ML20245L216

From kanterella
Jump to navigation Jump to search
SALP Repts 50-282/89-01 & 50-306/89-01 for Dec 1987- Apr 1989.Category 1 Rating Assigned in Areas of Plant Operations,Radiological Controls & Maint/Surveillance
ML20245L216
Person / Time
Site: Prairie Island  Xcel Energy icon.png
Issue date: 06/29/1989
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20245L209 List:
References
50-282-89-01, 50-282-89-1, 50-306-89-01, 50-306-89-1, NUDOCS 8907050408
Download: ML20245L216 (30)


See also: IR 05000282/1989001

Text

il

. . .
.

.

s

..-

.

'-

SALP 8-

,

1

1

l

SALP BOARD REPORT

U. S. NUCLEAR REGULATORY COMMISSION

REGION III

- - .

SYSTEMATIC-ASSESSMENT OF LICENSEE PERFORMANCE-

50-282/89001; 50-306/89001

Inspection Report Nos.

'

Northern States. Power' Company

Name of Licensee .

Pr'airie Island Nuclear Generating Plant

Name of Facility

l

December 1, 1987,'through April 30, 1989

Assessment Period j

.)

I

1

1.

l ,

i

8907050400 890629

ADOCK0500g2 .

'

PDR

,

a. .

w___-__--- . _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ - _ _ _ _ _ _

.

.

. . .

.

.

.g

..

qI

c i

.z

TABLE OF CONTENTS

Page No.

I -. INTRODUCTION . . . . . . . . . . . . . . . . . . . . . . . . . I

II. SUMMARY OF RESU LTS . . . . . . . . . . . . . . . . . . . . . 3

A. Overview . . . . . . . . . . . . . . . . . . . . . . . . 3

B. Other Areas of Interest . ............... 3

III. CRITERIA . . . . . . . . . . . . . . . . . . . . . . . . . . 4

~ ~ ~

IV. PERFORMANCE ANALYSIS . . . . . . . . . . . . . . . . . . . . 6

A. Plant Operations . . . . . . . . . . . . . . . . . . . . 6

B. Radiological Controls . . . . . . . . . . . . . . . . . 8

C. Maintenance / Surveillance . . . . . . . . . . . . . . . 10

D. Emergency Preparedness . . . . . . . . . . . . . . . . 13

E. Security . . . . . ..................14-

F. Engineering / Technical. Support . ............ 16

G. Safety Assessment / Quality Verification . . . . . . . . 20

V. SUPPORTING DATA AND SUMMARIES . . . . . . . ... . . . . . . 24

A. Licensee Activities . . . . . . . . . . . . . . . . . . 24

B. Inspection Activities . . . . . . . . . . . . . . . . . 25

C. Escalated Enforcement Actions . . . . . . . . .. . . . . 26

D. Confirmatory Action Letters (CALs)' . . . . . . . . . . 27

E. License Amendments Issued . . . . . . . . . . . . . . . 27

F. Review of Licensee Event Reports . . . . . . . . . . . 27

l

..

i

1

,

.

,.

..

. I. INTRODUCTION

L The Systematic Assessment of Licensee Performance (SALP) program is an

l integrated NRC staff effort to collect available observations and data

l on a periodic basis and to evaluate licensee performance on the basis

i

of.this information. The i rogram is supplemental to normal regulatory

processes used to ensure compliance with NRC rules and regulations. SALP

is intended to be sufficiently diagnostic to provide a rational basis for

allocating NRC resources and to provide meaningful feedback to the licensee's

management regarding the NRC's assessment of their facility's performance

in each functional area.

An NRC SALP Board, composed of the staff members listed below, met on

June 15, 1989, to review the observations and data on performance, and to

assess licensee performance in accordance with the guidance in NRC Manual

Chapter 0516, " Systematic Assessment of Licensee Performance." The

guidance and evaluation criteria are summarized in Section III of this

report. -The Board's findings and recommendations were forwarded to the

NRC Regional Administrator for approval and issuance.

This report is the NRC's assessment of the licensee's safety performance

at Prairie Island Nuclear Generating Plant for the period December 1, '1987,

through April 30, 1989.

- -

The SALP Board for Prairie Island was composed of: -

Name Title

C. J. Paperiello Deputy Regional Administrator

  • C. E. Norelius SALP Board Chairman, Director, Divi.; ion-

of Radiation Safety and Safeguards (DRSS)

  • E. G. Greenman Director, Divison of Reactor Projects (DRP)
  • H. J. Miller Director, Division of Reactor Safety (DRS)
  • W. L. Axelson Chief, Reactor Projects Branch No. 2
    • L. R. Greger Chief, Reactor Programs Branch
      • R. W. Cooper, II Chief, Engineering Branch
        • G. C. Wright Chief, Operations Branch.

B. L. Burgess Chief, Projects Section 2A l'

  • J. E. Hard Senior Resident Inspector, Prairie Island
  • L. A. Yandell Acting Project Director, Project

Directorate III-1, NRR l

  • D. C. Dilanni Project Manager, NRR

M. P. Phillips Chief, Operational Programs Section

D. H. Danielson Chief, Materials and Processes Section

M. C. Schumacher Chief, Radiological Controls and Chemistry

Section

T E. Vandel Reactor Inspector, DRS j

M. A. Kunowski Radiation Specialist, DRSS

R. N. Sutphin Project Inspector, DRP -

!

!

l

i

.

.'

..

l

.. C.'D.'Pederson Reactor Engineer, DRP. l

P. L..Hartman Senior. Resident Inspector, Monticello l

M. J. Smith Emergency Preparedness Specialist, DRSS

D. Funk Security Specialist, DRSS

J. L. Belanger Security. Specialist, DRSS

T. J. Madeda Security Specialist, DRSS

M. Moser Operations Engineer, NRR

T. Tella Reactor Inspector, DRS

1

  • Denotes voting members. (
    • Denotes voting member for Ra?lological Controls, Security and

Emergency Preparedness.

      • Denotes voting member for Maintenance and Surveillance.
        • Denotes voting member for Engineering and Technical Support.

/

!

<

- - e

)

i

l

..

.

2 .

i

!

>

i

-- .--__- ___- _ -____ _

.

'.

..

.

II. SUtiMARY OF RESULTS

A. Overview

This assessment period is from December 1,1987, through April 30,

1989. During this period, both units at Prairie Island operated

continuously, indicative of the licensec's effort and commitment to

the trip reduction program.

The areas of Radiological Controls, Emergency Preparedness and,

Maintenance and Surveillance each received a SALP Category 1,

remaining at a consistent level of good performance. Overall

performance in the Maintenance area was determined to be stronger.

than the performance observed in the Surveillance area. The area of.

Plant Operations improved to a SALP Category 1, primarily due to the

improvement in management oversight of this area. Two new areas

were rated this SALP period; Engineering / Technical Support and

Safety Assessment / Quality Verification, receiving SALP 2 and

SALP 1 ratings respectively. Security was rated a SALP 2, a decline

from the previous assessment period. The decline in this area was

attributed to a. lack of timely corrective action to address equipment

aging problems and a decline in enforcement history.

The performance ratings during the previous assessment period and

- -

this assessment period according to functional areas are given below:-

Rating Last Rating This

Functional Area Period Period Trend

Plant Operations 2 1

Radiological Controls 1 1

f

,

Maintenance / Surveillance 1/1 1

Emergency Preparedness l

1 1

Security 1 2

Engineering / Technical Support NR -2

Safety Assessment / Quality NR 1

'

Verification 1

i NR - Not Rated

l

'

B. Other Areas of Interest

None.

I

l

~

l i

3

i

1

_ _ _ _ _ . _ _ _ _ _ o

. .

.

. .

..

-

III. CRITERIA

Licensee performance is assessed in selected functional areas. Functional

areas normally represent areas significant to nuclear safety and the

environment. Some functional areas may. not be assessed because of little

or no licensee activities or lack of meaningful observations. Special

areas.may be added to highlight significant observations.

The following evaluation criteria were used to assess each functional

area:

1. Assurance of quality, including management involvement and control;

2. Approach to the resolution of technical issues from a safety

standpoint;

3. Responsiveness to NRC initiatives;

4. Enforcement history;

5. Operational events (including response to, analyses of, reporting

of, and corrective actions for);

'

, ,

6. Staffing (including management); and ,

7. Effectiveness of trcining and qualification program.

However, the NRC is not limited to these criteria and others may have

been used where appropriate.

On the basis of the NRC assessment, each functional area evaluated is

rated according to three performance categories. The definitions of

these performance categories are as follows:

Category 1: Licensee management attention and involvement are readily

evident and place emphasis on superior performance of nuclear safety or

safeguards activities, with the resulting performance substantially

exceeding regulatory requirements. Licensee resources are ample and

effectively used so that a high level of plant and personnel performance

is being achieved. Reduced NRC attention may be appropriate.

Category 2: Licensee management attention to and involvement in the

performance of nuclear safety or safeguards activities are good. The

licensee has attained a level of performance above that needed to meet

regulatory requirements. Licensee resources are adequate and reasonably

allocated so that good plant and personnel performance is being

l achieved. NRC attention may be maintained at normal levels. ,

l l

'

Category 3: Licensee management attention to and involvement in the l

performance of nuclear safety or safeguards activities are not* '

sufficient. The licensee's performance does not significantly exceed

l

l

I

4

_ _ _ _ - _ _ _ _ _ _ - - - _ _ _ _ - _ - _ - _ - .

.

- _ -

. .

,

..

. that needed to meet minimal regulatory requirements. Licensee resources

appear to be strained or not effectively used. NRC. attention should be

. increased above normal levels.

' The SALP report may include an appraisal of the performance trend in a

functional area for use as a predictive indicator if near-term performance

is of interest. Licensee performance during the last quarter of the

assessment period should be examined to determine whether a trend exists.

Normally, this performance trend should only be used if both a definite

trend is discernible and continuation of the' trend may result'in a change

in performance rating.

The trend, if used, is defined as:

Improving: Licensee performance was determined to be improving near the

close of the assessment period.

Declining: Licensee performance was determined to be declining near the

close.of the assessment period, and the licensee had not taken meaningful

steps to address this pattern.

z _ .- -

!

1

l

i

l

  • e

3

5

'

_ _ _ _ _ __________ - -__________________-__

,,-  ?. -

..

-

IV. PERFORMANCE ANALYSIS

A. Plant Operations

1. Analysis

Evaluation of this functional area was based on the results of

112 inspections by the resident-inspectors and two inspections

by regional inspectors.

Enforcement history in this' function &1 area during the'

assessment period was excellent with no violations identified.

During the previous assessment period,.five violations were

identified.

No reactor trips were experienced by either unit during the i

17-month assessment period. .The last reactor trip: occurred {

prior to the beginning of the SALP. period in July.1987. During'

the previous assessment period, there'_were four reactor trips

and in the-period beforeLthat one, there were six. trips. ~ Thus, .

continuous improvement'has been made regarding this area over j

the past three years. .)

Plantwide housekeeping. continues to. improve. Paint crews were ~

- "'

active continually,'especially in the auxiliary building.

Improvement was seen in the rate of cleanup following outages. ,

During the regional fire protection inspection, a walkthrough of- i

the screenhouse and the turbine and auxiliary buildings determined '

that the presence of combustibles.and other fire hazards were

kept to a minimum. Also witnessed during the fire protection

inspection were two firefighting training evolutions .that were .

conducted, in part, to satisfy the NRC annual . fire brigade - -

!

training requirements. .This type of. training was viewed.as J

very realistic and was conducted in a professional . manner by l

knowledgeable fire instructors.

~

. I

Staffing for plant operations continues to improve. At the.end

of the assessment period, the operations staff numbered 207, up  ;

from 99 at the end of the last period. Also, new employees were '

hired into Operations only after' satisfactorily passing  !

comprehensive psychological and aptitude examinations, which is a  !

procedure that was instituted during the period. Although

the total number of licensed reactor operators (R0s) and senior

reactor operators (SR0s) remained about constant, the number

of operator license candidates more than tripled from 6'to

19 during the period. This interest in. obtaining licenses

ultimately will relieve, to some extent, the amount of overtime

currently being worked by the' licensed operators. Of the 24%

overtime expended during the assessment period, 63% is outage

related and 37% non-outage. Another improvement instituted was

6

___ _ _ _ _ _ - _ _ _ _ _ - - .

i

.

  • .

,

. .

i

J

.

the full implementation of the Shift-Manager program on

September 1,1988. With this program, ecch crew has assigned

to it a-degreed Shift Manager in addition to the Shift Supervisor

for each unit.

i

i

During the assessment period, five SR0 and six R0 replacement i

examinations were given. Three SR0 and four RO candidates passed l

the examinations for a passing rate of 64%. As these results

were below the industry average, the licensee closely analyzed .

the examination results, reviewed the training practices, and i

established more rigorous standards for candidates in training  !

for NRC examinations. ,

The licensee was generally very responsive to NRC initiatives. f

The following are examples of licensee's responsiveness; i

improvements in the control room arrangements per human factors j

engineering recommendations; modernization of work stations for '

reactor operators; incorporation of Westinghouse Owners

Group Emergency Response Guidelines IA (ERG-1A) into updated )

Emergency Operating procedures; installation of continuous i

monitoring of thermal reactor power and meetings with the

operations staffs of other 2-loop Westinghouse designed plants.

- -

Luring the assessment period, Licensee Event Reports (LERs) ,

were written for three events involving errors by Operations

personnel. All of these were relatively minor events: the )

!

automatic start of a d.esel-driven cooling water pump when an j

improper valving sequunce was used, the failure to log one

reactor: parameter over a 2-hour period when the plant process

computer was temporarily inoperable, and the automatic start of

the D1 diesel generator as the result of missing a step _in a

test procedure. In the previous assessment period, there were

five such events involving personnel error.

The operating crews continue to perform in a professional

manner. New signs have been posted in the control room that

direct all control room visitors to obtain permission before

entering the operators' area. This control- of visitors helps

to minimize distractions to the operators. Another example of

good professional performance was the discovery by operators of

Foxboro controllers that were not performing their intended

safety function. The controllers in question monitor axial

flux tilt and are to initiate protection system action when a

tilt becomes severely pronounced. During a period of severe

flux tilt, the operators noted that one of four such controllers

was not responding as it should. This observation led to the

detection of an installation error that had been in existence

for several years. Another positive attribute that has been

noted is that senior Operations management is closely involved

with plant operation and interacts with the operatint) crews

nearly daily.

7

.

m__ _ _ _ . _ ___... _

_ _ _ _ _ _ _ _ _ _ _ _-

-

.

..

.

Unit availabilities at Prairie Island during the assessment

period were 92.1% and 85.6% respectively for Units 1 and 2.

Forced outage rates for the two units were 0.4% and 0.78% for

the period.

2. Performance Rating

The licensee's performance is rated Category 1 in this

functional area. The licensee's performance was rated

Category 2 in the previous assessment period.

l

l

3. Recommendations

.

None.

l

'

B. Radiological Controls _

l 1. Analysis

Evaluation of this functional area was based on the results of

three inspections by regional inspectors and observations by

the resident inspectors.

- "'

Enforcement history in this functional area remained excellent -

'

with no violations in the current 17-month assessment period

and none during the previous 18-month assessment period.

Staffing continues to be a licensee strength. The radiological

control staff is well-trained, experienced, with low turnover.

Strained labor management relations in the chemistry group were

noted early in the SALP period; however, work performance does

not appear to have been affected and the problems were essentially

resolved by the end of the SALP period. An experienced,

professionally certified health physicist was added to the

radiation protection staff late in this assessment period.

Although the radiological control staff is relatively small, it

communicates well internally and with other departmental staffs.

A total of five LERs related to this functional area were

submitted during the assessment period. Only one of these, a

late analysis of the contents of the gas decay tanks, was the

result of personnel error. One licensee event was reported in

this functional area during the previous assessment period.

Management involvement in ensuring quality was good during this

period. The strained labor / management relations in the chemistry

area revealed some management weaknesses, however, licensee-initiated

corrective actions were comprehensive and appeared to have

..

8

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - .

.

.

,

..

-

resolved the issues. During non-outage times, there are frequent-

short discussions with the staff on current work activities,

future plans and improvement items.

Licensee responsiveness to NRC concerns was good. The licensee

improved laundry equipment and monitoring techniques and i

significantly reduced the number of personnel contaminations

resulting from laundered protective clothing. Good performance

also included prompt correction of NRC-identified errors in

effluent release reports and a licensee commitment to evaluate

and correct, as appropriate, the air cleaning . systems' charcoal

absorber testing program.

The licensee's approach to resolution of technical issues

continues to be good. Collective person-rem doses for the last

two years (1987-1988) were 134 and 199 respectively. These were

very low cumulative doses which reflect the effectiveness of the 1

as-low-as-is-reasonably-achievable (ALARA) program and an -  ;

experienced plant staff. The licensee's contamination control 4

program continues to be very effective in maintaining the clean. '

areas of the plant, keeping the contamination in contaminated-

areas very low, and minimizing the number of personnel

contaminations. No problems were identified with solid radwaste

-~

or the radioactive waste transportation programs. Liquid and. ,,

!

gaseous releases continue to be very low with resulting offsite

doses generally less than 0.1% of allowed limits. Good

performance also included increased use of computer technology

to generate radiation work permits, calculate air sample data,

improve oversight of the gaseous and liquid radioactive

effluent release program, schedule work, and trend data. It

was noted, however, that certain chemistry records were maintained

only on electronic media without hard copy backup and were not 'j

protected from deletion or change. This practice is a weakness '

and is inconsistent with normally accepted quality assurance

(QA) practices.

l

Revision 9 to the Northern States Power Company (NSP) Offsite

Dose Calculation Manual (0DCM) has been reviewed and 13

discrepancies were identified, most of which were of a technical

nature and should have been addressed by the licensee in the

original submittal. This report has been transmitted to the

licensee with a request to consider the comments and suggestions

made, and to revise the ODCM as appropriate.

The effectiveness of the licensee's training and qualification

program has been good. Appropriate continuing training is

provided for the staff.

l

The quality of radiological confirmatory measurements is very

good with 45 agreements in 47 comparisons. The licehsee's

9

-

- _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ - -

-

.

\..

-

counting room quality control (QC) program was instrumental in

detecting an irregularity in one of the monitored gamma

spectroscopy parameters and effecting an investigation into

the cause.

2. Peformance Rating

The licensee's performance is rated Category 1 in this

functional area. The licensee's performance was rated

Category 1 during the previous assessment period.

3. Recommendations

None.

I

C. Maintenance / Surveillance

1. Analysis

Evaluation of this functional area was based on the results of

12 inspections conducted by the resident inspectors and seven by

regional inspectors. Maintenance and surveillance were separate

functional areas in the previous assessment period but have

been combined as one functional area for this assessment period.

Enforcement history in this functional area during this

assessment period indicated a decline. Seven Severity Level IV

violations were issued, compared to a total of three Severity

Level IV violations in the maintenance and surveillance areas

in the previous assessment period.

All of the violations were in the surveillance area. Four of

the violations resulted from the inspection of Unit I containment

integrated leak rate testing in 1988. The violations involved

failure to perform required local leak rate testing of selected

penetrations (electrical penetrations going back to 1983),

improper calibration of the flow meters, lack of required

capability to perform data reduction calculations, and improper

valve lineup. One violation was the result of engisiaered safety

features (ESF) bus relay testing which momentarily disabled the

bus while one of the emergency diesel generators (DG) was out of

service. Other violations were for routine testing not being

performed on the double doors to the shield building and on the

auxiliary building special ventilation zone, and failure to

perform testing of a containment airlock door. These violations,

related to surveillance activities during the assessment period,

are not indicative of a significant generic weakness in the

administration of the program. Routine surveillance are

generally performed on schedule and the results carefully

10

__

,

.

, .

..

-

reviewed by cognizant personnel to assure that regulatory and

performance requirements are met.

Operational events in this area did not indicate any pervasive

problems in the licensee's control of maintenance or surveillance

activities affecting plant operations. Of the 18 LERs issued

during this period, six involved this functional area. Four

were in the maintenance area including one due to equipment

failure. .Two LERs involving missed surveillance were the

result of personnel error. The reported events were not

considered to be safety significant except for the failure to

close of the Unit 2 emergency DG output breaker. None of these

events.resulted in a reactor trip. The,11censee's performance

in this area was slightly better than the previous'SALP period,

during which nine LERs were issued and two reactor scrams

occurred.

Management involvement to assure quality in the maintenance area

was very good. The maintenance program was effective and

properly implemented during this assessment period, although

some procedures for motor operated valve (MOV) maintenance were

noted as needing improvements. Work backlogs remained very low-

as in previous assessment periods. At the end of.this period,

- "'

only one week's backlog of safety-related and balance-of plan.t .

maintenance was outstanding. Additionally, none of the preventive

maintenance items (PMs) was overdue and very little rework (less

than 0.5%) was required during this assessment period.

In the area of surveillance, plant management was actively

involved in assuring water quality. Water chemistry data was

reviewed daily by laboratory management and weekly by plant

.

management. Corporate management committed to the Pressurized

Water Reactor (PWR) Owners Group Guidelines and overall quality

was generally maintained well below action levels. However, in-

the area of leak rate testing, the licensee's performance during

the early part of the assessment period required improvement,

since the licensee's consultant did not.have the capability to

perform all the required data reduction calculations that

resulted in improper implementation of the Type B and C leak

rate testing program. Improvement was noted in this area during j

the performance of leak rate testing in the latter part of the  ?

assessment period. As mentioned previously, routine surveillance

were conducted in accordance with regulatory and performance

requirements.

1

Plant staffing in the areas of maintenance and surveillance,

including inservice inspection (ISI) and chemistry appeared to

be adequate. One exception noted was during the Unit 1 leak

rate test. The engineer in charge of the test had to cover

other areas of work. This problem was. corrected during the

leak rate test of Unit 2 conducted during the latter part of

l .

!

11

.

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

.cj ,

. ,- ,

..

q

i

1

. the assessment period. The engineers assigned to the leak rate i

tests had a good knowledge'of the equipment.used but only a i

fair knowledge of the regulations (10 CFR 50, Appendix J). )

The maintenance and surveillance staffs including ISI and

chemistry staff appeared to be qualified and adequately trained j

in their fields. The effectiveness and experience of the- ]

craftsmen at Prairie Island were reflected in the excellent

overa11' performance of the plant. Forced outage rates were very

low and the plant experienced no reactor trips during the

period. Emergency DG availability was also good.

.

\

Overtime hours for the craftsmen assigned to Prairie Island i

remained low. Overtime worked at the plant amounted to about 7% j

of the regular hours for.these individuals. Of this 7%, 65% was  ;

outage related and 35% non-outage. Turnover rates of staff were i

very low.

The licensee's responsiveness to NRC initiatives was generally I'

good. Some examples were the licensee's actions in providing a

continuous pre-lube for the Fairbanks-Morse engines of the  ;

DGs, improvements in Limitorque valve maintenance program, and 1

prompt corrective actions for the problems identified during- J

Unit 1 containment leak rate tests. The'. licensee joined the ~

I

- -

Westinghouse Owner's Group and.also promptly instrumented the~' {

Unit 2 surge line with resistance temperature detectors during j

the April 1989 refueling outage. .j

i '

The licensee's identification-and resolution of technical issues

in this area was generally timely and adequate. The system

engineer concept has worked well at this station.' The system

engineers were involved in all phases of maintenance activities -

including review of completed mintenance. The engineering.

group was involved in failure tri.nding and predictive maintenance,

which has contributed well to the goals of low equipment i

unavailability and reduction in forced outage rate.

Several plant improvements made during the assessment period  !

were expected to improve the plant availability. The improvements

'

included a pre-lube system for the DGs, improved seals' for the ' ,

charging pumps, and Unit 1 steam generator tube sleeving. i

2. Performance Rating

The licensee's performance is rated Category 1-in this area.

The licensee's performance was rated Category 1 in both Maintenance

and Surveillance 4 the previous assessment period.

3. Recommendations

..  :

None.

12

--___

.- '.-

..

.1

l

!

-

D. Emergency Preparedness

l

1. Analysis q

!

Evaluation of this functional area was based on the results of j

one emergency preparedness (EP) exercise evaluation and  ;

one routine inspection conducted by regional inspectors.

Enforcement history in this functional area remained the same,

with no violations identified during this or the previous

assessment period. All concerns identified during the previous

assessment period were resolved in a timely manner.

No inspection concerns were identified during the 1988 routine

inspection; however, one concern identified during the 1988 exercise 1

remained open for evaluation during the next annual exercise. i

l

'

Management support of the EP program remains excellent at this

facility- and various program requirements remain part of daily j

plant surveillance and operations. Plant management has- l

approved and developed several EP program enhancements during  ;

this assessment period. The Technical Support Center (TSC) was j

evaluated by an outside human factors consulting firm. This 1

~ ~

evaluation led to the relocation of emergency response system- ~

1

computers, the development of a command and control area,_

enlargement of the NRC work area and the addition of telephone

jacks in the command and control area for NRC use. As a~ result

of the most recent emergency exercise, concerns remain relative

to the noise level in the TSC and the physical size of the EOF

to adequately accommodate a large response of licensee, State, )

4

County and Federal personnel during an actual emergency. )

i

The licensee's resolution of technical issues from a safety' )

standpoint was good as evidenced by the timeliness and i

thoroughness of corrective actions of all NRC and self-identified  ;

concerns. Tracking systems were used effectively to track

corrective actions taken on items identified during previous

,

inspections and also on items identified by a strong plant

audit program.

Events that resulted in the activation of the emergency plan

were properly identified and classified. Offsite notifications,

including those to the NRC, were made within the required time

frame. The prompt notification system was upgraded to prevent

operational problems that were encountered during ice storms.

This upgrade was accomplished within four weeks of self-

identification of the problem and was considered timely in view

of the amount of research and procurement that was necessary to

solve this concern.

..

13

_ _ _ _ _ _

,- .-

..

Staffing of the Emergency Response Organization (ER0) has

remained excellent throughout the assessment period. The

licensee has maintained a current roster of qualified personnel

to fill key positions in the emergency organization. A strong

offsite liaison program that supports the States of Minnesota

and Wisconsin and their respective counties is maintained by-

corporate management. The licensee assisted offsite support

groups in their efforts to improve their 1989 performance in

several ways. -A questionnaire was distributed to all offsite

groups to assess their needs, joint workshops were held to

coordinate work efforts, and cross training with each State was

conducted quarterly in an effort to improve communications

between utility personnel and offsite support groups.

Training and drill records indicated an excellent level of- staff

participation in training and drills. Interviews with various i

ERO personnel indicated a good awareness.of their emergency.

responsibilities. These results indicate an excellent.in-depth-

,

training and drill program and strong management support ~for

l the EP program. The licensee also successfully used the

!

training center simulator for emergency plan drills and

exercises. The simulator was programmed to drive actual l

displays'in the TSC and emergency offsite facility to enhance

'

! the realism of the drills and exercises. This program includes ~

F -

the capability to run the E0Ps on the plant simulator. The

,

exercise performance was very good, although the scenario was

l of average difficulty.

j. 2. performance Rating

The licensee's performance is rated Category 1 in this area.

The licensee's performance was rated ; Category 1 in the

previous SALP assessment period.

3. Recommendations

None.

E. Security

1. Analysis

l

Evaluation of this functional area was based on the results of

three routine security inspections by regional inspectors and

on routine observations of security force activities by the

resident inspectors.

A decline in the licensee's enforcement history was noted

during the assessment period. One Severity Level III and

three Severity Level IV violations were identified compared

14

______ _ _ - -

]

,

.

..

..

.

with no violations identified during the previous assessment

period. The Severity Level III violation involved the

. premature granting of unescorted access.to an unauthorized

individual as a result of a corporate administrative error.

The civil penalty for this violation was mitigated _in its i

entirety because of tSe licensee's' prompt and extensive j

corrective _ action and past excellent performance in the area- 1

of security. Although the violation was discovered and .!

logged by the licensee,-the licensee failed to. recognize the 'l

deportability of the issue. '

j

Management's role in assuring quality was mixed. Both corporate

and plant management were supportive of the security program as

evidenced by the allocation of additional personnel and material

resources. In response to an NRC identified weakness, the . 1

licensee, with the assistance of a security consultant, conducted

..

an assessment of the protected area barrier and intrusion alarm

system which resulted in the installation of several upgrades.

The exterior barrier upgrade project resulted in an innovative

and effective deterrent.to prevent penetrations-of.the perimeter.  !

In contrast, cencerns identified in the previous assessment

period, for the Secondary Alarm Station (SAS) relocation and

computer replacement still remain open.

- - ~

The licensee's security event reporting program was genera 11y'

adequate and reports were timely andLaccurate. There was  !

one security event report made during the assessment period. 11

As noted previously, one _ security' event was not reported as it. l

should have been which_ detracted from an otherwise sound program. )

This action resulted.in a violation and a procedural modification j

to the licensee's sec: rity' reporting program. In general,  ;

security-related records were complete, adequately maintained,

'

j

and available for NRC review.  !

The licensee's approach to the resolution;of technical issues

l

was good. The perimeter alarm system is aging bat with frequent

attention, generally continues to provide the necessary detection  !

capability. Maintenance support was closely monitored and a

consultant was retained to conduct'a complete component

evaluation of the system. The technical support to the computer

replacement project has been excellent. The implementation of

the miscellaneous safeguards amendments were technically sound

and timely. ,

The licensee's responsiveness to NRC initiatives.was exec 11ent.

Security management, both at a corporate and site level, is

cognizant of and responsive to security findings. The licensee's

response to enforcement issues, licensing matters, and inspection

findings were generally technically sound and timely. The

security superintendent's reviews of five published'HRC

15

.

!

-

. . 1

..

1

i

l

1

- Information Notices were comprehensive. However, the SAS issue 1

identified by the Regulatory Effectiveness Review (RER) team has

.

]

remained open since 1985. Although extensive, the project has j

gone beyond the established schedule and the licensee failed to _ j

notify the NRC of having exceeded the commitment date. Additionally, i

the computer replacement project has continued for two years.

The licensee is in the early stage of developtag a performance

monitoring program, which should improve licensee response in .,

this area. 'l

Security staffing levels are adequate to ensure a level of

performance that meets regulatory requirements. The site

security. staff was increased in order to address a problem

similar to a problem identified at Monticello. Although the

contractor providing uniformed security services was changed-

during the assessment period, the transition was smooth and j

without impediments as a result of close coordination with i

various levels of licensee management. . Security force training I

continues to be good. The tactical contingency training drill

involving FBI, local law enforcement and site security exceeded

the licensee's commitment.

2. Performance Rating ,

l

H- The licensee's performance is rated Category 2 in this area. -

l- The licensee's performance was rated Category 1 in the previous ,

SALP assessment period. This decline in performance was due to

lack of timely corrective action to address equipment aging

problems and a decline in enforcement history.

l 3. Recommendations

None.

J

l

l F. Engineering / Technical Support

]

1. Analysis

!

This is a new functional area and consequently was not rated in 1

l previous SALPs. Evaluation of this functional area was based J

on the results of eight routine inspections, including an ,

E0P inspection by regional inspectors, a procurement inspection i

by the Office of Nuclear Reactor Regulation (NRR) and several

inspections by the resident inspectors.  ;

Enforcement history during this SALP period included three

severity level IV violations. Since this area was not rated

during previous assessment periods, no prior enforcement

history is available for comparison. Confirmatory Action

Letter (CAL) RIII-87-013 relating to operator licenstng issues

l in the previous SALP period was satisfactorily closed during

l this period.

16

_ _ _ _ _ _ _ - _ ___-__ __________________ _

._.

-

. .

, .

..

i

Two events requiring the submittal of LERs in this' functional

area occurred during this assessment period. One resulted from

an incorrect change made to a surveillance procedure and the

other involved incorrect bolting materials on the secondary

side steam generator manways. The latter' event stemming from

an initial construction error was of limited safety significance.

i

Management involvement to easure quality in this functional area

was mixed. The system engineer concept utilized by the licensee

contributed significantly to the plant's ability to routinely

conduct refueling and maintenance outages in 30 to 35 days'.

Examples of system engineer contributions included identifying

the wrong bolting material for steam generator secondary manways

before installation and a special analysis of a Unit 2 extraction-

bellows that identified a fatigue failure design weakness. For- 1

IE Bulletin (IEB) 79-14, there was consistent evidence of prior  ;

planning and assignment of priorities for activities, and the 3

activities were controlled by well-stated and explicit procedures.

NSP corporate management has been actively involved in improving

the training program and has maintained interaction to address

operator licensing problems in the performance of operator

exams.

- - On the negative side, the results of the NRR Vendor Inspection .

Branch inspection indicate that weaknesses' existed in the areas l

of procurement and dedication of. commercial grade items and l

interfaces between NSP and its vendors. The inspection team I

identified significant deficiencies-in the procurement of

commercial grade items for eventual use in-safety-related

application.s. The deficiencies included the failure to properly

dedicate and provide documentation for commercial grade items

procured for use in safety-related applications. NSP failed to'

perform documented technical evaluations to identify attributes

such as the components' safety functions and critical-

characteristics, verifications of design and manufacturing / material

changes, and receipt inspection requirements beyond, generally,

a part number verification and a check for physical damage and

cleanliness. This resulted 1- the utilization of numerous

components of indeterminate quality and qualification in

safety"related applications.

The review of the vendor interface program also identified a

weakness in which certain vendor communications received at NSP

describing potential safety concerns were improperly and

incompletely assessed for their applicability. The inspectors

also identified several assessments that lacked the necessary

l level of documentation to permit clear understanding of the

disposition. For example, NSP failed to perform documented
  • e

17

_ _ _ _ _ _ _ _ _ _

_

_ _ _ _ _ _ _ _ _ _ _ _ - _ -

.

.

..

.

assessment of 17 Colt /FMED Services Information Letters (SIls)

for their applicability to the emergency diesel generators.

The licensee's resolution of technical issues was mixed. The

backlog of safety-related plant modifications remained manageable.

About 150 modifications were in process at the end of the

period. Of this amount, 47 were considered significant based on

cost or regulatory impact. Reevaluations of as-built safety-related

piping systems, performed by the licensee as a result of discrepancies

identified by the vendor regarding weight and center of gravity

with Copes Vulcan valves, in some cases exceeded USAS B.31.1.0 1976

i allowable stresses. As a result, the licensee was requested to

I submit to the NRC a justification for continued operation (JCO)

I

'

including acceptance criteria when encountering similar stress

level discrepancies. The licensee's initial response was found

to be unacceptable, and revised criteria were proposed and

ultimately accepted by the NRC. All post-fire safe shutdown

capability (10 CFR Part 50, Appendix R) technical issues were

resolved during this period. Technical support for those

resolved issues was excellent. One nontechnical issue remains

open.

During the SALP period, many examples of good quality engineering

- ~

work were evident in the management and resolution of licensing

issues. A licensee submittal in response to 10 CFR 50.62 ~ ~

anticipated transient without scram requirements, a Technical

Specifications (TS) change request based on the new 10 CFR Part 50,

Appendix K evaluation model for upper plenum injection, a

submittal involving the periodic surveillance requirement for

turbine valve testing, and the high flux range monitor low

setpoint submittal were all examples of high quality engineering.

The licensee's responsiveness to NRC initiatives was generally

good. Resident inspector questions related to the plant design

maximum cooling water inlet temperat.ures raised during the 1988

summer drought were researched and satisfactorily answered

in just a few days. Prairie Island was one of the first plants

to be audited by the NRC E0P inspection team that had incorporated

the Westinghouse Owners Group Emergency Response Guidelines 1A

(ERG-1A). In anticipation of this inspection, the licensee

conducted in April 1988 an audit of their E0P program,

procedures and activities. A1 action plan to correct the

numerous program and operations deficiencies was developed.

Additional concerns identified during the NRC E0P inspections

were subsequently added to those licensee items identified for

resolution. The licensee has implemented a very thorough and

technically sound approach to resolve the recent IEB 79-14

related issues. Major weaknesses in the requalification

examinations results were addressed during this SALP period

,

18

._.

. .. . _ . . . . . . . . . . .. .. .

. ._. . . .

. i

..

l

-1

'

l

-

and partially through program provisions the CAL was closed '

l

.. subsequent to an inspection performed in January 1988. Since

that time, further inspection of the current requalification

program has been conducted'. The licensee has now begun to

successfully implement the requalifica". ion program.

Staffing for engineering and technical support was good. For

complex plant modifications, significant reliance is placed on .!

consultants to conduct design and analytical efforts. Examples- I

of such modifications are the digital feedwater control system, l

the new plant computer, and the revised control room panels for

both units. Staffing considerations for the configuration

management program are in progress and, with the Superintendent

and the Lead Design Ergineer on board, activities are commencing.

'

Training and qualification effectiveness was. mixed. Although the

training and qualifications program did not ensure a high degree.

of success in passing NRC administered operator. licensing

examinations, the-licensee's evaluation and proposed corrective

actions appear to be' appropriate. .-In addition, although the ,

effectiveness of the new requalification program has not yet j

been evaluated, the licensee's developmental efforts and j

implementation of the revised requalification program are i

, ,

progressing very well. ,,

The licensee has demonstrated a generally conservative approach

to the engineering resolution of_ technical problems. However,

there are indications that thorough, aggressive engineering / technical

evaluation is not being conducted within all elements of the.  ;

l licensee engineering organization. Vendor interface, commercial i

grade dedication, and proper disposition and response to industry j

information notices are areas of concern that require management l

attention.

2. Performance Rating

The licensee's performance is rated Category 2 in'this area.

Since this is a new functional area, it was not rated in the l

previous assessment period. I

L 3. Recommendations l

/

None. )

!

..

1

!

19

l

l _ _ _ _ - . _ _ _ _

,

.

..

..

'

G. Safety Assessment / Quality Verification

1. Analysis

This is a new functional area and consequently was not rated in

previous SALPs. Evaluation of this area was based on results

of 12 inspections conducted by the resident inspectors,

one inspection by a Region III E0P team, and reviews by the

NRR Licensing Project Manager.

One Severity Level IV violation was noted during the assessment

period for failure to perfonn planned and periodic audits of

the E0Ps. During the previous assessment period. no violations

were identified in 'the functional area of Quality Programs and

Administrative Controls Affecting Quality.

One licensee event was assigned to this functional area for

the procedural inadequacy noted when the licensee was

reviewing the applicability of Information Notice No. 87-63,

" Inadequate Net Positive Suction Head in Low Pressure Safety

Systems," to Prairie Island. During this review, it was

discovered that in one of the E0Ps, under certain conditions,

the residual heat removal pumps could not support the flow

- -

demands that might be placed on them. The licensee responded -

to this discovery immediately by issuing a Special Order that

provided guidance on this subject to the operating crews.

Audits for quality are performed formally by two organizations: I

the plant Quality Engineering (QE) group and the corporate

QA group. Results of audits by these two groups were promptly  ;

brought to the attention of plant management. Immediate action '

was frequently taken by plant groups when an unsatisfactory

condition is pointed out by the auditors. In some instances,

written responses were required regarding corrective actions-

that have been or were to be taken. This system appeared to be

effective in tracking items raised by the auditors although the

plant QE organization reported some problems with the timeliness

of the 30-day responses required by plant procedures. Both QE

and QA were judged to be very effective in the performance

of their duties. For example, plant QE auditors uncovered

failures to meet company brazing requirements, incomplete

modification packages being turned over to Operations, mislabeled

and improperly fused electrical panels, damaged safety-related

instrumentation (during an outage), mispositioned process

valves, an improperly rebuilt governor for a diesel-powered

l cooling water pump, and many other items. Similarly, examples

of corporate QA effectiveness included the following: protection

'

system instrumentation and circuits were found not to be

response-time tested as required by TS (this area is1 till being

examined by the NRC), QA performed.significant research on the

.

4

20

- _ _ _ _ _ _ _ -

a

!

. 1

..

!

historical saquences that resulted in Foxboro controllers being. I

improperly installed _for monitoring axial flux tilts, and

full-time auditors have been assigned directly to the Prairie

~

Island site, one in April 1988 and the other in March 1989. One 1

of these auditors had significant knowledge of the plant, having  !

worked in Operations for many years. l

The onsite safety committee (Operations Committee or OC) k

continued to be very involved in the review of significant '

plant activities, including plant events. As evidence of the l

OC's active participation, this committee met 194 times during j

the assessment period, an average of 2.8 meetings per week. j

Safety evaluations required by 10 CFR 50.59 in general have i

been carefully' prepared and received close scrutiny by the OC

before approval. Minutes that summarize the DC discussions

improved during the period regarding the amount of detail i

included. '

The offsite safety committee (Safety Advisory Committee or l

SAC) also operated during the period in a generally effective {

manner. All areas required by plant TS to be reviewed by SAC  ?

appear to have been appropriately discussed. Membership of the

'

SAC, though of individuals very experienced in the nuclear i

~ ~

industry, did not change on any regular basis. For example,

there has not been a new member of SAC from outside the licensee's

organization for more than 10 years. A lack of new individuals

on the committee is a potential concern which the NRC feels the

licensee should consider. 4

i

Some minor weaknesses in the membership of the SAC regarding

the balance of NSP versus non-hSP members and the lack of detail

in the minutes of the SAC meetings were'noted. .Also, records of i

the experience and qualifications of the SAC members were not

uniform, maintained current, nor responsive to the need to

clearly establish the basis for the members' level of expertise.

,

An area in which the licensee can improve is keeping the NRC

better informed of plant activities and management concerns.

,

I

Several examples of failures to keep the NRC fully informed on

matters of interest were noted during the assessment period.

Many discussions were held with the plant manager and others on

this subject in an attempt to improve these communications. l

Examples included: station blackout project planning and policy- l

l decisions; untimely notification of occurrences such as the

345kV breaker failure, fire protection audit findings and a l

security. violation; changes in radiation protection practices- I

and an allegation the licensee received relevant to radiochemistry

issues. The latter example was significant in that the allegation

was also received in the Region III Office. This caused duplication

of efforts and coordination problems for the NRC. -

1

1

!

21

I

l

_ _ _ _ - -

- 1

!

!

.

"..

,

During the SALP assessment period, the licensee's management ,

'

actively supported licensing actions and their participation

indicated an indepth knowledge of the issues. The licensee's

submittals were maintained'at a high quality level and did not

require significant rework. In the upper plenum injection case,

the licensee took the initiative and assumed a lead role in

resolving long standing technical issues in conjunction with

industry groups. The licensee's submittal, describing the

evaluation model, was well prepared and the information was

adequate to prepare a safety evaluation requiring only minor

additional input. The licensee worked closely with the staff ,

in resolving various safety issues related to the TS upgrade i

that were initiated as a result of our requesting modifications j

to the licensee's proposed change. Answers to questions raised 1

during the course of preparing the safety evaluation were ,

technically sound and served to resolve the NRC's safety {

concerns. These activities resulted in six license amendments J

for each unit and an exemption to Appendix J of 10 CFR 50.

In most cases, the licensee has responded to the generic letters I

and bulletins in a timely manner and an examination of the j

responses indicated that the quality is generally adequate and 1

the responses are complete. These responses are currently under  !

review by the staff. One exception noted was the licensee's ~

{

~ ~

response to Bulletin 85-03 which was not thorough; and some  !

inconsistencies were found in the documentation during a field I

verification. Regarding NRC Information Notices, the licensee l

has in place a system for receiving, logging, assigning, and

tracking actions taken on every Information Notice received.

This system is working properly and effectively.

During this assessment period, the licensee submitted changes

to the Plant Security Plan in response to the rule change

pertaining to 10 CFR 73.55, Miscellaneous Amendments and Search

Requirements. The licensee also submitted a plan change

addressing vital equipment. Review of these submittals

indicated that the licensee had a clear understanding of the

Commission's security regulations, demonstrated by the quality

of the submittals received, and that there was clear evidence

of prior planning in developing the proposed changes.

Several areas of self-improvement were initiated by the licensee

during the assessment period such as the " Pursuit of Excellence"

program. Some examples from that program include the following:

week-long visits'are being made by all operating crews to other

operating nuclear plants; plant managers have begun meetings

with managers of other 2-loop Westinghouse plants; a

Configuration Management program that includes Safety System

Functional Inspection efforts is under way; and an Error

22

______ -_ 3

  • ;*

.

. Reduction Task Force is active in the investigation of all

events in which personnel error may have been involved.

Another self-improvement effort, that also was partly initiated

in response to NRC observations on the reduction of reactor

trips, is the installation of a digital feedwater control j

system. Unit 2 now has such a system which was installed and ]

tested during the April 1989 outage.

'

Another voluntary improvement being made partly in response to j

NRC interest is the installation of two new emergency DG. These

DG5 are scheduled for installation in late 1991 or early 1992

and will satisfy current NRC requirements for reliability of the

onsite power supply system.

The Prairie Island staff also has taken the lead in resolving

questions raised by NRC regarding the reliability of Fairbanks-Morse

opposed piston diesels. Units of this manufacture are used to I

drive the. existing emergency generators. Specifically, a

Fairbanks-Morse owners' group has been organized by NSP. The

initial meeting of this owners' group was held in mid-May 1989.

Recently the staff issued Generic _ letter 89-04 establishing

guidance for obtaining the required approval for implementation

- -

of the inservice testing (IST) of pumps and valves program ~

relief requests for those plants that do not have an NRC approved

program. Prairie Island is one of the few plants in the country

that has IST relief approved by the NRC. Specifically Prairie

Island had its first ten year period as well as the present

second ten. year period approved by the staff. The second

ten year period will end on December 16, 1993, for Unit I and

December 21, 1994, for Unit 2.

An area of weakness was identified regarding the licensee's

resolution of allegations forwarded by the NRC. An allegation

was investigated by the licensee following receipt by the NRC,

and the licensee reported its investigation results to the NRC.

However, the agency staff was unable to make a judgement on the

corrective actions taken from the contents of that report, so

supplemental information had to be obtained from the licensee.

Improvements need to be made in the area of allegation handling.

2. Performance Rating

The licensee's performance is rated Category 1 in this area.

Since this is a new functional area, it was not rated in the

previous assessment period.

3. Recommendations

..

None.

23

_ _ - _ - _

q

,

. ., 0

. . .

.

')

l

1

V. SUPPORTING DATA AND SUMMARIES

A.. . Licensee Activities

1. Unit 1-

Prairie Island' Unit I began the assessment period operating at

routine power levels up to 100%. On. August 23, 1988, the unit

was' shut down-for its annual refueling and maintenance outage.

'

(Cycle 12-13). The unit operated routinely-with no major

reactor outages or.significant load reductions through the end 4

of the SALP assessment period. 1

Unit 1 experienced four ESF actuations and no reactor trips.

Significant outages'and events that occurred during the i

assessment period'are summarized below, j

'

Unit 1 Significant Outages and Events

a '. During March 10-12, 1988, Unit l' shut down from 80% power

to repair'a reactor coolant leak that resulted from a

corroded canopy seal weld on an instrument column in the

reactor head.

b. During July'26-28,-1988, Unit 1 experienced a forced outage 1

and remained shutdown to repair generic problems with the

'

flux tilt controllers,

c. During August 23 - September 28, 1988, Unit-I was shut down

for its Cycle 12-13 ~ refueling and maintenance outage.

Activities included installation of new fuel assemblies, l

eddy current- tests, fuel shuffle, replacement of- the i

control roomE' panel, snubber testing, integrated leak

rate testing (ILRT) of containment, and inspection of 1

all steam generator (SG) tubes. 4

2. Unit 2

Prairie Island Unit 2 began the assessment period coasting down

in preparation for its Cycle 11-12{ refueling and maintenance

outage, which began on January 5, 1988. On February 13, 1988,

Unit 2 resumed routine operation, but was subsequently-taken

off line briefly to allow closure of transformer disconnects. ,

The unit operated as' load demands dictated at' power levels up. i

to 100%. On March 28, 1989, Unit 2 began its Cycle 12-13

'

refueling and maintenance outage and returned to service on

April 29, 1989. The assessment period ended with the unit ,

operating routinely.

..

24

i

._-

. - '. ~

..

There were no ESF actuations or reactor trips of Unit 2 during

the assessment period.

Significant outages and events that occurred during the assessment

period are summarized below.

' Unit 2 Significant Outages and Events

a. During January 5-February 13, 1988, Unit 2 was shut down

for its Cycle 11-12 refueling and maintenance outage.

Activities included a fuel shuffle, a feedwater piping

inspection, replacement of source range detectors, eddy

current test of all SG tubes, containment ILRT, testing

of Limitorque valve. operators, and measurement of thimble-

tube wear.

b. On Februtry 13, 1988, Unit 2 was taken off line to allow

closure of the transformer discontents,

c. During November 8-11, 1988, Unit 2 was shut down for

condenser repairs. Activities included repairs to a

feedwater line leak and a condenser tube leak,

- ~

d. During March 28-April 29, 1989, Unit 2 was shut down for.. ,

its Cycle 12-13 refueling and maintenance outage.

Activities included a fuel shuffle,. eddy current test of-

SG tubes, inspection of the installed SG tube plugs,

feedwater piping' inspection, replacement of the feedwater

control system, and. installation of anticipated transient

without scram mitigating circuitry.

B. Inspection Activities

Thirty-eight inspection reports are discussed in this SALP report

(December 1, 1987, through April 30,1989) and are listed in paragraph l

1 of this section, " Inspection Data." ' Table ~1 lists the -violations ,

per' functional area and their severity levels. Significant inspection i

activities are listed in paragraph 2 of this section, "Special

Inspection Summary."

.

1. Inspection Data

a. Unit =1

Docket No.: 50-282

Inspection Reports Nos.: 87017, 87018, 88001 through

88023, 88025, 88200, 89002, 89003, 89007 through 89012, and

89014. ,

Unit 2

'

b.

Docket.No.: 50-306 "*

l Inspection Reports Nos.: 87016, 87017, 88001 through

l

88014, 88016 through 88023, 88025, 88200, 89002, 89003,

89007 through 89013, and 89015.

i

25

_ _ _

_ _ _ _ _ _ _ _ _ _ _ _ _ - - _ -

.

..

Table I

Number of Violations in Each Severity Level

Unit 1 Unit 2 COMMON

Functional Areas III IV V III IV V III IV V

A. Plant Operations - - - - - - - - -

B. Radiological Controls - - - - - - - - -

C. Maintenance / Surveillance -

1

- - - - -

6 -

D. Emergency Preparedness - - - - - - - - -

E. Security -

1

- - - -

1 2 -

F. Engr / Tech Support - - - -

1 - -

2 -

G. Safety Assessment /

Quality Verification - - - - - - -

1 -

Unit 1 Unit 2 Common

IIT IV V III IV V III IV V

TOTALS -

2 - -

1

-

1 11 -

2. Special Inspection Summary

~ "'

a. During January 20-February 10, 1988, a special inspection ,

was conducted on the corrective actions taken regarding

the Operator Requalification Program, as described in

CAL-87-013-010A (Inspection Report Nos. 282/88003,306/88002).

b. During June 22-22, 1988, the annual EP exercise was

conducted (Inspection Report Nos. 282/88006,306/88006).

c. During June 6-21, :.988, a special inspection was conducted

to verify that the E0Ps were tec'mir sily correct (Inspection

Report Nos. 282/88010, 306/88010).

d. During September 1-16, 1988, an ISI inspection was conducted ,

(Inspection Report No. 282/88015). I

e. During September 16-October 26, 1938, an ILRT/ local leak

rate testing inspection was conducted (Inspection

Report Nos. 282/88016,306/88016).

f. During October 25-November 4,1988, a vendor inspection was i

conducted relating to the interface of procurement program "

(Inspection Report Nos. 282/88200,306/88200).

C. Escalated Enforcement Actions

A Severity Level'III violation was issued for a security event

involving improper access authorization and inadequate scteening of

individuals; however, no civil penalty was levied (Inspection Report

Nos. 282/88023, 306/88023; Enfor': ment Case No. EA-88-292).

26

_ _-__ _ ____-___ _ ____ _

,  :.

..

1

.

D. Confirmatory Action Letters i

None. ,

. E. License Amendments Issued

Amendments No. Description Date

82/75 Administrative Control 4/18/88

change, Figure TS 6.1-2 1

83/76' High Flux Power. Range. Low 5/31/88 q

Set Point changed

84/77 Change gF and FAg Using 9/16/88

The New Evaluation Model  !

for Appendix K j

85/78 Security Plan Revision -1/5/89

10 CFR Part 73-

4

86/79 Reduction in Turbine: 2/7/89 l

Valve Testing '

- .

F. Review of Licensee Event. Reports'

Unit'l LER Nos.: 87020, 88001 through G8011,.88013, 89001 and 89002.

Unit 2 LER Nos.: 88001, 88002, and 89001

Collectively, 18 LERs were issued in accordance with NUREG-1022

guidelines during this assessment period and are addressed in this

SALP 8 report.

Table 2

Licensee Event Reports

Causes Unit I- Unit 2

Personnel Errors 4 2

Design Deficiencies 7 0

External 0 0

Procedure Inadequacies 2 0

Equipment / Component 1 1

Other/ Unknown- 1 0

Totals 15 3

Table 3 shows a cause code comparison of SALP 7 and SALP 8. ..

I

\

27

.I

___=---__------_____-1---:-_ _ - - - - - . - -

. _ _ _

. .

.

!

,

~ q

l

i

'

-

Table 3

LERs Comparison

( 18-MO) .- -(17-MO)

Cause Areas SALP 7 SALP 8~

Personnel Errors 16 (57.0%) '6 (33.3%) l

Design Problems 3-(11.0%) 7 (38.9%) .I

External Causes l'( 4.0%) -0 ( 0.0%) l

Procedure Inadequacies 4 (14.0%) 2 (11.1%) 1

Equipment / Component 2 ( 7.0%) 2 (11.1%)'

Other/ Unknown 2 ( 7.0%) I'( 5.6%) 4

i

TOTALS 28* 18 8

FREQUENCY (LERs/MO) 1.6 1.16

)

  • Includes 4 voluntary LERs.

.

. -

,

NOTE: The.above'LER information was derived from a review of LERs 1

performed by NRC resident staff and may not completely coincide with'

the. licensee's cause code assignments. .

... .

I i

,

<

!

l

4

o

.1

1

i

-

l

28

.a

l