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At 0830 (CDT) on 05/06/2014, the Unit 3 reAt 0830 (CDT) on 05/06/2014, the Unit 3 reactor automatically scrammed due to low reactor water level as a result of a trip of both recirculation pumps. Main Steam Isolation Valves remained open with main turbine bypass valves controlling reactor pressure. Reactor feedwater pumps are in service to control reactor water level.</br>Primary Containment Isolation System Groups 2, 3, 6, and 8 containment isolation and initiation signals were received. Upon receipt of these signals all required components actuated as required. The Reactor Feedwater System controlled and maintained water level above the level 2 initiation setpoint.</br>Prior to the Scram, the reactor was operating at 100% power. A Core and Containment Cooling Systems Analog Trip Unit Functional Test was in progress. The cause of the recirculation pump trip is under investigation.</br>This event is reportable within 4 hours per 10CFR 50.72(b)(2)(iv)(B) 'any event or condition that results in actuation of the reactor protection system (RPS) when the reactor is critical except when the actuation results from and is part of a pre-planned sequence during testing or reactor operation.' It is also reportable within 8 hours per 10CFR 50.72(b)(3)(iv)(A) and requires an LER within 60 days per 10CFR 50.73(a)(2)(iv)(A).</br>The NRC Resident Inspector has been notified.</br>U1 and U2 remained at 100% power and were unaffected.</br>* * * UPDATE AT 1302 EDT ON 05/09/14 FROM TODD BOHANAN TO DONG PARK * * * </br>Investigation revealed that a failed power supply caused an Anticipated Transient Without Scram/Alternate Rod Insertion (ATWS/ARI) signal to be generated when a level 2 Reactor Water Level was simulated on one instrument. All systems responded to the ATWS/ARI signal as designed. This signal opened the Recirc Pump Trip breakers for both Recirculation Pumps and opened the ARI valves to bleed air from the Reactor Protection System (RPS) scram air header. The resulting transient caused reactor water level to dip below the RPS trip setpoint (level 3 Reactor Water Level), a normal plant response, and the automatic scram signal occurred. At the time of the RPS scram signal, all rods were inserting and reactor power was approximately 2-3% and lowering.</br>The NRC Resident Inspector has been notified.</br>Notified R2DO (Bonser).has been notified. Notified R2DO (Bonser).  
13:30:00, 6 May 2014  +
13:27:00, 6 May 2014  +
13:30:00, 6 May 2014  +
At 0830 (CDT) on 05/06/2014, the Unit 3 reAt 0830 (CDT) on 05/06/2014, the Unit 3 reactor automatically scrammed due to low reactor water level as a result of a trip of both recirculation pumps. Main Steam Isolation Valves remained open with main turbine bypass valves controlling reactor pressure. Reactor feedwater pumps are in service to control reactor water level.</br>Primary Containment Isolation System Groups 2, 3, 6, and 8 containment isolation and initiation signals were received. Upon receipt of these signals all required components actuated as required. The Reactor Feedwater System controlled and maintained water level above the level 2 initiation setpoint.</br>Prior to the Scram, the reactor was operating at 100% power. A Core and Containment Cooling Systems Analog Trip Unit Functional Test was in progress. The cause of the recirculation pump trip is under investigation.</br>This event is reportable within 4 hours per 10CFR 50.72(b)(2)(iv)(B) 'any event or condition that results in actuation of the reactor protection system (RPS) when the reactor is critical except when the actuation results from and is part of a pre-planned sequence during testing or reactor operation.' It is also reportable within 8 hours per 10CFR 50.72(b)(3)(iv)(A) and requires an LER within 60 days per 10CFR 50.73(a)(2)(iv)(A).</br>The NRC Resident Inspector has been notified.</br>U1 and U2 remained at 100% power and were unaffected.</br>* * * UPDATE AT 1302 EDT ON 05/09/14 FROM TODD BOHANAN TO DONG PARK * * * </br>Investigation revealed that a failed power supply caused an Anticipated Transient Without Scram/Alternate Rod Insertion (ATWS/ARI) signal to be generated when a level 2 Reactor Water Level was simulated on one instrument. All systems responded to the ATWS/ARI signal as designed. This signal opened the Recirc Pump Trip breakers for both Recirculation Pumps and opened the ARI valves to bleed air from the Reactor Protection System (RPS) scram air header. The resulting transient caused reactor water level to dip below the RPS trip setpoint (level 3 Reactor Water Level), a normal plant response, and the automatic scram signal occurred. At the time of the RPS scram signal, all rods were inserting and reactor power was approximately 2-3% and lowering.</br>The NRC Resident Inspector has been notified.</br>Notified R2DO (Bonser).has been notified. Notified R2DO (Bonser).  
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4.62963e-5 d (0.00111 hours, 6.613757e-6 weeks, 1.522e-6 months)  +  and 9.259259e-5 d (0.00222 hours, 1.322751e-5 weeks, 3.044e-6 months)  +
00:00:00, 9 May 2014  +
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01:50:50, 2 March 2018  +
13:27:00, 6 May 2014  +
-0.00208 d (-0.05 hours, -2.97619e-4 weeks, -6.849e-5 months)  +
13:30:00, 6 May 2014  +
Automatic Reactor Scram Due to Low Reactor Water Level During Instrument Testing  +
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3  +