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This page provides a simple browsing interface for finding entities described by a property and a named value. Other available search interfaces include the page property search, and the ask query builder.
List of results
- ML20009A488 + (ML20009A488)
- IR 05000498/1981020 + (ML20009A489)
- 05000333/LER-1981-049, Forwards LER 81-049/03L-0 + (ML20009A490)
- ML20009A491 + (ML20009A491)
- 05000333/LER-1981-049-03, /03L-0:on 810704,following Surveillance During Normal Operation,One of 16 Main Steam High Flow Instruments Did Not Respond Properly.Caused by Rust Plugging Pressure Snubber Sensing Line.Snubber Cleaned & Tested + (ML20009A494)
- ML20009A496 + (ML20009A496)
- ML20009A497 + (ML20009A497)
- ML20009A499 + (ML20009A499)
- ML20009A500 + (ML20009A500)
- ML20009A501 + (ML20009A501)
- ML20009A502 + (ML20009A502)
- 05000311/LER-1981-032, Forwards LER 81-032/03L-0.Detailed Event Analysis Encl + (ML20009A503)
- ML20009A504 + (ML20009A504)
- 05000311/LER-1981-032-03, /03L-0:on 810603,boron Injection Tank Concentration Decreased Below Tech Spec Limits.Caused by Safety Injection Initiated by High Streamline Flow from High Level in Steam Generator 22.Tank Borated + (ML20009A508)
- A810021, Forwards Response to NUREG-0737 TMI Action Plan Requirements & Meteorological Monitoring Sys Development Plan for Emergency Preparedness, Preliminary Rept Prepared by Dames & Moore Per NUREG-0654 + (ML20009A510)
- ML20009A511 + (ML20009A511)
- ML20009A512 + (ML20009A512)
- ML20009A514 + (ML20009A514)
- 0CAN078102, Informs That Further Repts & Evaluations Re EPRI PWR Safety & Relief Valve Test Program Will Be Submitted Per 801215 Schedule,As Modified on 810701 + (ML20009A515)
- ML20009A516 + (ML20009A516)
- ML20009A517 + (ML20009A517)
- W3P81-1566, Forwards Revision 6 to Physical Security Plan.Plan Withheld (Ref 10CFR2.790) + (ML20009A518)
- ML20009A519 + (ML20009A519)
- ML20009A522 + (ML20009A522)
- ML20009A523 + (ML20009A523)
- ML20009A525 + (ML20009A525)
- PNO-I-81-075, on 810706,unit Shut Down When Middle Seal of Reactor Coolant Pump 11B Failed.Seal Replacement Expected in 7 Days + (ML20009A526)
- 05000334/LER-1981-054-03, /03L-0:on 810527,outside Recirculation Spray PP2A Seal Water Level Low Alarm Sounded Following Surveillance Testing.Caused by Seal Package Retaining Ring Sticking & Preventing Proper Alignment.Seal Replaced & Retainer Lubed + (ML20009A527)
- 05000267/LER-1981-032-03, /03L-0:on 810428,hot Reheat Snubber HRS-244 Found Inoperable.Caused by Empty Hydraulic Oil Reservoir Due to Leaking Elbow Fitting.Fitting Tightened,Reservoir Refilled & Snubber Returned to Svc + (ML20009A528)
- 05000267/LER-1981-034, Forwards LER 81-034/03L-0.Detailed Event Analysis Encl + (ML20009A529)
- ML20009A530 + (ML20009A530)
- 05000334/LER-1981-055-03, /03L-0:on 810529,during Maint Surveillance Test, High Level Alarm on Safety Injection Accumulator 1C Was Discovered Above High Limit.Caused by Instrument Drift.Trip Voltage Adjusted + (ML20009A531)
- 05000298/LER-1981-010, Forwards LER 81-010/03L-0 + (ML20009A532)
- ML20009A533 + (ML20009A533)
- 05000267/LER-1981-034-03, /03L-0:on 810504,equipment Necessary to Terminate Release from Liquid Waste Sys & Reactor Sump Found Not Operating Properly.Caused by Plugged Sense Lines on Flow Element Associated W/Control Valve + (ML20009A534)
- ML20009A535 + (ML20009A535)
- 05000334/LER-1981-041-04, /04T-1:on 810513,tritium Level in Quarterly Composite of Weekly Grab Samples Collected from Oh River Was Found Higher than Tech Spec Requirements.Caused by Normal Plant Discharge.New Tech Spec Limits Submitted + (ML20009A536)
- 05000333/LER-1981-045, Forwards LER 81-045/03L-0 + (ML20009A537)
- ML20009A538 + (ML20009A538)
- 05000298/LER-1981-010-03, /03L-0:on 810505,static Inverter 1A Spike Suppressor Capacitor Failed Causing Inverter to Become Inoperable.Caused by Aging & Effects of High Ripple Charger + (ML20009A539)
- 05000219/LER-1981-021, Forwards LER 81-021/03L-0.Detailed Event Analysis Encl + (ML20009A540)
- ML20009A541 + (ML20009A541)
- 05000267/LER-1981-038, Forwards LER 81-038/03L-0.Detailed Event Analysis Encl + (ML20009A542)
- ML20009A543 + (ML20009A543)
- 05000333/LER-1981-045-03, /03L-0:on 810601,during Normal Operation,While Conducting Surveillance,Reactor Water Level Instrument Switch for Recirculation Pump Trip Failed.Caused by Age. Switch Replaced & Calibr.Instrument Returned to Svc + (ML20009A544)
- 05000334/LER-1981-056, Forwards LER 81-056/03L-0 + (ML20009A545)
- ML20009A546 + (ML20009A546)
- 05000293/LER-1981-021, Forwards LER 81-021/01T-0 + (ML20009A547)
- ML20009A548 + (ML20009A548)
- 05000219/LER-1981-021-03, /03L-0:on 810603,high Pressure Sensor Switches RE03B, C & D Were Found Tripping within 8 Lb of Setpoint. Caused by Sensor Repeatability.Switches Reset.Switches Will Be Replaced During Next Refueling Outage + (ML20009A549)