATE TEST / MARK NO. A-165. INSPECT. 1 1C5Y FAILURE DESCRIPTION:
 
lC VTL INSTR. BUS INVERTER BREAKER/CHANGE OVERLOAD.
OPERATING DATA REPORT Docket No .50-272 Date: 5~--o-=-=-9--~8~9~--------
1 RX CAVITY LIGHTING FAILURE DESCRIPTION:
Telephone: 935-6000 Completed by    Pell White                        Extension: ~4~4~5~1-------------
RX CAVITY LIGHTING/TROUBLESHOOT.
Operating Status
1 11SJ188 FAILURE DESCRIPTION:
: 1. Unit Name                         Salem No. 1     Notes
LEAKING THRU/CLEAN OFF BORIC ACID & CAP END OF PIPE.
: 2. Reporting Period                   April 1989
SALEr1 UNIT 1 890425112 1 11SJ189 FAILURE DESCRIPTION:
: 3. Licensed Thermal Power (MWt)             3411
LEAKING THRU/CLEAN OFF BORIC ACID & CAP END OF PIPE. 890425113 1 12SJ188 FAILURE DESCRIPTION:
: 4. Nameplate Rating (Gross MWe)             1170
LEAKING THRU/CLEAN OFF BORIC ACID & CAP END OF PIPE .. 890425119 1 12SJ189 FAILURE DESCRIPTION:
: 5. Design Electrical Rating (Net MWe)       1115
LEAKING THRU/CLEAN OFF BORIC ACID & CAP END OF PIPE.
: 6. Maximum Dependable Capacity(Gross MWe)1149
.MAJbR PLANT MODIFICATIONS MONTH APRIL 1989 *DCR NO. PRINCIPAL SYSTEM lEC-02065 Charging lEC-02066 Charging lEC-02173 Turbine Controls lEC-02271 Electrical
: 7. Maximum Dependable Capacity (Net MWe) 1106
* DCR -Design Change Request DOCKET NO.: 50*-272 UNIT NAME: Salem 1 DATE: May 10, 19 89 COMPLETED BY: P. White TELEPHONE:
: 8. If Changes Occur in Capacity Ratings (items 3 through 7) since Last Report, Give Reason     N/A
609/339-4455 DESCRIPTION This design change added a pulsation dampener to the discharge of the positive displacement charging pump. This design change added a suction stabilizer to the piping upstream of the #13 positive displacement charging pump. This design change installed AMSAC (ATWS Mitigation System Actuation Circuitry).
                          --~---------------~------------------------------------
This design change eliminated the 91% voltage vital bus transfer scheme between station power transformers and provided (3) 91% undervoltage relays wired to each vital bus providing inputs to its SEC unit for a 2 of 3 logic to the diesel generator.
: 9. Power Level to Which Restricted, if any (Net MWe)            N/A
e MAJOR PLANT MODIFICATIONS e DOCKET NO.: 50-272 REPORT MONTH APRIL 1989 UNIT NAME: Salem 1 *DCR lEC-02065 lEC-02066 lEC-02173 lEC-02271 DATE: May 10, 19 89 COMPLETED BY: P. White TELEPHONE:
                                                            ----~~~------------
609/339-4455 SAFETY EVALUATION 10 CFR 50.59 This design change added a pulsation dampener to the discharge of #13 positive displacement charging pump. The unit selected is _a gas charged bladder design which is currently in use at a number of other nuclear plants. There was no change to any plant process or discharge or to the environmental impact of the plant. "No unreviewed safety or environmental questions are involved.
: 10. Reasons for Restrictions, if any      N/A
This design change added a suction stabilizer to the piping upstream of #13 positive displacement charging pump. The unit selected is a gas charged bladder design which is currently in use at a number of other nuclear plants. There was no change to any plant process or discharge or to the environmental impact of the plant. No unreviewed safety or environmental questions are involved.
                                        ----------------~--------------~-------
This design change installed AMSAC (ATWS Mitigation Actuation Circuitry).
This Month    Year to Date        Cumulative
The system provides a diverse means for tripping the main steam turbine and initiating auxiliary feedwater in the event of an anticipated transient without a scram. There was no change to any plant process or discharge or to the environmental impact of the plant. No unreviewed safety or environmental questions are involved.
: 11. Hours in Reporting Period              719          2879                103752
This design change eliminated the 91% voltage vital bus transfer scheme between station power transformers and provided (3) 91% undervoltage relays wired to each vital bus providing inputs to its SEC unit for a 2 of 3 logic to the diesel generator.
: 12. No. of Hrs. Reactor was Critical        0           1862.33             66 494. 53
There was no change to any plant process or discharge or to the environmental impact of the plant. No unreviewed safety or environmental questions are involved.
: 13. Reactor Reserve Shutdown Hrs.          0               0                   0
* DCR -Design Change Request
: 14. Hours Generator On-Line                0           1811.75            64 447. 65
* SALEM UNIT NO. 1 SALEM GENERATING STATION MONTHLY OPERATING  
: 15. Unit Reserve Shutdown Hours            0                0                   0
: 16. Gross Thermal Energy Generated (MWH)                          0           6106848          201543640.4
: 17. Gross Elec. Energy Generated (MWH)                          0            2039200            66986380
: 18. Net Elec. Energy Generated (MWH)      -4020          1945095            63751219
: 19. Unit Service Factor                      0              62.9              62.1
: 20. Unit Availability Factor                0              62.9              62.1
: 21. Unit Capacity Factor (using MDC Net)                    0              61.1              55.6
: 22. Unit Capacity Factor (using DER Net)                    0              60.6              55.1 2 3. Unit Forced Outage Rate                0              12.2              22.1
: 24. Shutdowns scheduled over next 6 months      (type, date and duration of each)
NONE 25*. If shutdown at end of Report Period, Estimated Date of Startup:
Unit currently in 8th refueling outage scheduled start date May 26, 1989.
8-l-7.R2
 
HNIT SHUTDOWN AND POWER REDUCTIONS          Docket No.50-272
                                                                                          ~~~~~~~~-
REPORT MONTH APRIL 1989                  Unit Name Salem No.I Date      5-09-89 Completed by  Art Orticelle                                                    Telephone 609-935-6000 Extension 4451 Method of Duration          Shutting  License                            Cause and Corrective No. Date  Type    Hours    Reason  Down      Event    System   Component          Action to 1                2    Reactor    Report  Code 4     C od*e 5       Prevent Recurrence NUCLEAR REACTOR 0071  4-01-89    s      719      c      4       ------     CA      VESSEL        OVERHAUL GENERATOR MAJOR 0071  4-01-89    s      719      c      4        ------      HA      GENERA        OVERHAUL MAJOR TURBINE 007 1 4-01-89    s      719      c      4        ------      HA      TURBIN        OVERHAUL 1                  2 Reason                                3 Method              4 Exhibit G     5 Exhibit-F: Forced          A-Equipment Failure-explain            1-Man ua 1            Instructions    Salem as S: Scheduled        B-Maintenance or Test                  2-Manual Scram.      for Prepara-    Source C-Refue ling                            3-Automatic Scram. tion of Data D-Regulatory Restriction                4-Continuation of    Entry Sheets E-Operator Training & Licensing Exam      Previous Outage    for Licensee F-Administrative                        5-Load Reduction      Event Report G-Operational Error-explain            9-0ther                (LER) File H-Other-explain                                                (NUREG 0161)
 
PSE&G SALEM GENERATING STATION SAFETY RELATED WORK ORDER LOG SALEM UNIT 1 WO NO    UNIT  EQUIPMENT IDENTIFICATION 890125071 1    EMERG. AIR COMPRESSOR FAILURE DESCRIPTION: #1 EMERG. AIR COMPRESSOR OIL LEAK / REPLACE GASKET.
890330094 1    lSAll 8 FAILURE DESCRIPTION:  FAILED LEAK RATE TEST/MARK NO. A-157. INSPECT.
890330112 1   lSAll 9 "FAILURE DESCRIPTION: FAILED LEAK RATE TEST / MARK NO. A-165. INSPECT.
890410160 1   1C5Y FAILURE DESCRIPTION:   lC VTL INSTR. BUS INVERTER BREAKER/CHANGE OVERLOAD.
890413128 1   RX CAVITY LIGHTING FAILURE DESCRIPTION: RX CAVITY LIGHTING/TROUBLESHOOT.
890425105 1   11SJ188 FAILURE DESCRIPTION: LEAKING THRU/CLEAN OFF BORIC ACID & CAP END OF PIPE.
 
SALEr1 UNIT 1 890425112 1 11SJ189 FAILURE DESCRIPTION: LEAKING THRU/CLEAN OFF BORIC ACID & CAP END OF PIPE.
890425113 1 12SJ188 FAILURE DESCRIPTION: LEAKING THRU/CLEAN OFF BORIC ACID & CAP END OF PIPE ..
890425119 1 12SJ189 FAILURE DESCRIPTION: LEAKING THRU/CLEAN OFF BORIC ACID & CAP END OF PIPE.
 
.MAJbR PLANT MODIFICATIONS           DOCKET NO.:    50*-272
~EPORT MONTH   APRIL 1989             UNIT NAME:    Salem 1 DATE:    May 10, 19 89 COMPLETED BY:    P. White TELEPHONE:    609/339-4455
  *DCR NO.         PRINCIPAL SYSTEM        DESCRIPTION lEC-02065      Charging              This design change added a pulsation dampener to the discharge of the positive displacement charging pump.
lEC-02066        Charging              This design change added a suction stabilizer to the piping upstream of the #13 positive displacement charging pump.
lEC-02173        Turbine Controls      This design change installed AMSAC (ATWS Mitigation System Actuation Circuitry).
lEC-02271        Electrical            This design change eliminated the 91% voltage vital bus transfer scheme between station power transformers and provided (3) 91% undervoltage relays wired to each vital bus providing inputs to its SEC unit for a 2 of 3 logic to the diesel generator.
* DCR - Design Change Request
 
e MAJOR PLANT MODIFICATIONS e
DOCKET NO.:   50-272 REPORT MONTH   APRIL 1989               UNIT NAME:   Salem 1 DATE:  May 10, 19 89 COMPLETED BY:   P. White TELEPHONE:   609/339-4455
    *DCR          SAFETY EVALUATION 10 CFR 50.59 lEC-02065          This design change added a pulsation dampener to the discharge of #13 positive displacement charging pump. The unit selected is _a gas charged bladder design which is currently in use at a number of other nuclear plants. There was no change to any plant process or discharge or to the environmental impact of the plant. "No unreviewed safety or environmental questions are involved.
lEC-02066          This design change added a suction stabilizer to the piping upstream of #13 positive displacement charging pump. The unit selected is a gas charged bladder design which is currently in use at a number of other nuclear plants. There was no change to any plant process or discharge or to the environmental impact of the plant. No unreviewed safety or environmental questions are involved.
lEC-02173          This design change installed AMSAC (ATWS Mitigation Actuation Circuitry). The system provides a diverse means for tripping the main steam turbine and initiating auxiliary feedwater in the event of an anticipated transient without a scram. There was no change to any plant process or discharge or to the environmental impact of the plant. No unreviewed safety or environmental questions are involved.
lEC-02271          This design change eliminated the 91% voltage vital bus transfer scheme between station power transformers and provided (3) 91% undervoltage relays wired to each vital bus providing inputs to its SEC unit for a 2 of 3 logic to the diesel generator. There was no change to any plant process or discharge or to the environmental impact of the plant. No unreviewed safety or environmental questions are involved.
* DCR - Design Change Request
* SALEM GENERATING STATION MONTHLY OPERATING  


==SUMMARY==
==SUMMARY==
  -UNIT NO. 1 APRIL 1989 The Unit was shutdown for the entire period for a refueling outage. Major work accomplished during the period included the following:
  - UNIT NO. 1 APRIL 1989 SALEM UNIT NO. 1 The Unit was shutdown for the entire period for a refueling outage.
: 1. Reassembly of nos. 12 & 14 Reactor Coolant Pump Seals; 2. Containment Fan Coil Unit service water piping replacement;
Major work accomplished during the period included the following:
: 3. Eddy current examination of Steam generator tubes, and 4. Fuel element ultrasonic testing and full face visual inspection
: 1. Reassembly of nos. 12 & 14 Reactor Coolant Pump Seals;
: 5. Replacement of Vital Instrument Inverter Fuel element visual inspection and ultrasonic testing disclosed a total of eleven (11) assemblies requiring further examination.
: 2. Containment Fan Coil Unit service water piping replacement;
An evaluation of the affected assemblies cleared six (6) for re-use, five (5) were identified for replacement.
: 3. Eddy current examination of Steam generator tubes, and
Eddy current testing showed thirty two tubes indicating greater than 30% wear and all 362 row one tubes are to be plugged. Additionally, three plugs from previously plugged tubes have been removed for analysis as a follow up to the North Anna tube plug failure.
: 4. Fuel element ultrasonic testing and full face visual inspection
. *'
: 5. Replacement of Vital Instrument Inverter Fuel element visual inspection and ultrasonic testing disclosed a total of eleven (11) assemblies requiring further examination. An evaluation of the affected assemblies cleared six (6) for re-use, five (5) were identified for replacement.
* REFUELING INFORMATION DOCKET NO.: 50-272 COMPLETED BY: P. White UNIT NAME: Salem 1 DATE: May 10, 19 89 TELEPHONE:
Eddy current testing showed thirty two tubes indicating greater than 30% wear and all 362 row one tubes are to be plugged. Additionally, three plugs from previously plugged tubes have been removed for analysis as a follow up to the North Anna tube plug failure.
609/935-6000 EXTENSION:
 
4497 Month APRIL 1989 1. Refueling information has changed from last month: YES X NO 2. Scheduled date for next refueling:
.*'
March 28, 1989 3. Scheduled date for restart following refueling:
* REFUELING INFORMATION DOCKET NO.:   50-272 COMPLETED BY:       P. White                 UNIT NAME:   Salem 1 DATE:   May 10, 19 89 TELEPHONE:   609/935-6000 EXTENSION:   4497 Month   APRIL 1989
May 24, 1989 4. A) Will Technical Specification changes or other license amendments be required?
: 1. Refueling information has changed from last month:
YES NO NOT DETERMINED TO DATE X B) Has the reload fuel design been reviewed by the Station Operating Review Committee?
YES   X           NO
YES NO X If no, when is it scheduled?
: 2. Scheduled date for next refueling:         March 28, 1989
May 1989 5. Scheduled date(s) for proposed licensing action: May if required 6. Important licensing considerations associated with refueling:
: 3. Scheduled date for restart following refueling: May 24, 1989
: 7. 8. 9. NONE Number of Fuel Assemblies:
: 4. A)   Will Technical Specification changes or other license amendments be required?
A) Inc ore B) In Spent Fuel Storage Present licensed spent fuel storage capacity:
YES             NO NOT DETERMINED TO DATE     X B)   Has the reload fuel design been reviewed by the Station Operating Review Committee?
Future spent fuel storage capacity:
YES             NO     X If no, when is it scheduled? May 1989
Date of last refueling that can be discharged to spent fuel pool assuming the present licensed capacity:
: 5. Scheduled date(s) for subm~tting proposed licensing action:
8-1-7.R4 193 540 1170 1170 September 2001}}
May if required
: 6. Important licensing considerations associated with refueling:
NONE
: 7. Number of Fuel Assemblies:
A)   Inc ore                                             193 B)   In Spent Fuel Storage                               540
: 8. Present licensed spent fuel storage capacity:             1170 Future spent fuel storage capacity:                       1170
: 9. Date of last refueling that can be discharged to spent fuel pool assuming the present licensed capacity:                                   September 2001 8-1-7.R4}}

Revision as of 10:18, 21 October 2019

Monthly Operating Rept for Apr 1989 for Salem,Unit 1.W/ 890511 Ltr
ML18101A479
Person / Time
Site: Salem PSEG icon.png
Issue date: 04/30/1989
From: Miller L, Orticelle A
Public Service Enterprise Group
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
NUDOCS 8905230340
Download: ML18101A479 (10)


Text

e

.*.-o PS~G Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038 Salem Generating Station flay 11, 1989 U.S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555

Dear Sir:

MONTHLY OPERATING REPORT SALEM NO. 1 DOCKET NO. 50-272 In compliance with Section 6.9.1.6, Reporting Requirements for the Salem Technical Specifications, the original copy of the monthly operating reports for the month of April 1989 are being sent to you.

Average Daily Unit Power Level Operating Data Report Unit Shutdowns and Power Reductions Safety Related Maintenance Major Plant Modification Operating Summary Refueling Information sk~

L. K. Miller General Manager -

Salem Operations RH: sl cc: Mr. William T. Russell Regional Administrator USNRC Region I 631 Park Avenue King of Prussia, PA 19406 Enclosures 8-l-7.R4

- :=~*:')(- ):"*1:i::::*:(

- - - ")*-*4(").,:. - ..**, (l~.'JI""

  • ,=_,"=' ~A

~b~- ~fiocK o5otu272 R PDC The Energy People ff14

'l I 95-2189 (SM) 12-88

.e AVERAGE DAILY UNIT POWER LEVEL Docket No. 50-272 Unit Name Salem # 1 Date 5-09-89 Completed by Art Orticelle Telephone 609-935-6000 Extension 4451 Month APRIL 1989 Day Average Daily Power Level Day Average Daily Power Level (MWe-NET) (MWe-NET) 1 0 17 0 2 0 18 0 3 0 19 0 4 0 20 0 5 0 21 0 6 0 22 0 7 0 23 0 8 0 24 0 9 0 25 0 10 0 26 0 11 0 27 0 12 0 28 0 13 0 29 0 14 0 30 0 15 0 31 16 0 P. 8.1-7 Rl j,G'*:f

OPERATING DATA REPORT Docket No .50-272 Date: 5~--o-=-=-9--~8~9~--------

Telephone: 935-6000 Completed by Pell White Extension: ~4~4~5~1-------------

Operating Status

1. Unit Name Salem No. 1 Notes
2. Reporting Period April 1989
3. Licensed Thermal Power (MWt) 3411
4. Nameplate Rating (Gross MWe) 1170
5. Design Electrical Rating (Net MWe) 1115
6. Maximum Dependable Capacity(Gross MWe)1149
7. Maximum Dependable Capacity (Net MWe) 1106
8. If Changes Occur in Capacity Ratings (items 3 through 7) since Last Report, Give Reason N/A

--~---------------~------------------------------------

9. Power Level to Which Restricted, if any (Net MWe) N/A

~~~------------

10. Reasons for Restrictions, if any N/A

~--------------~-------

This Month Year to Date Cumulative

11. Hours in Reporting Period 719 2879 103752
12. No. of Hrs. Reactor was Critical 0 1862.33 66 494. 53
13. Reactor Reserve Shutdown Hrs. 0 0 0
14. Hours Generator On-Line 0 1811.75 64 447. 65
15. Unit Reserve Shutdown Hours 0 0 0
16. Gross Thermal Energy Generated (MWH) 0 6106848 201543640.4
17. Gross Elec. Energy Generated (MWH) 0 2039200 66986380
18. Net Elec. Energy Generated (MWH) -4020 1945095 63751219
19. Unit Service Factor 0 62.9 62.1
20. Unit Availability Factor 0 62.9 62.1
21. Unit Capacity Factor (using MDC Net) 0 61.1 55.6
22. Unit Capacity Factor (using DER Net) 0 60.6 55.1 2 3. Unit Forced Outage Rate 0 12.2 22.1
24. Shutdowns scheduled over next 6 months (type, date and duration of each)

NONE 25*. If shutdown at end of Report Period, Estimated Date of Startup:

Unit currently in 8th refueling outage scheduled start date May 26, 1989.

8-l-7.R2

HNIT SHUTDOWN AND POWER REDUCTIONS Docket No.50-272

~~~~~~~~-

REPORT MONTH APRIL 1989 Unit Name Salem No.I Date 5-09-89 Completed by Art Orticelle Telephone 609-935-6000 Extension 4451 Method of Duration Shutting License Cause and Corrective No. Date Type Hours Reason Down Event System Component Action to 1 2 Reactor Report Code 4 C od*e 5 Prevent Recurrence NUCLEAR REACTOR 0071 4-01-89 s 719 c 4 ------ CA VESSEL OVERHAUL GENERATOR MAJOR 0071 4-01-89 s 719 c 4 ------ HA GENERA OVERHAUL MAJOR TURBINE 007 1 4-01-89 s 719 c 4 ------ HA TURBIN OVERHAUL 1 2 Reason 3 Method 4 Exhibit G 5 Exhibit-F: Forced A-Equipment Failure-explain 1-Man ua 1 Instructions Salem as S: Scheduled B-Maintenance or Test 2-Manual Scram. for Prepara- Source C-Refue ling 3-Automatic Scram. tion of Data D-Regulatory Restriction 4-Continuation of Entry Sheets E-Operator Training & Licensing Exam Previous Outage for Licensee F-Administrative 5-Load Reduction Event Report G-Operational Error-explain 9-0ther (LER) File H-Other-explain (NUREG 0161)

PSE&G SALEM GENERATING STATION SAFETY RELATED WORK ORDER LOG SALEM UNIT 1 WO NO UNIT EQUIPMENT IDENTIFICATION 890125071 1 EMERG. AIR COMPRESSOR FAILURE DESCRIPTION: #1 EMERG. AIR COMPRESSOR OIL LEAK / REPLACE GASKET.

890330094 1 lSAll 8 FAILURE DESCRIPTION: FAILED LEAK RATE TEST/MARK NO. A-157. INSPECT.

890330112 1 lSAll 9 "FAILURE DESCRIPTION: FAILED LEAK RATE TEST / MARK NO. A-165. INSPECT.

890410160 1 1C5Y FAILURE DESCRIPTION: lC VTL INSTR. BUS INVERTER BREAKER/CHANGE OVERLOAD.

890413128 1 RX CAVITY LIGHTING FAILURE DESCRIPTION: RX CAVITY LIGHTING/TROUBLESHOOT.

890425105 1 11SJ188 FAILURE DESCRIPTION: LEAKING THRU/CLEAN OFF BORIC ACID & CAP END OF PIPE.

SALEr1 UNIT 1 890425112 1 11SJ189 FAILURE DESCRIPTION: LEAKING THRU/CLEAN OFF BORIC ACID & CAP END OF PIPE.

890425113 1 12SJ188 FAILURE DESCRIPTION: LEAKING THRU/CLEAN OFF BORIC ACID & CAP END OF PIPE ..

890425119 1 12SJ189 FAILURE DESCRIPTION: LEAKING THRU/CLEAN OFF BORIC ACID & CAP END OF PIPE.

.MAJbR PLANT MODIFICATIONS DOCKET NO.: 50*-272

~EPORT MONTH APRIL 1989 UNIT NAME: Salem 1 DATE: May 10, 19 89 COMPLETED BY: P. White TELEPHONE: 609/339-4455

  • DCR NO. PRINCIPAL SYSTEM DESCRIPTION lEC-02065 Charging This design change added a pulsation dampener to the discharge of the positive displacement charging pump.

lEC-02066 Charging This design change added a suction stabilizer to the piping upstream of the #13 positive displacement charging pump.

lEC-02173 Turbine Controls This design change installed AMSAC (ATWS Mitigation System Actuation Circuitry).

lEC-02271 Electrical This design change eliminated the 91% voltage vital bus transfer scheme between station power transformers and provided (3) 91% undervoltage relays wired to each vital bus providing inputs to its SEC unit for a 2 of 3 logic to the diesel generator.

  • DCR - Design Change Request

e MAJOR PLANT MODIFICATIONS e

DOCKET NO.: 50-272 REPORT MONTH APRIL 1989 UNIT NAME: Salem 1 DATE: May 10, 19 89 COMPLETED BY: P. White TELEPHONE: 609/339-4455

  • DCR SAFETY EVALUATION 10 CFR 50.59 lEC-02065 This design change added a pulsation dampener to the discharge of #13 positive displacement charging pump. The unit selected is _a gas charged bladder design which is currently in use at a number of other nuclear plants. There was no change to any plant process or discharge or to the environmental impact of the plant. "No unreviewed safety or environmental questions are involved.

lEC-02066 This design change added a suction stabilizer to the piping upstream of #13 positive displacement charging pump. The unit selected is a gas charged bladder design which is currently in use at a number of other nuclear plants. There was no change to any plant process or discharge or to the environmental impact of the plant. No unreviewed safety or environmental questions are involved.

lEC-02173 This design change installed AMSAC (ATWS Mitigation Actuation Circuitry). The system provides a diverse means for tripping the main steam turbine and initiating auxiliary feedwater in the event of an anticipated transient without a scram. There was no change to any plant process or discharge or to the environmental impact of the plant. No unreviewed safety or environmental questions are involved.

lEC-02271 This design change eliminated the 91% voltage vital bus transfer scheme between station power transformers and provided (3) 91% undervoltage relays wired to each vital bus providing inputs to its SEC unit for a 2 of 3 logic to the diesel generator. There was no change to any plant process or discharge or to the environmental impact of the plant. No unreviewed safety or environmental questions are involved.

  • DCR - Design Change Request
  • SALEM GENERATING STATION MONTHLY OPERATING

SUMMARY

- UNIT NO. 1 APRIL 1989 SALEM UNIT NO. 1 The Unit was shutdown for the entire period for a refueling outage.

Major work accomplished during the period included the following:

1. Reassembly of nos. 12 & 14 Reactor Coolant Pump Seals;
2. Containment Fan Coil Unit service water piping replacement;
3. Eddy current examination of Steam generator tubes, and
4. Fuel element ultrasonic testing and full face visual inspection
5. Replacement of Vital Instrument Inverter Fuel element visual inspection and ultrasonic testing disclosed a total of eleven (11) assemblies requiring further examination. An evaluation of the affected assemblies cleared six (6) for re-use, five (5) were identified for replacement.

Eddy current testing showed thirty two tubes indicating greater than 30% wear and all 362 row one tubes are to be plugged. Additionally, three plugs from previously plugged tubes have been removed for analysis as a follow up to the North Anna tube plug failure.

.*'

  • REFUELING INFORMATION DOCKET NO.: 50-272 COMPLETED BY: P. White UNIT NAME: Salem 1 DATE: May 10, 19 89 TELEPHONE: 609/935-6000 EXTENSION: 4497 Month APRIL 1989
1. Refueling information has changed from last month:

YES X NO

2. Scheduled date for next refueling: March 28, 1989
3. Scheduled date for restart following refueling: May 24, 1989
4. A) Will Technical Specification changes or other license amendments be required?

YES NO NOT DETERMINED TO DATE X B) Has the reload fuel design been reviewed by the Station Operating Review Committee?

YES NO X If no, when is it scheduled? May 1989

5. Scheduled date(s) for subm~tting proposed licensing action:

May if required

6. Important licensing considerations associated with refueling:

NONE

7. Number of Fuel Assemblies:

A) Inc ore 193 B) In Spent Fuel Storage 540

8. Present licensed spent fuel storage capacity: 1170 Future spent fuel storage capacity: 1170
9. Date of last refueling that can be discharged to spent fuel pool assuming the present licensed capacity: September 2001 8-1-7.R4