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Information Notice 1999-14, Unanticipated Reactor Water Draindown at Quad Cities Unit 2, Arkansas Nuclear One Unit 2, & FitzPatrick5 May 1999Unanticipated Reactor Water Draindown at Quad Cities Unit 2, Arkansas Nuclear One Unit 2, & FitzPatrick
NRC Generic Letter 1998-0228 May 1998NRC Generic Letter 1998-002: Loss of Reactor Coolant Inventory and Associated Potential for Loss of Emergency Mitigation Functions While in a Shutdown Condition
Information Notice 1997-83, Recent Events Involving Reactor Coolant System Inventory Control During Shutdown5 December 1997Recent Events Involving Reactor Coolant System Inventory Control During Shutdown
Information Notice 1996-65, Undetected Accumulation of Gas in Reactor Coolant System and Inaccurate Reactor Water Level Indication During Shutdown11 December 1996Undetected Accumulation of Gas in Reactor Coolant System and Inaccurate Reactor Water Level Indication During Shutdown
Information Notice 1996-56, Problems Associated with Testing, Tuning, or Resetting of Digital Control Systems While at Power22 October 1996Problems Associated with Testing, Tuning, or Resetting of Digital Control Systems While at Power
Information Notice 1996-42, Unexpected Opening of Multiple Safety Relief Valves5 August 1996Unexpected Opening of Multiple Safety Relief Valves
Information Notice 1996-37, Inaccurate Reactor Water Level Indication and Inadvertent Draindown During Shutdown18 June 1996Inaccurate Reactor Water Level Indication and Inadvertent Draindown During Shutdown
Information Notice 1996-05, Partial Bypass of Shutdown Cooling Flow from Reactor Vessel18 January 1996Partial Bypass of Shutdown Cooling Flow from Reactor Vessel
Information Notice 1994-52, Inadvertent Containment Spray and Reactor Vessel Draindown at Millstone Unit 115 July 1994Inadvertent Containment Spray and Reactor Vessel Draindown at Millstone Unit 1
Information Notice 1994-36, Undetected Accumulation of Gas in Reactor Coolant System24 May 1994Undetected Accumulation of Gas in Reactor Coolant System
Information Notice 1993-89, Potential Problems with BWR Level Instrumentation Backfill Modifications26 November 1993Potential Problems with BWR Level Instrumentation Backfill Modifications
Information Notice 1993-62, Thermal Stratification of Water in BWR Reactor Vessels10 August 1993Thermal Stratification of Water in BWR Reactor Vessels
Information Notice 1993-27, Level Instrumentation Inaccuracies Observed During Normal Plant Depressurization8 April 1993Level Instrumentation Inaccuracies Observed During Normal Plant Depressurization
NRC Generic Letter 1992-0419 August 1992NRC Generic Letter 1992-004 - Resolution of Issues Related to Reactor Vessel Water Level Instrumentation in BWRs Pursuant to 10 CFR 50.54(F)
Information Notice 1992-16, Loss of Flow from the Residual Heat Removal Pump During Refueling Cavity Draindown25 February 1992Loss of Flow from the Residual Heat Removal Pump During Refueling Cavity Draindown
ML20082G8979 August 1991Lilco Responses to Petitioner Filings of 910805 & 06.* W/Certificate of Svc
Information Notice 1990-22, Unanticipated Equipment Actuations Following Restoration of Power to Rosemount Transmitter Trip Units23 March 1990Unanticipated Equipment Actuations Following Restoration of Power to Rosemount Transmitter Trip Units
ML20236E17310 March 1989Requests Review of Encl camera-ready Tech Specs to Document & Certify Accuracy W/Facility Usar,Per 890301 Meeting
NUREG-1126, Forwards camera-ready Version of Tech Specs for Review15 November 1988Forwards camera-ready Version of Tech Specs for Review
ML20155F3436 October 1988Safety Evaluation Supporting Util Request to Operate Facility at 25% Power Re Accident Evaluation
ML20154F39514 September 1988Safety Evaluation Supporting Request to Operate Facility at 25% Power Re Accident Evaluation
SNRC-1397, Forwards Rev 1 of Updated Sar,Rev 3 of Fire Hazard Analysis Rept & 10CFR50.59 Rept for 860101-870607.Format for 10CFR50.59 Rept Listed.Jd Leonard Affidavit Encl4 December 1987Forwards Rev 1 of Updated Sar,Rev 3 of Fire Hazard Analysis Rept & 10CFR50.59 Rept for 860101-870607.Format for 10CFR50.59 Rept Listed.Jd Leonard Affidavit Encl
ML20235E59826 June 1987Assessment of Shoreham Nuclear Power Station Secondary Containment Severe Accident Mitigation Capability, Final Ltr Rept
ML20215H63512 June 1987Considerations Re Certain Aspects of Severe Accident Mitigation Afforded by Operation of Shoreham at Reduced Power, Final Ltr Rept
ML20215K71312 June 1987Considerations Re Certain Aspects of Severe Accident Mitigation Afforded by Operation of Shoreham at Reduced Power, Final Ltr Rept
ML20215M3024 May 1987Forwards Amend 5 to License NPF-36 & Safety Evaluation. Amend Revises Tech Specs to Change Reactor Water Level Setpoints for Closure of Main Steam Isolation & Line Drain Valves from Level 2 to Lower Level of Level 1
ML20215M3984 May 1987Amend 5 to License NPF-36,revising Tech Specs to Change Reactor Vessel Water Level Setpoint for Closure of Main Steam Isolation & Line Drain Valves from Level 2 to Lower Level of Level 1
ML20215M4184 May 1987Safety Evaluation Supporting Amend 5 to License NPF-36
ML20206H44314 April 1987Request for Authorization to Increase Power to 25% & Motion for Expedited Commission Consideration.* Apps 1-11 & Certificate of Svc Encl.Related Correspondence
IR 05000322/198700219 February 1987Insp Rept 50-322/87-02 on 870117-21.No Violations or Deviations Noted.Major Areas Inspected:Procedure Review,Test Witnessing & Preliminary Results Evaluation of Periodic Containment Integrated Leak Rate Test
ML20206J9379 February 1987Forwards Quarterly Status Rept for Fourth Quarter of Calendar Year 1986,in Response to Direction Given in House Rept 97-850.NRC Licensing Activity During Period of Rept Includes Issuance of full-power License for Perry Unit 1
ML20210L9565 February 1987Forwards NRR Monthly Status Rept,Including Info Available as of 870131.Rept Identifies Potential or Actual Licensing Delay for Shoreham,Comanche Peak Unit 1,Braidwood Unit 1 & Seabrook Unit 1
ML20214U20231 January 1987Technical Rept 86.2SH Verification of IPE for Shoreham. W/ 870313 Release Memo
ML20212J45721 January 1987Application for Amend to License NPF-36,incorporating License Change Application 6 & Revising Tech Specs to Implement Design Change to Lower Reactor Vessel Water Level Setpoint of MSIVs & Steam Line Drain Valves
ML20212J47521 January 1987Proposed Tech Specs,Incorporating License Change Application 6 to Implement Design Change to Lower Reactor Vessel Water Level of MSIVs & Steam Line Drain Valves from Level 2 to Level 1
SNRC-1308, Forwards Application for Amend to License NPF-36, Incorporating License Change Application 6 & Revising Tech Specs to Implement Design Change to Lower Reactor Vessel Water Level Setpoint.W/Certificate of Svc.Fee Paid21 January 1987Forwards Application for Amend to License NPF-36, Incorporating License Change Application 6 & Revising Tech Specs to Implement Design Change to Lower Reactor Vessel Water Level Setpoint.W/Certificate of Svc.Fee Paid
IR 05000322/198509824 November 1986Forwards SALP Rept 50-322/85-98 for Mar 1985 - Feb 1986, Initially Forwarded on 860714 & Related Correspondence.Rept Changes Unwarranted Based on 860729 Meeting & Util 860826 Comments.Licensee Overall Performance Acceptable
ML20203D42714 July 1986SALP Rept 50-322/85-98 for Mar 1985 - Feb 1986
SNRC-1261, Rev 1 to Transient Analysis Lesson Plan30 May 1986Rev 1 to Transient Analysis Lesson Plan
ML20154L9644 March 1986Amend 2 to License NPF-36,revising Tech Specs to Reflect Conversion of One of Two Low Range Reactor Bldg Standby Vent Sys Noble Gas Radiation Monitors to Low Range Plant Vent Stack Noble Gas Radiation Monitor
ML20138K68030 November 1985a Review of the Shoreham Nuclear Power Station Probabilistic Risk Assessment.Internal Events and Core Damage Frequency
SNRC-1215, Forwards Executive Summary Rept,For Low Power Testing.Four Sys Will Require Retesting.Minor HPCI & RCIC Testing for Controls Tuning & Addl Testing on Reactor Vessel Water Level Instrumentation Will Proceed Following Outage12 November 1985Forwards Executive Summary Rept,For Low Power Testing.Four Sys Will Require Retesting.Minor HPCI & RCIC Testing for Controls Tuning & Addl Testing on Reactor Vessel Water Level Instrumentation Will Proceed Following Outage
ML20138C87921 October 1985Proposed Tech Specs Re Conversion of Reactor Bldg Standby Ventilation Sys low-range Noble Gas Radiation Monitor to Vent Stack low-range Nobel Gas Radiation Monitor
IR 05000322/19850352 October 1985Insp Rept 50-322/85-35 on 850830-0913.No Violations Noted. Major Areas Inspected:Startup Test Program Activities & Licensee Investigation of Reactor Water Level Indication Problems & Unplanned Reactor Scrams
IR 05000322/198503020 September 1985Insp Rept 50-322/85-30 on 850803-31.No Violations Noted. Major Areas Inspected:Operations Conducted Under Power Ascension Test Program & Status of Previous Open Items.Four Items Closed & Two New Items Opened
IR 05000322/198502723 August 1985Insp Rept 50-322/85-27 on 850628-0802.No Violations Noted. Major Areas Inspected:Startup & Testing Conducted After Issuance of 5% License & Licensee Action on Opening of Primary Containment Purge Valves on 850710
ML20128M13731 July 1985Technical Specifications for Shoreham Nuclear Power Station, Unit No. 1.Docket No. 50-322.(Long Island Lighting Company)
PNO-I-85-053, on 850726,scram Signal Generated Due to Low Reactor Water Level.Normal Suction Valve from Suppression Pool for Loop a Opened Before Alternate Suction for Shutdown Cooling Valve Closed.Approx 3,000 Gallons Drained26 July 1985PNO-I-85-053:on 850726,scram Signal Generated Due to Low Reactor Water Level.Normal Suction Valve from Suppression Pool for Loop a Opened Before Alternate Suction for Shutdown Cooling Valve Closed.Approx 3,000 Gallons Drained
ML20128H18824 June 1985Affidavit of Jd Leonard Re Issuance of Low Power License. Certificate of Svc Encl
ML20244B44519 June 1985Forwards Response of Licensee to Motion for Stay of Low Power License,For Filing.W/Certificate of Svc