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At 0957 EST on 02/21/13, Unit 1 Reactor auAt 0957 EST on 02/21/13, Unit 1 Reactor automatically tripped from 100% power, due to a turbine trip. The turbine trip was caused by a loss of both main feedwater (MFW) pumps. The 1A motor driven auxiliary feedwater (AFW) pump auto started to feed the "A" and "B" Steam Generators (S/G). The 1B motor driven AFW pump was unavailable due to planned maintenance, so the turbine driven AFW pump was manually started to feed the "C" and "D" S/Gs.</br>The reactor trip was uncomplicated. All control rods fully inserted. Decay heat removal is to the main condenser via the turbine bypass valves. There was no primary to secondary leakage. Electrical buses are being supplied via offsite power. Steam generator levels are being returned to normal and MFW has been reset and is available. All other plant systems functioned as designed during and after the reactor trip. There is no impact on Unit 2. There is no impact on the health and safety of the public. The loss of the MFW pumps is still under investigation.</br>The licensee has informed the NRC Resident Inspector.e has informed the NRC Resident Inspector.  +
14:57:00, 21 February 2013  +
48,775  +
12:49:00, 21 February 2013  +
14:57:00, 21 February 2013  +
At 0957 EST on 02/21/13, Unit 1 Reactor auAt 0957 EST on 02/21/13, Unit 1 Reactor automatically tripped from 100% power, due to a turbine trip. The turbine trip was caused by a loss of both main feedwater (MFW) pumps. The 1A motor driven auxiliary feedwater (AFW) pump auto started to feed the "A" and "B" Steam Generators (S/G). The 1B motor driven AFW pump was unavailable due to planned maintenance, so the turbine driven AFW pump was manually started to feed the "C" and "D" S/Gs.</br>The reactor trip was uncomplicated. All control rods fully inserted. Decay heat removal is to the main condenser via the turbine bypass valves. There was no primary to secondary leakage. Electrical buses are being supplied via offsite power. Steam generator levels are being returned to normal and MFW has been reset and is available. All other plant systems functioned as designed during and after the reactor trip. There is no impact on Unit 2. There is no impact on the health and safety of the public. The loss of the MFW pumps is still under investigation.</br>The licensee has informed the NRC Resident Inspector.e has informed the NRC Resident Inspector.  +
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100  +
00:00:00, 21 February 2013  +
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02:01:43, 2 March 2018  +
12:49:00, 21 February 2013  +
-0.0888 d (-2.13 hours, -0.0127 weeks, -0.00292 months)  +
14:57:00, 21 February 2013  +
Automatic Reactor Trip Due to Turbine Trip on Loss of Both Main Feed Pumps  +
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1  +