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05000293/FIN-2018003-012018Q3PilgrimFailure to Identify an Adverse Condition Associated with Elevated Standby Gas Treatment System Accumulator LeakageThe inspectors identified a Green non-cited violation (NCV) of Technical Specifications 3.7.B.1.c because Entergy exceeded the TS allowed outage time for the standby gas treatment system (SBGT) when the station did not identify an adverse condition associated with elevated air accumulator leakage in the system.
05000333/FIN-2018002-012018Q2FitzPatrickLicensee-Identified Violation

This violation of very low safety significance was identified by Exelon and has been entered into Exelons CAP and is being treated as an NCV, consistent with Section 2.3.2 of the Enforcement Policy

Violation: 10 CFR 71.5 requires that licensees who transport licensed material comply with the applicable requirements of the Department of Transportation (49 CFR). 49 CFR 172.202(a)(1) and (a)(2) require that the shipping description on the shipping paper include the proper shipping name and identification number for the material. 49 CFR 172.302(a) requires that shipments in bulk packages be marked with the identification number. Contrary to the above, on July 12, 2016, the shipping description on the shipping paper for shipment JAF-2016-1613 from FitzPatrick to Tennessee did not include the proper shipping name and identification number for the material. Exelon identified the error during a subsequent review of the shipping paperwork. Significance/Severity Level: No examples of transportation issues are presented in IMC 0612, Appendix E (Examples of Minor Issues). IMC 0609, Appendix D, Section VII.C.e.1 lists examples of Green findings that include documentation deficiencies including failure to properly document compliance with 49 CFR requirements such as shipping papers. Corrective Action Reference: Exelon placed this issue into its CAP as CR-JAF-2016-02857. Corrective actions included providing a corrected shipping paper to the facility in Tennessee that had received the package.
05000354/FIN-2018001-012018Q1Hope CreekImplementing Procedures for Beyond Design Basis FLEX Mitigating Strategies Not FollowedA Green finding was identified by the inspectors for multiple examples of PSEG not following the station specific procedures that implement the Salem and HCGS Final Integrated Plans for Beyond Design Basis Diverse and Flexible Coping Strategies (FLEX) Mitigating Strategies, EM-SA-100-1000 and EM-HC-100-1000, respectively. Specifically, since compliance with the FLEX order was met on November 10, 2016, PSEG did not follow the common PSEG fleet preventive maintenance (PM) process and diesel fuel oil testing program procedures, MA-AA-716-210, CY-AB-140-410, and SC.OP-LB.DF-0001 for the annual fuel oil sampling of FLEX equipment. In addition to this, between December 6, 2017, and March 8, 2018, PSEG did not follow site specific procedures for FLEX equipment unavailability and mitigation capability protection in accordance with the HCGS and Salem procedures, OP-HC-108-115-1001 and OP-SA-108-115-1001, Operability Assessment and Equipment Control Program, respectively.
05000247/FIN-2018001-012018Q1Indian PointFailure to Incorporate Adequate Test Controls for Quarterly Stroke Close Testing of the Steam Supply Valves to Turbine-Driven Auxiliary Feedwater PumpThe inspectors identified a Green NCV of 10 CFR Part 50, Appendix B, Criterion XI, Test Control, when Entergy did not assure that surveillance tests required to demonstrate that structures, systems, and components will perform satisfactorily in service are identified and performed in accordance with written test procedures which incorporate the requirements and acceptance limits contained in applicable design documents. Specifically, during quarterly stroke testing of the steam isolation valves to the 22 turbine-driven auxiliary feedwater pump, PCV-1310A and PCV-1310B, Entergy did not ensure that these valves traveled to the closed position as required to verify that the safety function was met.
05000354/FIN-2018001-022018Q1Hope CreekConcern Regarding As-Found Values for Safety Relief Valve Lift Setpoints Exceed Technical Specification Allowable LimitOn October 22, 2016, PSEG staff received results that the as-found setpoint tests for the main steam SRV pilot stage assemblies had exceeded the lift setting tolerance prescribed in technical specification 3.4.2.1. Specifically, ten of the 14 pilot stage assemblies tested experienced drift beyond the +/- 3 percent tolerance permitted by technical specification3.4.2.1. PSEG staff concluded that the cause of the setpoint drift was attributed to corrosion bonding between the pilot disc and seating surfaces, and that is consistent with industry experience. This condition was reportable under 10 CFR 50.73(a)(2)(i)(B) as any operation or condition which was prohibited by the plants technical specifications. Based on a review of the Cycle 20 test results of the main steam SRV pilot stage assembly setpoint tests, and the nature of the predominant failure mechanism (corrosion bonding), the inspectors concluded that an unacceptable number (greater than one) of SRVs likely and reasonably became inoperable at some indeterminate time during the operating cycle. As documented in Inspection Results, 71152, Observations in this report, there is a history of SRV lift setpoint test failures due to a long-standing, generic issue with Target Rock 2-stage SRVs. In particular, PSEG staff has been active with the Boiling Water Reactor Owners Group in evaluating SRV setpoint drift issues, and has an auditable history of their implementation of corrective actions, specifically intended to address their chronic SRV setpoint drift issue. Notwithstanding their efforts, PSEG staff has been unsuccessful in realizing an improvement in SRV performance in this area. PSEG staff has elected to implement additional corrective actions beginning the spring 2018 refueling outage. Specifically, they plan to reinstitute platinum coating of the pilot valve disc, and they plan to install the recently redesigned 3-stage Target Rock SRV in a phased approach.While this issue has not been effectively resolved, PSEGs post-test evaluations have demonstrated that, in their as-found condition, the SRVs would have satisfactorily performed their intended safety function (i.e.,mitigating the consequences of a postulated accident); and therefore, was of low safety significance.Additional NRC review is necessary to determine the appropriateness of PSEGs corrective actions to date, given the corrective action options available, and whether there was an associated violation of NRC requirements in addition to the consequential violation of technical specification 3.4.2.1. Planned Closure Actions: The NRC is continuing a review of the generic issue with the 2-stage Target Rock SRVs and the associated safety significance. The results of this review will be considered in determining the appropriateness of PSEGs corrective actions to date and whether an associated violation of NRC requirements existed, as well as the characterization of the consequential violation of technical specification 3.4.2.1.PSEG Actions: Specific to the fall 2016 SRV lift setpoint test results, all 14 of the SRVs were refurbished and adjusted as necessary; and were all tested and demonstrated to meet the required +/- 1 percent as-left tolerance prior to installation. PSEG also planned additional corrective actions, to be implemented during the spring 2018 refueling outage, including: 1) to re-evaluate the platinum coating process of the pilot valve disc for the existing 2-stage SRVs, and 2) to procure and install the recently re-designed 3-stage Target Rock SRV in a phased approach. Finally, PSEG communicated with the SRV vendor concerning the re-design of the 3-stage SRV following a prior identification (May 2015) of a substantial safety hazard to ensure that the re-design addressed the identified problems.Corrective Action References: Notification/Order 20747318, 20772038, and 80110848 This review closes LER 05000354/2016-003 and Supplemental LER 05000354/2016-003-01
05000286/FIN-2018001-022018Q1Indian PointInadequate Procedure for Placing Chemical and Volume Control System Demineralizer In ServiceA self-revealing Green NCV of Technical Specification 5.4.1, Procedures, was identified because Entergy failed to provide adequate guidance in 3-SOP-CVCS-004, Placing the CVCS Demineralizers In or Out of Service. Specifically, Entergy did not provide adequate procedural direction to prevent exceeding the reactor coolant filter differential pressure while placing the demineralizers in service. As a result, the pressurizer water level technical specification limit was exceeded and the CVCS piping upstream of the filter was over-pressurized resulting in diaphram ruptures on valves CH-305 and CH-352 thereby spreading contamination throughout the Primary Auxiliary Building.
05000220/FIN-2017004-052017Q4Nine Mile PointLicensee-Identified ViolationThe following violation of very low safety significance (Green) was identified by Exelon and is a violation of NRC requirements which meets the criteria of the NRC Enforcement Policy for being dispositioned as a NCV. Title 10 CFR 50.65(a)(4) requires, in part, ...the licensee shall assess and manage the increase in risk that may result from the proposed maintenance activities. Exelon procedure WC-AA-101-1006, On-Line Risk Management and Assessment, Revision 001, Section 4.1.3, states to consider work activities that cause equipment to be unavailable (e.g., trains of systems) for assessment of risk under the requirements of 10 CFR 50.65(a)(4). Contrary to the above, on October 17, 2017, Exelon identified a discrepancy in PARAGON (risk software) that resulted in an improper risk assessment for the days planned work. Review and correction of the error resulted in an elevated risk condition of Yellow during Nine Mile Point Unit 1, 11 feedwater pump (FW) maintenance. This performance deficiency was determined to be more than minor because it adversely affected the human performance attribute of the Mitigating Systems cornerstone and affected cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, on October 17, 2017, Exelon identified a planned activity that resulted in an unplanned Yellow risk activity during planned maintenance of the 11 FW pump. In addition, IMC 0612, Appendix E, Examples of Minor Issues, under Section 7, Maintenance Rule, Example E for inadequate risk assessment states in part that a more-than-minor issue would put the plant into a higher licensee-established risk category. The finding was evaluated using IMC 0609, Appendix K, Maintenance Risk Assessment and Risk Management Significance Determination Process. The finding was determined to affect the overall plant risk with the 11 FW Pump being out of service for maintenance with PARAGON not elevating the overall plant risk from green to yellow. The risk deficit was elevated and determined to not be greater than 1E-6 event per year for Incremental Core Damage Probability Differential and not greater than 1E-7 events per year for Incremental Large Early Release Probability Differential. Therefore, the finding was determined to be of very low safety significance (Green). Exelon entered this issue into its CAP as IR 04064241.
05000410/FIN-2017004-042017Q4Nine Mile PointIneffective Correction Action Results in Failure of Instrument Air SystemThe inspectors documented a self-revealing Green finding (FIN) of CNG-CA-1.01-1000, Corrective Action Program, Revision 01100, because Nine Mile Point Nuclear Station (NMPNS) failed to implement corrective actions at NMPNS Unit 2 to remove and replace all un-annealed red brass piping for the instrument air system during the April 2008 refueling outage. Specifically, on July 13, 2017, Unit 2 experienced a rupture of un-annealed red brass instrument air pipe which resulted in a feedwater pump trip and a reactor recirculation pump runback to 49 percent. Exelons corrective actions for the July 13, 2017 failure of un-annealed red brass instrument air piping included wrapping the instrument air piping with a material that both supports the piping and prevents potential stress corrosion cracking. Exelon has developed work orders to replace the piping in the upcoming outage in spring 2018. Exelon also improved staff training for accountability and work checking to verify that generated work orders are completed and closed out. Exelon entered this issue into the corrective action program (CAP) as issue report (IR) 04031685, and performed a corrective action program evaluation (CAPE). This finding is more than minor because it is associated with the design control attribute of the Initiating Events cornerstone and affected the cornerstone objective of limiting the likelihood of those events that upset plant stability and challenge critical safety functions during power operations. Specifically, NMPNS staff failed to complete corrective actions to replace Unit 2 un-annealed red brass instrument air piping, which was susceptible to stress corrosion cracking, resulting in a feedwater pump trip and a reactor recirculation runback to 49 percent on July 13, 2017. The inspectors evaluated the finding using IMC 0609, Attachment 4, Initial Characterization of Findings, issued on October 7, 2016, and Exhibit 1 of IMC 0609, Appendix A, The Significance Determination Process for Findings At-Power, issued June 19, 2012. The inspectors determined that the finding was of very low safety significance (Green) because it did not result in the complete or partial loss of a support system that contributes to the likelihood of, or cause, an initiating event and affected mitigation equipment. The inspectors determined that this finding did not have a cross-cutting aspect because the performance deficiency occurred greater than 3 years ago; therefore, it is not considered to be indicative of current plant performance.
05000410/FIN-2017004-032017Q4Nine Mile PointInadequate Operability Determination forImpairedInternal Flood BarrierAn NRC-identified Green NCV of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, was identified when Exelon failed to perform an adequate operability determination in accordance with OP-AA-108-115, Operability Determinations, Revision 20, upon identification of Unit 2 degraded internal flood barriers that support operability of emergency core cooling system (ECCS) equipment. Specifically, from November 21 until December 10, 2017, Exelon failed to properly evaluate the excavation of internal flood barriers and concluded there was a reasonable expectation for operability of the supported ECCS systems. Exelon entered this issue into the CAP as IR 04082686. Corrective actions included conducting a detailed evaluation of operability for the supported safety-related systems, additional training associated with TS 3.0.9, including a focus on the need for risk assessments when entering TS 3.0.9, and a procedure change to CC-AA-201, Plant Barrier Control Program, and CC-NM-201-1001, Plant Barrier Control Program Implementation, which is the NMPNS specific procedure to address the vulnerabilities associated with impairing multiple required barriers. This finding is more than minor because it is associated with the human performance attribute of the Mitigating Systems cornerstone and affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, from November 21 until December 10, 2017, Exelon failed to adequately evaluate the operability of a degraded internal flooding barrier and the potential impact on operability of the supported ECCS system equipment. The inspectors identified that the internal flood barrier was excavated such that there was not sufficient material to ensure adequate flood protection, and resulted in a reasonable doubt for the operability of the supported ECCS systems. This finding is also similar to example 3.j and 3.k of IMC 0612 Appendix E, Examples of Minor Issues, issued August 11, 2009, because the condition identified by the inspectors resulted in a reasonable doubt for the operability of the ECCS supported systems and additional analysis was necessary to verify operability. In accordance with IMC 0609.04, Initial Characterization of Findings, and Exhibit 2 of IMC 0609, Appendix A, The Significance Determination Process for Findings At-Power, issued June 19, 2012, the inspectors determined that the finding was of very low safety significance (Green), because the finding was not a design or qualification deficiency, did not represent a loss of system safety function, and did not screen as potentially risk significant due to vulnerability to external initiating events. This finding has a cross-cutting aspect in the area of Human Performance, Work Management, because Exelon failed to implement a process of planning, controlling, and executing work activities such that nuclear safety is the overriding priority. As a result, Exelon personnel failed to recognize that work activities that impaired internal flood barriers on both Division I and II low pressure ECCS pump rooms were executed simultaneously, which led to an unplanned entry into TS Limiting Condition for Operation (LCO) 3.0.9. (H.5)
05000220/FIN-2017004-022017Q4Nine Mile PointInadequate Fill and VentProcedure for Control Room Chiller Results in Unplanned LCO EntryAn NRC-identified Green NCV of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, was identified for Exelons failure to ensure that activities affecting quality were prescribed in a manner appropriate to the circumstances for the Unit 1 control room chiller system. Specifically, Exelon procedure N1-OP-49, Control Room Ventilation System, Revision 03800, Section H.5, Venting of Control Room Chiller Circulating Water Pump 11 and 12 Discharge Piping, led personnel to inadequately fill and vent the 12 control room chiller during system restoration from maintenance, while in a single chiller lineup. As a result, on October 15, 2017, control room chiller 12 tripped on low flow, and due to a prior trip of 11A control room chiller compressor, an unplanned 7-day LCO in accordance with TS 3.4.5.e, Control Room Air Treatment System, was entered due to an insufficient number of available chiller compressors to provide adequate control room cooling. Exelon entered this issue into the CAP as IR 04090200. Corrective actions included generating a procedure change to correct N1-OP-49 Section H.5, which provides instruction for filling and venting when in a single chiller lineup This finding is more than minor because it is associated with the procedure quality attribute of the Barrier Integrity cornerstone and adversely affected the cornerstone objective of providing reasonable assurance that physical design barriers protect the public from radionuclide releases caused by accidents or events. Specifically, Exelon failed to prescribe an adequate fill and vent procedure for the Unit 1 control room chillers which led to a trip of the 12 chiller on low flow while troubleshooting of chiller compressor 11A was on-going, resulting in an unplanned TS LCO entry. The inspectors evaluated this finding using IMC 0609.04, Initial Characterization of Findings, and Exhibit 3 of IMC 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power. The performance deficiency did not represent a degradation of the radiological barrier function provided for the control room. Additionally, the performance deficiency did not represent a degradation of the barrier function of the control room against smoke or a toxic atmosphere. Therefore, this finding was determined to be of very low safety significance (Green). This finding has a cross-cutting aspect in the area of Problem Identification and Resolution, Evaluation, because between 2014 and 2017 the inspectors noted over 20 issue reports documenting issues affecting reliability of the control room chiller system. Exelon failed to thoroughly evaluate the issues associated with the chillers to ensure that resolutions address causes and extent of conditions commensurate with their safety significance. Specifically, Exelon failed to effectively evaluate previous chiller trips and to prevent additional trips of the chiller system such as the one that occurred on October 15, 2017. (P.2) (Section 1R12.b.2)
05000220/FIN-2017004-012017Q4Nine Mile PointMain Control Room Annunciators 10 CFR 50.65(a)(2) Demonstration Not MetAn NRC-identified Green non-cited violation (NCV) of Title 10 of the Code of Federal Regulations (10 CFR) 50.65 (a)(2), was identified because Exelon did not adequately demonstrate that the performance of the Unit 1 main control room (MCR) annunciators was effectively controlled through performance of appropriate preventive maintenance. Specifically, Exelon did not identify and properly account for functional failures of the MCR annunciators in June 2017, and therefore did not recognize that the annunciator system exceeded its performance criteria and required a Maintenance Rule (a)(1) evaluation. On December 7, 2017, Exelon entered the issue into their CAP as IR 04081698 and performed a review of the events identified by the inspectors that were applicable to the maintenance rule annunciator system. Corrective actions included Exelon determining that the events were functional failures, and initiated an (a)(1) evaluation based on the MCR annunciator system functional failures exceeding the designated performance criteria of an allowable one functional failure per 24 months.This finding is more than minor because it is associated with the equipment performance attribute of the Mitigating Systems cornerstone and affects the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences (i.e. core damage). Specifically, following the two failures of the main control annunciator panel in June 2017, Exelon did not identify the failures as functional failures, and consequently, did not establish goals and monitoring criteria in accordance with 10 CFR 50.65(a)(1). In accordance with IMC 0609.04, Initial Characterization of Findings, and Exhibit 2 of IMC 0609, Appendix A, The SDP for Findings At-Power, issued June 19, 2012, the inspectors determined that the finding was of very low safety significance (Green) because the finding did not affect the design or qualification of a mitigating structure, system, or component (SSC), did not represent a loss of system and/or function, did not involve an actual loss of a function of at least a single train or two separate safety systems for a greater time than allowed by technical specifications (TS), and did not represent an actual loss of function of one or more non-TS trains of equipment designated as high safety-significant in accordance with the licensees maintenance rule program. T his finding has a cross-cutting aspect in the area of Human Performance, Consistent Process, in that Exelon failed to use a consistent, systematic approach to make decisions. Specifically, Exelon did not ensure their review process for issues entered into the CAP was effectively implemented to ensure proper evaluations for all applicable maintenance rule systems affected by a n SSC failure. (H.13)