ENS 53014: Difference between revisions
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| utype = GE-4, GE-4, GE-4 | | utype = GE-4, GE-4, GE-4 | ||
| cfr = 10 CFR 50.72(b)(3)(v)(D) | | cfr = 10 CFR 50.72(b)(3)(v)(D) | ||
| emergency class = Non Emergency | | emergency class = Non Emergency | ||
| notification date = 10/13/2017 22:46 | | notification date = 10/13/2017 22:46 | ||
| notification by = Stewart Wetzel | | notification by = Stewart Wetzel | ||
| NRC officer = Richard Smith | | NRC officer = Richard Smith | ||
| event date = | | event date = 10/13/2017 17:00 CDT | ||
| last update date = | | last update date = 10/13/2017 | ||
| title = | | title = Accident Mitigation - High Pressure Coolant Injection Declared Inoperable | ||
| event text = | | event text = On October 13, 2017 at 1700 CDT, Unit 1 High Pressure Coolant Injection (HPCI) was declared Inoperable due to discovery of a leak on a sensing line to 1-PCV-073-0043, Lube Oil Cooler & Gland Seal Condenser Pressure Control Valve. The leak is a steady stream located where the sense line connects to the valve. | ||
On October 13, 2017 at 1700 CDT, Unit 1 High Pressure Coolant Injection (HPCI) was declared Inoperable due to discovery of a leak on a sensing line to 1-PCV-073-0043, Lube Oil Cooler & Gland Seal Condenser Pressure Control Valve. The leak is a steady stream located where the sense line connects to the valve. | |||
This constitutes an unplanned HPCI System inoperability and requires an 8 hour ENS notification in accordance with 10 CFR 50.72(b)(3)(v)(D), due to the failure of a single train system affecting accident mitigation and a 60 day written report in accordance with 10 CFR 50.73(a)(2)(v)(D). | This constitutes an unplanned HPCI System inoperability and requires an 8 hour ENS notification in accordance with 10 CFR 50.72(b)(3)(v)(D), due to the failure of a single train system affecting accident mitigation and a 60 day written report in accordance with 10 CFR 50.73(a)(2)(v)(D). | ||
The NRC Resident Inspector has been notified by the Licensee. | The NRC Resident Inspector has been notified by the Licensee. | ||
| URL = https://www.nrc.gov/reading-rm/doc-collections/event-status/event/2017/20171016en.html#en53014 | |||
| URL = https://www.nrc.gov/reading-rm/doc-collections/event-status/event/ | |||
}}{{unit info | }}{{unit info | ||
| Unit = | | Unit = 1 | ||
| type = | | type = GE-4 | ||
| Scram code = | | Scram code = N | ||
| Reactor critical = | | Reactor critical = Y | ||
| Initial power = | | Initial power = 100 | ||
| Initial reactor mode = | | Initial reactor mode = Power Operation | ||
| Current power = | | Current power = 100 | ||
| Current reactor mode = | | Current reactor mode = Power Operation | ||
}} | }} | ||
{{ENS-Nav}}[[Category:Power Reactor]] | {{ENS-Nav}}[[Category:Power Reactor]] |
Latest revision as of 20:52, 30 October 2018
Where | |
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Browns Ferry Alabama (NRC Region 2) | |
Reporting | |
10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | |
Time - Person (Reporting Time:+0.77 h0.0321 days <br />0.00458 weeks <br />0.00105 months <br />) | |
Opened: | Stewart Wetzel 22:46 Oct 13, 2017 |
NRC Officer: | Richard Smith |
Last Updated: | Oct 13, 2017 |
53014 - NRC Website
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