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 Start dateReporting criterionTitleEvent descriptionSystemLER
ENS 5395424 March 2019 18:45:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Reactor Automatic Trip on Turbine TripOn March 24, 2019, at 1445 EDT, Indian Point Unit 2 automatically tripped on a turbine trip due to a loss of excitation. All control rods fully inserted and plant equipment responded normally to the unit trip. This RPS (reactor protection system) actuation is reportable under 10 CFR 50.72(b)(2)(iv)(B). The auxiliary feedwater system actuated following the automatic trip as expected. This specified system actuation is reportable under 10 CFR 50.72(b)(3)(iv)(A). During the event offsite power remained available and stable. No primary or secondary reliefs lifted. Unit 2 is in Mode 3 at normal operating temperature and pressure. Decay heat removal is via the steam generators to the atmospheric steam dumps. No radiation was released. Indian Point Unit 3 was unaffected by this event and remains defueled in a scheduled refueling outage. A post trip investigation is in progress. The licensee has notified the NRC Resident Inspector The New York State Public Service Commission, Consolidated Edison System Operator, and New York State Independent System Operator were also notified.Steam Generator
Auxiliary Feedwater
Decay Heat Removal
Control Rod
ENS 5393715 March 2019 17:00:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Trip Due to Turbine Generator TripOn March 15, 2019 at 1300 EDT, Indian Point Unit 2 automatically tripped offline from mode 1 - 100% power operations. Reactor Operators verified the reactor trip and the plant is currently stable in mode 3. All automatic systems functioned as required. The auxiliary feedwater system actuated following the trip, as expected. All control rods fully inserted upon the trip, as expected. This event is reportable under 10 CFR 50.72(b)(3)(iv)(A) and 10 CFR 50.72(b)(2)(iv)(B). The unit remains on offsite power in hot standby at normal operating temperature and pressure. Decay heat is being removed from the steam generators via the auxiliary feedwater system and the condensate steam dump valves. Unit 3 remains in mode 6 for a scheduled refueling outage. The licensee notified the NRC Resident Inspector, the local transmission company, and New York State Independent System Operator. The Indian Point Unit 2 automatic trip was caused by the trip of the main generator. The cause of the generator trip is unknown at this time.Steam Generator
Auxiliary Feedwater
Control Rod
ENS 5361118 September 2018 04:00:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor Trip Due to a Steam Leak on a High Pressure Feedwater HeaterDue to a steam leak on the reheater line to 36C Feedwater Heater, operators initiated a manual trip of the reactor, verified the reactor trip, and closed all Main Steam Isolation Valves. The plant is currently stable in Mode 3 with the steam leak isolated. The Auxiliary Feedwater System actuated following the trip as expected. This is reportable under 10 CFR 50.72(b)(3)(iv)(A) and 10 CFR 50.72(b)(2)(iv)(B). The unit remains on offsite power in Hot Standby at normal operating temperature and pressure. Decay heat is being removed from the steam generators via the Auxiliary Feedwater System and atmospheric steam dumps. Unit 2 was unaffected and remains at 100 percent power. The licensee notified the NRC Resident Inspector, the State of New York, and the local transmission company.Steam Generator
Feedwater
Main Steam Isolation Valve
Auxiliary Feedwater
ENS 5334820 April 2018 01:07:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor Trip Due to Turbine IssueWhile performing a turbine startup, a turbine control anomaly caused a steam generator level transient. The rise in steam generator level above the setpoint caused the turbine to automatically trip. The high steam generator level of 73 percent caused a feedwater isolation signal at 2107 EDT, which also tripped both Main Boiler Feed Pumps. The tripping of the Main Boiler Feed Pumps auto started the motor driven Aux Boiler Feed Pumps 21 and 23. The reactor was manually tripped at 2108 EDT in accordance with AOP-FW-1 Loss of Main Feedwater. All control rods inserted. Electrical power is being provided from offsite via the Station Aux Transformer. Decay heat removal is being provided via the Atmospheric Dump Valves. An investigation into the cause of the turbine control anomaly is underway. The NRC Resident Inspector has been notified. The event did not have an affect on Unit 3 and there is no primary to secondary leakage.Steam Generator
Feedwater
Decay Heat Removal
Control Rod
ENS 5321616 February 2018 07:01:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Trip Due to Loss of Excitation on Main GeneratorOn February 16, 2018 at 02:01 EST Indian Point Unit 3 automatically tripped on a turbine trip due to a loss of main generator excitation. All control rods fully inserted and all plant equipment responded normally to the unit trip. This is reportable under 10 CFR 50.72(b)(2)(iv)(B). The auxiliary feedwater system actuated following the automatic trip as expected. This is reportable under 10 CFR 50.72(b)(3)(iv)(A). During the event offsite power remained available and stable. No primary or secondary reliefs lifted. The plant is stable, in Mode 3, at no load operating temperature and pressure. Decay heat removal is via the steam generators to the main condenser via the condenser steam dumps. No radiation was released. Indian Point Unit 2 was unaffected by this event and remains at 100 percent power. A post trip investigation is in progress. The licensee has notified the NRC Resident Inspector.Steam Generator
Auxiliary Feedwater
Decay Heat Removal
Main Condenser
Control Rod
ENS 530524 November 2017 00:22:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Indian Point Unit 3 Reactor Trip on Low Steam Generator Level

On November 3rd, 2017 at 2022 EDT, the Indian Point Unit 3 Reactor Protection system automatically actuated at 100 percent power. Annunciator first out indication was from 33 SG (Steam Generator) Low Level. This automatic reactor trip is reportable to the NRC under 10 CFR 50.72(b)(2)(iv)(B). All control rods fully inserted on the reactor trip. All safety systems responded as expected. The Auxiliary Feedwater System actuated as expected. Offsite power and plant electrical lineups are normal. All plant equipment responded normally to the unit trip. No primary or secondary code safeties lifted during the trip. The Auxiliary Feedwater System actuated following the automatic trip as expected. This is reportable under 10 CFR 50.72(b)(3)(iv)(A). The Emergency Diesel Generators did not start as offsite power remained available and stable. The Unit remains on offsite power and all electrical loads are stable. Unit 3 is in Hot Standby at normal operating temperature and pressure with decay heat removal using auxiliary feedwater to the steam generators and normal heat removal through the condenser via the high pressure steam dumps. Unit 2 was unaffected and remains at 100 percent power. A post trip investigation is in progress. The licensee indicated that Radiation Monitor number 14 spiked twice during the transient, however, is currently not indicating any signs of radiation. The licensee will notify the NRC Resident Inspector and the NY Public Service Commission.

  • * * UPDATE AT 1523 EST ON 11/06/17 FROM RAMIREZ OVIDIO TO JEFF HERRERA * * *

The initial notification stated that Indian Point Unit 3 Reactor Tripped on 33 SG (Steam Generator) Low Level, this is incorrect. Indian Point Unit 3 Reactor Tripped on a Turbine Trip. The Turbine Trip was caused by a Generator Back-up Lockout Relay. The Turbine Trip was the 'first' annunciator first-out but was acknowledged instead of silenced during initial operator actions. The Turbine Trip first-out being acknowledged allowed a Low Steam Generator first-out to later annunciate. A Low Steam Generator Level is an expected condition post trip. This update does not change any actions taken by the operating team or required notifications under 10 CFR 50.72(b)(2)(iv)(B) and 10 CFR 50.72(b)(3)(iv)(A). A post trip investigation remains in progress. The licensee will notify the NRC Resident Inspector and the NY Public Commission. Notified the R1DO(Cook)

Steam Generator
Reactor Protection System
Emergency Diesel Generator
Auxiliary Feedwater
Decay Heat Removal
Control Rod
ENS 5282926 June 2017 04:00:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release
10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor Trip Due to Loss of Main FeedpumpOn June 26, 2017, at 1531 (EDT), Indian Point Unit 2 inserted a manual reactor trip prior to Steam Generator levels reaching the automatic reactor trip setpoint. Steam Generator water level perturbation resulted from a loss of 22 Main Boiler Feed Pump. All Control Rods verified inserted. The Auxiliary Feedwater System started as designed and supplied feedwater to the Steam Generators. Heat removal is via the Main Condenser through the High Pressure Steam Dumps. Offsite power is being supplied through the normal 138kV feeder 95332. The cause of the 22 Main Boiler Feed Pump loss is currently under investigation. Entergy is issuing a press release/news release on this issue. Unit 2 is stable and in Mode 3. There was no impact on Unit 3. The licensee notified the State of New York and the NRC Resident Inspector.Steam Generator
Feedwater
Auxiliary Feedwater
Main Condenser
Control Rod
ENS 520676 July 2016 13:38:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Trip While Performing TestingOn July 6, 2016 at 0938 EDT Indian Point Unit 2 experienced a trip from 100% steady state power during the performance of reactor protection testing. The cause of the trip is under investigation. All control rods fully inserted and all systems responded as expected. The auxiliary feedwater system actuated as expected on a low level in the steam generators which occurs as a result of a trip from full power. Auxiliary feedwater is maintaining steam generator levels and decay heat removal is via the steam generators to the main condenser. Offsite power and plant electrical line ups are normal with the exception of 13.8kV feeder 33332 which remains out of service during the replacement of breaker BT4-5. No primary or secondary code safety relief valves lifted. The reactor is in Mode 3 and stable. Indian Point Unit 3 was unaffected and remains at 100% steady state power. The NRC Resident Inspector has been notified. The licensee notified the New York Public Service Commission and the New York Independent System Operator. Indian Point indicated they have issued a press release regarding the event.Steam Generator
Auxiliary Feedwater
Decay Heat Removal
Safety Relief Valve
Main Condenser
Control Rod
ENS 517757 March 2016 15:18:0010 CFR 50.72(b)(3)(iv)(A), System ActuationEmergency Diesel Generators Auto-Started on Valid Actuation SignalDuring Emergency Diesel Generator (EDG) surveillance testing, the normal 480V Bus 3A supply breaker tripped open. All EDGs auto-started as per plant design. During restoration of normal power to the 480V Buses, 23 EDG output breaker opened on overcurrent. All plant systems responded as per design. There was no loss of core cooling since steam generators were coupled with an operational RCP. No other ESF (Engineered Safety Feature) equipment automatically started. The 480V Bus 3A normal supply breaker was replaced and the cause of both issues is under investigation. Indian Point Unit 2 remains in a stable MODE 5 condition with all 480V Buses energized via normal power. The NRC Resident has been informed. The licensee will inform the New York Public Service Commission.Steam Generator
Emergency Diesel Generator
05000247/LER-2016-002
ENS 5160615 December 2015 00:06:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Trip Due to Main Generator LockoutAt 1906 (EST) on 12/14/2015, Indian Point Unit 3 received a Main Generator Lockout trip signal, and the reactor automatically tripped. Site personnel reported seeing arcing on a 345kV output transmission line tower. At the time of the trip, there was moderate rain and fog in the area. The site fire brigade leader investigated the reports of arcing and found no evidence of fire; fire brigade response was not required. All automatic systems functioned as designed and all control rods inserted automatically. Auxiliary Feedwater Pumps started automatically due to expected low steam generator levels following a reactor trip from 100% power. Unit 3 is being maintained in Mode 3 with decay heat removal via steam dumps to the condenser. Offsite power remains available and in service from 138kV to the 480V safeguards buses. The cause of the Main Generator Lockout signal is being investigated. Unit 2 was not impacted and continues to operate at 100% power. The NRC Resident Inspector has been notified. After the trip, operators observed high vibrations on the 33 reactor coolant pump which eventually returned to normal range. The licensee will be notifying the New York Public Service Commission and their local Independent System Operator. A press release will be issued by the Communications Department.Steam Generator
Auxiliary Feedwater
Decay Heat Removal
Control Rod
ENS 515865 December 2015 22:31:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor Trip Initiated Due to Multiple Dropped Control RodsAt 1731 (EST) on December 5, 2015, Indian Point Unit 2 Control Room operators initiated a Manual Reactor Trip due to indications of multiple dropped Control Rods. The initiating event was a smoldering Motor Control Center (MCC) cubicle in the Turbine Building that supplies power to the Rod Control System. The unit is stable in Mode 3 with heat sink provided by Auxiliary Feedwater and decay heat removal is via the steam dumps to the condenser. Offsite Power remains in service. The smoldering MCC cubicle had power removed from it when 24 MCC breaker tripped on overcurrent. The affected cubicle has ceased smoldering and is being monitored by on-site Fire Brigade trained personnel. The trip of 24 MCC removed power to 22 Battery Charger, 22 DC Bus remained powered from the 22 Battery without interruption, and 22 Battery Charger was subsequently repowered. The cause of the smoldering MCC is being investigated and a post reactor trip evaluation is being conducted by the licensee. There was no impact on Unit 3, which continues to operate at 100% power. The licensee has notified the NRC Resident Inspector and appropriate State and Local authorities.Auxiliary Feedwater
Decay Heat Removal
Control Rod
ENS 512118 July 2015 18:25:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor Trip Due to Lowering Steam Generator Water LevelsIndian Point Unit 3 was manually tripped at 1427 EDT due to lowering steam generator water levels. At 1425 EDT, #31 condensate pump tripped, causing the lowering water levels. There were no immediate complications on the trip and the unit is stable in Mode 3. Auxiliary feedwater actuated as expected and is in service. All rods inserted and decay heat is being rejected to the condensers. Offsite electrical power is in service. Unit 2 is stable at 100% power. The licensee plans on issuing a press release. The licensee notified the NRC Resident Inspector and New York Public Service Commission.Steam Generator
Auxiliary Feedwater
ENS 5115615 June 2015 23:20:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Reactor Trip Due to Turbine Trip

On June 15, 2015 at 1920 EDT, Indian Point Unit 3 received a Turbine trip which directly led to a Reactor trip. Operators entered (plant procedure) E-0, Reactor Trip or Safety Injection. All control rods fully inserted. All safety systems responded as expected. The Auxiliary Feedwater (AFW) system actuated as expected. Offsite power and electrical lineups are normal. No primary or secondary code safety valves lifted. All MSIVs are open and the Main Condensers are being used as the heat sink. The Reactor is in Mode 3 and stable. Unit 2 was unaffected and remains at 100% power. Preliminary investigation determined that Breaker Number 1 in the Ring Bus was intentionally opened (by plant personnel on switching orders from the district operator) due to a problem on W93 (output feeder from Ring Bus). Subsequently Breaker #3 went open and caused a Turbine/Reactor trip of the Unit. The licensee notified the NRC Resident Inspector.

  • * * UPDATE FROM BOB WALPOLE TO DANIEL MILLS ON 6/16/15 AT 1320 EDT * * *

The licensee previously identified "a problem on W93" which was a mistake and should have been stated as "a problem on W97". All other information was stated correctly. The NRC Resident Inspector has been notified. Notified R1DO (Bickett).

Auxiliary Feedwater
Main Condenser
Control Rod
ENS 510609 May 2015 21:50:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release
10 CFR 50.72(a)(1)(i), Emergency Class Declaration
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Unusual Event Declared Due to Main Transformer Fire

At 1750 EDT (05/09/15,) Indian Point Unit 3 experienced a fire on the 31 Main Transformer resulting in a unit trip. An Unusual Event was declared at 1801 EDT. The onsite fire brigade was mobilized. Offsite fire fighting assistance was requested. The fire was reported extinguished at 1815 EDT. The reactor was shutdown by an automatic trip. Plant response to the trip was as expected with no complications. The 31 and 33 Auxiliary Feed Pumps are operating and feeding the steam generators. Accountability is being performed. The plant is stable in mode 3, all control rods fully inserted, with normal offsite electrical power, and decay heat is being released to the main condenser. There was no impact on Unit 2 which continues to operate at 100% power. The licensee has notified the NRC Resident Inspector and state and local authorities. Notified DHS SWO, FEMA OPS Center, DHS NICC Watch Officer, and Nuclear SSA via email.

  • * * UPDATE FROM LUKE HEDGES TO JOHN SHOEMAKER AT 2037 ON 5/9/15 * * *

Oil from 31 Main Transformer has spilled into the discharge canal and has made its way into the river. Plant personnel are sandbagging drains and release paths. IPEC (Indian Point Energy Center) has contacted its environmental contractor, who is expected onsite at 2100 EDT to assist with cleanup. The National Response Center was notified at 1945 EDT and issued notification number 1116011. A message was left with the Westchester County Department of Health at 1953 EDT. The NY State DEC (Department of Environment Conservation) was contacted at 1955 EDT and issued notification number 1501459. The licensee has notified the NRC Resident Inspector. Indian Point Unit 3 remains in an Unusual Event at this time. Notified R1DO (Schroeder).

  • * * UPDATE FROM LUKE HEDGES TO JOHN SHOEMAKER AT 2141 ON 5/9/15 * * *

Indian Point Unit 3 exited the Unusual Event at 2103 EDT. The basis for exiting the Unusual Event is that the fire is out and field operators report they have been successful in cooling the transformer. The licensee has notified the NRC Resident Inspector and state and local authorities. Notified R1DO (Schroeder), R1RA (Lew), NRR (Dean), NRR EO (Morris), NRR EO (Howe), and IRD (Grant). Notified DHS SWO, FEMA OPS Center, DHS NICC Watch Officer, and Nuclear SSA via email.

Steam Generator
Main Transformer
Main Condenser
Control Rod
ENS 5036113 August 2014 15:57:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor TripOn August 13, 2014 at 1157 EDT, the Indian Point Unit 3 Reactor Protection System automatically actuated at 100% power due to Over Temperature Delta Temperature logic. At the time of the trip, pressurizer pressure Channel 1 was in test for maintenance, though testing was suspended at this time for lunch. All control rods fully inserted on the reactor trip. All plant equipment responded normally to the unit trip. This is reportable under 10 CFR 50.72(b)(2)(iv)(B). The plant is stable in Mode 3 at this time. The Auxiliary Feedwater System actuated following the automatic trip as expected. This is reportable under 10 CFR 50.72(b)(3)(iv)(A). The Emergency Diesel Generators did not start as offsite power remained available and stable. The unit remains on offsite power and all electrical loads are stable. No primary or secondary relief valves lifted. The plant is in Hot Standby at normal operating temperature and pressure with decay heat removal using auxiliary feedwater to the steam generators, and normal heat removal through the condenser via condenser steam dumps. There was no radiation released. Indian Point Unit 2 was not affected by this event and remains at 100% power. A post trip investigation is in progress. The licensee notified the NRC Resident Inspector.Steam Generator
Reactor Protection System
Emergency Diesel Generator
Auxiliary Feedwater
Decay Heat Removal
Control Rod
ENS 498026 February 2014 20:53:0010 CFR 50.72(b)(3)(iv)(A), System ActuationUnanticipated Auxiliary Feedwater Pump Start After Securing Emergency Diesel GeneratorThis report is being made in accordance with 10CFR50.72(b)(3)(iv)(A) for an Auxiliary Feedwater System Actuation. The monthly surveillance on 31 Emergency Diesel Generator (EDG) was conducted on 6 February 2014. The EDG was unloaded and its output breaker opened at 1553 (EST). At this time, the Non-SI Blackout Logic Defeated indication in the control room changed state from 'not illuminated' (logic defeated) to 'illuminated' (logic not defeated) without operator action. The steam-driven 32 Auxiliary Boiler Feed Pump (ABFP) auto started but did not inject water into the steam generators. The discharge valves are normally closed. Operators verified normal steam generator levels and level control and that all 480VAC Safeguards buses remained energized, then secured 32 ABFP and placed it back into AUTO. Indian Point 3 remains at full power in Mode 1. This event did not cause any change in power. The Senior NRC Resident and the NY State Public Service Commission have been informed.Steam Generator
Emergency Diesel Generator
Auxiliary Feedwater
ENS 496987 January 2014 02:15:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Trip on Low Steam Generator Water Level Due to a Failed Main Feedwater Reg ValveOn January 6th, 2014 at 2115 EST Indian Point Unit 3 experienced an Automatic Reactor Trip due to '33 Steam Generator Steam flow/Feed flow Mismatch.' Operators entered emergency procedure E-0, Reactor Trip or Safety Injection. All control rods fully inserted, all safety systems responded as expected, and off-site power remained in-service. No primary or secondary safety valves actuated due to the trip. This is reportable under 10CFR50.72(b)(2)(iv)(B). The main condenser is being used for heat sink. Unit 2 remains stable at 100% power. The Auxiliary Feedwater System actuated following the automatic trip as expected. This is reportable under 10CFR50.72(b)(3)(iv)(A). Investigation is underway to determine the cause of the 33 Steam Generator Mismatch condition. The licensee will inform local and other government agencies and issue a press release. The licensee has informed the State of New York and the NRC Resident Inspector.Steam Generator
Feedwater
Auxiliary Feedwater
Main Condenser
Control Rod
ENS 491713 July 2013 11:41:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Reactor Trip Following Loss of Instrument Air to Main Feedwater Regulating ValvesOn July 3, 2013, at 0741 EST, the Indian Point Unit 2 CCR received a trip of both Main Boiler Feed Pumps (MBFP) and entered 2-AOP�FW-1, Loss of Feedwater. The unit was manually tripped at 0741 per 2-AOP-FW�1 due to the trip of both MBFPs. Operators entered E-O, Reactor Trip or Safety Injection. All control rods fully inserted. All safety systems responded as expected. The Auxiliary Feedwater (AFW) System actuated as expected. Offsite power and plant electrical lineups are normal. No primary or secondary code safety valves lifted. The 23 and 24 Main Steam Isolation Valves (MSIV) failed closed as a result of the loss of Instrument Air (IA). The 21 and 22 MSIVs remain open with the Main Condensers being used for heat sink. The reactor is in Mode 3 and stable. Unit 3 was unaffected and remains at 100% power. Preliminary investigations determined a two inch copper IA line in the switchyard which is normally buried had a failed coupling causing loss of IA to the main feedwater regulating valves. The IA line traversed an excavated area of the switchyard going to the Auxiliary Boiler Feed Pump (ABFP) Building. AFW operated using the Nitrogen backup supply to ABFP control valves until Instrument Air was restored to the ABFP building. An investigation is in progress. The licensee notified the NRC Resident Inspector.Feedwater
ENS 4885427 March 2013 10:01:0010 CFR 50.72(b)(3)(iv)(A), System Actuation
10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge
Safety Injection Actuation During Testing

On March 27, 2013 at 0601 EDT, the Safety Injection System automatically actuated while in Mode 3 during performance of I&C (Instrument and Control) testing due to faulty test equipment. All plant equipment responded normally to the safety injection. This is reportable under 10 CFR 50.72(b)(2)(iv)(A). The plant is stable in Mode 3 at this time. The Auxiliary Feedwater System actuated following the safety injection signal as expected. This is reportable under 10 CFR 50.72(b)(3)(iv)(A). The unit remains on offsite power and all electrical loads are stable. No primary or secondary relief valves lifted. The plant is in Hot Standby at 1140 psig and 395 degrees F with decay heat removal using auxiliary feedwater to the steam generators and normal heat removal through the atmospheric steam dumps. There was no radiation released. Indian Point Unit Two was not affected by this event and remains at 100% power. Notified NRC Resident Inspector. Notified NRC Emergency Operations Center Duty Officer. The Safety Injection was reset and all plant equipment was restored to normal alignment. Pressurizer level remained in the indication range during the Safety Injection. The cause of the Safety Injection is still under investigation, but appears to be related to a faulty jumper necessary for the test.

  • * * UPDATE FROM MICHAEL McCARTHY TO DONALD NORWOOD AT 1335 EDT ON 3/27/2013 * * *

The event reported above resulted in additional reportable actuations under 10 CFR 50.72(b)(3)(iv)(A). These were: 1) RPS actuation, 2) Phase A containment isolation, 3) Containment fan cooler unit actuation, and 4) Emergency Diesel Generator actuation (start but did not load). The licensee notified the NRC Resident Inspector of the 1335 EDT update. Notified R1DO (Krohn).

Steam Generator
Emergency Diesel Generator
Auxiliary Feedwater
Decay Heat Removal
05000286/LER-2013-005
ENS 4875013 February 2013 18:55:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor Trip on Low Steam Generator Water LevelAt 1352 (hrs. EST), the Unit 2 CCR (Central Control Room) noted a trip of both heater drain tank pumps and entered Abnormal Operating Procedure 2-AOP-FW-1, 'Loss of Feedwater'. Prior to the event, Instrumentation and Controls personnel were performing testing on the heater drain tank level control system. Turbine load was reduced per plant procedures, however a manual reactor trip was initiated at 1355 due to an inability to maintain steam generator water levels. The team subsequently entered E-0, 'Reactor Trip or Safety Injection'. All control rods fully inserted. All safety systems responded as expected with the exception of source range detector N-31 and intermediate range detector N-35. N-31 and N-35 were declared inoperable. The auxiliary feedwater system actuated as expected and provided feedwater to maintain steam generator water level. Decay heat removal is via the steam generators to the main condensers. Offsite power and plant electrical lineups are normal. No primary or secondary code safety relief valves lifted. The reactor is in Mode 3 and stable. Unit 3 was unaffected and remains at 100% power. An investigation is in progress. Unit 2 is currently at normal operating pressure and temperature. The licensee plans to issue a press release on this event. The licensee notified the State of New York Public Service Commission and the NRC Resident Inspector.Steam Generator
Feedwater
Auxiliary Feedwater
Decay Heat Removal
Safety Relief Valve
Main Condenser
Control Rod
ENS 4845430 October 2012 02:41:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Rps Actuation on Generator TripOn October 29, 2012, at 2241EDT, the Reactor Protection System automatically actuated at 100% reactor power due to a direct electrical trip to the Unit 3 Main Turbine Generator. The generator trip resulted in a turbine/reactor trip. All control rods fully inserted on the reactor trip. All plant equipment responded normally to the unit trip. This is reportable under 10 CFR 50.72(b)(2)(iv)(B). The plant is stable in Mode 3 at this time. The Auxiliary Feedwater System actuated following the automatic trip as expected. This is reportable under 10 CFR 50.72(b)(3)(iv)(A). The Emergency Diesel Generators did not start as offsite power remained available and stable. The unit remains on offsite power and all electrical loads are stable. No primary or secondary relief valves lifted. The plant is in Hot Standby at normal operating temperature and pressure with decay heat removal using auxiliary feedwater to the steam generators and normal heat removal through the condenser via condenser steam dumps. There was no radiation released. Indian Point Unit 2 was not affected by this event and remains at 100% power. A post trip investigation is in progress. The licensee notified the NRC Resident Inspector.Steam Generator
Reactor Protection System
Emergency Diesel Generator
Auxiliary Feedwater
Main Turbine
Decay Heat Removal
Control Rod
ENS 479996 June 2012 10:12:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Unit 2 Experienced an Automatic Reactor Trip on Turbine Main Generator TripOn June 6, 2012, at approximately 0612 hours, Indian Point Unit 2 reactor automatically tripped from 100% steady state power due to a turbine-main generator electrical trip. All rods fully inserted. Investigation into the generator trip is in progress. All systems responded as expected. The Auxiliary Feedwater system actuated and responded as expected and is maintaining steam generator levels. Decay heat removal is via the steam generators to the main condenser. Offsite power and plant electrical lineups are normal. No primary or secondary code safety relief valves lifted. The reactor is in Mode 3 and stable. Unit 3 was unaffected and remains at 100% power. The NRC Resident Inspector has been notified, and the licensee issued a press release.Steam Generator
Auxiliary Feedwater
Decay Heat Removal
Safety Relief Valve
Main Condenser
ENS 4758210 January 2012 09:36:0010 CFR 50.72(b)(2)(iv)(B), RPS System ActuationExcessive Leakage from Rcp Seal Return

Plant shutdown from 100% due to increased leakage from 21 RCP (Reactor Coolant Pump) seal return was commenced at 0100 EST. A manual reactor trip was actuated in accordance with plant procedures at 25% power. Auxiliary feedwater pump was placed in service prior to the reactor trip, per plant procedures. Decay heat is being removed via the condenser steam dumps. All offsite power sources are available. All equipment operated as expected. The licensee has notified the NRC Resident Inspector and other government agencies.

  • * * RETRACTION FROM CHARLES ROKES TO HOWIE CROUCH AT 0940 EST ON 2/15/12 * * *

Subsequent review concluded the condition did not meet reporting criteria. A normal plant shutdown was initiated in accordance with plant procedures for a known problem with the 21 RCP # 1 seal whose seal leakoff rate had reached an administrative alarm limit. Shutdown was not required by the Technical Specifications. On January 10, 2012, at 0100 hours (EST) a plant shutdown commenced per plant operating procedure 2-POP-2.1. At 0436 hours, the reactor was manually tripped in accordance with procedure 2-POP-3.1. This event is not reportable as the reactor trip was part of a normal shutdown for corrective maintenance. The licensee has notified the NRC Resident Inspector. Notified R1DO (Powell).

Auxiliary Feedwater
ENS 4717719 August 2011 22:05:0010 CFR 50.72(b)(3)(iv)(A), System ActuationPartial Loss of Offsite Power Resulting in Edg AutostartAt 1805 Indian Point Unit 3 experienced a loss of normal 138 KV Offsite Power (LOOP) during a thunderstorm in the area. The Station Auxiliary Transformer (SAT) protection circuitry actuated and de-energized 6.9 KV buses 5 and 6. Thirty two and 33 Emergency Diesel Generators (EDGs) auto-started and loaded onto Safeguards buses 5A and 6A per plant design. The corresponding blackout logic resulted in an auto start of 32 and 33 Auxiliary Feed Water pumps (AFW). The plant remained in Mode 1; however, due to the loss of two 6.9 KV buses, three Circulating Water pumps (CW) tripped as designed, which caused main condenser backpressure to rise (i.e., vacuum degraded). As a result of rising condenser backpressure, a manual turbine load reduction to 75% power was performed. The reactor remains stable at 75% power and buses 5 and 6 have been manually re-energized from the alternate 13.8 KV offsite power source and the Emergency Diesel Generators have been unloaded, shutdown, and realigned for auto start capability. The only unusual system response was 32 Component Cooling Water (CCW) pump did not auto-start on a low pressure signal when the remaining pumps were stripped and re-Ioaded by the EDG sequencing logic due to a problem with the closing spring on the supply breaker. CCW system pressure was observed to be at normal levels when 31 and 33 CCW pumps were loaded on the EDGs. 32 CCW pump remains inoperable due to the breaker issue. There was no impact to the operation of Unit 2 during this event. The licensee has notified the NRC Resident Inspector and the New York State Public Service Commission.Emergency Diesel Generator
Auxiliary Feedwater
Main Condenser
ENS 466491 March 2011 16:00:0010 CFR 50.72(b)(3)(iv)(A), System ActuationEmergency Diesel Generators Start on a Loss of Power from 138 Kv CircuitAt 1100 EST, Indian Point Unit 2 experienced a loss of offsite power from the 138 Kv circuit. All three Emergency Diesel Generators automatically started as required. All other plant systems functioned as required. Restoration of offsite power from the 13.8 Kv offsite circuit is in progress. Investigation into the loss of the 138 Kv circuit is ongoing. Indian Point, Unit 2 continues in Mode 1 at 100 % power. Indian Point, Unit 2 is in a 72 hour LCO due to a loss of 1 of 2 offsite circuits. Unit 3 was not affected. The licensee has notified the NRC Resident Inspector and will be notifying the Public Service Commission of the State of New York.Emergency Diesel Generator
ENS 464007 November 2010 23:39:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release
10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(a)(1)(i), Emergency Class Declaration
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Alert Declared Due to Explosion in the 21 Main Transformer

At 1849 EST, the licensee declared an Alert due to an explosion in the 21 Main Transformer. As a result of the loss of the transformer, Unit 2 experienced a reactor trip. Plant response to the trip was normal and the plant is stable in Mode 3. At 1839 hrs., the licensee activated their Emergency Response Organization. Additionally, there was a report of smoke issuing from a metering station at the site boundary. Offsite assistance has been requested to investigate the metering station. No injuries were reported and the licensee is investigating whether any other equipment damage occurred as a result of the transformer failure.

  • * * UPDATE FROM NICK LIZZO TO HOWIE CROUCH AT 2200 EST ON 11/07/10 * * *

On November 7, 2010, at 1839 hours, the Reactor Protection System automatically actuated at 100% Reactor Power when the 21 Main Transformer failed. The failure resulted in a turbine / reactor trip. All plant equipment responded normally to the unit trip. This is reportable under 10 CFR 50.72(b)(2)(iv). The transformer failure was characterized as an explosion that meets the IPEC (Indian Point Energy Center) EAL criteria 8.2.3. An Alert was declared at 1849 hours. The plant is stable in Mode 3 at this time. The Auxiliary Feedwater System actuated following the manual trip, as expected. This is reportable under 10 CFR 50.72(b)(3)(iv)(A). The Emergency Diesel Generators did not start as offsite power remained available and stable. The Station Auxiliary Transformer tap changer has remained at the maximum tap changer position and is inoperable, however the unit remains on offsite power and all electrical loads are stable. No primary or secondary relief valves lifted. The plant is in Hot Standby at normal temperature and pressure with residual heat removal using auxiliary feedwater and normal heat removal through the condenser via steam dumps. There was no radiation released. Indian Point Unit Three was not affected by this event and remains at 100% power. A post trip investigation is in progress. A one hour notification of the Alert Declaration was made to the NRC Emergency Operations Duty Center officer Howie Crouch at 1907 (hrs. EST). The licensee has notified the NRC Resident Inspector, the New York State Public Service Commission, New York State EMA and local county officials. Notified R1DO (White).

  • * * UPDATE FROM CHARLES LAVERDE TO HOWIE CROUCH AT 2230 EST ON 11/07/10 * * *

At 2218 EST, the licensee exited the Alert emergency declaration. The exit criteria was that: 1) The plant was in or was proceeding to cold shutdown, 2) No radiation release was in progress or anticipated 3) All radiation levels in the plant were stable or decreasing, and 4) No limitation on access to all plant areas. The licensee has notified the NRC Resident Inspector. Notified IRD (Gott), R1DO (White), NRR EO (Bahadur), FEMA (Heyman), DHS (Doyle), HHS (Gruenspecht), USDA (John) and DOE (Turner).

  • * * UPDATE ON 11/8/2010 AT 1228 FROM MICHAEL McCARTHY TO MARK ABRAMOVITZ * * *

Approximately 50-100 gallons of oil from the transformer reached the Hudson River. The licensee notified the National Response Center and the New York State Department of Environmental Conservation. The licensee notified the NRC Resident Inspector. Notified the R1DO (White).

Reactor Protection System
Emergency Diesel Generator
Auxiliary Feedwater
Main Transformer
Residual Heat Removal
05000247/LER-2010-009
ENS 4624110 September 2010 01:29:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor Trip Due to Service Water Leak in the Main Generator Exciter HousingOn September 9, 2010, at approximately 2129 hours (EDT), Indian Point 3 manually tripped the reactor from the control room following indications of a service water leak in the Main Generator Exciter housing. Unit 3 is currently stable in mode 3. All automatic actions occurred as required. All control rods fully inserted. No primary or steam generator safety relief valves lifted. The motor driven auxiliary feedwater pumps automatically started on low steam generator level as designed. Decay heat removal is via the steam generators to the main condenser. Offsite power is available and supplying all safeguards busses. Unit 2 is unaffected and remains in Mode 5 in a forced outage for 21 RCP (Reactor Coolant Pump) repair. During the Fast Bus Transfer (the) 34 Reactor Coolant Pump tripped. The cause is being investigated. There was an inadvertent release of CO2 to 31 Main Boiler Feed Pump. The cause was due to the suction relief valve lifting which has subsequently reseated. The NRC Sr. Resident Inspector and New York State Public Service Commission have been notified. The reactor is currently being maintained at normal operating temperature and pressure.Steam Generator
Service water
Auxiliary Feedwater
Decay Heat Removal
Safety Relief Valve
Main Condenser
Control Rod
ENS 462293 September 2010 14:58:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Unit 2 Experienced an Automatic Reactor Trip Due to High Steam Generator LevelOn September 3, 2010, at approximately 1058 hrs., Indian Point Unit 2 automatically tripped from 41% power due to High Steam Generator Level. At the time of the trip, Unit 2 was performing a power reduction to take the unit offline for a planned maintenance outage. Unit 2 is currently stable in Mode 3. All automatic actions occurred as required. All control rods fully inserted with the exception of rod H-8 - which indicates 26 inches withdrawn. No primary or steam generator safety or relief valves lifted. The motor driven auxiliary feedwater pumps automatically started on low steam generator level as designed. Decay heat removal is via the steam generators to the main condenser. Offsite power is available and supplying all safeguards busses. The cause of the trip and rod H-8 position indication are under investigation. Unit 3 is unaffected and remains in Mode 1 at 100% power. The NRC Resident Inspector has been notified. Offsite notification was made to the State of New York. No press releases are planned.Steam Generator
Auxiliary Feedwater
Decay Heat Removal
Main Condenser
Control Rod
ENS 4562411 January 2010 20:59:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Trip Due to Main Generator Electrical TripAt 1559 on January 11, 2010, Indian Point Unit 2 tripped from 100% power due to a main generator electrical trip. The investigation into the generator trip is ongoing. All systems responded as expected. The auxiliary feedwater system responded as expected and is maintaining steam generator water levels. Decay heat removal is via the steam generators to the main condenser. Offsite power and plant electrical lineups are normal. No primary or secondary side relief valves lifted. The reactor plant is in mode 3 and stable. Indian Point Unit 3 was not affected and remains at 100% power. The licensee notified the NRC Resident Inspector and the N.Y. State Public Service Commission. The licensee intends to notify the Mayor's Office and issue a press release.Steam Generator
Auxiliary Feedwater
Decay Heat Removal
Main Condenser
ENS 454743 November 2009 02:41:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Reactor Trip Due to Turbine Trip Caused by a Generator Lock-Out Relay ActuationAt 2242 on November 2, 2009 Indian Point Unit 2 reactor tripped from 100% due to a turbine trip. The turbine tripped due to a generator lockout relay actuation. The investigation into the relay actuation is ongoing. All systems responded as expected. Auxiliary feed water is providing steam generator feed and levels are being maintained. No steam safeties opened and no coolant system relief or safety valves actuated. The reactor plant is in mode 3 and stable. Unit 3 was unaffected and remains at 100%. The trip was characterized as uncomplicated. All rods fully inserted and stabilized at the normal mode 3 no-load Tave and pressure. The shutdown electrical lineup is normal and the unit was not in any significant LCOs at the time of the trip. The licensee stated that they were not performing any maintenance or surveillances at the time of the trip. Initial investigation has not revealed any obvious generator electrical system issues but a detailed investigation is ongoing. The licensee has notified State and local authorities and the NRC Resident Inspector.Steam Generator
Auxiliary Feedwater
ENS 4530627 August 2009 23:45:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Trip Due to Turbine TripAt 1945 on 8/27/09 Indian Point Unit #3 automatically tripped due to a turbine trip signal. The cause for this automatic trip is under investigation. All auxiliary feedwater pumps started as expected. All control rods inserted as expected. Currently, Indian Point #3 is in Mode 3. The reactor coolant system is at Normal Operating Temperature, Pressure and Level. Offsite power is available and supplying all safeguards busses. Heat removal is to the main condenser via the steam dumps. Indian Point Unit 2 is unaffected and remains in Mode 1 at 100% power. The (NRC) Resident Inspector has been notified.Reactor Coolant System
Auxiliary Feedwater
Main Condenser
Control Rod
ENS 4525511 August 2009 00:32:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Indian Point Unit 3 Automatically Tripped During ThunderstormIndian Point Unit 3 automatically tripped from 100% power at 2032 (EDT) on 8/10/2009 due to (a) generator trip. Indian Point Unit 3 is currently in mode 3. All control rods inserted on the trip. No safety relief valves lifted due to the trip. The motor driven aux feedwater pumps automatically started on low steam generator level and are being used to maintain steam generator level. Condenser steam dumps are maintaining reactor temperature. After the trip , (the) 6.9kv bus 2 did not transfer to offsite power and is de-energized resulting in a loss of (the) '34' RCP (Reactor Coolant Pump). (The) 480v bus 2A was energized by the diesel generator. Plant operators are investigating the cause of the generator trip and loss of bus 2. Unit 2 was unaffected and remains in mode 1 at 100% power. The licensee has notified the NRC Resident Inspector. The licensee informed the State of New York and plans on issuing a press release.Steam Generator
Feedwater
Safety Relief Valve
Control Rod
ENS 4509828 May 2009 10:25:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Trip Resulting from a High Steam Generator Level Turbine TripAt 0530 EDT a power reduction commenced due to elevated vibrations on 32 MBFP (Main Boiler Feedwater Pump). When reactor power reached 60% the team was attempting to stabilize reactor power when a level excursion occurred in 32 steam generator. When level reached its high level turbine trip set point an automatic reactor trip occurred and all systems responded as expected. Auxiliary feedwater actuated as expected. The Unit is currently in mode 3 and stable with auxiliary feed water in service and reactor temperature maintained with the steam dumps to the main condenser. Investigation into the cause of the steam generator level excursion is in progress. Offsite power is available and supplying safeguard busses. Unit 2 was unaffected and remains at 100% power. The (NRC) Resident Inspector has been notified. No safety or relief valves lifted during this event.Steam Generator
Feedwater
Auxiliary Feedwater
Main Condenser
ENS 4506915 May 2009 05:53:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor Trip Due to Failure of the Main Feedwater Regulating ValveOn May 15, 2009 Indian Point Unit 3 initiated a manual Reactor Trip at 0153 in response to a failure of 33 Main Feed Regulating Valve. 33 Main Feed Regulating Valve failed open causing 33 Steam Generator Level to rise. A manual Reactor Trip signal was inserted when it was determined that the level rise in 33 Steam Generator could not be corrected. As a result of the reactor trip, the Auxiliary Feedwater System automatically actuated per plant design. Unit 3 is currently in Mode 3. This results in a condition that resulted in an actuation of the Reactor Protection System which is reportable under 10 CFR 50.72(b)(2)(iv)(B). The valid actuation of the Auxiliary Feedwater System is reportable under 10 CFR 50.72(b)(3)(iv)(A). All rods inserted during the trip. There were no relief or safety valves that lifted during the transient. The electrical grid is stable and is in the normal shutdown electrical lineup. The plant is being maintained at normal operating temperature and pressure using steam dumps to condenser to remove decay heat. Unit 2 was not affected by the trip. The licensee notified the New York Public Service Commission and the NRC Resident Inspector.Steam Generator
Feedwater
Reactor Protection System
Auxiliary Feedwater
ENS 449673 April 2009 15:36:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor Trip Due to Loss of 21 MbfpAt 1136 hours on April 3, 2009 with the plant in mode 1, Indian Point Energy Center Unit 2 experienced a 21 Main Boiler Feed Pump (MBFP) trip. Following the MBFP trip the turbine runback circuit did not actuate as expected. The plant operators attempted to perform a manual main turbine runback and inserted a manual reactor trip based on the impending trip signal of Steam Generator low level. Auxiliary feedwater automatically started as expected. Troubleshooting of the cause of the transient is in progress. Unit 2 is stable in mode 3 with AFW in service. Heat removal is to the main condenser via the steam dumps. Offsite power is available and supplying all safeguards busses. Unit 3 is not affected and remains in mode 6 for 3R15. The (NRC) Resident Inspector has been notified.Steam Generator
Auxiliary Feedwater
Main Turbine
Main Condenser
ENS 447492 January 2009 15:09:0010 CFR 50.72(b)(3)(iv)(A), System ActuationUnexpected Autostart of Emergency Diesel Generator During Surveillance TestingDuring performance of 3-PT-M62C (Rev 7) 480V Undervoltage/Degraded Grid Protection System Bus 6A Functional Test, Bus 6A was inadvertently de-energized. (Number) '32' Emergency Diesel Generator (EDG) autostarted and is supplying Bus 6A. Additionally, '32' and '33' Auxiliary Feed Pumps started due to ESF actuation based on loss of Bus 6A. All equipment operated as required. Investigation is in progress as to the cause of loss of power to Bus 6A. Bus 6A remains energized by '32' EDG. The licensee informed the NRC Resident Inspector.Emergency Diesel Generator
ENS 445549 October 2008 16:54:0010 CFR 50.72(b)(3)(iv)(A), System ActuationEmergency Diesel Generator and Auxillary Feedwater Actuation Due to Bus UndervoltageOn October 9, 2008, during scheduled monthly testing per surveillance procedure 3-PT-M62C, '480 volt Undervoltage Degraded Grid Protection System Bus 6A Functional,' the normal supply power to 480 volt safeguards Bus 6A de-energized resulting in the start and load of Bus 6A by the 32 Emergency Diesel Generator (EDG), and the actuation of the '33' motor driven Auxiliary Feedwater Pump (AFWP), and the '32' steam driven AFWP. All equipment performed as designed. Auxiliary feedwater (AFW) was injected into the Steam Generators (SG). Core reactivity changes as a result of AFW injection resulted in an 0.1% increase in reactor power. SG level change from normal of approximately 1-2% with no actuation of SG alarms, no challenge to automatic control, and no rod movement. No significant change to the Nuclear Instrumentation was observed. Normal supply power was restored to bus 6A and the EDG-32 returned to Auto. Investigation into the cause of the event is in progress. Unit 2 was unaffected and is at 100% power. The licensee notified the NRC Resident inspector.Steam Generator
Feedwater
Emergency Diesel Generator
Auxiliary Feedwater
ENS 443834 August 2008 16:00:0010 CFR 50.72(b)(3)(iv)(A), System ActuationSpecified System Actuation - Both Auxiliary Boiler Feedwater Pumps Started UnexpectedlyOn August 4, 2008 at approximately 1200 hours, both motor driven auxiliary boiler feed pumps automatically started during the performance of procedure 3PT-M13B1, 'Reactor Protection Logic Channel Functional Test Train B'. Operations secured the pumps and returned them to auto at approximately 1207 hours. The event did result in water addition to the steam generators but Operations did not observe any reactivity changes on the nuclear instrumentation. The cause of the event is under investigation. Operators did observe a 2% increase in steam generator water level but no limits or alarms were approached. The licensee has notified the NRC Resident Inspector and New York State Public Service Commission.Steam Generator
Feedwater
ENS 4415321 April 2008 15:25:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor Trip Due to Lowering Steam Generator Water LevelOn April 21 2008, at approximately 1123 hours, during power ascension from a scheduled refueling outage, Unit 2 experienced an inadvertent main turbine runback. The runback initiated for unknown reasons from an initial reactor power of approximately 37%. As a result of the runback, operators observed decreasing steam generator levels and initiated a manual reactor trip at 1125 hours. As a result of the reactor trip, the auxiliary feedwater pumps actuated on a low steam generator level as designed. Prior to the runback, one of two main feedwater pumps was operating. The unit is stable and in Mode 3. Operators closed the main steam isolation valves as a result of indications of lowering RCS temperature. A 4-hour non-emergency notification is provided for a reactor trip while critical and 8 hour non-emergency notification is provided for a valid actuation of the auxiliary feedwater system. All rods inserted as expected. Decay heat is being removed by AFW through the atmospheric steam dumps. Offsite power is in a normal configuration. The licensee notified the NRC Resident Inspector.Steam Generator
Feedwater
Main Steam Isolation Valve
Auxiliary Feedwater
Main Turbine
ENS 4409125 March 2008 15:18:0010 CFR 50.72(b)(3)(iv)(A), System ActuationInadvertent Actuation of Emergency Diesel Generator During Surveillance TestingOn March 25, 2008, during scheduled monthly testing per surveillance procedure M628, '480 Volt Undervoltage Degraded Grid Protection System Bus 5A Functional', an Instrumentation & Control technician conducting the test inadvertently caused an undervoltage condition on 480 volt AC safeguards Bus 5A, resulting in the automatic actuation of the associated Emergency Diesel Generator (EDG)-33. In accordance with design EDG-33 started and loads on Bus 5A were stripped and required loads were sequenced back onto Bus 5A. All equipment performed as designed. Normal power for Bus 5A has been restored and all equipment returned to pre-event condition. Investigation into the cause of the event is in progress. Unit 2 is currently in a refueling outage and was unaffected. Licensee has notified the NRC Resident Inspector and the State Public Service Commission.Emergency Diesel Generator
ENS 4408924 March 2008 02:16:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor Trip - Loss of Speed on MbfpThe Indian Point Unit 2 reactor was manually tripped from 94% power at 2216 on 3/23/08 due to a loss of speed on 22 main boiler feed pump (MBFP). Indian Point Unit 2 is currently in mode 3 with all automatic actions for a manual reactor trip occurring as required. Indian Point Unit 2 was in a coast down in advance of a scheduled refueling outage. The reactor was manually tripped as required by abnormal operating procedure 2-AOP-FW-001. All control rods inserted on the trip. No safety or relief valves lifted due to the trip. The motor driven aux feedwater pumps automatically started on low steam generator level and are being used to maintain steam generator level. Condenser steam dumps are maintaining reactor temperature. The Unit 2 electrical lineup is the normal shutdown electrical lineup. The licensee has notified the state Public Service Commission. Unit 3 was unaffected and remains in mode 1 at 100% power. The licensee has notified the NRC Resident Inspector. The licensee expects to issue a media release.Steam Generator
Feedwater
Control Rod
ENS 432856 April 2007 15:11:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release
10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(a)(1)(i), Emergency Class Declaration
Main Generator Transformer Explosion - No Impact on Plant Safety Related Systems

At 1143 on 4/6/07 the licensee declared an Unusual Event due to a main transformer explosion in the protected area. The event was declared in accordance with EAL 8.2.2. Unit 3 automatically tripped due to a load reject at the main generator. The Unit is currently stable at normal operating temperature and pressure. Decay heat is being removed via the steam dumps to the main condenser. All emergency diesel generators are available if needed but safety buses are currently supplied with offsite power. At the transformer site the deluge system actuated and the fire brigade responded. The fire was out at the time of the report The licensee informed the NRC Resident Inspector.

* * * UPDATE AT 1232 ON 4/6/07 FROM LAUGHLIN TO HUFFMAN * * *

The offsite local fire department was called by the licensee but their support was not needed and they were released.

* * * UPDATE AT 1259 ON 4/6/07 FROM LAUGHLIN TO HUFFMAN * * * 

The licensee exited Unusual Event at 1247 based on the fact that the fire was confirmed to be extinguished, there was no damage to safety equipment and the plant was in a safe and stable condition.

* * * UPDATE AT 1440 ON 4/6/07 FROM PRUSSMAN TO KNOKE * * * 

On April 6 at 1143 hours, an unusual event was declared based on Emergency Action Level 8.2.2, an explosion in the 'B' phase of the 31 main transformer. This is a one hour reportable event to the NRC made at 1159 hours. This is an update of EN 43285. The NUE was terminated at 1247 hours. The State and County were also notified of the unusual event. A press release was made. Although no one was injured as a result of this event, a four hour report is being made since this is related to on-site personnel safety. The main generator tripped and this resulted in a consequential reactor trip. The Reactor Protection System shut down the reactor at 1109 hours, a four hour report. The plant operated as designed and the Auxiliary Feedwater System actuated, an eight hour report. The fire was reported to the Control Room at 1111 hours. The fire was put out in less than 15 minutes. The event is currently under investigation. The header information in this event was revised as a result of this update to indicate 'Offsite Notification.'

Reactor Protection System
Emergency Diesel Generator
Auxiliary Feedwater
Main Transformer
Main Condenser
ENS 432723 April 2007 08:16:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor Trip While Performing Boiler Feed Pump MaintenanceThe Indian Point Unit 3 reactor was manually tripped at 04:16 on 4/3/2007 due to low steam generator levels that occurred while the 31 MBFP (main boiler feed pump) speed control was being isolated for maintenance. Indian Point Unit 3 is currently in mode 3 with all automatic actions for a manual reactor trip occurring as required. Unit 2 was unaffected and remains in mode 1 at 100% power. The reactor was manually tripped when steam generator levels reduced to 18% in all four steam generators. All rods inserted on the trip. No safety or relief valves lifted due to the trip. The motor driven aux feedwater pumps automatically started on low steam generator level and are being used to maintain steam generator level. Atmospheric steam dumps are maintaining reactor temperature. The Unit 3 electrical lineup is the normal shutdown electrical lineup. The licensee has notified the state Public Service Commission. The licensee will notify the NRC Resident Inspector.Steam Generator
Feedwater
ENS 4319928 February 2007 11:35:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor Trip Following Malfunction of Pressure TransmitterAt approximately 0633 AM on February 28, 2007, control room operators manually initiated a reactor trip after observing decreasing steam generator levels as a result of low feed water flow. Control room alarms indicated low main feed water pump suction pressure which was subsequently, attributed to a malfunction of the main feed water pump low suction pressure cutback pressure transmitter (PT-408B) on the common main feed pump water supply header. The malfunction of the main feed pump water low suction cutback pressure transmitter resulted in a cutback of both main feed water pumps reducing main feed water flow to the steam generators and causing decreasing steam generator levels. All control rods fully inserted and all safety systems responded as expected. The auxiliary feedwater system actuated as expected from low steam generator levels which occurs as a result of a full power reactor trip. The emergency diesel generators (EDGs) did not start as offsite power remained available. The plant was stabilized in hot shutdown with the (Auxiliary Feedwater System) providing decay heat removal via the main condenser. The main feed water pumps are shutoff and secured. The event is under investigation and a post trip review is being conducted. A courtesy call to stakeholders will be made. All EDGs remain available in standby. No steam generator Power Operated Relief Valves or Main Steam Safety Valves lifted. The licensee notified state and will notify local authorities. The licensee plans to issue a press release. The licensee notified the NRC Resident Inspector.Steam Generator
Feedwater
Emergency Diesel Generator
Auxiliary Feedwater
Main Steam Safety Valve
Decay Heat Removal
Main Condenser
ENS 4301630 November 2006 19:45:0010 CFR 50.72(b)(3)(iv)(A), System ActuationAuxiliary Feedwater Pump Automatic Start

On November 30, 2006, at approximately 14:45 hours, an Auxiliary Feed Water (AFW) System actuation signal was generated as a result of maintenance activities on the 21 Main Boiler Feed Pump (MBFP). Both motor driven AFW pumps were running at the time and were not automatically started due to previously being placed in service to provide feed water flow to the steam generators. The actuation signal isolated the Steam Generator blowdown Containment Isolation Valves. Both MBFPs were isolated and not feeding the steam generators at the time the actuation signal was generated. The plant was in Mode 3 (Hot Standby) for a forced outage and 21 MBFP was in a maintenance / test condition. The automatic actuation occurred due to the reset oil pressure lowering below the trip set point and initiating an automatic actuation signal. The licensee notified the NRC Resident Inspector.

  • * * UPDATE ON 12/01/06 AT 0151 EST BY MR. TROULET TO MACKINNON * * *

At 2100 on 11/30/2006, as a result of continuing work activities on the 21 MBFP an AFW System actuation signal was generated. Both motor driven AFW pumps were running at the time and were not automatically started due to previously being placed in service to provide feed water flow to the steam generators. 21 MBFP has been successfully placed in service." The NRC Resident Inspector was notified of this update by the licensee. Notified R1DO (James Dwyer).

Steam Generator
Auxiliary Feedwater
05000425/LER-2015-002
ENS 4299315 November 2006 19:00:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Trip During Electrical Main Generator TroubleshootingOn November 15, 2006, at 14:00 hours, an automatic reactor trip occurred during troubleshooting of the Main Generator Exciter Generrex power supply, when an electrical spike resulted in a turbine trip which caused a reactor trip. All control rods fully inserted and safety equipment operated as expected. The Auxiliary Feedwater (AFW) System actuated as expected as a result of a low steam generator level from the reactor trip and started the motor driven AFW pumps. The Emergency Diesel Generators did not start as offsite power remained available. The plant was stabilized in hot standby with decay heat being removed by the main condenser. There were no radiation releases. The condition is under investigation and a post trip review is being conducted. No PORVs or SG safety valves lifted during the event. The electrical plant is in a normal shutdown lineup and the EDGs are operable in standby. There was no affect on Unit 3 operation due to this event. The licensee notified the NRC Resident Inspector, and stated that IPEC communications has transmitted an IPEC Status Report which provides a status to local, state, and federal agencies.Steam Generator
Emergency Diesel Generator
Auxiliary Feedwater
Main Condenser
Control Rod
ENS 4280024 August 2006 15:35:0010 CFR 50.72(b)(3)(iv)(A), System ActuationMain Feedwater Pump Trip During StartupOn August 24, 2006, at approximately 1135 hours, during startup from a reactor trip on August 23, 2006, a trip of Main Boiler Feedwater Pump (MBFP) 21 sent an actuation signal to automatically start both motor driven Auxiliary Feedwater Pumps (AFPs) as well as isolate steam generator blowdown, and close MBFP discharge valve BFD-2-21. At the time, the plant was at about 1% power and both motor driven AFPs were in operation. All plant responses were as expected. The cause of the MBFP trip is under evaluation. Offsite power is normal and emergency diesel generators are operable." The plant is currently at 8% power. The licensee notified the NRC Resident Inspector.Steam Generator
Feedwater
Emergency Diesel Generator
Auxiliary Feedwater
ENS 4279723 August 2006 14:35:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Scram Due to Mismatch of Primary Power and Secondary Load Indications

On August 23, 2006, at 1035 hours, the Reactor Protection System was manually actuated while at reduced load of approximately 68 percent reactor power upon indication of an apparent disparity in net electric load. It was determined that the cyclic operation of the condenser steam dumps varied steam to the turbine resulting in the indicated drop in electrical output power from about 500 Mwe to 150 Mwe. The manual trip is reportable under 10 CFR 50.72(b)(2)(iv). The event started when heater drain tank pumps 21 and 22 tripped, apparently due to a failure of the automatic heater drain level control valves that could not be manually corrected from the single controller. Reactor operators reduced load in accordance with station procedures to respond to the trip of the heater drain tank pumps and stabilized reactor power at 77%. As a result of the required load reduction delta flux was outside of the operational limit envelope specified at 77% reactor power. This required a further load reduction to less than 50 percent as per Technical Specification 3.2.3. At approximately 68% percent power the reactor was manually tripped due to the mismatch of primary power and secondary load indications. The Auxiliary Feedwater System actuated following the manual trip as expected. This is reportable under 10 CFR 50.72(b)(3)(iv)(A). A high-high water level signal was received on the 22 Steam Generator. This was due to a feedwater regulating valve that did not fully close. The feedwater isolation valves closed. All other safety systems actuated as required and safety equipment operated as expected. The Emergency Diesel Generators did not start as offsite power remained available and stable. No primary or secondary relief valves lifted. The plant is in Hot Standby at normal temperature and pressure with residual heat removal using auxiliary feedwater and normal heat removal through the condenser via steam dumps. There was no radiation released. A post trip investigation will be performed prior to restart. The licensee notified the NRC Resident Inspector.

      • UPDATE FROM GEORGE DAHL TO JOHN KNOKE AT 1830 EDT ON 08/23/06 ***

This is an update of non-emergency Event Notification 42797 that was previously made on August 23, 2006. Clarification is provided to include reporting of the Event Classification for actuation of a second system (automatic feedwater isolation) as an 8-Hr. Non-Emergency per 10 CFR 50.72(b)(3)(iv)(A). This update revises the wording as follows: The feedwater isolation valve was manually closed. After receipt of the high-high level trip signal, 21, 23, and 24 feedwater isolation valves automatically closed. This is also reportable under 10 CFR 50.72(b)(3)(iv)(A). The licensee notified the NRC Resident Inspector. Notified R1DO (Conte).

Steam Generator
Feedwater
Reactor Protection System
Emergency Diesel Generator
Auxiliary Feedwater
Residual Heat Removal
ENS 4272021 July 2006 14:30:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor Trip Due to Sparks from Under Main Generator

At 1031 hours on July 21, 2006, the reactor operator manually tripped the reactor from 100% power resulting in turbine trip and actuation of auxiliary feedwater. This is reportable under 10 CFR 50.72(b)(2)(iv)(B). 31 Reactor Coolant Pump tripped after the reactor trip. All other systems operated as expected. Steam is being condensed by the condenser. The reactor was tripped due to an abnormal condition under the main generator; electrical arcing/sparking was observed. The reactor will remain shutdown until the cause of the arcing/sparking is identified and corrected. There was no indication of fire but the fire brigade was called out. The observed arcing and sparking from underneath the main generator secured after the turbine trip. All control rods fully inserted on the reactor trip. The electric plant is in a normal shutdown lineup and the EDGs are operable. The unit is stable and Unit 2 was not affected. The licensee notified the NRC Resident Inspector and the New York Public Service Commission.

  • * * UPDATE PROVIDED BY DON CROULET TO JEFF ROTTON AT 1416 EDT ON 07/21/06 * * *

Licensee reported the AFW actuation as a Specified System Actuation per 10 CFR 50.72(b)(3)(iv)(A). The licensee notified the NRC Resident Inspector. Notified the R1DO (Kinneman)

Auxiliary Feedwater
Control Rod
ENS 426876 July 2006 07:52:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Reactor Trip Due to Generator Differential

Indian Point Unit 3 tripped on Generator Differential (Direct Generator Trip). Current conditions are stable, mode 3 operation with all automatic actions occurring properly. Steam Generators levels are stable on aux. feed water. Unit 2 was unaffected by the trip. All control rods inserted fully and decay heat is being removed via steam dump to the condenser. All required safety related systems are working properly and the electrical buses and diesel generators are in their normal alignment. The licensee will notify the NRC Resident Inspector.

  • * * UPDATE AT 0938 ON 07/06/08 B. ROKES TO W. GOTT * * *

The Auxiliary Feedwater System actuated and the Auxiliary Feedwater Pump started as designed due to the reactor trip. The actuation of the Auxiliary Feedwater System was the result of Steam Generator shrink/swell effect due to the reactor trip at full power. The actuation of the Auxiliary Feedwater System is an eight-hour non-emergency event reportable under 10 CFR 50.72(b)(3)(iv). The licensee will notify the NRC Resident Inspector. Notified R1DO (P. Henderson)

Steam Generator
Auxiliary Feedwater
Control Rod