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 Issue dateTitleTopic
ML20084N64631 March 1977Followup AO 50-249/75-44A:on 751125,offgas Activity Increased.Ge Insp Revealed Major Defect in Fuel Assembly DD-418.Assembly Removed from ReactorFuel cladding
ML20084E36329 June 1976Supplemental AO 50-237/75-11A:on 750127,core Spray Injection Line through-wall Cracks Discovered.Stainless Steel Portion of Core Spray Piping from Vessel Nozzle to Second Isolation Valve Replaced w/SA-333 Grade 6 Carbon Steel
ML20084N68329 June 1976Supplemental AO 50-249/1975-42A:motor Operated Valve 3-1501-5D Failed to Open During Testing Due to Thermal Overload Trip.Caused by Undersized Overload Heaters.Overload Heater Will Be Replaced W/Larger Capacity Unit
ML20084D11913 April 1976AO 50-237/75-39A:on 750612,diesel Generator Experienced Starting Failures.Possibly Caused by Two Gouged & Burred Areas on Ring Gear.Ring Gear Repaired
ML20084D15414 January 1976AO 50-237/75-38A Supplementing AO-50-237/75-38 Re Failure of MO-2-1301-2 Valve to Operate.Apparently Caused by Excessive Cycling of Valve.Valve Stem Probably Experienced Metal Fatigue Due to Multiple Actuations
ML20090E45817 December 1975Supplemental AO 50-237/75-44:diesel Generator Failed to Start.Caused by Air Relay Valve Failure Due to Sticking O-rings.O-rings Replaced
ML20084N65411 December 1975AO 50-249/75-44:on 751125,offgas Increase Exhibited Which May Have Represented Abnormal Degradation of Fuel Cladding.Cause Unknown.Investigation UnderwayFuel cladding
ML20090E43220 November 1975AO 50-237/75-52:on 751116,MSIV AO 2-203-1C Closing Time Found Below Tech Spec Section 3.7.D.1.Caused by Out of Adjustment Hydraulic Bleedoff Valve.Bleedoff Valve Readjusted
ML20090E4756 November 1975AO 50-237/75-51:on 751031,torus Water Level Exceeded Tech Spec Limit During HPCI Sys Surveillance.Caused by Operator Failure to Verify Proper Valve Lineup.Water Pumped from Torus Until Level Dropped Below Tech Spec Limits
ML20084N68820 October 1975AO 50-249/75-42:on 750920,motor Operated LPCI Suction Valve 3-1501-5D Failed to Open Twice During Testing. Apparently Caused by Defective Valve Motor.Valve Motor Will Be Replaced
ML20090E44717 October 1975AO 50-237/75-48:on 751007,through-wall Crack Discovered in Drywell/Torus Nitrogen Purge Line 1604-18.Caused by Rapid & Uneven Contraction of Line Tee Connection Due to Liquid Nitrogen Impingement Resulting from Boiler Failure
ML20090E47817 October 1975AO 50-237/75-49:on 751009,LPCI Loop Selection Logic Circuitry Failed to Select Preferred B Loop.Caused by Out of Calibr Differential Switch 261-34 & Electrically Shorted Switch 261-34D.Mod to Provide Signal Dampening Initiated
ML20084N83315 October 1975Supplemental AO 50-249/75-22:plant Mod Being Initiated to Eliminate Valve Seat Failures Due to Cryogenic StressPacking leak
ML20090E4819 October 1975AO 50-237/75-45:on 750929,HPCI Turbine Failed to Trip at Designated Reactor Coolant Level.Caused by Open Circuit in Turbine Trip Solenoid Valve Coil Due to Failure of Cold Solder Joint within Coil.Hpci Trip Solenoid Valve Replaced
ML20090E4829 October 1975AO 50-237/75-46:on 750929,reactor Scrammed on High Drywell Pressure During Drywell Inerting Process.Caused by Operator Valving Error,Allowing Nitrogen Flow to Bypass Inerting Pressure Control Valve Into Drywell.Operators Cautioned
ML20084N6717 October 1975AO 50-249/75-43:on 750927,leak Discovered in Drain Line from Feedwater Heater 3D3 to Heater 3C3.Caused by Poor Weld Installation of Drain Line Pipe Support.Crack Ground Out & Pipe Rewelded
ML20090E4642 October 1975AO 50-237/75-44:on 750923,diesel Generator Failed to Start.Caused by Operator Failure to Follow Monthly Insp Procedure & QC Procedure for safety-related Component Replacement.Air Start Sys Inspected & Seal Ring Replaced
ML20090E47019 September 1975AO 50-237/75-43:on 750911,diesel Generator Cooling Water Pump Main Breaker Tripped.Caused by Excessive Heat Buildup within Breaker Housing.Breakers on Buses Replaced & Cover Plates Removed for Ventilation
ML20084N69116 September 1975AO 50-249/75-41:on 750908,intermediate Range Monitors 11, 12,14,16 & 18 Failed to Respond During Plant Startup. Apparently Caused by Personnel Accidentally Loosening Cables.Cables Replaced
ML20090E4918 September 1975AO 50-237/75-42:on 750829,diesel Generator Cooling Water Pump Tripped,Followed by Diesel Generator Trip on High Temp. Cause Not Established.Investigation of Cooling Water Pump & Associated Breakers Continuing
ML20084N8414 September 1975AO 50-249/75-37:on 750826,pressure Switches PS3-263-53A,53B & 53C Had Setpoints Above Tech Spec Limit.Apparently Caused by Setpoint Drift Due to Long Periods at Zero Pressure. Setpoints Reset
ML20084N7774 September 1975AO 50-249/75-38:on 750826,pressure Switches 3-263-52A1 & 52A2 Found W/Setpoints Above Tech Spec Limit.Apparently Caused by Setpoint Drift Due to Long Periods of Inactivity. Switches Reset
ML20084N7284 September 1975AO 50-249/75-40:on 750827,during Routine Instrument Surveillance,Pressure Switches PS3-263-51A & 51B Had Setpoints Above Tech Spec Limit.Caused by Drifting Due to Long Periods at Zero Pressure.Switches Reset
ML20084N7483 September 1975AO 50-249/75-39:on 750826,overload Relay Tripped Twice on Motor Operated Isolation Valve 3-220-1.Caused by Defective Overload Relay.Relay Replaced
ML20084N7942 September 1975AO 50-249/75-36:on 750823,reactor High Pressure Sensors 263-55A,55B & 55C Found W/Setpoints Above Tech Spec Limit. Apparently Caused by Extended Periods at Zero Pressure. Switches Reset
ML20084N86629 August 1975AO 50-249/75-35:on 750821,circuit Breaker 152-3403 Failed to Trip During Breaker Trip Test.Caused by Failure of Trip Coil.Breaker Replaced
ML20084N88215 August 1975AO 50-249/75-34:on 750807,isolation Condenser High Flow Switches 1349A & B Exhibited Instrument Setpoint Drift.Cause Unknown.Switches Reset
ML20084N90531 July 1975AO 50-249/75-32:on 750721,clamp Bolt Keeper Tack Welds on Jet Pumps 6 & 17 Failed.Caused by Poor Tack Welding.Clamp Bolt Keepers Rewelded & Successfully Retested
ML20085E9559 July 1975AO BFAO-50-260/759T:on 750709,broken Stem Found on second- Stage Pilot of Main Steam Release Valve 1.Break Point Just Under Lock Nut Above Actuating Piston.Site Inspector Advised
ML20084N9143 July 1975AO 50-249/1975-31:on 750626,cracks Discovered on Collet Housings of Control Rod Drives 984,883,1032 & 1099. Apparently Caused by Temp Cycles Drive Experiences During Reactor Scram.Analyses Initiated
ML20084D2113 July 1975AO 50-237/75-36:on 750606,MSIV-1C 10% Closure Limit Switch Failed.Caused by de-energized 10% Closure Relay.Switch Reassembled W/Less Torque Applied to Switch Contact Assembly Screws.Switch Operated Successfully
ML20084E0463 July 1975AO 50-237/75-22:on 750507,vol Bounded by Valves 2-301-98 & 2-301-99 Exceeded Max Allowable Limits During Local Leak Rate Testing.Caused by Dirty Mating Surfaces of Disc & Seat. Seating Surfaces Cleaned & Valve Returned to Svc
ML20084D17725 June 1975AO 50-237/75-58:on 750615,isolation Condensor Outboard Steam Supply Valve MO-2-1301-2 Found W/Bent Stem.Possibly Caused by Combination of Excessive Cycling of Valve 1301-2 & Maladjustment of Limit Switches for Valve Travel
ML20084D03823 June 1975AO 50-237/75-41:on 750613,electromatic Relief Valve 2-203-3C Failed to Operate During Test at Rated Pressure.Apparently Caused by Leaking Seal Rings in Valve.Valves Replaced by Rebuilt Valves & Successfully Tested
ML20084D05320 June 1975AO 50-237/75-40:on 750611,five Arrays Exhibited 5% Scram Times Exceeding Tech Specs Limits During 2x2 Array Test. Caused by High Regulated Pressure in Scram Valve Air Header. Regulator Reset to Correct Pressure
ML20084N77420 June 1975Followup to AO Rept Re Correlation of Fuel Failures, Identified by Wet Sipping Tests to Calcualted Violations of GE Pciomr
ML20084D14118 June 1975AO 50-237/75-39:on 750612,diesel Generator Failed to Start During Surveillance Run.Cause Not Known.Suitable Action to Be Taken When Cause Determined
ML20084N97513 June 1975AO 50-249/1975-30:on 750605,standby Liquid Control Pump Discharge Relief Valves Found at Setpoints Lower than Tech Spec Limits.Caused by Setpoint Drift.Valves Cleaned & Reset
ML20084D19113 June 1975AO 50-237/75-37:on 750604,diesel Generator Failed to Start on First Attempt.Cause Undetermined.Suitable Action Will Be Taken When Cause Determined
ML20084D2165 June 1975AO 50-237/75-35:on 750526,explosion Occurred in B Offgas Sys.Cause Not Determined.Load Drop to Minimize Releases Into Bldg Started
ML20084D2215 June 1975AO 50-237/75-33:on 750526,torus Level Found to Be Low.Caused by Personnel Error.Water Pumped from Condensate Storage Into Torus Via HPCI Min Flow Line.Importance of Card Tagging Procedures Emphasized
ML20084D2253 June 1975AO 50-237/75-32:on 750526,electromagnetic Relief Valve 203-3B Failed to Open During post-maint Testing of Valves. Cause Unknown.Corrective Actions to Be Determined When Cause Discovered
ML20084D41230 May 1975AO 50-237/75-31:on 750522,containment Cooling Svc Water Valve MO-1501-3A Failed to Control Flow During Scheduled Surverillance.Cause Not Determined.Design Mods for Valves Being Evaluated
ML20084D42730 May 1975Ao:On 750520,electromagnetic Relief Valve 2-203-3C Failed to Open During Scheduled Surveillance.Caused by Adjustment Problem in Pilot Valve Linkage.Capscrew Out of Adjustment. All Electromagnetic Relief Valves Adjusted
ML20084D43229 May 1975AO 50-237/75-29:on 750519,limit Switch Indicating 10% Closure on 1C MSIV Failed During Startup.Caused by Failure to Reinstall 1C Limit Switch & to Perform Tests.Switch Reinstalled
ML20084D88127 May 1975AO 50-237/75-27:on 750421,control Rod Withdrawn for Friction Testing While Both GE & Util Employees within Direct Line of Sight of Core.Caused by Disregard of Master Procedure & Failure of Testing Procedure to Include Precaution
ML20084D88323 May 1975AO 50-237/75-26:on 750415,diesel Generator Starting Air Motors Failed to Start Diesel Engine.Caused by Motor Pinion Gears Jamming Against Teeth of Ring Gear Preventing Proper Engagement.Vendor Suggested Mod to Regulate Pressure
ML20084D37823 May 1975AO 50-237/75-25:on 750116,Noshua Silver Duct Tape Dropped Into Reactor Vessel Annulus from Feedwater Sparger Work Platform.On 750516,decision Made to Start Reactor W/O Recovering Tape Rendering Tape Drop Reportable
ML20084D44123 May 1975AO 50-237/75-28:on 750506,containment Cooling Svc Water Valves MO-1501-3A & 3B Failed to Control Flow During Lpci/ Containment Cooling Logic Test.Caused by Bent Valve Stems. Increased Size Stem Valves on Order
ML20084E04321 May 1975AO 50-237/75-23:on 750511,diesel Generator Overheated After Inadvertent Fast Start & ECCS Inadvertently Initiated. Overheating Caused by Loss of Cooling Water Pump Suction. ECCS Initiation Caused by Valving Out Flow Check Valve