ENS 57195: Difference between revisions

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Unit 2 is being supplied by offsite power. All control rods fully inserted. Steam generators are being fed by both motor driven auxiliary feedwater pumps. Decay heat is being removed via the steam dump system to the main condenser. Preliminary evaluation indicates plant systems functioned normally following the reactor trip. D.C. Cook Unit 2 remains in Mode 3 to repair the previously reported reactor coolant system leakage through valve 2-QRV-251, 'CVCS [chemical and volume control system] charging pumps discharge flow control' valve packing.
Unit 2 is being supplied by offsite power. All control rods fully inserted. Steam generators are being fed by both motor driven auxiliary feedwater pumps. Decay heat is being removed via the steam dump system to the main condenser. Preliminary evaluation indicates plant systems functioned normally following the reactor trip. D.C. Cook Unit 2 remains in Mode 3 to repair the previously reported reactor coolant system leakage through valve 2-QRV-251, 'CVCS [chemical and volume control system] charging pumps discharge flow control' valve packing.
The NRC Resident Inspector has been notified.
The NRC Resident Inspector has been notified.
| URL = https://www.nrc.gov/reading-rm/doc-collections/event-status/event/2024/20240628en.html#en57195
| URL = https://www.nrc.gov/reading-rm/doc-collections/event-status/event/2024/20240701en.html#en57195
}}{{unit info
}}{{unit info
| Unit = 2
| Unit = 2

Latest revision as of 07:20, 1 July 2024

ENS 57195 +/-
Where
Cook American Electric Power icon.png
Michigan (NRC Region 3)
Reporting
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Time - Person (Reporting Time:+1.98 h0.0825 days <br />0.0118 weeks <br />0.00271 months <br />)
Opened: Rob Eisenman
14:03 Jun 27, 2024
NRC Officer: Brian P. Smith
Last Updated: Jun 28, 2024
57195 - NRC Website
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