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 Start dateReporting criterionTitleEvent descriptionSystemLER
ENS 5407822 May 2019 06:56:0010 CFR 50.72(b)(3)(v)(A), Loss of Safety Function - Shutdown the Reactor
10 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual Heat
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Technical Specification Required Shutdown

On 5/22/2019, the 'A' Control Structure Chiller (Div I) tripped due to a loss of (motor control center) MCC 0B136. The 'B' Control Structure Chiller was already inoperable due to Div II (Emergency Service Water) ESW being out of service for planned maintenance. With the loss of Control Structure HVAC System the ability to maintain temperatures in various spaces including relay rooms, Control Room Floor Cooling and Emergency Switchgear rooms was lost. The 'B' Control Structure Chiller was restarted at 0251 EDT and cooling was reestablished to the required areas, however the 'B' chiller is not considered operable at this time. Units 1 and 2 entered (Technical Specification) TS 3.0.3 at 0256 EDT and a controlled shutdown of both units commenced, Unit 2 at 0340 EDT and Unit 1 0350 EDT. This constitutes a TS required shutdown and requires a 4 hour (Emergency Notification System) ENS notification in accordance with 10 CFR 50.72(b)(2)(i). The failure also requires an 8 hour ENS notification in accordance with 10 CFR 50.72(b)(3)(v) due to the loss of a safety function. The licensee needs to restore the 'B' loop of ESW to exit the Limiting Condition of Operation (LCO). The licensee is currently performing a flow surveillance, once complete and assuming the data is acceptable, the licensee will be able to exit the LCO. The units are in a normal electrical lineup. The licensee will be notifying the state of Pennsylvania FEMA Operations Center. The licensee has notified the NRC Resident Inspector.

  • * * UPDATE ON 05/22/2019 AT 1302 FROM SCOTT MYRTHEL TO THOMAS KENDZIA * * *

On 5/22/2019 at 0601 EDT Susquehanna Steam Electric Station reported a shutdown had been commenced at 0340 EDT for Unit 2 and 0350 EDT for Unit 1 due to inoperability of both control structure chillers. Power has been restored to MCC 0B136, and at 0901 EDT the 'A' control structure chiller was declared operable and LCO 3.0.3 was exited. Power reduction for both units was halted at 0901 EDT and preparations for power restoration initiated. As of 1255 EDT on 5/22/2019, Unit 1 power is 94% and Unit 2 power is 92%. Notified the R1DO (Arner).

HVAC
ENS 533103 April 2018 04:19:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialLoss of Secondary Containment Following Surveillance TestingOn April 3, 2018 at 0019 (EDT), the Susquehanna control room received indication that a loss of Secondary Containment Zone 3 differential pressure had occurred. Control room operators noted the loss following completion of surveillance testing. The cause is under investigation. Zone 3 differential pressure was restored to greater than 0.25 inches WC (water column) at 0145 (EDT). Zone 3 differential pressures being less than 0.25 inches WC constitutes a loss of Secondary Containment based on not meeting requirements of SR (Surveillance Requirement) 3.6.4.1.1. This event is being reported under 10 CFR 50.72(b)(3)(v)(C) and per the guidance of NUREG-1022, Revision 3, Section 3.2.7, as a loss of a Safety Function. There is no redundant Susquehanna Secondary Containment system. The NRC Resident Inspector has been notified.Secondary containment
ENS 5320212 February 2018 03:03:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialSecondary Containment Differential Pressure Out of SpecificationOn February 11, 2018 at 2203 (EST), the Susquehanna Control Room received indication that a loss of Secondary Containment Zone 2 differential pressure (DP) had occurred. Control Room operators noted a differential pressure of <.25" WC (inches Water Column) for several seconds. System DP was restored to normal in 1 minute. The cause of the pressure swings is under investigation. Zone 2 differential pressures being less than 0.25" WC constitutes a loss of Secondary Containment based on not meeting requirements of SR 3.6.4.1.1. This event is being reported under 10 CFR 50.72(b)(3)(v)(c) and per the guidance of NUREG 1022 Rev 3 section 3.2.7 as a loss of a Safety Function. There is no redundant Susquehanna Secondary Containment system. The licensee notified the NRC Resident Inspector.Secondary containment
ENS 5309830 November 2017 15:26:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialSecondary Containment Differential Pressure Briefly Indicated Outside of Tech Spec LimitOn November 30, 2017 at 1026 EST, the Susquehanna Control Room received indication that a loss of Secondary Containment Zone 2 differential pressure had occurred. Control Room operators noted a differential pressure of 0.0 inch WC (water column) for several seconds, followed by a high DP of 0.5 inch WC. System DP was restored to normal in 3 minutes. The cause of the pressure swings is under investigation. Zone 2 differential pressures being less than 0.25 inch WC constitutes a loss of Secondary Containment based on not meeting requirements of SR 3.6.4.1.1. This event is being reported under 10 CFR 50.72(b)(3)(v)(c) and per the guidance of NUREG 1022, Rev. 3, Section 3.2.7 as a loss of a Safety Function. There is no redundant Susquehanna Secondary Containment system. The licensee notified the NRC Resident Inspector.Secondary containment05000387/LER-2017-007
ENS 5297316 September 2017 17:30:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialLoss of Secondary Containment Differential PressureOn September 16th, 2017 at 1330 hrs. (EDT), a loss of secondary containment differential pressure (D/P) occurred due to an equipment failure. This caused a reduction in Reactor Building Zone 2 (Unit 2) D/P to less than the required 0.25 inches WC per SR (Surveillance Requirement) 3.6.4.1.1. 2V206B, Reactor Building Zone 2 Equipment Compartment Exhaust Fan, was manually started and Reactor Building Zone 2 D/P was restored to greater than 0.25 inches WC by 1333 hrs. Reactor Building Zone 1 (Unit 1) and Zone 3 (Units 1&2) ventilation remained in service and stable. This event is being reported under 10 CFR 50.72(b)(3)(v)(c) and per the guidance of NUREG 1022, Rev. 3, section 3.2.7, as a loss of a Safety Function. There is no redundant Susquehanna Secondary Containment system. The licensee has notified the NRC Resident Inspector.Secondary containment05000388/LER-2017-009
ENS 528929 August 2017 00:44:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialLoss of Secondary Containment Differential PressureOn August 8th, 2017 at 2044 hrs. (EDT) a loss of secondary containment differential pressure (D/P) occurred due to an apparent equipment failure. This caused a reduction in Reactor Building Zone II (Unit 2) D/P to less than the required 0.25 inch WC (water column) per SR (Surveillance Requirement) 3.6.4.1.1. Reactor Building Zone II Exhaust Fans were manually swapped and Reactor Building Zone II D/P was restored to greater than 0.25 inch WC by 2112 hrs. Reactor Building Zone 1 (Unit 1) and Zone 3 (Units 1&2) ventilation remained in service and stable. This event is being reported under 10 CFR 50.72(b)(3)(v)(c) and per the guidance of NUREG 1022 Rev 3 section 3.2.7 as a loss of a Safety Function. There is no redundant Susquehanna Secondary Containment system. The licensee notified the NRC Resident Inspector.Secondary containment
ENS 5284410 July 2017 06:50:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialLoss of Secondary Containment Due to Failure of Non-Safety Related Discharge DamperOn July 10th, 2017 at 0250 hrs. (EDT) a loss of secondary containment differential pressure (D/P) occurred due to failure of a non-safety related discharge damper associated with 2V205B Reactor Building Zone II Exhaust Fan. This caused a reduction in Reactor Building Zone II (Unit 2) D/P to less than the required 0.25 inches WC (Water Column). 2V205A Reactor Building Zone II Exhaust Fan was manually started and Reactor Building Zone II D/P was restored to greater than 0.25 inches WC by 0301 hrs. Reactor Building Zone 1 (Unit 1) and Zone 3 (Units 1&2) ventilation remained in service and stable. This event is being reported under 10 CFR 50.72(b)(3)(v)(c) and per the guidance of NUREG 1022, Rev. 3, section 3.2.7 as a loss of a Safety Function. There is no redundant Susquehanna Secondary Containment system. The licensee notified the NRC Resident Inspector.Secondary containment05000388/LER-2017-006
ENS 5282624 June 2017 14:28:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialLoss of Secondary ContainmentOn June 24, 2017 at 1028 (EDT), a loss of secondary containment occurred due to trip of 2V217A Zone III Filtered Exhaust Fan causing a reduction in D/P (differential pressure) to less than the required 0.25 WC (water column). 2V217B Zone III Filtered Exhaust Fan started on low flow in AUTO as designed and secondary containment D/P was restored to greater than 0.25 WC by 1029 hours. This event is being reported under 10 CFR 50.72(b)(3)(v)(c) and per the guidance of NUREG 1022, Rev. 3, section 3.2.7 as a loss of a safety function. There is no redundant Susquehanna secondary containment system. The licensee notified the NRC Resident Inspector.Secondary containment05000388/LER-2017-005
ENS 527979 June 2017 09:09:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialExhaust Fan Breaker Failure Causing Low Secondary Containment Differential PressureOn June 9, 2017 at 0509 (EDT), Secondary Containment Zone 3 (Unit 1 and 2 Reactor Building) differential pressure lowered to 0 (inches) WG (water gauge) during a routine restoration due to equipment failure. One of the two Unit 1 Zone 3 exhaust fan breakers experienced a failure that during procedural restoration caused Secondary Containment Zone 3 to experience a positive differential pressure. Required differential pressure per SR 3.6.4.1.1 could not be maintained. Zone 3 differential pressure was recovered to (greater than) 0.25 (inches) WG following restart of Unit 2 Zone 3 Secondary Containment fans. All other Zones of Secondary Containment were unaffected by this event. This event is being reported under 10 CFR 50.72(b)(3)(v)(C) and per the guidance of NUREG 1022 Rev 3 section 3.2.7 as a loss of a Safety Function. There is no redundant Susquehanna Secondary Containment System. The NRC Resident Inspector has been notified.Secondary containment
ENS 525998 March 2017 07:39:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialLoss of Secondary Containment Due to Containment Fan TripOn March 08, 2017 at 0239 hours (EST), Secondary Containment Zone 3 (Unit 1 and 2 Reactor Building) differential pressure lowered to 0 (inches) WG due to a trip of the running Zone 3 Secondary Containment fans. The fan trip was caused by a human performance error during a Unit 2 outage related activity. Required differential pressure per SR 3.6.4.1.1 could not be maintained. Zone 3 differential pressure recovered to (greater than) 0.25 (inches) WG at 0255 hours after restart of Zone 3 Secondary Containment fans. All other Zones of Secondary Containment were unaffected by this event. This event is being reported under 10 CFR 50.72(b)(3)(v)(C) and per the guidance of NUREG 1022 Rev. 3 section 3.2.7 as a loss of a Safety Function. There is no redundant Susquehanna Secondary Containment System. The licensee informed the NRC Resident Inspector.Secondary containment
ENS 5255215 February 2017 18:37:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialLoss of Secondary Containment Differential Pressure

On February 15, 2017 at 1337 (EST), Secondary Containment Zone 1 (Unit 1 Reactor Building) differential pressure lowered to 0 inches WG (Water Gauge) due to a trip of the running Unit 1 B Filtered Exhaust Fan. Required differential pressure per SR (Surveillance Requirement) 3.6.4.1.1 could not be maintained. Zone 1 differential pressure recovered to greater than 0.25 inches WG less than one minute later after start of the standby Zone 1 Filtered Exhaust Fan. Zone 2 (Unit 2 Reactor Building) and Zone 3 (Common Areas of Unit 1&2 Reactor Buildings) ventilation remained in service and stable. This event is being reported under 10 CFR 50.72(b)(3)(v)(C) and per the guidance of NUREG-1022, Rev 3 section 3.2.7 as a loss of a Safety Function. There is no redundant Susquehanna Secondary Containment System. Post-maintenance testing was underway when the fan tripped. While the investigation is on-going to determine the cause, the licensee does not believe the maintenance or testing caused the fan to trip The licensee has notified the NRC Resident Inspector.

  • * * RETRACTION FROM RONALD FRY TO DONALD NORWOOD AT 0833 EDT ON 4/12/2017 * * *

The Unit 1 B Filtered Exhaust Fan trip that resulted in loss of secondary containment differential pressure occurred during post maintenance testing (PMT). The PMT was being performed following replacement of a flow controller associated with the Unit 1 B Filtered Exhaust Fan. In support of the PMT, Technical Specification (TS) 3.6.4.1 Condition A had been entered and was in effect at the time of the fan trip. The maintenance and the associated PMT were performed in accordance with approved work instructions/procedure. Subsequent to the initial report, Susquehanna troubleshooting determined that the fan trip was the result of an internal leak in the newly installed controller that prevented the new controller from functioning properly. The condition was therefore determined to have been the result of the completed maintenance. NUREG-1022, Section 3.2.7, includes the following guidance: '...reports are not required when systems are declared inoperable as part of a planned evolution for maintenance or surveillance testing when done in accordance with an approved procedure and the plant's TS (unless a condition is discovered that would have resulted in the system being declared inoperable).' Following completion of the troubleshooting, Susquehanna determined that, per NUREG-1022, Section 3.2.7, the event was not reportable. Secondary Containment was declared inoperable as a part of a planned evolution for maintenance which was done in accordance with an approved procedure and the Susquehanna TS. The discovered condition was not a pre-existing condition that would have resulted in the system being declared inoperable prior to the planned maintenance activity. The licensee notified the NRC Resident Inspector. Notified R1DO (Jackson).

Secondary containment
ENS 5236916 November 2016 15:45:0010 CFR 50.72(b)(3)(v)(A), Loss of Safety Function - Shutdown the Reactor
10 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual Heat
10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Failure of Unit 2 B Engineered Safeguards System Bus Sync Selector SwitchOn November 16, 2016 at 1045 (EST), Unit 2 B ESS (Engineered Safeguards System) Bus Sync Selector switch failed and was unable to be switched out of the ON position. The failure rendered all other sync selector switches associated with Emergency Diesel Generators and Off-Site supplies to the ESS buses unable to fulfill their intended function of allowing manual transfer between power supplies to the ESS buses. This resulted in the inability of Unit 1 and Unit 2 to comply with SR (Surveillance Requirements) 3.8.1.8 and 3.8.1.16 thus requiring declaration of Operating AC Sources inoperable. This condition could have prevented the fulfillment of the safety function of systems required to maintain the reactor in a safe shutdown condition, remove residual heat, control the release of radioactive material, and mitigate the consequences of an accident. Subsequent actions were taken in accordance with station procedures to remove fuses for the affected sync circuit, restoring the manual transfer function to all but the Unit 2 B ESS bus. One Emergency Diesel and one offsite source remain inoperable with the fuses removed. At no time were any ESS buses disconnected from offsite power. All ESS buses remained capable of being automatically energized from their respective emergency diesel in an emergency. The licensee has notified the NRC Resident Inspector.Emergency Diesel Generator
ENS 5226627 September 2016 20:44:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialSecondary Containment Leakage Exceeding Requirements

On September 27, 2016 at 1644 (EDT), damaged ductwork was identified in the secondary containment boundary associated with reactor building zone 3 (Units 1 and 2) recirculation plenum. The size of the hole in the secondary containment boundary was determined to be 22.5 square inches. Due to exceeding allowable total leakage in the current secondary containment isolation configuration, a violation of SR 3.6.4.1.5 (occurred). Action to establish a tested configuration with sufficient inleakage margin to restore compliance with SR 3.6.4.1.5 was completed September 27, 2016 at 2115 hrs. This event is being reported under 10 CFR 50.72(b)(3)(v)(C) and per the guidance of NUREG 1022, Rev 3, Section 3.2.7 as a loss of a Safety Function. There is no redundant Susquehanna Secondary Containment System. The licensee notified the NRC Resident Inspector.

  • * * RETRACTION AT 1444 EST ON 11/23/2016 FROM MANU SIVARAMAN TO MARK ABRAMOVITZ * * *

Following the 8 hour 10 CFR 50.72 notification made on September 27, 2016 (EN 52266), further engineering analysis determined that the as-found tear in the Zone 3 ductwork did not impact the ability of Secondary Containment to perform its safety function and that Secondary Containment was not inoperable as a result of the condition. To support the determination, a drawdown test was conducted in a limiting configuration (i.e. least inleakage margin). No substantial change in drawdown testing results were observed over the last three tests. These tests spanned over seven years. Additionally, repairs were promptly made to the affected area. As a result, this event notification is being retracted as it is not reportable pursuant to 10 CFR 50.72(b)(3)(v)(C). The licensee notified the NRC Resident Inspector. Notified the R1DO (Dwyer).

Secondary containment
ENS 5225522 September 2016 07:20:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialLoss of Secondary Containment Differential PressureOn September 22, 2016, at 0320 (EDT), Secondary Containment Zone 2 (Unit 2 Reactor Building) differential pressure lowered to 0.15 (inch) WG due to a stuck non-safety related exhaust damper on the in service Zone 2 exhaust fan. Required differential pressure per SR 3.6.4.1.1 could not be maintained. Zone 2 differential pressure recovered to greater than 0.25 (inch) WG on September 22, 2016 at 0342 (EDT) by starting the standby Zone 2 exhaust fan. Zone 1 (Unit 1 Reactor Building) and Zone 3 (Unit 1&2 Reactor Buildings) ventilation remained in service and stable. This event is being reported under 10 CFR 50.72(b)(3)(v)(C) and per the guidance of NUREG 1022 Rev 3 section 3.2.7 as a loss of a Safety Function. There is no redundant Susquehanna Secondary Containment System. The Licensee notified the NRC Resident Inspector.Secondary containment05000388/LER-2016-006
ENS 5192513 May 2016 05:10:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Manual Reactor Scram Due After Loss of an Essential Motor Control CenterAt approximately 0110 hours (EDT) on May 13, 2016, Susquehanna Steam Electric Station Unit Two reactor was manually scrammed by plant operators due to a sustained loss of AC power to essential plant loads. Power to MCC 2B246 was lost at 2355 on May 12, 2016, resulting in a loss of Drywell cooling. Drywell pressure increased to 1.3 psig when operators placed the mode switch to the shutdown position to manually SCRAM the reactor. All rods inserted as expected. Reactor water level lowered to -27 inches and was immediately restored by normal feedwater level control. Level 3 (+13 inch) PCIS isolations occurred, along with an initiation of the RCIC system (-30 inches). Once adequate level was verified, RCIC was overridden. Pressure was controlled with turbine bypass valves, and subsequently main steam line drains. All safety systems functioned as expected. The power loss also tripped Reactor Building HVAC, causing a loss of secondary containment differential pressure resulting in a loss of safety function. Due to the loss of drywell cooling, high drywell pressure actuations and a second reactor SCRAM signal, this signal was automatic, occurred at 0314 hours. HPCI (which automatically initiated on high drywell pressure) was subsequently overridden and declared inoperable, resulting in a loss of safety function. (HPCI did not inject into the vessel). The reactor is currently stable in Mode 3. Initial reports from the field indicate a phase to phase fault on the MCC 2B246 bus bars. The licensee has notified the NRC Resident Inspector and will be issuing a press release.Feedwater
Secondary containment
HVAC
Main Steam Line
ENS 5187220 April 2016 01:59:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialInoperable Secondary ContainmentOn April 19th, 2016 at 2159 (EDT), Secondary Containment became inoperable due to failure to meet Surveillance Requirement (SR 3.6.4.1.1) on Unit 1 and Unit 2. The inoperability was caused when Reactor Building differential pressure was discovered to be less than Technical Specification requirements (-0.25 inches of water gauge). Secondary Containment was restored April 19, 2016 at 2222 by adjusting intake louvers in accordance with off normal operating procedure ON-RBHVAC-201. This event is being reported under 10 CFR 50.72(b)(3)(v)(c) and per the guidance of NUREG 1022 Rev 3 section 3.2.7 as a loss of a Safety Function. There is no redundant Susquehanna Secondary Containment system. The licensee notified the NRC Resident Inspector.Secondary containment05000388/LER-2016-003
ENS 518516 April 2016 17:37:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialReactor Building Airlock Doors Opened SimultaneouslyOn April 6th, 2016 at 1337 (EDT) and 1343 (EDT) Secondary Containment became inoperable due to failure to meet a Surveillance Requirement (SR 3.6.4.1.3) on Unit 1 and Unit 2. The inoperability was caused when two separate sets of Reactor Building airlock doors were sequentially opened during a medical emergency to transport an individual. Each set of airlock doors was opened momentarily to allow passage. Secondary Containment was restored April 6, 2016 at 1344 (EDT) when the transport evolution was complete. This event is being reported under 10 CFR 50.72(b)(3)(v)(c) and per the guidance of NUREG 1022 Rev 3 section 3.2.7 as a loss of a Safety Function. There is no redundant Susquehanna Secondary Containment system. The NRC Resident Inspector has been notified.Secondary containment05000387/LER-2016-010
ENS 5183030 March 2016 02:56:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialLoss of Secondary Containment Differential PressureOn March 29, 2016 at 2256 (EDT), Secondary Containment Zone 2 (Unit 2 Reactor Building) differential pressure lowered to 0.0 (inches) WG (water gauge) due to a failed closed discharge damper on the in service Zone 2 exhaust fan. Required differential pressure per SR 3.6.4.1.1 could not be maintained. Zone 2 ventilation was restored by starting the standby Zone 2 exhaust fan. Zone 2 differential pressure recovered to (greater than) 0.25 (inches) WG at 2321 hours. Zone 3 (Unit 1&2 Reactor Buildings) ventilation remained in service and stable. Zone 1(Unit 1 Reactor Building) ventilation remained in service however it is not required in this mode of Operation. This event is being reported under 10 CFR 50.72(b)(3)(v)(C) and per the guidance of NUREG 1022 Rev 3 section 3.2.7 as a loss of a Safety Function. There is no redundant Susquehanna Secondary Containment System. The licensee has notified the NRC Resident Inspector.Secondary containment05000387/LER-2016-012
ENS 517778 March 2016 07:32:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialSecondary Containment Differential Pressure Outside SpecificationOn March 8, 2016 at 0232 hours (EST), Secondary Containment Zone 3 (Unit 1&2 Reactor Building) differential pressure lowered to 0.16 inches water gauge when securing Unit 1 Zone 3 HVAC for planned maintenance. Required differential pressure per SR 3.6.4.1.1 could not be maintained in the intended alignment. Zone 3 ventilation was restored to the original alignment and Zone 3 differential pressure recovered to greater than 0.25 inches water gauge at 0335 hours. Zone I (Unit 1 Reactor Building) and Zone II (Unit 2 Reactor Building) ventilation remained in service and stable. Station engineering and maintenance are investigating the Zone 3 HVAC system to determine the cause. This event is being reported under 10 CFR 50.72(b)(3)(v)(C) and per the guidance of NUREG 1022, Rev. 3 section 3.2.7 as a loss of a Safety Function. There is no redundant Susquehanna Secondary Containment System. The NRC Resident Inspector has been notified.Secondary containment
HVAC
ENS 517642 March 2016 18:30:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialSecondary Containment InoperableOn March 2, 2016 at 1330 hrs. (EST), Secondary Containment became inoperable due to failure to meet a Surveillance Requirement (SR 3.6.4.1.3). The inoperability was caused when Unit 2 Reactor Building Airlock doors were inadvertently opened simultaneously. Secondary Containment was restored March 2, 2016 at 1331 hrs. when the doors were closed. This event is being reported under 10 CFR 50.72(b)(3)(v)(C) and per the guidance of NUREG 1022, Rev. 3, section 3.2.7, as a loss of a Safety Function. There is no redundant Susquehanna Secondary Containment system. The licensee has notified the NRC Resident Inspector.Secondary containment
ENS 5175022 February 2016 18:45:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialUnit 1 Secondary Containment Inoperable When Personnel Opened Both Access Doors SimultaneouslyOn February 22, 2016 at 1345 (EST). Secondary Containment became inoperable due to failure to meet a Surveillance Requirement (SR 3.6.4.1.3) on Unit 1. The inoperability was caused when Unit 1 Reactor Building Airlock doors were inadvertently opened simultaneously. Secondary Containment was restored February 22, 2016 at 1346 when the doors were closed. This event is being reported under 10 CFR 50.72(b)(3)(v)(C) and per the guidance of NUREG 1022, Rev. 3 section 3.2.7 as a loss of a Safety Function. There is no redundant Susquehanna Secondary Containment system. The licensee informed the NRC Resident Inspector.Secondary containment05000387/LER-2016-002
05000387/LER-2016-001
ENS 515886 December 2015 10:46:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialLoss of Secondary Containment Differential Pressure Due to Exhaust Fan Trip

On December 06, 2015 at 0546 (EST), Reactor Building Zone 1 Secondary Containment differential pressure lowered to less than 0.25 inch Water Column (WC) (degrading vacuum) when the running Reactor Building Zone 1 exhaust fan tripped. This required a TS 3.6.4.1 entry for failure to meet SR 3.6.4.1.1 on Unit 1 and Unit 2.

The standby fan automatically started, restoring of Reactor Building Zone 1 Secondary Containment differential pressure to greater than -0.25 inch WC. Field operators confirmed proper system response at 0553 (EST) December 06, 2015. This event is being reported under 10 CFR 50.72(b)(3)(v)(c) and per the guidance of NUREG 1022 Rev 3 section 3.2.7 as a loss of a Safety Function. " The licensee has notified the NRC Resident Inspector.

Secondary containment
ENS 515876 December 2015 08:50:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialLoss of Secondary Containment Differential Pressure Due to Icing of Intake Supply Plenum Screens

On December 06, 2015 at 0350 (EST), Reactor Building Zone 1 Secondary Containment differential pressure lowered to less than 0.25 inch Water Column (WC) (degrading vacuum) when the intake supply plenum screens were found to be iced over. This required a TS 3.6.4.1 entry for failure to meet SR 3.6.4.1.1 on Unit 1 and Unit 2.

Snow melt heaters were manually started to melt the ice allowing restoration of Reactor Building Zone 1 Secondary Containment differential pressure to greater than 0.25 inch WC at 0434 on December 06, 2015. This event is being reported under 10 CFR 50.72 (b)(3)(c) and per the guidance of NUREG 1022 Rev 3 section 3.2.7 as a loss of a Safety Function. There is no redundant Susquehanna Secondary Containment system. The licensee has notified the NRC Resident Inspector.

Secondary containment
ENS 515761 December 2015 17:45:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialSecondary Containment Inoperable Due to Reactor Building Airlock Doors Being Opened SimultaneouslyOn December 1, 2015 at 1245 EST, Secondary Containment became inoperable due to the failure to meet a Surveillance Requirement (SR 3.6.4.1.3) on Unit 2. The inoperability was caused when RB (Reactor Building) airlock doors were inadvertently opened simultaneously. Secondary Containment was restored December 1, 2015 at 1246 EST when the doors were closed. This event is being reported under 10 CFR 50.72(b)(3)(v)(c) and per the guidance of NUREG 1022, Rev 3, section 3.2.7 as a loss of a Safety Function. There is no redundant Susquehanna Secondary Containment system. The licensee notified the NRC Resident Inspector.Secondary containment
ENS 5153312 November 2015 16:32:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialSecondary Containment Inoperable

On November 12, 2015 at 1132 hrs. (EST), Secondary Containment became inoperable due to failure to meet SR 3.6.4.1.1 requirements on Unit 2.

The inoperability was caused when RB (Reactor Building) Zone II differential pressure (D/P) oscillated between 0.23 and 0.43 inches WG (water gauge) (less than SR 3.6.4.1.1 requirement of greater than or equal to 0.25 inches WG). The oscillations subsided at 1501 (EST) and RB Zone II D/P continues to be maintained at approximately 0.35 inches WG. This event is being reported under 10 CFR 50.72(b)(3)(v)(c) and per the guidance of NUREG 1022 Rev 3 section 3.2.7 as a loss of a Safety Function. There is no redundant Susquehanna Secondary Containment system. The licensee notified the NRC Resident Inspector.

Secondary containment
ENS 5143229 September 2015 14:30:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialBoth Trains of the Standby Gas Treatment System Declared InoperableOn 9/29/15 at 1020 EDT, the 'B' train of Standby Gas Treatment System was declared inoperable for planned testing. On 9/29/15 at 1030 EDT, during performance of a surveillance on Unit 1 Reactor Pressure Vessel water level instrumentation, one channel was found to not meet acceptance criteria. The failed level channel is part of the initiation logic for the 'A' train of Standby Gas Treatment. This resulted in a loss of safety function for the Standby Gas Treatment System. On 9/29/15 at 1145 EDT, the 'B' train of Standby Gas Treatment was restored to operable by restoring from the planned testing. This event is being reported under 10 CFR 50.72(b)(3)(v)(c) and per the guidance of NUREG 1022 Rev 3 section 3.2.7 as a loss of a Safety Function. The NRC Resident Inspector has been informed.Reactor Pressure Vessel
Standby Gas Treatment System
05000387/LER-2015-006
ENS 5135527 August 2015 17:47:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialBrief Loss of Secondary Containment Due to Both Airlock Doors Open Simultaneously

On 8/27/2015 at 1347 (EDT), a cart and personnel were being traversed through an airlock in the Unit 2 reactor building and both airlock doors were inadvertently opened at the same time for a brief period of time (approximately one minute). Secondary Containment differential pressure was maintained throughout the time period that the doors were opened. The doors serve as a Secondary Containment boundary and at least one in series is required to be closed at all times for Secondary Containment Operability. This event is being reported under 10 CFR 50.72(b)(3)(v) and per the guidance of NUREG 1022 Rev 3 section 3.2.7 as a loss of a Safety Function. There is no redundant Susquehanna Secondary Containment System. The licensee notified the NRC Resident Inspector.

  • * * RETRACTED ON 10/22/15 AT 1645 EDT FROM ALEX MCLELLAN TO DONG PARK * * *

NUREG-1022, Revision 3, Section 3.2.7, 'Event or Condition that Could Have Prevented Fulfillment of a Safety Function,' states, in part, that 'events covered in paragraph (b)(3)(v) of this section may include one or more procedural errors, equipment failures, and/or discovery of design, analysis, fabrication, construction, and/or procedural inadequacies.' The level of judgment for reporting an event or condition under this criterion is a reasonable expectation of preventing fulfillment of a safety function. A SSC (System, Structure, and/or Component) that has been declared inoperable is one in which the SSC capability has been degraded to the point where it cannot perform with reasonable expectation or reliability. For SSCs within the scope of this criterion, a report is required when: - There is a determination that the SSC is inoperable in a required mode or other specified condition in the TS (Technical Specification) applicability, -The inoperability is due to one of more personnel errors, including procedure violations; equipment failures; inadequate maintenance; or design, analysis, fabrication, equipment qualification, construction, or procedural deficiencies, and -No redundant equipment in the same system was operable. Subsequent to the reporting of this condition, Susquehanna Nuclear, LLC performed an investigation of the event. Below are the results. When the airlock doors were opened at the same time, they were being operated as designed. Each individual had a 'green' light, which allowed them to open each door. Based on the investigation, the doors were open at the same time for approximately one second. In summary, the inoperability of Secondary Containment was not due to personnel error or a procedure violation. At the time of the event, both airlock doors were operable. No equipment failures, inadequate maintenance, or design, analysis, fabrication, equipment qualification, construction, or procedural deficiencies were identified. In summary, based on the above, the identified condition is not reportable in accordance with 10 CFR 50.72(b)(3)(v), for an event or condition, that at the time of discovery, could have prevented the fulfillment of a safety function. As such, this 8-hour event notification is being retracted. The licensee has notified the NRC Resident Inspector. Notified R1DO (Gray).

Secondary containment
ENS 5126927 July 2015 15:18:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialLoss of Secondary Containment Due to Opening Single Door Without Proper Authorization

On July 27, 2015 at 1118 (EDT), Secondary Containment became inoperable requiring a Technical Specification 3.6.4.1 entry for failure to meet SR (Surveillance Requirement) 3.6.4.1.1 on Unit 1 and Unit 2.

The inoperability was caused by Zone 2 differential pressure lowering to less than 0.25 inches WC when a secondary containment door was opened without appropriate authorization. The secondary containment door was closed at 1149 and secondary containment D/P verified greater than 0.25 inches WC at 1205. This event is being reported under 10 CFR 50.72(b)(3)(v)(c) and per the guidance of NUREG 1022 Rev. 3 section 3.2.7 as a loss of a Safety Function. There is no redundant Susquehanna Secondary Containment system. The loss of secondary containment occurred due to multiple openings of Door 104R which provides access to area of the building that provides alternate access to the building roof, but this door is not the normal access to the building roof The licensee notified the NRC Resident Inspector.

Secondary containment05000388/LER-2015-006
ENS 510404 May 2015 18:39:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialLow Differential Pressure Resulting in Loss of Secondary ContainmentOn May 4, 2015 at 1439 (EDT), during maintenance activities on Unit 2 Zone 3 fan discharge exhaust dampers, the control room received a low DP (Differential Pressure) alarm and other confirmatory indications of a loss of building DP. Secondary Containment DP was restored after approximately 2 minutes. The fan exhaust dampers are outside the isolation dampers, therefore, there was no impact on the SGTS (Standby Gas Treatment System) ability to drawdown secondary containment. This event is being reported under 10 CFR 50.72(b)(3)(v)(c) and per the guidance of NUREG 1022 Rev 3. section 3.2.7, as a loss of a Safety Function. There is no redundant Susquehanna Secondary Containment System. The licensee has notified the NRC Resident Inspector.Secondary containment05000387/LER-2015-005
ENS 5101727 April 2015 12:50:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialSecondary Containment Boundary Door Found AjarOn 4/27/2015 at 0850 (EDT), Secondary Containment (Unit 1 Reactor Building) Boundary Door-721 was found ajar. The door was closed by operators. A status walkdown was performed and no other doors were found in this condition. Although, Secondary Containment differential pressure was maintained throughout the time period that the door was not fully closed and latched. The door serves as a Secondary Containment boundary and is required to be closed for Secondary Containment Operability. This event is being reported under 10 CFR 50.72(b)(3)(v) and per the guidance of NUREG 1022 Rev 3 section 3.2.7 as a loss of a Safety Function. There is no redundant Susquehanna Secondary Containment System. This door is in the railroad bay and was posted as a containment boundary door. Investigation into why this door was not closed and latched is continuing. The licensee notified the NRC Resident Inspector.Secondary containment05000387/LER-2015-004
ENS 5100122 April 2015 02:58:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialInoperable Secondary ContainmentOn April 21, 2015 at 2258 (EDT), Secondary Containment became inoperable requiring a Technical Specification 3.6.4.1 entry for failure to meet SR 3.6.4.1.1 on Unit 1 and Unit 2. The inoperability was caused by Zone 3 differential pressure lowering to less than 0.25 (inches Water Column) when Zone III fans tripped during 30mph wind gusts. Fans were restarted and differential pressure restored to greater than 0.25 (inches Water Column) at 2314 hrs. April 21, 2015. This event is being reported under 10 CFR 50.72(b)(3)(v)(c) and per the guidance of NUREG 1022 Rev 3 section 3.2.7 as a loss of a Safety Function. There is no redundant Susquehanna Secondary Containment system. The licensee notified the NRC Resident Inspector.Secondary containment05000387/LER-2015-003
ENS 5097411 April 2015 04:51:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialSecondary Containment Inoperable Due to Failure of Running Fans

On April 11, 2015 at 0051 EDT, Secondary Containment became inoperable requiring a Technical Specification 3.6.4.1 entry for failure to meet SR (Surveillance Requirement) 3.6.4.1.1 on Unit 1 and Unit 2, loss of required differential pressure.

The inoperability was caused by a loss of normal Zone 2 differential pressure due to loss of running fans and failure to start of standby fans. The cause is being investigated. Engineering and maintenance personnel implemented a Temporary Engineering Change, which allowed restoration of one set of fans and dampers. Normal secondary containment differential pressure was restored. Technical Specification 3.6.4.1 was exited at 0320 EDT. This event is being reported under 10 CFR 50.72(b)(3)(v)(c) and per the guidance of NUREG 1022 Rev 3 section 3.2.7 as a loss of a Safety Function. There is no redundant Susquehanna Secondary Containment system. The NRC Resident Inspector was notified. Temporary Engineering Change consisted of removing air to a previously running fan discharge damper so it would close and allow standby fans to start.

Secondary containment05000387/LER-2015-002
ENS 5088513 March 2015 13:19:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialLoss of Secondary Containment Due to Ventilation Plenum Door Open

On March 13, 2015 at 0919 (EDT), Secondary Containment became inoperable, requiring a Technical Specification 3.6.4.1 entry for failure to meet SR (Surveillance Requirement) 3.6.4.1.1 on Unit 1 and Unit 2.

The inoperability was caused by Zone 2 differential pressure lowering to less than 0.25 inches WC (water column) when an air handling plenum door was opened for an extended period. The plenum door was closed and differential pressure restored to greater than 0.25 inches WC at 0930 on March 13, 2015. This event is being reported under 10 CFR 50.72(b)(3)(v)(c) and per the guidance of NUREG 1022 Rev. 3 Section 3.2.7, as a loss of a Safety Function. There is no redundant Susquehanna Secondary Containment system. The licensee notified the NRC Resident Inspector.

Secondary containment05000388/LER-2015-002
ENS 505955 November 2014 16:15:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialSecondary Containment Zones 2 and 3 Unintentionally CrosstiedOn November 5, 2014 at 1115 (EST), Secondary Containment Zone 3 (Unit 1 & 2 Reactor Building) was unintentionally crosstied to Secondary Containment Zone 2 (Unit 2 Reactor Building) for several seconds during passage of personnel through a personnel airlock. Secondary Containment Zone 2 & Zone 3 ventilation remained in service and stable. LCO 3.6.4.1 was entered and exited based on the prohibited crosstie of Secondary Containment Zones. Tech Spec Secondary Containment Operability requires that at least one door remain closed for airlocks where two doors are provided when an access opening between Secondary Containment Zones is being used for exit and entry. This event is being reported under 10 CFR 50.72(b)(3)(v)(C) and per the guidance of NUREG 1022 Rev. 3 section 3.2.7 as a loss of a Safety Function. There is no redundant Susquehanna Secondary Containment System. The licensee has notified the NRC Resident Inspector.Secondary containment05000388/LER-2014-001
ENS 5005524 April 2014 06:30:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialLoss of Secondary Containment During Routine Swap of a Power SuppliesOn April 24, 2014 at 0230 (EDT), Secondary Containment Zone 3 (Unit 1&2 Reactor Building) differential pressure lowered to 0.10 (negative inches) WG (Water Gauge) when restoring Unit 1 Zone 3 HVAC during a routine swap of RPS power supplies, due to a trip of the Unit 1 Zone 3 Supply fan. Zone 3 differential pressure was restored to > 0.25 (negative inches) WG at 0243 hours. Zone I (Unit 1 Reactor Building) ventilation is isolated with secondary containment relaxed for refuel outage on Unit 1. Zone II (Unit 2 Reactor Building) ventilation remained in service and stable. Zone 3 differential pressure recovered to SR 3.6.4.1.1 requirements of 0.25 WG (negative inches) at 0243 hours and was verified to be stable. LCO 3.6.4.1 was entered at 0230 hours and exited at 0313 hours. Tech Spec Secondary Containment Operability requires a negative pressure of at least 0.25 (negative inches) WG for all three Reactor Building Ventilation Zones when secondary containment is required. This event is being reported under 10CFR50.72(b)(3)(v)(C) and per the guidance of NUREG-1022,Rev 3 section 3.2.7 as a loss of a Safety Function. There is no redundant Susquehanna Secondary Containment System. The licensee notified the NRC Resident Inspector.Secondary containment
HVAC
Reactor Building Ventilation
ENS 5004017 April 2014 07:35:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialLoss of Secondary Containment During Preparation for Loca/Loop TestingOn April 17, 2014 at 0335 EDT, Secondary Containment Zone 3 (Unit 1&2 Reactor Building) differential pressure went to 0.15 inches WG (negative) following securing Unit 1 Zone 3 HVAC in preparation for a LOCA/LOOP test. Zone 3 HVAC was restored at 0420 EDT. Zone I (Unit 1 Reactor Building) ventilation is isolated with secondary containment relaxed for refuel outage on Unit 1. Zone II (Unit 2 Reactor Building) ventilation remained in service and stable. Zone 3 differential pressure recovered to SR 3.6.4.1.1 requirements of 0.25 inches WG (negative) at 0420 EDT and was verified to be stable. LCO 3.6.4.1 was entered at 0335 EDT and exited at 0420 EDT. Tech Spec Secondary Containment Operability requires a negative pressure of at least 0.25 inches water gauge (WG) for all three Reactor Building Ventilation Zones. This event is being reported under 10 CFR 50.72(b)(3)(v)(C) and per the guidance of NUREG-1022 Rev 3 section 3.2.7 as a loss of a Safety Function. There is no redundant Susquehanna Secondary Containment System. The licensee informed the NRC Resident Inspector.Secondary containment
HVAC
Reactor Building Ventilation
ENS 498848 March 2014 08:25:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialUnit 2 Loss of Secondary Containment Due to Discharge Damper FailureOn March 8, 2014 at 0325 (EST), Secondary Containment Zone 2 (Unit 2 Reactor Building) differential pressure went to 0.0 inches WG (water gauge) following a routine transfer of Unit 2 Reactor Protection System (RPS) Power supplies. Upon restoration from the RPS power supply transfer, one of the Reactor Building Exhaust Fans tripped due to a malfunction of its discharge damper. Zone 2 HVAC was restored at 0335 by placing the other train of fans in service. Zone I (Unit 1 Reactor Building) and III (Common Refuel Floor Area) ventilation remained in service and stable. Zone 2 differential pressure recovered to SR 3.6.4.1.1 requirements of 0.25 inches WG within a few minutes and was verified to be stable. LCO 3.6.4.1 was entered at 0325 and exited at 0354. Tech Spec for Secondary Containment Operability requires a negative pressure of at least 0.25 inches water gauge for all three Reactor Building Ventilation Zones. There have been no further perturbations in differential pressure and secondary containment remains operable. This event is being reported under 10 CFR 50.72(b)(3)(v)(C) and per the guidance of NUREG 1022 Rev 3 section 3.2.7 as a loss of a safety function. There is no redundant Susquehanna Secondary Containment System. The licensee notified the NRC Resident Inspector.Secondary containment
Reactor Protection System
HVAC
Reactor Building Ventilation
ENS 498674 March 2014 05:25:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialSecondary Containment Declared Inoperable During Surveillance TestingOn March 4, 2014 at 0025 EST, Secondary Containment drawdown testing surveillance failed to meet acceptance criteria of SR 3.6.4.1.5 due to maximum flow rate exceeding the allowable value. Secondary Containment drawdown testing was being performed on Reactor Building Zone 1 and Zone 3 with Zone 2 HVAC shutdown. Upon failure of the surveillance, Secondary Containment ventilation was realigned to a previous successfully tested and known operable alignment for Zones 1, 2 and 3. This alignment consists of all Reactor Building Zones in service and Zone 3 aligned to the Railroad Bay. Upon restoration of Secondary Containment ventilation to a known operable alignment, operability was restored and Secondary Containment LCO 3.6.4.1 was cleared at 0128 EST on March 4, 2014. This event is being reported under 10 CFR 50.72(b)(3)(v)(c) and per the guidance of NUREG-1022, Rev. 3, Section 3.2.7 as a loss of a Safety Function. There is no redundant Susquehanna Secondary Containment system. The licensee informed the NRC Resident Inspector.Secondary containment
HVAC
05000387/LER-2014-003
ENS 4982112 February 2014 12:11:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialSecondary Containment Boundry Door Found AjarOn February 12, 2014 at 0711 EST, secondary containment (Unit 1 reactor building) boundary door-612 was found propped ajar with a secondary containment boundary sign stuck in the door jam, holding the door open. Upon discovery, the sign was removed from the door jam and the door was verified closed. A status walk down was performed and no other doors were found in this condition. Although secondary containment differential pressure was maintained throughout the time period that the door was open, the door serves as a secondary containment boundary and is required to be closed for secondary containment operability. Secondary containment alignment for removal of the 818 foot elevation (refuel floor) hatch removal had been performed at 0105 EST, February 12, 2014 and the last record of access to the area by security card reader occurred at 0044 EST by the operator performing the ventilation alignment. The potential duration of inoperability based on the available information is approximately 6.5 hours. Past operability evaluation is being performed. This event is being reported under 10 CFR 50.72(b)(3)(v) and per the guidance of NUREG 1022 Rev. 3 section 3.2.7 as a loss of a safety function. There is no redundant Susquehanna secondary containment system. The licensee notified the NRC Resident Inspector.Secondary containment05000387/LER-2014-002
ENS 496147 December 2013 14:50:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialSecondary Containment Fails Retest of Drawdown Surveillance TestOn December 7, 2013 at 0950 (EST), Susquehanna Steam Electric Station (SSES) Secondary Containment drawdown testing failed to meet acceptance criteria of Tech Spec Surveillance Requirement SR 3.6.4.1.5 due to inleakage flow rate exceeding the allowable value. SSES previously entered SR 3.0.3 at 0900 (EST) on 11/15/2013, due to not meeting the requirements of SR 3.6.4.1.4 and 3.6.4.1.5 because of an untested alignment of the Unit 1 Reactor Building Railroad Bay (101 bay). Corrective maintenance was performed on several boundary components (doors and hatches) along with multiple inspections. The test being performed on 12/7/2013 was to be a retest for the previously failed surveillance (performed on 11/20/13). LCO 3.6.4.1 was entered at 0950 (EST) in support of this test. During the test, it was determined that the maintenance performed did not produce the desired outcome. As a result, the retest was not successful. The 101 Bay ventilation was realigned to the previously known operable configuration. Upon completion of this realignment, LCO 3.6.4.1 was cleared at 1349 (EST) and operability restored. Note that SR 3.0.3 remains in effect for the unsuccessful, untested configuration. This event is being reported under 10 CFR 50.72(b)(3)(v)(c) and per the guidance of NUREG 1022, Rev. 3 section 3.2.7 as a loss of a Safety Function. There is no redundant Susquehanna Secondary Containment System. See EN #49565 for the previous surveillance test failure, performed on 11/20/13. The licensee has notified the NRC Resident Inspector.Secondary containment
ENS 4958827 November 2013 15:01:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialUnit 1 Reactor Building Secondary Containment Differential Pressure Out of SpecificationOn November 27, 2013 at 1001 (EST), Susquehanna Steam Electric Station operators observed secondary containment differential pressure was at 0.04 inches water gauge for Zone I (Unit 1 Reactor Building). Tech Spec Secondary Containment Operability requires a negative pressure of at least 0.25 inches water gauge. Zone II (Unit 2 Reactor Building) and III (Common Refuel Floor Area) ventilation remained in service and stable. Zone I differential pressure was impacted due to equipment malfunction. The inservice reactor building exhaust fan discharge damper developed an air leak at the solenoid operator. Zone 1 Building D/P was restored to within the required band at 1111 (EST) by placing the standby train exhaust fan, which was out of service for maintenance, in operation and verified to be stable. LCO 3.6.4.1 was entered for both units at 1001 (EST) and exited at 1131 (EST). This event is being reported under 10 CFR 50.72(b)(3)(v) and per the guidance of NUREG 1022 Rev 3 section 3.2.7 as a loss of a Safety Function. There is no redundant Susquehanna Secondary Containment System. The NRC Resident Inspector has been informed.Secondary containment
ENS 4956521 November 2013 03:40:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialSecondary Containment Fails Drawdown Surveillance TestingOn November 20, 2013 at 2240 (EST), secondary containment drawndown testing surveillance failed to meet acceptance criteria SR 3.6.4.1.5 due to maximum flow rate exceeding the allowable value. SSES (Susquehanna Steam Electric Station) previously entered SR 3.0.3 at 0900 on 11/15/2013 due to not meeting SR 3.6.4.1.4 and SR 3.6.4.1.5 because of an untested alignment of the 101 bay with ventilation aligned as a no zone during past performances of the drawdown testing surveillance. The surveillance being performed on 11/20/2013 was testing this previously unsurveilled alignment. Upon failure of the surveillance, secondary containment ventilation was realigned to the previously tested 818 hatch alignment. Upon restoration of secondary containment ventilation to a known operable alignment, secondary containment LCO 3.6.4.1 was cleared and operability restored. This event is being reported under 10 CFR 50.72(b)(3)(v)(c) and per the guidance of NUREG 1022, Rev. 3 section 3.2.7 as a loss of a Safety Function. There is no redundant Susquehanna Secondary Containment System. The licensee has placed administrative controls on the 101 bay doors to prevent loss of secondary containment during the investigation to determine the reason for the surveillance test failure. The licensee has notified the NRC Resident Inspector.Secondary containment
ENS 4953113 November 2013 07:26:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialSecondary Containment Zone II Differential Pressure Lost During Recovery from Ventilation Drawdown Test

On November 13, 2013 at 0226 (EST), Secondary Containment Zone II (Unit 2 Reactor Building) differential pressure was lost during restoration of a ventilation drawdown test. During restoration Unit 2 'A' Train Reactor Building Ventilation fans tripped. The 'B' Train fans were placed in service and secondary containment was restored. Zone I (Unit 1 Reactor Building) and III (Common Refuel Floor Area) ventilation remained in service and stable. Zone II differential pressure recovered within a few minutes and was verified to be stable. LCO 3.6.4.1 was exited for both units at 0257 (EST). Tech Spec Secondary Containment Operability requires a negative pressure of at least 0.25 inches water gauge. There have been no further perturbations in differential pressure and secondary containment remains operable. This event is being reported under 10 CFR 50.72(b)(3)(v)(c) and per the guidance of NUREG 1022 Rev 3 section 3.2.7 as a loss of a Safety Function. There is no redundant Susquehanna Secondary Containment System. The cause of the Unit 2 "A" Train Reactor Building ventilation fans tripping is still under investigation. The licensee has notified the NRC Resident Inspector.

  • * * RETRACTION ON 1/10/14 AT 1657 EST FROM DOUG LAMARCA TO NESTOR MAKRIS * * *

NUREG-1022, Revision 3 states, ' reports are not required when systems are declared inoperable as part of a planned evolution for maintenance or surveillance testing when done in accordance with an approved procedure and the plant's TS (unless a condition is discovered that would have resulted in the system being declared inoperable).' The event reported in this event notification occurred during a pre-planned evolution for surveillance testing that was done in accordance with an approved procedure and the Susquehanna Technical Specifications. The loss of differential pressure occurred during restoration from the surveillance test and occurred prior to completing the planned evolution and declaring the system OPERABLE. Specifically, the trip of the fans occurred when restoring the Reactor Building normal ventilation after a Zone 1, 2, and 3 isolation (returning back to normal ventilation from the Standby Gas Treatment System). The secondary containment boundary and standby gas treatment system were unaffected. This event occurred as a result of the testing process and would not have occurred during normal operation of the system. There was no discovered condition that would have resulted in the safety function of the system being declared inoperable under normal, non-testing conditions. Based on the above additional information, PPL is retracting this report. Susquehanna was in a planned evolution and did not discover a condition that could have prevented performing a safety function. The licensee has notified the NRC Resident Inspector. Notified the R1DO (Schmidt).

Secondary containment
Reactor Building Ventilation
Standby Gas Treatment System
ENS 494921 November 2013 07:09:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialSecondary Containment Differential Pressure Not within Limits Following Trip of Exhaust FanOn November 1, 2013 at 0309 EDT, Secondary Containment Zone I (Unit 1 Reactor Building) differential pressure was lost following a routine transfer of Reactor Protection System Power supplies. Upon restoration from the power supply transfer, one of the Reactor Building Exhaust Fans tripped. There were no obvious malfunctions associated with the equipment and fan was able to be restarted. Zone II (Unit 2 Reactor Building) and III (Common Refuel Floor Area) ventilation remained in service and stable. Zone I differential pressure recovered within a few minutes and was verified to be stable. LCO 3.6.4.1 was entered for both units at 0309 EDT and exited at 0315 EDT. Tech Spec Secondary Containment Operability requires a negative pressure of at least 0.25 inches water gauge. There have been no further perturbations in differential pressure and secondary containment remains operable. This event is being reported under 10 CFR 50.72(b)(3)(v) and per the guidance of NUREG 1022 Rev 3 section 3.2.7 as a loss of a Safety Function. There is no redundant Susquehanna Secondary Containment System. The licensee notified the NRC Resident Inspector. See similar event number #49489.Secondary containment
Reactor Protection System
ENS 4948931 October 2013 06:51:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialSecondary Containment Differential Pressure Not within Limits Following Trip of Exhaust FanOn October 31, 2013 at 0251, Secondary Containment Zone I (Unit 1 Reactor Building) differential pressure was lost following a routine transfer of Reactor Protection System Power supplies. Upon restoration from the power supply transfer, one of the Reactor Building Equipment Compartment Exhaust Fans tripped. There were no obvious malfunctions associated with the equipment and fan was able to be restarted. Zone II (Unit 2 Reactor Building) and III (Common Refuel Floor Area) ventilation remained in service and stable. Zone I differential pressure recovered within a few minutes and was verified to be stable. LCO 3.6.4.1 was entered for both units at 0251 and exited at 0255. Tech Spec Secondary Containment Operability requires a negative pressure of at least 0.25 inches water gauge. There have been no further perturbations in differential pressure and secondary containment remains operable. This event is being reported under 10 CFR 50.72(b)(3)(v) and per the guidance of NUREG 1022 Rev 3 section 3.2.7 as a loss of a Safety Function. There is no redundant Susquehanna Secondary Containment System. The licensee has notified the NRC Resident Inspector.Secondary containment
Reactor Protection System
ENS 4946523 October 2013 10:20:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialReactor Building Differential Pressure Less than Required by Technical SpecificationsOn October 23, 2013 at 0620, Susquehanna Steam Electric Station operators observed secondary containment differential pressure was at negative 0.17 inches water gauge for Zone II (Unit 2 Reactor Building). Tech Spec Secondary Containment Operability requires a negative pressure of at least 0.25 inches water gauge. Zone I (Unit 1 Reactor Building) and III (Common Refuel Floor Area) ventilation remained in service and stable. Zone II differential pressure was restored to within the required band by manual damper adjustment in about 15 minutes and was verified to be stable. LCO 3.6.4.1 was entered for both units at 0620 and exited at 0635. This event is being reported under 10 CFR 50.72(b)(3)(v) and per the guidance of NUREG 1022 Rev 3 section 3.2.7 as a loss of a Safety Function. There is no redundant Susquehanna Secondary Containment System. The licensee has notified the NRC Resident Inspector.Secondary containment
ENS 4943213 October 2013 08:20:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialSecondary Containment Differential Pressure at Zero Inches Water GaugeOn October 13, 2013 at 0420 (EDT), Susquehanna Steam Electric Station control room operators received an alarm for a local secondary containment ventilation control panel. Investigation revealed that Zone II (Unit 2 Reactor Building) secondary containment differential pressure was at zero inches water gauge. Tech Spec Secondary Containment Operability requires a negative pressure of at least 0.25 inches water gauge. All fans and dampers appeared to be operating normally and there was no apparent equipment malfunction. Zone I (Unit 1 Reactor Building) and III (Common Refuel Floor Area) ventilation remained in service and stable. Zone II differential pressure recovered within five minutes and was verified to be stable. LCO 3.6.4.1 was entered for both units at 0420 and exited at 0425. There have been no further perturbations in differential pressure and secondary containment remains operable. This event is being reported under 10 CFR 50.72(b)(3)(v) and per the guidance of NUREG 1022 Rev. 3 section 3.2.7 as a loss of a Safety Function. There is no redundant Susquehanna Secondary Containment System. The licensee has notified the NRC Resident Inspector.Secondary containment
ENS 4852520 November 2012 11:45:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialCondition That Could Have Prevented Automatic Isolation of Reactor Water Cleanup System

Susquehanna Unit 2 discovered a condition that could have prevented the primary containment isolation valves for the reactor water cleanup (RWCU) system from automatically isolating on a high differential flow instrumentation signal. The RWCU system high differential flow signal was found to be indicating downscale due to an instrument failure. Both divisions of the RWCU high differential flow isolation logic utilize the same differential flow instrument loop. Thus, this single instrument failure would have prevented automatic isolation of the RWCU inboard and outboard primary containment isolation valves on a high differential flow signal. The other RWCU primary containment isolation instrumentation functions remained operable and the associated RWCU system primary containment isolation valves were capable of being remotely closed by the control room operators. At the time of discovery, Unit 2 was in Mode 2 due to an unplanned shutdown and all control rods had already been fully inserted as part of a soft shutdown sequence. The licensee has notified the NRC Resident Inspector.

  • * * RETRACTION FROM DUTTRY TO KLCO ON 1/11/13 AT 2155 EST * * *

Following the ENS report (EN 48525), Susquehanna determined that although the RWCU high differential flow isolation instrumentation would have prevented automatic isolation of the RWCU inboard and outboard primary containment isolation valves on a high differential flow signal, the RWCU high flow isolation instrumentation would detect a high flow condition and generate an isolation signal that would close the isolation valves. The RWCU high differential flow instrumentation is downstream of the RWCU pumps and it calculates the difference (delta) in flow between the inlet and the outlet of the RWCU heat exchangers. The SSES (Susquehanna Steam Electric Station) Technical Specification (TS) Bases Section 3.3.6.1 states that the RWCU Differential Flow signal is to detect a break in the RWCU system (pipe severance and separation). Engineering analysis determined that the RWCU pumps would run-out if a break occurs downstream of the pumps and the RWCU system flow rate would be approximately 1000 gpm, with one RWCU pump in operation. The flow rate would be higher for two RWCU pumps in operation. Therefore, RWCU isolation would occur from the RWCU Flow - High isolation signal due to a flow rate that is greater than 472 gpm (TS Table 3.3.6.1-1). This high flow isolation does not rely on the RWCU high differential flow instrumentation. The above analysis is consistent with the FSAR discussion in section 7.3.1.1a.2.4.1.9.3. Based on the above, Susquehanna has determined that the RWCU isolation function would still be completed if a pipe break occurred downstream of the RWCU heat exchangers and the RWCU high differential flow instrumentation is inoperable. Since there was no loss of safety function of structures or systems that are needed to control the release of radioactive material, this ENS report is retracted. The licensee will notify the NRC Resident Inspector.

Primary containment
Reactor Water Cleanup
Control Rod
ENS 4784417 April 2012 19:40:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialUnit 2 Secondary Containment Affected by Violation of Unit 1 Secondary Containment Integrity During Outage

At 1540 (EDT) on 4/17/12, with Unit 1 in mode 5 and Unit 2 in mode 1, the Work Control Center was notified that the U1 #2 Main Stop Valve (MSV) was disassembled. The U1 #2 MSV was required to be intact to maintain Unit 1 Secondary Containment. Ongoing work on the D Main Steam Line Outboard Valve created a pathway that violated Unit 1 secondary containment integrity. Unit 1 Secondary Containment is required to be operable for Unit 2 while Unit 1 Zone 1 is aligned to the Recirculation Plenum. Unit 1 Zone 1 was isolated from the recirculation plenum and Unit 2 Secondary Containment was restored at 1643 (EDT) on 4/17/12. Unit 2 Secondary Containment differential pressures were maintained throughout the event. This is considered a loss of an entire safety function and requires an 8 hour report per 10CFR50.72(b)(3)(v)(C). The licensee is still investigating the cause but it appears to be associated with recent administrative changes to the Reactor Vessel draining definition and work process procedures. The licensee has notified the NRC Resident Inspector.

      • RETRACTION FROM RON FRY TO S. SANDIN ON 6/7/12 AT 0205 EDT ***

The licensee is retracting this report based on the following: On April 17, 2012, work on the Unit 1 'D' Main Steam Line Outboard Valve with the Unit 1 #2 Main Stop Valve disassembled created a pathway that violated Unit 1 secondary containment integrity. Since Unit 1 Secondary Containment is required to be operable for Unit 2 while Unit 1 Zone 1 would be aligned to the Recirculation Plenum in the event of a secondary containment isolation signal, the condition impacted Unit 2 Secondary Containment. Susquehanna considered the impact a loss of safety function and reported the impact in accordance with 10CFR50.72(b)(3)(v)(C). Following the ENS report, Susquehanna analyzed the impact of the opening. Calculations were performed that show secondary containment would have maintained the dose consequences to the public and control room operators within regulatory limits (10 CFR 50.67) assuming a Unit 2 design basis accident (Unit 1 was in a refueling outage at the time of the condition). Based on the above information, Susquehanna has determined that there was no loss of safety function and this ENS report is retracted. The licensee informed the NRC Resident Inspector. Notified R1DO(Cahill).

Secondary containment
Main Steam Line
ENS 439635 February 2008 23:45:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Irradiated Fuel Movement Performed with a Required Accident Mitigation/Radiation Release System BypassedOn February 5, 2008 EST at 1845 hours it was discovered that irradiated fuel moves had been performed during the previous shift with both Unit 1 and Unit 2 refuel floor high exhaust radiation monitors bypassed. The condition affected both Susquehanna Units. The radiation monitors are required to be operable for conditions noted in footnotes (a) and (b) in Technical Specification Tables 3.3.6.2-1 and 3.3.7.1-1 (i.e. operations with a potential for draining the reactor vessel, and during CORE ALTERATIONS and during movement of irradiated fuel assemblies in the secondary containment). The function of these instruments is to initiate systems that limit fission product release during and following certain postulated fuel handling accidents and to minimize the consequences of radioactive material in the control room environment. No movement of irradiated fuel assemblies was in progress when the issue was discovered. The event has been determined to be reportable within 8 hours under 10 CFR 50.72(b)(3)(v)(C) and 10 CFR 50.72(b)(3)(v)(D). The radiation monitors were bypassed on 1/31/08, as allowed, during a fuel pool activity NOT involving fuel movement. Approximately one hour of fuel movement occurred during the time the radiation monitors were bypassed. The oncoming shift manager identified the discrepancy during the shift turnover prior to assuming the shift. The licensee has notified the NRC Resident Inspector.Secondary containment