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This notification is being made to report … This notification is being made to report that Salem Unit 2 has experienced an automatic reactor trip at 1130 EST. The reactor trip was caused by 24BF19, 24 steam generator feedwater regulation valve, not responding to demand signal that resulted in a reactor trip due to 24 steam generator lo-lo level. The cause of the 24BF19 failure to respond to demand is under investigation.</br>21, 22 & 23 AFW pumps all auto started as expected on the reactor trip feeding the steam generators. 23 AFW pump has been shutdown by procedure. 21 & 22 AFW pumps are maintaining steam generator levels with decay heat removal via the main steam dump system. All control & shutdown rods fully inserted on the reactor trip.</br>Salem Unit 2 is currently in mode 3. Reactor coolant system temperature is 547 degrees F with pressure at 2235 psig. There are no shut down technical specifications action statements in effect. </br>All ECCS and ESF systems are available. All safety related equipment responded as expected. There were no personnel injuries associated with this event.</br>The licensee will inform the Lower Alloways Creek Township, the State of New Jersey, and the State of Delaware. The licensee has informed the NRC Resident Inspector. The licensee has informed the NRC Resident Inspector. +
16:30:00, 25 November 2012 +
48,534 +
15:13:00, 25 November 2012 +
16:30:00, 25 November 2012 +
This notification is being made to report … This notification is being made to report that Salem Unit 2 has experienced an automatic reactor trip at 1130 EST. The reactor trip was caused by 24BF19, 24 steam generator feedwater regulation valve, not responding to demand signal that resulted in a reactor trip due to 24 steam generator lo-lo level. The cause of the 24BF19 failure to respond to demand is under investigation.</br>21, 22 & 23 AFW pumps all auto started as expected on the reactor trip feeding the steam generators. 23 AFW pump has been shutdown by procedure. 21 & 22 AFW pumps are maintaining steam generator levels with decay heat removal via the main steam dump system. All control & shutdown rods fully inserted on the reactor trip.</br>Salem Unit 2 is currently in mode 3. Reactor coolant system temperature is 547 degrees F with pressure at 2235 psig. There are no shut down technical specifications action statements in effect. </br>All ECCS and ESF systems are available. All safety related equipment responded as expected. There were no personnel injuries associated with this event.</br>The licensee will inform the Lower Alloways Creek Township, the State of New Jersey, and the State of Delaware. The licensee has informed the NRC Resident Inspector. The licensee has informed the NRC Resident Inspector. +
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92 +
00:00:00, 25 November 2012 +
Modification date"Modification date" is a predefined property that corresponds to the date of the last modification of a subject and is provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a>.
02:02:25, 2 March 2018 +
15:13:00, 25 November 2012 +
true +
-0.0533 d (-1.28 hours, -0.00762 weeks, -0.00175 months) +
16:30:00, 25 November 2012 +
New Jersey + and Delaware +
Automatic Reactor Trip Due to Steam Generator Feedwater Regulator Valve Not Responding to Demand Signal +
URL"URL" is a <a href="/Special:Types/URL" title="Special:Types/URL">type</a> and predefined property provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a> to represent URI/URL values.