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This page provides a simple browsing interface for finding entities described by a property and a named value. Other available search interfaces include the page property search, and the ask query builder.
List of results
- 05000413/LER-1987-031, :on 870729,vent Gas Radiation Monitor Found Inoperable.Caused by non-conservative High Radiation Alarm Setpoint.Setpoint Returned to Original Setting & Policy Will Be Clarified + (ML20238E972)
- PLA-2913, Monthly Operating Repts for Aug 1987 + (ML20238E974)
- ML20238E975 + (ML20238E975)
- 05000440/LER-1987-058, :on 870815,control Rods Withdrawn Prior to Performing Source Range Monitors Signal to Noise Ratio Verification.Caused by Operator Error.Operators Involved Counseled.Tech Specs Rounds Will Be Revised + (ML20238E976)
- ML20238E978 + (ML20238E978)
- ML20238E979 + (ML20238E979)
- 05000245/LER-1987-001-01, :on 870113,insp on All Model 4160 Vac Load Ctrs Revealed Cracking Along Horizontal Noryl Insulators. Caused by GE Mfg Defect.Plant Replaced Cracked Insulation W/Bayblend Insulation to Preclude Recurrence + (ML20238E982)
- B12661, Proposed Tech Specs,Allowing Positive Moderator Temp Coefficient at Reactor Power Levels Less than 100% to Support Cycle 2 Reload + (ML20238E984)
- 05000413/LER-1987-030, :on 870726,failure to Perform Type C Leak Rate Test on Valve 1NI-120B Following Replacement of Torque Switch Occurred.Caused by Inadequate Retest Policy.Retest Performed.Memo Re Leak Rate Tests to Be Issued + (ML20238E987)
- ML20238E989 + (ML20238E989)
- TXX-6677, Forwards Response to NRC Requesting Addl Info on Groundwater Withdrawal Rates from 1979 to Present,Per Util 870429 Request for Extension of CP CPPR-127.Info Suppls Table 5.1 of Plant Fes (NUREG-0775) + (ML20238E991)
- ML20238E992 + (ML20238E992)
- ML20238E993 + (ML20238E993)
- B12648, Proposed Tech Specs,Changing Limiting Condition for Operation 3.4.6.2(c) on Page 3/4 4-9 from 0.5 Gpm to 0.15 Gpm for Any One Steam Generator + (ML20238E995)
- TXX-6716, Interim Deficiency Rept CP-87-18 Re Errors Identified During Review of Struther-Wells Qualification Documentation for Component Cooling Water Hxs.Initially Reported on 870608. Evaluation Continuing.Next Rept Will Be Provided by 871106 + (ML20238E999)
- ML20238F000 + (ML20238F000)
- ML20238F001 + (ML20238F001)
- ML20238F002 + (ML20238F002)
- ML20238F003 + (ML20238F003)
- 3F0987-10, Forwards Rev 4 to Modified Amended Security Plan,Per 10CFR50.54(p).Rev Withheld (Ref 10CFR73.21) + (ML20238F005)
- 05000271/LER-1987-007, :on 870812,18 & 23,while Performing Type C Leak Rate Testing,Listed Valves Found to Have Seat Leakage Above Tech Spec Requirements.Util Will Perform Maint on Valves to Determine Cause of Failure + (ML20238F006)
- B12663, Forwards Nonproprietary WCAP-11497 & Proprietary WCAP-11496, Resistance Temp Detector Bypass Elimination Licensing Rept for Millstone Unit 3. Proprietary Rept Withheld (Ref 10CFR2.790) + (ML20238F007)
- 05000265/LER-1998-005, Forwards LER 98-005-00,per 10CFR50.73(a)(2)(vii)B. Commitments Made by Util,Listed + (ML20238F009)
- 05000321/LER-1987-014-01, :on 870808,10 & 13 Main Control Room Environ Control Sys Went Into Pressurization Mode of Operation. Caused by Geiger-Mueller Tube Failures.Equipment Replaced & Recalibr + (ML20238F010)
- ML20238F011 + (ML20238F011)
- 05000265/LER-1998-005-07, :on 980729,HPCI Subsystem Turning Gear Failed to Engage Automatically Rendering HPCI Subsystem Inoperable. Caused by Failed Limit Switch in Tgr Logic.Limit Switch & Pressure Switch Were Replaced + (ML20238F013)
- 05000327/LER-1985-031, :on 850729,auxiliary Bldg Isolation Occurred Due to High Radiation Levels from Cracked Chemical & Vol Control Sample Line Weld.Caused by Fatigue of Metal in Weld. Brace Will Be Installed by Next Outage + (ML20238F016)
- 05000245/LER-1987-032-01, :on 870811,first Stage Bypass Switches Failed to Meet Tech Spec Requirements.Caused by Setpoint Drift from Extended Periods of Depressurization.Switches Recalibrated to Conform to Tech Specs + (ML20238F017)
- ML20238F019 + (ML20238F019)
- 05000414/LER-1987-022-01, :on 870728,main Feedwater Isolation Occurred Due to hi-hi Steam Generator Water Level.Caused by Debris in Feedwater Control Valve Positioner.Valve Positioner Replaced & Calibr Check Completed + (ML20238F020)
- TXX-6676, Forwards Rev 0 to QA Dept Procedure Nqa 3.07-1.01, Technical Audit Program & Rev 3 to Engineering Assurance Program Engineering Functional Evaluation,Comanche Peak Steam Electric Station + (ML20238F022)
- ML20238F025 + (ML20238F025)
- ML20238F026 + (ML20238F026)
- B12601, Proposed Tech Spec 5.4, Containment, Deleting General Statements Made About Containment Penetrations & Associated Basis + (ML20238F029)
- ML20238F030 + (ML20238F030)
- ML20238F033 + (ML20238F033)
- IR 05000445/1998004 + (ML20238F035)
- ML20238F036 + (ML20238F036)
- ML20238F038 + (ML20238F038)
- ML20238F039 + (ML20238F039)
- NRC-87-0129, Submits Info Re Facility Operation W/Reduced Feedwater Temp & Operation W/Moisture Separator Reheater out-of-svc,per 870814 Request.Util Believes That Other Aspects of Two Issues Require Resolution & Proposes to Meet W/Nrc Staff + (ML20238F040)
- ML20238F043 + (ML20238F043)
- 05000461/LER-1998-022, :on 980729,discovered That Surveillance Testing of Div 2 DG Fuel Oil Transfer Pump & Div 2 DG Fuel Oil Storage Tank Had Not Been Performed.Caused by Data Input Error.Will Update & Verify Completion Dates in Database + (ML20238F046)
- PNO-III-87-105, on 870807,reactor Manually Scrammed.Caused by Variations in Feedwater Flow to Reactor & Leakage from Feedwater Sys.Ndt Performed Small Diameter Feedwater Piping & Other High Stress Areas + (ML20238F047)
- ML20238F048 + (ML20238F048)
- ML20238F049 + (ML20238F049)
- ML20238F052 + (ML20238F052)
- ML20238F053 + (ML20238F053)
- ML20238F056 + (ML20238F056)
- ML20238F057 + (ML20238F057)
- 05000413/LER-1987-032, :on 870729,engineer Determined That Battery Banks in 125 Volt Dc Vital Instrumentation & Control Power Sys Inoperable.Caused by Mgt/Qa Deficiency.Intercell Resistance Readings Taken + (ML20238F059)