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Category:Code Relief or Alternative
MONTHYEARML22255A1022022-09-21021 September 2022 Authorization and Safety Evaluation for Alternative Relief Request No. 10 - Hardship or Unusual Difficulty Without Compensating Increase in Level of Quality or Safety ML22151A0012022-06-0707 June 2022 Authorization and Safety Evaluation for Relief Request 20, Revision 1 ML22038A1872022-02-0909 February 2022 Authorization and Safety Evaluation for Relief Request No. 19 (RR19) - the Use of an Alternative to ASME Code Case N-729-6 for Replacement Reactor Vessel Closure Head Penetration Nozzle 85 ML22020A4052022-01-24024 January 2022 Summary of January 14, 2022, Teleconference with Florida Power & Light Co. Regarding Verbal Authorization of Request for Alternative to the Requirements of ASME Code for Examination of Closure Head CEDM Housing 27 Canopy Seal Weld ML22026A1022022-01-13013 January 2022 RAIs for RR 20 - Alternate Examination of Canopy Seal Weld Control Element Drive Mechanism Number 27 Housing ML22011A0852022-01-0707 January 2022 Relief Request Number 10 Acceptance Review ML21236A1312021-09-30030 September 2021 Authorization of RR 15 Regarding Extension of ASME Requirements Related to Reactor Pressure Vessel Weld Examinations from 10 to 20 Years ML21027A2262021-02-17017 February 2021 Approval of Alternative to ASME Code, Section XI to Use an Alternative Inservice Inspection Schedule for the Reaction Vessel Closure Head Bolting ML20329A4022021-02-0303 February 2021 Approval of Alternative to Use ASME Code Case N-513-4 for Alternative Repair of Intake Cooling Water System L-2020-160, Extension of St. Lucie Unit 2 RPV Welds from 10 to 20 Years2020-10-30030 October 2020 Extension of St. Lucie Unit 2 RPV Welds from 10 to 20 Years ML20099A3482020-06-25025 June 2020 Safety Evaluation for Relief Request for Fifth Ten-Year Inservice Inspection (ISI) Interval - Alternative Risk-Informed Inservice Inspection Program for Class 1 and 2 Piping Welds L-2018-188, Inservice Inspection Plan - Fifth Ten-Year Interval Unit 1 Relief Request 62018-09-28028 September 2018 Inservice Inspection Plan - Fifth Ten-Year Interval Unit 1 Relief Request 6 ML18106B1212018-04-25025 April 2018 Proposed Alternative to Use Encoded Phased Array Ultrasonic Examination Techniques ML18018A0332018-01-26026 January 2018 Safety Evaluation of Relief Requests for the Fifth 10-Year Inservice Testing Program (EPID L-2017-LLR-0113; L-2017-LLR-0017, L-2017-LLR-0018, L-2017-LLR-0119, L-2017-LLR-0120, L-2017-LLR-0121, and L-2017-LLR-0122) ML17341A4422018-01-0404 January 2018 Relief from the Requirements of the ASME Code Relief Request No. 3 for the Fifth 10-Year Inservice Inspection Interval (CAC No. MF9288; EPID L-2017-LLR-0003) ML17334A9362018-01-0404 January 2018 Relief from the Requirements of the ASME Code Regarding Relief Request No. 17, Revision 0, for the Fourth 10-Year Inservice Inspection Interval (CAC No. MF9826; EPID L-2017-LLR-0043) ML17263A1202017-10-27027 October 2017 Inservice Inspection Plan Fourth 10-Year Interval Relief Request No. 16 (CAC No. MF9827; EPID L-2017-LLR-0044) L-2017-183, Fifth 10-Year Inservice Testing (IST) Program Interval Relief Requests PR-01 Through PR-06, and PR-09,2017-10-0606 October 2017 Fifth 10-Year Inservice Testing (IST) Program Interval Relief Requests PR-01 Through PR-06, and PR-09, ML17219A1742017-08-31031 August 2017 Relief from the Requirements of the ASME Code Regarding Relief Request 12 for the Fourth 10-Year Inservice Inspection Interval L-2017-121, Proposed Alternative for the Use of Encoded Phased Array Ultrasonic Examination Techniques in Lieu of Radiography2017-07-24024 July 2017 Proposed Alternative for the Use of Encoded Phased Array Ultrasonic Examination Techniques in Lieu of Radiography ML17132A1672017-07-10010 July 2017 Inservice Inspection Plan Fourth 10 Year Interval Relief Request No. 13 L-2017-113, Inservice Inspection Plan, Fourth Ten-Year Interval Unit 1 Relief Request No. 16, Revision 02017-06-12012 June 2017 Inservice Inspection Plan, Fourth Ten-Year Interval Unit 1 Relief Request No. 16, Revision 0 L-2017-112, Inservice Inspection Plan, Fourth Ten-Year Interval Unit 1 Relief Request No. 17, Revision 02017-06-12012 June 2017 Inservice Inspection Plan, Fourth Ten-Year Interval Unit 1 Relief Request No. 17, Revision 0 ML17110A2702017-05-10010 May 2017 Inservice Inspection Plan Fourth 10-year Interval Relief Request No. 14 Rev 0 - ML16330A1182016-12-15015 December 2016 NextEra Fleet - Safety Evaluation for Proposed Alternative to the American Society of Mechanical Engineers Operation and Maintenance Code by Adoption of Approved Code Case OMN-20, Inservice Test Frequency (CAC Nos. MF8195 Through MF8201) ML16292A7612016-11-0202 November 2016 Inservice Inspection Plan Fourth 10 Year Interval Relief Request No. 11 ML15196A6232015-08-10010 August 2015 Relief Request No. 7 for Use of an Alternative to the Requirements of the ASME Code ML14013A3042014-01-30030 January 2014 Relief Request No. 7 Regarding Alternative Repair for Intake Cooling Piping ML13316A5552013-12-11011 December 2013 Relief Request Number 5 for Examination of Cold Leg Dissimilar Metal Welds ML13308C4262013-11-25025 November 2013 Relief from the Requirements of the American Society of Mechanical Engineers Code Regarding Extension of Pressure Retaining Boundary During System Leakage Test ML12313A4152012-11-0909 November 2012 Relief from the Requirements of the ASME Code ML11143A0772011-07-0101 July 2011 Relief from the Requirements of the ASME Code, Relief Request No. 9 ML11136A1382011-06-23023 June 2011 Fourth 10-Year Interval Inservice Inspection Program Plan Relief Request No. 4 and Third 10-Year Interval Inservice Inspection Program Plan Relief Request No. 11 ML1003212812010-02-0505 February 2010 Third 10-Year Internal Inservice Inspection Program Plan Request for Relief 31, Revision 1 and Request for Relief 32, Revision 1 (Tac No. ME0662) L-2010-001, Inservice Inspection Plan, Fourth Ten-Year Interval Relief Request No. 62010-01-15015 January 2010 Inservice Inspection Plan, Fourth Ten-Year Interval Relief Request No. 6 ML0904103622009-02-12012 February 2009 Relief Request No. 3, Request for Alternative to ASME Code, Section XI Repair Requirements for Refueling Water Tank Bottom, TAC MD9268 ML0828404942008-11-26026 November 2008 SE for the Continued Use of Risk-Informed Inservice Inspection Program ML0824700892008-09-25025 September 2008 Safety Evaluation of Relief Request for St. Lucie Fourth 10-year Pump and Valve Inservice Testing Program ML0805000752008-03-0404 March 2008 Safety Evaluation of Relief Request No. 29, to Use Alternative Plant Conditions on Class 1 Piping and Valves TAC No. MD5145) L-2007-195, Inservice Inspection Plan Fourth Ten-Year Interval Unit 1 Relief Request 12007-12-0707 December 2007 Inservice Inspection Plan Fourth Ten-Year Interval Unit 1 Relief Request 1 L-2007-144, Submittal of Fourth Ten-Year Interval In-Service-Test Program2007-09-11011 September 2007 Submittal of Fourth Ten-Year Interval In-Service-Test Program ML0612900562006-05-26026 May 2006 Relief Request No. 5, Rev. 1 Regarding Repair of Small Bore Piping Nozzles ML0602704862006-02-10010 February 2006 Safety Evaluation for Relief Request No. 28 Steam Generator Manway Studs ML0531401962005-11-22022 November 2005 Relief Request, Reactor Coolant Piping Hot Leg Alloy-600 Small Bore Nozzles ML0507303852005-03-14014 March 2005 Ltr, Correction to SE St. Lucie, Unit 2, Ltr, Correction to SE Methodology and SG Tube Plugging Limit Change for Amendment No. 138 ML0502103922005-01-21021 January 2005 RR #6 & 7, Vessel Head Penetration Weld Repair & Flaw Evaluation (TAC Nos. MC3860, 3861) ML0501002222005-01-19019 January 2005 Ltr, Relief Request No. 8 for Radiographic Inspection of Intake Cooling Water System Piping ML0500700852005-01-10010 January 2005 Relief, Correction to SE for Relaxation Request No. 3 ML0416105142004-06-0808 June 2004 Relief, 1995 Edition Through the 1996 Addenda & Select ASME Code, Section XI, Appendix Viii, Supplement 10 Provisions, Regarding Third 10-Year Inservice Inspection Interval ML0410408512004-04-13013 April 2004 Relief, Inservice Inspection of Reactor Vessel Bottom Area & Piping in Covering Trenches 2022-09-21
[Table view] Category:Safety Evaluation
MONTHYEARML23219A0032023-09-0101 September 2023 SLRA SER Rev 1 ML23200A1462023-07-21021 July 2023 Safety Evaluation Related to the SLRA of St. Lucie Plant, Units 1 and 2 ML22255A1022022-09-21021 September 2022 Authorization and Safety Evaluation for Alternative Relief Request No. 10 - Hardship or Unusual Difficulty Without Compensating Increase in Level of Quality or Safety ML22038A1872022-02-0909 February 2022 Authorization and Safety Evaluation for Relief Request No. 19 (RR19) - the Use of an Alternative to ASME Code Case N-729-6 for Replacement Reactor Vessel Closure Head Penetration Nozzle 85 ML21342A2092022-01-14014 January 2022 Issuance of Amendment Nos. 252 and 207 to Allow Risk-Informed Completion Times (RICT) for the 120-Volt Alternating Current (AC) Instrument Bus Requirements ML21236A1312021-09-30030 September 2021 Authorization of RR 15 Regarding Extension of ASME Requirements Related to Reactor Pressure Vessel Weld Examinations from 10 to 20 Years ML21022A2192021-02-26026 February 2021 Issuance of Amendment No. 206 to Replace the Current Time-Limited Reactor Coolant System Pressure/Temperature Limit Curves and LTOP Setpoints with Curves and Setpoints That Will Remain Effective for 55 Effective Full Power Years ML21027A2262021-02-17017 February 2021 Approval of Alternative to ASME Code, Section XI to Use an Alternative Inservice Inspection Schedule for the Reaction Vessel Closure Head Bolting ML20329A4022021-02-0303 February 2021 Approval of Alternative to Use ASME Code Case N-513-4 for Alternative Repair of Intake Cooling Water System ML20259A2982020-11-18018 November 2020 Issuance of Amendment No. 205 Regarding Modification of the Reactor Coolant Pump Flywheel Inspection Program ML20237F2572020-10-30030 October 2020 Issuance of Amendment Nos. 251 and 204 Regarding Adoption of Emergency Action Level Schemes Pursuant to NEI 99-01, Revision 6 Development of Emergency Action Levels for Non-Passive Reactors ML20099A3482020-06-25025 June 2020 Safety Evaluation for Relief Request for Fifth Ten-Year Inservice Inspection (ISI) Interval - Alternative Risk-Informed Inservice Inspection Program for Class 1 and 2 Piping Welds ML20023B3782020-02-19019 February 2020 Safety Evaluation for Relief Request RR-16, Alternate Repair of 2B Boric Acid Makeup Pump Revision for the Fourth 10-Year Inservice Inspection Interval ML20015A1232020-02-0606 February 2020 Proposed Alternative to Use Encoded Phased Array Ultrasonic Examination Techniques ML19266A0722020-01-27027 January 2020 Issuance of Amendment Nos. 250 and 202 Regarding Technical Specification Changes to Allow the Performance of Selected Emergency Diesel Generator Surveillance Requirements During Power Operation ML19254B5332019-09-30030 September 2019 Safety Evaluation for Relief Request RR#15, Revision 0, Regarding Limited Piping Examinations ML19148A7442019-07-31031 July 2019 Issuance of Amendment Nos. 161, 249, 200, 287, and 281 to Add Technical Specification Limiting Condition for Operation 3.0.6 ML19203A1662019-07-26026 July 2019 Issuance of Exigent Amendment No. 248 Technical Specification 3/4.8.1 Change to Allow for a One-Time Extension of the Allowed Outage Time for One Emergency Diesel Generator ML19115A2812019-05-31031 May 2019 Safety Evaluation for Relief Request No. 6 for the Fifth 10 Year Inservice Inspection Interval ML19058A4922019-04-23023 April 2019 Issuance of Amendment 198 Regarding Technical Specification Changes to Reduce the Number of Control Element Assemblies ML18274A2242018-11-0202 November 2018 Issuance of Amendment Nos. 246 and 197 Regarding Technical Specifications Site Area Map ML18256A0982018-10-30030 October 2018 Safety Evaluation for Relief Request No.5 for the Fifth 10-Year Inservice Inspection Interval ML18129A1492018-07-0909 July 2018 Issuance of Amendments Regarding Technical Specification Changes Related to the Auxiliary Feedwater System (CAC Nos. MG0237 and MG0238; EPID L-2017-LLA-0296) ML18106B1212018-04-25025 April 2018 Proposed Alternative to Use Encoded Phased Array Ultrasonic Examination Techniques ML18046A7122018-03-26026 March 2018 Issuance of Amendments Regarding the Unusual Event Fire Related Emergency Action Level Scheme ML18018A0332018-01-26026 January 2018 Safety Evaluation of Relief Requests for the Fifth 10-Year Inservice Testing Program (EPID L-2017-LLR-0113; L-2017-LLR-0017, L-2017-LLR-0018, L-2017-LLR-0119, L-2017-LLR-0120, L-2017-LLR-0121, and L-2017-LLR-0122) ML17334A9362018-01-0404 January 2018 Relief from the Requirements of the ASME Code Regarding Relief Request No. 17, Revision 0, for the Fourth 10-Year Inservice Inspection Interval (CAC No. MF9826; EPID L-2017-LLR-0043) ML17341A4422018-01-0404 January 2018 Relief from the Requirements of the ASME Code Relief Request No. 3 for the Fifth 10-Year Inservice Inspection Interval (CAC No. MF9288; EPID L-2017-LLR-0003) ML17257A0152017-10-31031 October 2017 Issuance of Amendments Regarding Technical Specification Changes Related to the Reactor Protection System and Limiting Condition for Operation 3.0.5 ML17263A1202017-10-27027 October 2017 Inservice Inspection Plan Fourth 10-Year Interval Relief Request No. 16 (CAC No. MF9827; EPID L-2017-LLR-0044) ML17248A3792017-10-23023 October 2017 Issuance of Amendments to Revise the Renewed Facility Operating Licenses Fire Protection License Conditions (CAC Nos. MF9681 and MF9682; EPID L-2017-LLA-0230) ML17235A5652017-10-0505 October 2017 Issuance of Amendments Regarding Technical Specification Changes Related to Component Cyclic or Transient Limits ML17219A1742017-08-31031 August 2017 Relief from the Requirements of the ASME Code Regarding Relief Request 12 for the Fourth 10-Year Inservice Inspection Interval ML17195A2912017-08-14014 August 2017 Issuance of Amendments Regarding Relocation of Radiation Monitor Requirements from Technical Specifications to Licensee-Controlled Documents ML17132A1672017-07-10010 July 2017 Inservice Inspection Plan Fourth 10 Year Interval Relief Request No. 13 ML17110A2702017-05-10010 May 2017 Inservice Inspection Plan Fourth 10-year Interval Relief Request No. 14 Rev 0 - ML17027A0782017-04-0707 April 2017 Issuance of Amendments Regarding Technical Specifications for Inservice Testing Programs (CAC Nos. MF8202 Through MF8209) ML17038A2252017-03-29029 March 2017 Issuance of Amendment No. 188 Regarding Emergency Diesel Generator Day Tank Volume ML16330A1182016-12-15015 December 2016 NextEra Fleet - Safety Evaluation for Proposed Alternative to the American Society of Mechanical Engineers Operation and Maintenance Code by Adoption of Approved Code Case OMN-20, Inservice Test Frequency (CAC Nos. MF8195 Through MF8201) ML16251A1282016-12-0505 December 2016 Issuance of Amendments to Update Appendix B to the Renewed Facility Operating License to Incorporate the 2016 Biological Opinion ML16292A7612016-11-0202 November 2016 Inservice Inspection Plan Fourth 10 Year Interval Relief Request No. 11 ML16166A4242016-10-0505 October 2016 St. Lucie Plant, Unit Nos. 1 and 2 - Issuance of Amendments Regarding the Use of a New Computer Code to Model the Containment Vacuum Analyses ML16183A1382016-09-19019 September 2016 Issuance of Amendments Regarding Technical Specification Change to Eliminate the Moderator Temperature Coefficient Surveillance Test at the End of Cycle ML16210A3742016-08-30030 August 2016 Issuance of Amendments Regarding the Adoption of Technical Specifications Task Force (TSTF) Traveler TSTF-422, Revision 2 ML16103A3972016-07-28028 July 2016 Issuance of Amendments Regarding Removal of Technical Specification for Cleaning Fuel Oil Storage Tank Sediment and Relocating Procedures to Licensee Controlled Documents ML16167A4732016-07-0505 July 2016 Safety Evaluation Regarding Implementation of Mitigating Strategies and Reliable Spent Fuel Pool Instrumentation Related to Orders EA-12-049 and EA-12-051 ML16139A5882016-05-27027 May 2016 Inservice Inspection Plan Fourth 10-Year Interval Relief Request No. 10, Revision 0 ML16124A3832016-05-25025 May 2016 St. Lucie Plant, Unit No. 1 - Issuance of Amendment Regarding Changes to the Snubber Surveillance Requirements (CAC No. MF6490) ML16063A1212016-04-19019 April 2016 Redacted - Issuance of Amendment Regarding License Amendment Request for the Transitioning to Areva Fuel ML15344A3462016-03-31031 March 2016 Issuance of Amendments Regarding Transition to a Risk-Informed, Performance-Based Fire Protection Program in Accordance with Title 10 of the Code of Federal Regulations Section 50.48(c) (CAC Nos. MF1373 & MF1374) 2023-09-01
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September 21, 2022 ST. LUCIE NUCLEAR PLANT UNIT NO. 2, AUTHORIZATION AND SAFETY EVALUATION FOR ALTERNATIVE RELIEF REQUEST NO. 10 - HARDSHIP OR UNUSUAL DIFFICULTY WITHOUT COMPENSATING INCREASE IN LEVEL OF QUALITY OR SAFETY (EPID L-2021-LLR-0089)
LICENSEE INFORMATION Recipients Name and Address: Mr. Bob Coffey Executive Vice President, Nuclear and Chief Nuclear Officer Florida Power & Light Company 700 Universe Blvd.
Mail Stop: EX/JB Juno Beach, FL 33408 Licensee: Florida Power and Light Plant Name(s) and Unit(s): St. Lucie Nuclear Plant, Unit 2 Docket No(s).: 50-389 APPLICATION INFORMATION Submittal Date: December 17, 2021 Submittal Agencywide Documents Access and Management System (ADAMS) Accession No.: ML21351A134 Alternative Provision: The licensee requested an alternative under Title 10 of the Code of Federal Regulations (10 CFR), paragraph 50.55a(z)(2).
ISI Requirement: American Society of Mechanical Engineer (ASME) Boiler & Pressure Vessels Code (Code), Section XI, Rules for Inservice Inspection of Nuclear Power Plant Components, Subsection IWB-2500, Examination Category B-O, Pressure Retaining Welds in Control Rod Drive Housings, Item B14.20.
Applicable Code Edition and Addenda: The applicable Code of Record for the fourth 10-year ISI Interval at St. Lucie 2 is ASME Code, Section XI, 2007 Edition through 2008 Addenda.
Brief Description of the Proposed Alternative: In lieu of ASME required volumetric, or surface (inside surface) ISI examinations of welds 1 through 4, on 10 percent of peripheral control element drive mechanism (CEDM) housings at St. Lucie Plant Unit 2, the subjects welds will continue to receive VT-2 examination as required by Examination Category B-P with the Reactor Coolant Pressure Boundary (RCPB) system leakage test conducted prior to startup from each refueling outage. Florida Power & Light (FPL) will perform nondestructive examinations, in accordance with ASME Code Section XI requirements, on 12 CEDM weld number 5 locations accessible via the 10 inspection ports. The examination of the accessible
welds (weld # 5) on 12 periphery CEDMs combined with the periodic system leakage tests provides an acceptable method for identification of degradation.
Reactor pressure vessel closure head (RPVCH) support structure disassembly would be required to obtain access to the subject welds. In addition, the CEDM Coil Stack Assembly (drive motor coils) would require disassembly which is a high-risk activity that involves disassembly of sensitive electrical components that position control rods which function to control reactivity and safe shutdown. There is risk of damage to components during disassembly and restoration as well as alignment and post maintenance testing that could severely impact the plant with an extended off-line condition to properly obtain long lead replacement parts, if required. The estimated dose for the disassembly, examination, and re-assembly of a single CEDM to facilitate the examination of welds 1 through 4 is 3.36 rem.
The proposed alternative has been requested in accordance with the provisions of 10 CFR 50.55a(z)(2), hardship without a compensation increase in quality and safety.
For additional details on the licensees request, please refer to the documents located at the ADAMS Accession No(s) identified above.
STAFF EVALUATION On April 24, 2015 (ML15026A405), the NRC approved a similar alternative, Relief Request Number 14, for the third 10-year lSI interval for St. Lucie Plant Unit 2. The St. Lucie Plant Unit 2 RPVCH, including CEDMs, was replaced in 2008. There are 96 CEDM housings with 32 CEDM housings located on the peripheral. Each CEDM housing contains five welds. ASME Code requires that all 5 CEDM housing welds in 10 percent of the peripheral CEDMs receive ISI examinations. To satisfy this requirement at St. Lucie Plant Unit 2, welds in a minimum of 4 peripheral housings would need to be inspected. As stated above, the proposed alternative is applicable to welds number 1 through 4. Weld number 5 will be inspected as required by ASME Code Section XI. Weld number 5 in twelve CEDM housings will receive an ultrasonic examination.
To perform the code required examination on welds number 1 through 4, FPL would need to disassemble the CEDM housing, such as removing the seismic shroud, cooling shroud, coil stack assembly, electrical cables, and other components. The removal and reinstallation of these assemblies would expose plant personnel to an estimated radiological dose of 3.36 rem per housing inspected. In addition, the assembly and disassembly of the CEDM housing may introduce human errors that may cause adverse effects on the operation of the CEDM.
Therefore, the NRC staff has determined that it is a hardship and unusually difficult for FPL to perform either surface or volumetric examinations of CEDM weld Nos. 1 through 4 in accordance with the ASME Code, Section XI. Given this hardship, the NRC staff reviewed the licensees proposed alternative to determine if it provides a reasonable assurance of structural integrity of the subject components.
CEDM housing weld number 1 joins the upper pressure housing (UPH) upper end fitting to the UPH tube which are fabricated from 316 SS. The weld material used for weld number 1 is type 316L SS consumable inserts and bare wire filler material. These base and weld materials are generally considered resistant to stress corrosion cracking (SCC) in a pressurized water reactor (PWR) RCS environment with a typical dissolved oxygen content of < 20 parts per billion (ppb) and a limiting value of 100 ppb. The RCS chemistry at St. Lucie Plant Unit 2 is controlled to reduce oxygen by the chemistry control program with a steady state limit of 100 ppb and a normal value of < 5 ppb during normal operation. If trapped air and limited mixing of RCS fluid at
the top of the CEDM UPH were to exist, resulting in a higher dissolved oxygen content, the relatively low operating temperature at weld number 1 creates an environment where SCC is unlikely to occur.
Weld number 2 joins the UPH tube to the lower end UPH end fitting, which are fabricated from 316 SS. The weld material used for weld number 2 is type 316L SS consumable inserts and bare wire filler material. As discussed above, these materials are generally considered resistant to SCC in a PWR RCS environment with a typical dissolved oxygen content of < 20 ppb with a limiting value of 100 ppb which is within the bounds of St. Plant Lucie Unit 2 RCS chemistry controls. Therefore, SCC is unlikely to occur in weld number 2.
The motor housing is fabricated from F403 modified martensitic SS using ASME Code Case N-2. Code Case N-2 requires that heat treatment for F403 is performed by either annealing or normalizing and tempering at 1250 F°. Either heat treatment produces a microstructure that has a low susceptibility to SCC. The top and bottom of the motor housing have a weld buildup (butter) using ERNiCrFe-7A (alloy 52M) weld filler metal followed by an ASME Code compliant post-weld heat treatment (PWHT) at 1250 to 1400°F. PWHT of the butter reduces residual stress and tempers the weld heat effected zone (HAZ) in the F403 material, which becomes hardened during the welding process. Reducing residual stress and tempering of the HAZ greatly reduces the potential for SCC. Alloy 52M is generally considered resistant to SCC in a PWR RCS environment, with no known cracking identified by operating experience in the US PWR fleet.
After PWHT, weld number 3 (alloy 52M) joins the F348 SS motor housing upper end fitting to the weld buildup (butter) on the F403 modified martensitic SS motor housing (top end). F348 is a columbium/tantalum stabilized stainless steel and is generally resistant to SCC in the PWR RCS environment. Therefore, it is unlikely that SCC would occur. Weld number 4 joins the alloy 52M butter on the lower end of the motor housing to the RPVCH alloy 690 penetration tube using ERNiCrFe-2 (alloy 52) filler metal or ENiCrFe-7 (alloy 152) shielded manual arc welding electrodes. Alloys 690, 52, and 152 are generally considered resistant to SCC in a PWR RCS environment, with no known cracking identified by operating experience in the US PWR fleet.
For the current St. Lucie Plant Unit 2 RPVCH, the CEDM sub-components and weld materials are similar to the previous CEDMs except that alloy 600 material and weld material (alloys 82/182) in the original RPVCH CEDMs has been replaced with alloy 690 and its compatible alloy 52/52M/152 weld materials, which are significantly more resistant to SCC. The previous RVCH was inservice for 25-years. No degradation was reported during the 25-year service history of the old CEDMs. Given the degradation free service history of similar materials in the previous and current CEDMs at St. Lucie Plant Unit 2, the change to alloys 690/52M/52/152 in lieu of alloys 600/82/182, as well as the service history of similar CDEMs in the nuclear fleet, degradation of these welds is unlikely.
A VT-2 examination is performed of all CEDMs from the 62 ft containment elevation looking down from the platform above the CEDM housings during the reactor coolant system leakage test conducted prior to startup from each refueling outage. A mandatory RPVCH bare metal visual examination, in accordance with ASME Code Case N-729-6, as modified by 10 CFR 50.55a(g)(6)(ii)(D), is performed on the St. Lucie Plant Unit 2 RPVCH every 5 years.
These examinations, coupled with the RCS inventory balance every 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> during operation, reactor cavity sump inlet flow monitoring system, containment atmosphere radiation gas monitoring system, and the containment atmosphere radiation particulate monitoring system, provides reasonable assurance that any significant leakage in the CEDM housings would be detected before leakage became a safety concern.
Based on the above, the NRC staff finds that the licensees proposed alternative provides reasonable assurance of structural integrity of subject welds and is, therefore, acceptable.
CONCLUSION The NRC staff has determined that complying with the specified requirements described in the licensees request referenced above would result in hardship or unusual difficulty without a compensating increase in the level of quality and safety.
The proposed alternative provides reasonable assurance of structural integrity of the subject components. The NRC staff concludes that the licensee has adequately addressed the regulatory requirements set forth in 10 CFR 50.55a(z)(2).
The NRC staff authorizes the use of proposed alternative, Relief Request 10, at St. Lucie Plant Unit 2 for the remainder of the fourth 10-year Inservice Inspection Interval which is scheduled to end on August 7, 2023.
All other ASME BPV Code, Section XI, requirements for which an alternative was not specifically requested and authorized remain applicable, including third-party review by the Authorized Nuclear Inservice Inspector.
Principal Contributor: Davis, Robert Date: September 21, 2022 Digitally signed by David David J. J. Wrona Date: 2022.09.21 Wrona 15:00:32 -04'00' David J. Wrona, Chief Plant Licensing Branch II-2 Division of Operating Reactor Licensing Office of Nuclear Reactor Regulation cc: Listserv
ML22255A102 *By Memo OFFICE NRR/DORL/LPL2-2/PM NRR/DORL/LPL2-2/LA NRR/DNRL/NPHP/BC*
NAME NJordan RButler MMitchell (JCollins for)
DATE 9/09/2022 9/15/2022 8/30/2022 OFFICE NRR/DORL/LPL2-2/BC NRR/DORL/LPL2-2/PM NAME DWrona NJordan DATE 9/20/2022 9/21/2022