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Category:SAFETY EVALUATION REPORT--LICENSING & RELATED ISSUES
MONTHYEARML20057F2261993-09-30030 September 1993 Safety Evaluation Supporting Exemption Request from Requirements of 10CFR50.54(q) for License NPF-82 ML20056C7181993-07-14014 July 1993 SE Supporting Amend 10 to License NPF-82 ML20056A2001990-07-31031 July 1990 Safety Evaluation Supporting Amend 6 to License NPF-82 ML20055E3911990-06-25025 June 1990 Safety Evaluation Supporting Amend 5 to License NPF-82 ML20235M1941989-02-0808 February 1989 SER Accepting Util Response to NRC Bulletin 88-005 Re Identifying,Locating & Testing Nonconforming Flanges & Fittings Supplied by Piping Supplies,Inc,West Jersey Mfg Co & Chews Landing Mfgs ML20196E5961988-11-30030 November 1988 Safety Evaluation Supporting Amend 10 to License NPF-36 ML20196B6831988-11-30030 November 1988 Safety Evaluation Supporting Amend 9 to License NPF-36 ML20155F3531988-10-0606 October 1988 Safety Evaluation Supporting Util 870414 Request for Authorization to Increase Power to 25% of Full Rated Power W/Listed Conditions.Licensee Evaluation of Operation & Proposal for Inspecting Components Must Be Augmented ML20155F3431988-10-0606 October 1988 Safety Evaluation Supporting Util Request to Operate Facility at 25% Power Re Accident Evaluation ML20155F3381988-10-0606 October 1988 Safety Evaluation Supporting Util Request for Authorization to Operate Facility at 25% Power Re Sys & Procedures for Accident Mitigation ML20154K0101988-09-19019 September 1988 Safety Evaluation Supporting Util 840309,850621 & 860606 Responses to Generic Ltr 83-28, Required Actions Based on Generic Implication of Salem ATWS Events, Items 3.1.1, 3.1.2,3.2.1,3.2.2 & 4.5.1 ML20154F4031988-09-14014 September 1988 Safety Evaluation Supporting Request to Operate Facility at 25% Power Re Safety of Prolonged Operation at 25% Power ML20154F3951988-09-14014 September 1988 Safety Evaluation Supporting Request to Operate Facility at 25% Power Re Accident Evaluation ML20154F3921988-09-14014 September 1988 Safety Evaluation Supporting Request to Operate Facility at 25% Power Re Sys & Procedures for Accident Mitigation ML20154R9391988-05-31031 May 1988 Safety Evaluation Supporting Plant Primary Property Damage Insurance Exemption ML20236F7141987-10-19019 October 1987 Safety Evaluation Supporting Amend 8 to License NPF-36 ML20234B8201987-09-14014 September 1987 SER on Util 830414,851023 & 860227 Responses to Generic Ltr 82-33 Re post-accident Monitoring Instrumentation Meeting Requirements of Reg Guide 1.97 as Applied to Emergency Response Facility ML20237G4701987-08-14014 August 1987 Safety Evaluation Supporting Amend 7 to License NPF-36 ML20214K3961987-05-18018 May 1987 Safety Evaluation Supporting Amend 6 to License NPF-36 ML20215M4181987-05-0404 May 1987 Safety Evaluation Supporting Amend 5 to License NPF-36 ML20211N5921986-12-0909 December 1986 Safety Evaluation Supporting Amend 4 to License NPF-36 ML20213D5001986-11-0303 November 1986 Safety Evaluation Supporting Amend 3 to License NPF-36 ML20205E0601986-08-0101 August 1986 SER of Tdi Owners Group Program to Validate & Upgrade Quality of Tdi Diesel Generators for Nuclear Emergency Standby Svc.Technical Solution Available to Address Problem ML20154L9801986-03-0404 March 1986 Safety Evaluation Supporting Amend 2 to License NPF-36 ML20138N6701985-12-0606 December 1985 Safety Evaluation Supporting Amend 1 to License NPF-36 ML20058E1851982-07-15015 July 1982 Safety Evaluation Supporting Order Extending Const Completion Date to 830331 1993-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20140G4481997-05-0101 May 1997 Part 21 Rept Re Potential Defect in Component of Dsrv & Dsr Enterprise Standby Diesel Generator Sys.Recommends That Springs Be Inspected on Periodic Basis,Such as During Refueling Outages ML20135D8011996-11-26026 November 1996 Part 21 Rept Re Two Safety Related Valves Supplied by Velan Valve Corp Were Not in Compliance W/Originally Supplied QA Documentation.Returned Valves to Velan in May 1996 & on 961120 Velan Advised That Valves Had Been Misplaced ML20080G4691995-01-26026 January 1995 Record of Telcon W/Nrc & Licensees 950126 to Clarify Position Re Dispositioning of Exempt Sources Listed in Section 6.3.3 of Shoreham Termination Survey Final Rept Dtd Oct 1994 ML20069F0001994-01-24024 January 1994 Vols 1-4 to Shoreham Decommissioning Project Termination Survey Final Rept ML20058K3841993-12-0909 December 1993 Part 21 Rept Re Potential Defect in Component of Dsrv & Dsr Enterprise Standby DG Sys,Regarding Potential Problem W/ Subcover Assembled Atop Power Head ML20057F2261993-09-30030 September 1993 Safety Evaluation Supporting Exemption Request from Requirements of 10CFR50.54(q) for License NPF-82 ML20056C7181993-07-14014 July 1993 SE Supporting Amend 10 to License NPF-82 ML20045B3551993-06-11011 June 1993 LER 93-001-00:on 930429,refueling Jib Crane Moved in Vicinity of Spent Fuel Pool Using vendor-supplied Lifting Eye in Violation of NUREG-0612.Caused by Failure to Identify Crane as Heavy Load.Meetings held.W/930611 Ltr ML20045C8881993-06-0808 June 1993 Vols 1 & 2 to Refueling Jib Crane 1T31-CRN-008A Incident Root Cause Analysis. W/One Oversize Encl ML20044C1181993-02-28028 February 1993 Shoreham Nuclear Power Station Updated Decommissioning Plan. ML20128P6451993-02-28028 February 1993 Snps Decommissioning Project Termination Survey Final Rept for Steam Turbine Sys (N31) ML20128P7431993-02-19019 February 1993 Rev 3 to 93X027, Nuclear QA Surveillance Rept ML20127H2301993-01-15015 January 1993 Part 21 Rept Re Potential Defeat in Component of Dsrv & Dsr Enterprise Standby DG Sys.Starting Air Distributor Housing Assemblies Installed as Replacement Parts at Listed Sites ML20126B0421992-12-17017 December 1992 Final Part 21 Rept Re Potential Problem W/Steel Cylinder Heads.Initially Reported on 921125.Caused by Inadequate Cast Wall Thickness at 3/4-inch-10 Bolt Hole.Stud at Location Indicated on Encl Sketch Should Be Removed ML20125C7161992-12-0707 December 1992 Part 21 Rept Re Possibility for Malfunction of Declutching Mechanisms in SMB/SB-000 & SMB/SB/SBD-00 Actuators. Malfunction Only Occurs During Seismic Event.Balanced Levers May Be Purchased from Vendor.List of Affected Utils Encl ML20127P5861992-11-23023 November 1992 Followup to 921005 Part 21 Rept Re Potential Defect in SB/SBD-1 Housing Cover Screws.Procedure Re Replacement of SBD-1 Spring Cover Bolts Encl.All Fasteners Should Be Loosened & Removed.List of Affected Utils Encl ML20128B9641992-10-31031 October 1992 Rev 0 to Shoreham Decommissioning Project Termination Survey Plan ML20118B4391992-09-11011 September 1992 Part 21 Rept Re Degradation in Abb Type 27N Undervoltage Relays Used in Electrical Switchgear.Recommends That Users Review Applications Requiring Exposures Greater than 1E03 Rads TID W/Time Delay Function Option ML20099H5781992-07-31031 July 1992 Rev 4 to Shoreham Defueled Sar ML20114A6311992-07-28028 July 1992 Shoreham Decommissioning Plan ML20101K5791992-06-25025 June 1992 Long Island Power Authority Shoreham Decommissioning Project,Shoreham Nuclear Power Station,Technical Rept on Water Processing & Water Mgt Activities for Reactor Pressure Vessel & Wet Cutting Station ML20094L1271992-03-13013 March 1992 Amend 1 to Part 21 Rept 159 Re Potential Defect in Power Cylinder Liner.Initially Reported on 920115.Caused by Liner/ Block Fit & Localized Matl Microstructure.All Drawings & Specs Revised to Address Matl Design Requirements ML20082M5081991-08-26026 August 1991 Rev 3 to Shoreham Defueled Sar PM-91-125, Monthly Operating Rept for Jul 1991 for Shoreham Nuclear Power Station1991-07-31031 July 1991 Monthly Operating Rept for Jul 1991 for Shoreham Nuclear Power Station PM-91-112, Monthly Operating Rept for Jun 1991 for Shoreham Nuclear Power Station1991-06-30030 June 1991 Monthly Operating Rept for Jun 1991 for Shoreham Nuclear Power Station PM-91-075, Monthly Operating Rept for Apr 1991 for Shoreham Nuclear Power Station1991-04-30030 April 1991 Monthly Operating Rept for Apr 1991 for Shoreham Nuclear Power Station ML20024G7171991-04-22022 April 1991 LER 91-001-00:on 910324,RB Normal Ventilation Sys (Rbnvs) Outboard Exhaust Valve Closed for No Apparent Reason.Cause Inconclusive.Sys Restored to Normal Lineup & Rbnvs Outboard Valve Will Be Stroked on Routine basis.W/910422 Ltr SNRC-1806, Revised Pages 2 & 6 to Encl a of 10CFR50.59 Annual Rept for 19901991-04-15015 April 1991 Revised Pages 2 & 6 to Encl a of 10CFR50.59 Annual Rept for 1990 PM-91-058, Monthly Operating Rept for Mar 1991 for Shoreham Nuclear Power Station1991-03-31031 March 1991 Monthly Operating Rept for Mar 1991 for Shoreham Nuclear Power Station PM-91-037, Monthly Operating Rept for Feb 1991 for Shoreham Nuclear Power Station1991-02-28028 February 1991 Monthly Operating Rept for Feb 1991 for Shoreham Nuclear Power Station PM-91-016, Monthly Operating Rept for Jan 1991 for Shoreham Nuclear Power Station1991-01-31031 January 1991 Monthly Operating Rept for Jan 1991 for Shoreham Nuclear Power Station SNRC-1797, 10CFR 50.59 Annual Rept of Facility Changes,Procedure Changes,Tests & Experiments for Jan-Dec 19901990-12-31031 December 1990 10CFR 50.59 Annual Rept of Facility Changes,Procedure Changes,Tests & Experiments for Jan-Dec 1990 SNRC-1794, Shoreham Nuclear Power Station Annual Operating Rept,19901990-12-31031 December 1990 Shoreham Nuclear Power Station Annual Operating Rept,1990 SNRC-1799, Lilco 1990 Annual Rept1990-12-31031 December 1990 Lilco 1990 Annual Rept ML20069Q3901990-12-31031 December 1990 Shoreham Nuclear Power Station Decommissioning Plan. (Filed in Category P) ML20028H0231990-09-28028 September 1990 LER 90-007-00:on 900907,unplanned Actuation of ESF Sys Occurred During I&C Surveillance Test.Caused by Inadequate procedure.SP44.650.16 Revised to Require That Leads Lifted & Individually separated.W/900928 Ltr ML20056A2001990-07-31031 July 1990 Safety Evaluation Supporting Amend 6 to License NPF-82 PM-90-097, Monthly Operating Rept for June 1990 for Shoreham Nuclear Power Station1990-06-30030 June 1990 Monthly Operating Rept for June 1990 for Shoreham Nuclear Power Station ML20055E3911990-06-25025 June 1990 Safety Evaluation Supporting Amend 5 to License NPF-82 PM-90-083, Monthly Operating Rept for May 1990 for Shoreham Nuclear Power Station1990-05-31031 May 1990 Monthly Operating Rept for May 1990 for Shoreham Nuclear Power Station 05000322/LER-1987-0351990-05-16016 May 1990 LER 87-035-02:on 871221,880106 & 0330,high Energy Line Break Logic Isolations of RWCU & Main Steam Line Drain Valves Occurred.Caused by Problems W/Temp Monitoring Units. Grounding Scheme Changed & Transformers Rewired 05000322/LER-1986-0321990-05-16016 May 1990 LER 86-032-01:on 860728,RWCU Isolated on High Differential Flow Sensed by Steam Leak Detection Sys While Placing Filter Demineralizers in Operation.Cause Not Determined. Operating Procedures Revised to Monitor RWCU Sys 05000322/LER-1987-0091990-05-16016 May 1990 LER 87-009-01:on 870203,full Reactor Trip Occurred Due to Perturbation in Ref Leg.Caused by Spurious Low Level Reactor Pressure Vessel Water Level Signal.Existing Level & Pressure Transmitters Replaced W/Newer Models 05000322/LER-1989-0031990-05-16016 May 1990 LER 89-003-01:on 890310,emergency Diesel Generator (EDG) 102 Manually Shutdown During 18-month Surveillance Test Due to Failure of EDG Output Breaker.Cause Not Determined. Replacement Breaker Installed in Cubicle 102-8 05000322/LER-1985-0591990-05-16016 May 1990 LER 85-059-01:on 851219,half Reactor Trip,Full NSSS Shutoff Sys Isolation & Reactor Bldg Standby Ventilation Sys Initiation Occurred Due to Loss of Power to Reactor Protection Sys Bus B.Assembly Breaker Reset 05000322/LER-1988-0151990-05-16016 May 1990 LER 88-015-02:on 880916,seismic Monitoring Instrumentation, Including Peak Acceleration Recorders,Removed from Svc for More than 30 Days Due to Corrosion on Scratch Plates.Cover Gasket Replaced & Thermal Barrier Mount to Be Installed 05000322/LER-1988-0031990-05-16016 May 1990 LER 88-003-01:on 880322,unplanned Automatic Initiation of Reactor Bldg Standby Ventilation Sys Side a Occurred During Deenergization of Relay.Caused by Close Placement of Relay Terminals.Wiring Inside Electrical Panels Reworked 05000322/LER-1986-0141990-05-16016 May 1990 LER 86-014-01:on 860305,full Reactor Trip Occurred Due to Momentary False Low Vessel Level Signal,Causing Hydraulic Pressure Spike in Ref Leg A.Bourton Tube Type Pressure Transmitter Replaced W/Rosemount Model 1153 05000322/LER-1987-0121990-05-16016 May 1990 LER 87-012-01:on 870504,uplanned Actuation of ESF Occurred. Caused by Technician Loosing Footing & Accidently Hitting Outside Cover of Level Switch.Permanent Ladders & Platforms Installed at Head Tank Level Switches 05000322/LER-1988-0171990-05-16016 May 1990 LER 88-017-01:on 881025,discovered That Seismic Monitoring Instrumentation Returned to Svc Prior to Verifying Sys Operability & Special Rept Not Written.Caused by Personnel Error.Surveillance Engineer Reassigned 1997-05-01
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NUCLEAR REGULATORY COMMISSION WASHINGTON, D. C. 20555 l
SAFETY EVALUATION BY THE OFFICE OF NUCLEAR REACTOR REGULATION SUPPORTING AMENDMENT NO. 5 TO FACILITY OPERATING LICENSE NO. NPF-36 LONG ISLAND LIGHTING COMPANY SHOPEHAM NUCLEAR POWER STATION DOCKET NO. 50-322 1.0 INTWDUCTION By letter dated January 21, 1987 (Ref. 1), LILCo the licensee for Shoreham Nuclear Power Station, proposed a change to the Technical Specifications (TS). The main purpose of this change is to reduce challenges to the safety relief valves (SRVs). This would be accomplished by changing the water level setpoint for closure of the main steam isolation valves (MSIVs) and main steam line drain valves (MSLDVs) from level 2 to the lower Level 1. The probability of closing a MSIV due to variation of water level following a r ram would thus be reduced. With the MSIVs open and the main condenser available, prime mover steam for the reactor feed pump turbines will also remain available to allow continued operation of the condensate and main feedwater sys'.em. This will aid in water level recovery before the low level isolation setpoint is reached.
! Should level I be reached, MSIV closure will cause reactor pressure to rise causino the SRVs to open and discharge to the suppression pool. The new heat l load for the suppressier pool will be reduced by the amount of heat picked up l by the main condenser while the level is dropping from level 2 to Level 1.
l l 2.0 EVALUATION The licensee's request to lower the water level trip setpoint for MSIV closure is consistent with staff solutions for NUREG-0737. Item II.K.3.16 " reduction l of challenges and failures of relief valves". In addition, the General l Electric Information Letter, SIL No. 367, also reconnends the lower trip i
setpoint. The staff evaluation of the change in setpoint is discussed below.
2.1 Loss of Coolant Accident (LOCA) and Main Steam Line Break (MSLB) o LOCA The present limiting LOCA is based on the time the hot node remains uncovered. The area corresponding to the break is 85% of the design basis accident (DBA). To justify the setpoint change, LOCA analyses for the 85% DBA, with a staff approved ECCS code was perfonned. The licensee stated that with
! the MSIV isolation occurring at Level 1, and other paraneters unchanged, there I was no change in the peak cladding temperature (FCT) or the total core area i
8705130227 870504 PDR ADOCK 05000322 P PDR
uncovered when compared with MSIV isolation at Level 2. With the new level setpnint, the MSIV remained open for three seconds longer than with closure at level 2. The licensee stated that the resulting additional percentage loss of reactor coolant due to the longer closure time is negligible. This is acceptable to the staff since there is no significant change from previous analyses.
For a small break LOCA there is a potential of initiation of MSIV closure at the proposed lower level setpoint. The licensee stated that based on plants similar to Shoreham, there is an increase of about 30 F for a limiting PCT of 1500* F. It was concluded that for this event, the change on the margin of safety was insignificant. We find this acceptable.
o MSLB MSLB was nnt analyzed. Presently, for this event, MSIV isolation occurs prior to Level 2 and closure is initiated by signals other than water level. We find this acceptable since lower level setpoint will not effect the existing MSLB results.
2.2 Abnonnal Operational Transients The transient event for loss of feedwater flow would be affected by the change in the MSIV isolation setpoint from Level 2 to Level 1. This abnonnal operation transient was analyzed. The licensee stated the following:
- a. RCIC and HPCI systers which are initiated at Level 2. keep the water above Level 1.
- b. The pressurization that occurs with isolation at Level 2 does not occur.
This is acceptable to the staff since there is no adverse effect with regard i to safe reactor operation.
3.0 TECHNICAL SPECIFICATION (TS) CHANGES We have reviewed the following TS changes:
TABLE 3.3.2-1 for isolation actuation instrumentation TABLE 3.3.?-2 for isolation actuation instrumentation setpoints TABLE 3.3.2-3 for isolation system instrumentation respense time l TABLE 4.3.2.1-1 for isolation actuation instrumentation surveillance recuirements Bases for figure E 3/4 3-1 for reactor vessel water levels We conclude that the proposed changes are acceptable.
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4.0 ENVIRONMENTAL CONSIDERATION
This amendment relates to changes .in requirements with respect to the instal-lation or use of a facility component located within the restricted area as *
' defined in Part 20. The staff has determined that the amendment involves no significant increase in the amounts, and no significant change in the types, of any effluents that may_be released offsite, and that there.is no sienificant increase in. individual or cumulative occupational radiation exposure. The-Commission has previously issued a proposed finding that this amendment involves no significant hazards consideration and there has been no public comment on such finding. Accordingly, this amendment meets the eligibility criteria for
- categorical exclusion set forth in 10 CFR 51.22(c)(9). Pursuant to 10 CFR 51.22(b), no environmental impact statement nor environmental assessment need be prepared in connection with the issuance of this amendment.
5.0 CONCLUSION
We have reviewed and found acceptable, for the reasons discussed above, the licensees justification for the proposed TS changes to . lower the water level setpoint for the MSIVs and MSLDVs from level 2 to Level 1.
The staff has concluded, based on the considerations discussed above, that:
(1) there is reasonable assurance that the health and safety of the cublic will not be endangered by operat'on in the proposed manner, and (2) such activities will be conducted in compliance with the Commission's regulatiors, and the issuance of this amendment will not be inimical to the common defense and the security or to the health and safety of the public.
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Principal Contributor: D. Katze >
s Dated: May 4, 1987