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Category:INTERNAL OR EXTERNAL MEMORANDUM
MONTHYEARML20207J7561999-02-19019 February 1999 Forwards Proposed Transmittal Ltr & Comments on Physical Protection Plan in Response to Verbal Request from Rancho Seco to Provide Addl Comments on ISFSI Physical Protection Installation NUREG-1299, Forwards Continuation of Curtiss Papers to Be Filed Under Commission Correspondence in Pdr.Advanced Copy Sent to Pdr. List of Documents Included in Four Boxes Encl1994-06-29029 June 1994 Forwards Continuation of Curtiss Papers to Be Filed Under Commission Correspondence in Pdr.Advanced Copy Sent to Pdr. List of Documents Included in Four Boxes Encl ML20056E4571993-08-0505 August 1993 Forwards Technical Review Rept Re, Tardy Licensee Actions Initiated Because of Delayed Replacement of Batteries in Uninterruptible Power Supplies at Plant ML20056C8421993-07-13013 July 1993 Notification of Significant Licensee Meeting W/Util on 930727 to Discuss Decommissioning & General Status ML20058D1231990-10-25025 October 1990 Notification of Significant Meeting on 901030 W/Util in Herald,Ca to Discuss Licensee Organization,Staffing,Plant Status & Status of Licensee Programs ML20062A8381990-10-12012 October 1990 Notification of 901017 Meeting W/Util in Rockville,Md,To Discuss Plant Decommissioning Funding ML20059P0831990-10-12012 October 1990 Notification of 901017 Meeting W/Nrc in Rockville,Md to Discuss Decommissioning of Facilities ML20055E2821990-06-28028 June 1990 Forwards Documents in Response to Subpoena Re M Akins,Et Al ML20055E2981990-04-13013 April 1990 Responds to Civil Subpoena Re M Akings Et Al.Chronological Sort of Dbase File Created to Account for Documents Released Encl ML20148T1891990-04-10010 April 1990 Responds to Request for Info Re Congressional Inquiries on Tracking & Closeout of Issues Raised Re Incident Investigation Team (IIT) Investigations of Plants.Actions Assigned by EDO in Response to Plant IITs Addressed ML20055C3521990-02-26026 February 1990 Notification of 900305 Meeting W/Util in Rockville,Md to Discuss Status of Licensing Activities for Facility ML20248E9391989-09-29029 September 1989 Forwards AEOD Technical Review Rept on Debris in Containment Recirculation Pumps.No Occurrences Found to Involve Actual Accumulation of Debris in Containment Sumps.Immediate Corrective Actions Completed ML20248C8311989-09-20020 September 1989 Request for Hearing by Alchemie.* Forwards Response & Request for Hearing,In Response to NRC 890818 Order Modifying License & Order to Show Cause Why Licenses Should Not Be Revoked,For Appropriate Action ML20247K3421989-09-12012 September 1989 Forwards Transcript of 890829 Meeting W/Util in Rockville,Md Re Status of Plant & Associated Closure Plans ML20247H9261989-09-0909 September 1989 Advises That SALP Meeting for Facilities Scheduled for 891115.Assessment Input Should Be Submitted by 891016 ML20246F0401989-08-23023 August 1989 Notification of 890906 Meeting W/Golden State Energy (Gse) in Rockville,Md to Discuss Potential License Transfer from Smud to Gse ML20246J5101989-08-23023 August 1989 Notification of Cancellation of 890906 Meeting W/Golden State Energy in Rockville,Md to Discuss Potential License Transfer for Plant from Smud ML20245F1261989-08-0909 August 1989 Updates Status Following Smud Ratepayer Vote on 890606 to Close Plant,Per 890619 Staff Requirements Memo.Eligible Voters Voted 53 to 47% to Close Plant.Nrc Evaluating Util Closure Process & Will Meet W/Licensee Re Decommissioning ML20245H0111989-08-0909 August 1989 Notification of 890829 Meeting W/Smud in Rockville,Md to Discuss Closure & Decommissioning Plans & Preliminary Details of Potential License Transfer for Facility ML20245E8501989-08-0707 August 1989 Advises of Reassignments in Project Mgt Duties Due to Recent Reorganization of Standardization & Life Extension Project Directorate ML20245H6451989-08-0404 August 1989 Requests Closure of Outstanding Action Item 87-0198,per 870617 Request Re Review & Evaluation of Acceptability of Fairbanks-Morse Diesel Generator Bearings.Action Completed W/Submittal of Transfer of Lead Responsibility to NRR ML20248D1431989-07-27027 July 1989 Forwards Proposed Generic Ltr Requesting Voluntary Licensee Participation in ERDS & Requests That Proposed Generic Ltr Be Sent to All Licensees of Power Reactors,Except for Participants & Licensees of Listed Plants ML20247B7541989-07-19019 July 1989 Confirms That Licensee 880711,890221 & 0630 Responses to NRC Bulletin 88-004, Potential Safety-Related Pump Loss, Acceptable.Licensing Action for TACs 69886,69887,69893 & 69894 Considered Complete ML20247E6721989-07-17017 July 1989 Proposes Closeout of Plant Correspondence Control Ticket Re Environ Conservation Organization Request for Notification Whenever License Amend Requests Result in Impairment of Plant Operability.Intervenor Will Be Placed on Svc List ML20246K5991989-07-12012 July 1989 Notification of 890725 Meeting W/Util in Birmingham,Al to Discuss Status of Current Licensing Activities & Corporate Initiatives for Plants.Meeting Agenda Encl ML20246L6801989-07-10010 July 1989 Notification of Significant Licensee Meeting 89-101 W/Util on 890718 in King of Prussia,Pa to Discuss Util Engineering Reorganization ML20247A9561989-07-0606 July 1989 Notification of 890717 Meeting W/Lead Plant Utils in Rockville,Md to Discuss Implementation of Revised STS ML20244C4511989-06-0909 June 1989 Notification of 890619 Meeting W/Util & Bechtel at Plant Site to Discuss Resolution of Geologic & Seismic Issues. Meeting Will Be Followed by Field Trip ML20246H3771989-05-12012 May 1989 ALAB-913.* Advises That Time Provided within Which Commission May Act to Review Aslab Decision ALAB-913 Expired.Commission Declined Review.Decision Became Final on 890501.W/Certificate of Svc.Served on 890512 ML20246P9601989-05-10010 May 1989 Discusses 890413 Meeting W/Rosemount & Industry Re Malfunctions of Rosemount Transmitters.List of Attendess, Agenda,Nrc Info Notice 89-042 & Viewgraphs Encl ML20055E4911989-05-0101 May 1989 Forwards Draft Documents & Supporting Info Proposed for Plant Notice of Violation & Proposed Imposition of Civil Penalties Re Release of Radioactive Liquid Effluents & Emergency Preparedness ML20245E9781989-04-17017 April 1989 Forwards Regulatory History AC83-2 Re Licensee Action During Natl Security emergency,10CFR50 (54FR7178) ML20245B7501989-04-15015 April 1989 Forwards Engineering Evaluation Rept on BWR Overfill Events Resulting in Flooding of Steam Lines.Potential for Equipment Damage Believed to Exist & Any Damage Occurring Should Be Fixed Prior to Restart ML20245B6531989-04-15015 April 1989 Forwards Evaluation Rept on BWR Overfill Events Resulting in Flooding of Steam Lines.Events Determined to Involve Deficiencies in Control Sys ML20245B6421989-04-15015 April 1989 Forwards Engineering Evaluation Rept on BWR Overfill Events Resulting in Steam Line Flooding.Though Little Actual Damage Experienced,Potential for Equipment Damage Believed to Exist & Any Damage Occurring Should Be Fixed Prior to Restart ML20245B6191989-04-15015 April 1989 Forwards Evaluation Rept Re BWR Overfill Events Resulting in Steam Line Flooding.All Events Included Reactor Depressurization Followed by Uncontrolled Condensate or Condensate Booster Pumps Injection or Both ML20244E2681989-04-12012 April 1989 Summary of Operating Reactors Events Meeting 89-015 on 890412.Discussion of Events,List of Attendees & Three Significant Items Identified for Input Into NRC Performance Indicator Program & Summary of Reactor Scrams Also Encl ML20244A5461989-04-10010 April 1989 Notification of 890503 Meeting W/Util in Rockville,Md to Discuss Using Leak Before Break Methodology on Lines Connected to RCS ML20244A5571989-04-10010 April 1989 Notification of 890502 Meeting W/Util in Rockville,Md to Discuss Nonlinear Piping Analysis to Remove Snubbers & Pipe Supports ML20247B7351989-03-24024 March 1989 Notification of 890503 Meeting W/B&W,Inel & Util in Rockville,Md to Discuss Licensing Submittals for Plants ML20055E3341989-03-15015 March 1989 Notifies of Meeting on 890317 W/Util to Discuss Results of Licensee Investigation Re Incident Involving Resins in Liquid Effluent Waste Stream During 890115-19 ML20236A9721989-03-0707 March 1989 Forwards Feb 1989 Status Rept Re Current Review Milestones for Each Std Plant Project ML20235S6271989-02-28028 February 1989 Notification of 890307 Meeting W/Bwr Owners Group in Rockville,Md to Discuss Items of Current Interest.Agenda Encl ML20246N3171989-02-23023 February 1989 Notification of 890313 Meeting w/C-E in Rockville,Md to Discuss Results of Salem Project & Licensing of Future C-E Projects ML20245E9441989-01-31031 January 1989 Forwards Proposed plant-specific Backfit for Improved Auxiliary Feedwater Sys Reliability Analyses for Required Improvement in Secondary DHR Capability at Plant ML20055D8221989-01-13013 January 1989 Advises That Commission Has Not Objected to Intention to Issue Notice of Violation & Proposed Imposition of Civil Penalty for Violation of Requirements of Plant Radioactive Liquid Effluent Programs ML20196C2701988-12-0202 December 1988 Notification of 881207 Meeting W/Util in Rockville,Md to Discuss Dcrdr Submittal of 880825 ML20196B6081988-11-29029 November 1988 Forwards Status Rept for Nov 1988 Re Std Plant Design Technical Reviews ML20206M9231988-11-23023 November 1988 Lists Questions Raised by Board Study of Licensee Environ Repts on Facilities,For Responses & Comments.Served on 881125 ML20195J0141988-11-22022 November 1988 Notification of 881214 Meeting W/Util in Rockville,Md to Discuss Licensing Actions at Plants 1999-02-19
[Table view] Category:MEMORANDUMS-CORRESPONDENCE
MONTHYEARML20207J7561999-02-19019 February 1999 Forwards Proposed Transmittal Ltr & Comments on Physical Protection Plan in Response to Verbal Request from Rancho Seco to Provide Addl Comments on ISFSI Physical Protection Installation NUREG-1299, Forwards Continuation of Curtiss Papers to Be Filed Under Commission Correspondence in Pdr.Advanced Copy Sent to Pdr. List of Documents Included in Four Boxes Encl1994-06-29029 June 1994 Forwards Continuation of Curtiss Papers to Be Filed Under Commission Correspondence in Pdr.Advanced Copy Sent to Pdr. List of Documents Included in Four Boxes Encl ML20056E4571993-08-0505 August 1993 Forwards Technical Review Rept Re, Tardy Licensee Actions Initiated Because of Delayed Replacement of Batteries in Uninterruptible Power Supplies at Plant ML20056C8421993-07-13013 July 1993 Notification of Significant Licensee Meeting W/Util on 930727 to Discuss Decommissioning & General Status ML20058D1231990-10-25025 October 1990 Notification of Significant Meeting on 901030 W/Util in Herald,Ca to Discuss Licensee Organization,Staffing,Plant Status & Status of Licensee Programs ML20059P0831990-10-12012 October 1990 Notification of 901017 Meeting W/Nrc in Rockville,Md to Discuss Decommissioning of Facilities ML20062A8381990-10-12012 October 1990 Notification of 901017 Meeting W/Util in Rockville,Md,To Discuss Plant Decommissioning Funding ML20055E2821990-06-28028 June 1990 Forwards Documents in Response to Subpoena Re M Akins,Et Al ML20055E2981990-04-13013 April 1990 Responds to Civil Subpoena Re M Akings Et Al.Chronological Sort of Dbase File Created to Account for Documents Released Encl ML20148T1891990-04-10010 April 1990 Responds to Request for Info Re Congressional Inquiries on Tracking & Closeout of Issues Raised Re Incident Investigation Team (IIT) Investigations of Plants.Actions Assigned by EDO in Response to Plant IITs Addressed ML20055C3521990-02-26026 February 1990 Notification of 900305 Meeting W/Util in Rockville,Md to Discuss Status of Licensing Activities for Facility ML20248E9391989-09-29029 September 1989 Forwards AEOD Technical Review Rept on Debris in Containment Recirculation Pumps.No Occurrences Found to Involve Actual Accumulation of Debris in Containment Sumps.Immediate Corrective Actions Completed ML20248C8311989-09-20020 September 1989 Request for Hearing by Alchemie.* Forwards Response & Request for Hearing,In Response to NRC 890818 Order Modifying License & Order to Show Cause Why Licenses Should Not Be Revoked,For Appropriate Action ML20247K3421989-09-12012 September 1989 Forwards Transcript of 890829 Meeting W/Util in Rockville,Md Re Status of Plant & Associated Closure Plans ML20247H9261989-09-0909 September 1989 Advises That SALP Meeting for Facilities Scheduled for 891115.Assessment Input Should Be Submitted by 891016 ML20246J5101989-08-23023 August 1989 Notification of Cancellation of 890906 Meeting W/Golden State Energy in Rockville,Md to Discuss Potential License Transfer for Plant from Smud ML20246F0401989-08-23023 August 1989 Notification of 890906 Meeting W/Golden State Energy (Gse) in Rockville,Md to Discuss Potential License Transfer from Smud to Gse ML20245H0111989-08-0909 August 1989 Notification of 890829 Meeting W/Smud in Rockville,Md to Discuss Closure & Decommissioning Plans & Preliminary Details of Potential License Transfer for Facility ML20245F1261989-08-0909 August 1989 Updates Status Following Smud Ratepayer Vote on 890606 to Close Plant,Per 890619 Staff Requirements Memo.Eligible Voters Voted 53 to 47% to Close Plant.Nrc Evaluating Util Closure Process & Will Meet W/Licensee Re Decommissioning ML20245E8501989-08-0707 August 1989 Advises of Reassignments in Project Mgt Duties Due to Recent Reorganization of Standardization & Life Extension Project Directorate ML20245H6451989-08-0404 August 1989 Requests Closure of Outstanding Action Item 87-0198,per 870617 Request Re Review & Evaluation of Acceptability of Fairbanks-Morse Diesel Generator Bearings.Action Completed W/Submittal of Transfer of Lead Responsibility to NRR ML20248D1431989-07-27027 July 1989 Forwards Proposed Generic Ltr Requesting Voluntary Licensee Participation in ERDS & Requests That Proposed Generic Ltr Be Sent to All Licensees of Power Reactors,Except for Participants & Licensees of Listed Plants ML20247B7541989-07-19019 July 1989 Confirms That Licensee 880711,890221 & 0630 Responses to NRC Bulletin 88-004, Potential Safety-Related Pump Loss, Acceptable.Licensing Action for TACs 69886,69887,69893 & 69894 Considered Complete ML20247E6721989-07-17017 July 1989 Proposes Closeout of Plant Correspondence Control Ticket Re Environ Conservation Organization Request for Notification Whenever License Amend Requests Result in Impairment of Plant Operability.Intervenor Will Be Placed on Svc List ML20246K5991989-07-12012 July 1989 Notification of 890725 Meeting W/Util in Birmingham,Al to Discuss Status of Current Licensing Activities & Corporate Initiatives for Plants.Meeting Agenda Encl ML20246L6801989-07-10010 July 1989 Notification of Significant Licensee Meeting 89-101 W/Util on 890718 in King of Prussia,Pa to Discuss Util Engineering Reorganization ML20247A9561989-07-0606 July 1989 Notification of 890717 Meeting W/Lead Plant Utils in Rockville,Md to Discuss Implementation of Revised STS ML20246D8841989-06-19019 June 1989 Staff Requirements Memo Re 890601 Briefing on Operating Reactors & Fuel Facilities in Rockville,Md.Commission Expressed Disappointment in Long Term Operating Performance of Turkey Point Nuclear Power Plant ML20244C4511989-06-0909 June 1989 Notification of 890619 Meeting W/Util & Bechtel at Plant Site to Discuss Resolution of Geologic & Seismic Issues. Meeting Will Be Followed by Field Trip ML20246H3771989-05-12012 May 1989 ALAB-913.* Advises That Time Provided within Which Commission May Act to Review Aslab Decision ALAB-913 Expired.Commission Declined Review.Decision Became Final on 890501.W/Certificate of Svc.Served on 890512 ML20246P9601989-05-10010 May 1989 Discusses 890413 Meeting W/Rosemount & Industry Re Malfunctions of Rosemount Transmitters.List of Attendess, Agenda,Nrc Info Notice 89-042 & Viewgraphs Encl NUREG-1353, Board Notification 89-003:forwards Listed Documents Re Spent Fuel Pool Accidents for Resolution of Generic Issue 82, Beyond DBA in Spent Fuel Pools, Including NUREG-13531989-05-0202 May 1989 Board Notification 89-003:forwards Listed Documents Re Spent Fuel Pool Accidents for Resolution of Generic Issue 82, Beyond DBA in Spent Fuel Pools, Including NUREG-1353 ML20055E4911989-05-0101 May 1989 Forwards Draft Documents & Supporting Info Proposed for Plant Notice of Violation & Proposed Imposition of Civil Penalties Re Release of Radioactive Liquid Effluents & Emergency Preparedness ML20245C5351989-04-21021 April 1989 Staff Requirements Memo Re 890407 Briefing in Rockville,Md Re Readiness of Plant to Restart ML20245E9781989-04-17017 April 1989 Forwards Regulatory History AC83-2 Re Licensee Action During Natl Security emergency,10CFR50 (54FR7178) ML20245B6531989-04-15015 April 1989 Forwards Evaluation Rept on BWR Overfill Events Resulting in Flooding of Steam Lines.Events Determined to Involve Deficiencies in Control Sys ML20245B7501989-04-15015 April 1989 Forwards Engineering Evaluation Rept on BWR Overfill Events Resulting in Flooding of Steam Lines.Potential for Equipment Damage Believed to Exist & Any Damage Occurring Should Be Fixed Prior to Restart ML20245B6421989-04-15015 April 1989 Forwards Engineering Evaluation Rept on BWR Overfill Events Resulting in Steam Line Flooding.Though Little Actual Damage Experienced,Potential for Equipment Damage Believed to Exist & Any Damage Occurring Should Be Fixed Prior to Restart ML20245B6191989-04-15015 April 1989 Forwards Evaluation Rept Re BWR Overfill Events Resulting in Steam Line Flooding.All Events Included Reactor Depressurization Followed by Uncontrolled Condensate or Condensate Booster Pumps Injection or Both ML20244E2681989-04-12012 April 1989 Summary of Operating Reactors Events Meeting 89-015 on 890412.Discussion of Events,List of Attendees & Three Significant Items Identified for Input Into NRC Performance Indicator Program & Summary of Reactor Scrams Also Encl ML20244A5571989-04-10010 April 1989 Notification of 890502 Meeting W/Util in Rockville,Md to Discuss Nonlinear Piping Analysis to Remove Snubbers & Pipe Supports ML20244A5461989-04-10010 April 1989 Notification of 890503 Meeting W/Util in Rockville,Md to Discuss Using Leak Before Break Methodology on Lines Connected to RCS ML20247B7351989-03-24024 March 1989 Notification of 890503 Meeting W/B&W,Inel & Util in Rockville,Md to Discuss Licensing Submittals for Plants ML20055E3341989-03-15015 March 1989 Notifies of Meeting on 890317 W/Util to Discuss Results of Licensee Investigation Re Incident Involving Resins in Liquid Effluent Waste Stream During 890115-19 ML20236A9721989-03-0707 March 1989 Forwards Feb 1989 Status Rept Re Current Review Milestones for Each Std Plant Project ML20235S6271989-02-28028 February 1989 Notification of 890307 Meeting W/Bwr Owners Group in Rockville,Md to Discuss Items of Current Interest.Agenda Encl ML20246N3171989-02-23023 February 1989 Notification of 890313 Meeting w/C-E in Rockville,Md to Discuss Results of Salem Project & Licensing of Future C-E Projects NUREG/CR-5176, Updated Board Notification 89-01 Re Lll NUREG/CR-5176, Seismic Failure & Cask Drop Analyses of Spent Fuel Pools at Two Representative Nuclear Power Plants1989-02-14014 February 1989 Updated Board Notification 89-01 Re Lll NUREG/CR-5176, Seismic Failure & Cask Drop Analyses of Spent Fuel Pools at Two Representative Nuclear Power Plants ML20245E9441989-01-31031 January 1989 Forwards Proposed plant-specific Backfit for Improved Auxiliary Feedwater Sys Reliability Analyses for Required Improvement in Secondary DHR Capability at Plant ML20055D8221989-01-13013 January 1989 Advises That Commission Has Not Objected to Intention to Issue Notice of Violation & Proposed Imposition of Civil Penalty for Violation of Requirements of Plant Radioactive Liquid Effluent Programs 1999-02-19
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, , */ %,, UNITED STATES !
! o NUCLEAR REGULATORY COMMISSION
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.t / REGION V
.7 1450 MARIA LANE, SUITE 210 WALNUT CREEK, CALIFORNIA 94596
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J' APR 131986 t
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MEMORANDUM FOR: C. J. Heltemes, Jr. , Director t Office for Analysis ar.d Evaluation of ,
Operational Data ,
FROM: John B. Martin, Regional Administrator l
SUBJECT:
\' t ABNORMAL OCCURRENCE REPORT TO CONGRESS FOR RANCHO SECO DECEMBER 26, 1985 EVENT In accordance with a phone conversation between J. L. Crews of my staff and P. E. Bobs of your office on March 31, 1986, a draft of an Abnormal Occurrence Report is enclosed. The enclosure addresses the December 26, 1985 event subject, loss of ICS power and overcooling transient.
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, , Regional Administra r .
Enclosure:
As stated cc:
J. L. Crews P. E. Bobe >
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ENCLOSURE 4 e.
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-h LOSS OF INTEGRATED CONTROL SYSTEM POWER AND OVERC00 LING TRANSIENT t
. The following'information pertaining to this event is also being reported .
concurrently in the Federal Register. Appendix A (see the third general criterion) of this report notes that major deficiencies in design, construction, use of, or management controls for licensed facilities or material can be considered an abnormal occurrence.
's
'Date and place on December 26, 1085, Rancho Seco Nuclear Generating Station, located in Clay, California, about 25 miles southeast of Sacramento, experienced a loss of de power within the integrated control system (ICS) while the plant was open.:ing at 76 percent power. Following the loss of ICS de power, the reactor tripped on high reactor coolant system (RCS) pressure followed by a rapid overcooling transient and automatic initiation of the safety features actuation system on low RCS pressure. The overcooling transient continued until ICS de pcver was restored 26 minutes after its loss. The significance of the event is that a nonsafety related system failure initiated a plant transient which could have been more severe under other postulated scenarios,
- l. The Rancho Seco Nuclear Generating Station, operated by the Sacramento Municipal Utility District (SMUD) is a 916-MWe Babcock & Wilcox (B&W)-designed pressurized water reactor. The plant received an NRC operating license in 1974
- Nature and probable Consequences At 4
- 14 a.m. on December 26, 1985, the plant was operating at 76 percent power, when a loss of integrated control system (ICS) de power occurred as a result of a single failure. The loss of de power to the ICS (a nonsafety-related system) caused a number of feedwater and steam valves.to l b reposition automatically and also caused the loss of remote control of the .
l affected valves from the control room. In addition, the main feedwater (MFW) pump turbines slowed to minimum speed and the auxiliary feedwater (AFW) pumps started. The immediate result was a reactor coolant system (RCS) l undercooking condition that resulted in the reactor tripping on high pressure. The reactor trip was followed by an overcooling condition that resulted in safety features actuation and excessive RCS cooldown.
The transient was initiated by the failure of a single module in the nonsafety-related ICS (i.e. the spurious tripping of the power supply module that interrupted all +/-24 Vdc power). The most probable cause of this failure was a design weakness that apparently made.the circuit susceptible to erratic operation if " contact resistance" between the 24 Vdc bus and the power supply monitor were to develop, and the development of a high resistance connection (i.e. a bad crimp connection) in the wiring between the
+24 Vdc bus and the power supply monitor which exposed the design weakness and caused the module to trip.
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The operators were not immediately able to restore de power within the ICS, As a result, nonlicensed operators were sent to isolate the affected steam and f eedwater valves locally with handwheels. During the first 7 minutes of the incident, the excessive steam and feedwater flows resulted in a rapid RCS cooldown of over 100 'F. The pressurizer emptied and a small bubble formed in the reactor vessel head. The RCS cooldown continued and the RCS
) depressurized to about 1064 psig and then began to repressurize. This l repressurizatf.on resulted in the RCS entering the B&W-designated pressurized I thermal shock (PTS) region. -The atmospheric dump valves and turbine bypass valves were isolated within 9 minutes after the reactor trip. However, the operators experienced difficulty closing the ICS-controlled AFW flow control valves. One of the flow control valves was "inally shut; however, the second AFW flow control valve was damaged and failed open. lhe associated AFW manual isolation valve was found to be stuck open. Therefore, both AFW pumps continued to feed and overfill one steam generator. Since the plant has no main steam isolation valves, water began to overflow into the main steam lines.
About 26 minutes after the reactor trip, the operators restored power within the ICS by reclosing two switches in an ICS cabinet. The operators were then able to close the open AFW flow control valve from the control room, which stopped the RCS cooldown, and started stabilizing the plant. The RCS had cooled down a total of 180 'F in this 26-minute period.
! While changing a valve lineup in the suction of the pump used to supply RCS makeup (makeup pump), the last suction valve to the makeup pump was inadvertently shut. This resulted in the overheating and destruction of the makeup pump. About 450 gallons of contaminated water were spilled on the floor. This failure did not directly affect the incident since a high ;
pressure inj ection (HPI) pump was available to supply RCS makeup. In {
addition, the spilled water did not result in any significant onsite or '
offsite radioactivity release or personnel dose.
i Operators later stabilized the plant and brought it to a cold shutdown . j without a significant release of radioactivity to the environment and without ;
significant additional damage to plant equipment. I The December 26, 1985 overcooling incident did not seriously threaten the integrity of the Rancho Seco reactor vessel. However, the plant has had a number of overcooling incidents in its 12-year operating history. Each time this occurs the potential exists for additional operator errors and equipment i failures that might exacerbate the event and seriously threaten reactor integrity. Thus, the significance of this incident lies in the fact that under alternate scenarios more serious consequence could occur.
The incident at Rancho Seco was also significant because a single failure in the integrated control system (ICS), which is a nonsafety-related system, subjected the plant to an undesirable overcooling transient. During the transient, the RCS cooled down 180*F in 26 minutes, the pressurizer emptied, a bubble formed in the reactor vessel head. the plant entered the pressurized thermal shock region, the safety features actuation system (SFAS) actuated, and water overflowed from a steam generator into the main steam lines. .
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Cause or Causes i 4
The fundamental causes for this transient were design weaknesses and vulnerabilities in the ICS and in the equipment controlled by that system. .
These weaknesses and vulnerabilities were not adequately compensated by other' design features, plant procedures or operator training. These weaknesses and vulnerabilities were largely known to Sacramento Municipal Utility District (SMUD) and the NRC staff by virtue of a number of precursor events and through related analyses and studies. Yet, adequate plant modifications were not made so that this event would be improbable, or so that its course or consequences would be significantly altered.
Actions Taken To Prevent Recurrence Licensee i
The licensee has undertaken extensive study (including controlled I disassembly, examination and testing) of the multiple failures associated with the event to determine root causes and to take corrective actions to prevent recurrence. Some specific improvements have been identified by these efforts and are being implemented prior to plant startup. These are described in the licensee's February 19, 1986 summary report to the NRC s (Reference 1).
Plant Modifications l 1. Replacement of power distribution wiring of the ICS Power Supply Monitor, to reduce the resistance in series with the voltage being monitored.
- 2. !
Provision of failed closed features and/or control room manual control I capability for turbine bypass valves, atmospheric dump valves, and auxiliary feedwater flow control valves, under circumstances of ICS J i fcilure. .
1 Training Classroom and simulator training relating to response to ICS power loss conditions, handling of overcooling and potential pressurized thermal shock, recovery from scfety system actions and implementation of emergency plan procedures.
Maintenance Program i
- 1. Repair of damaged equipment that is required for normal and abnormal operating conditions.
- 2. Verification of acceptable condition of equipment in the non-nuclear systems of the plant.
- 3. Development of a preventive maintenance program for non-nuclear, balance-of-plant equipment.
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. 4 Emergency Procedures Development of event related procedures to complement the symptom related emergency procedures, for ICS power loss and safety feature actuation .
system recovery.
!gC, l
Upon being notified of the event, the NRC Resident Inspectors for the plant arrived shortly thereafter. They observed licensee actions to assure the plant remained in a stable condition and began an initial investigation of the circumstances associated with the event.
On December 26, 1985, the Regional Administrator of the NRC Region V Office forwarded two Confirmatory Action Letters to the licensee (References 2 and 3)-
indicating that the licensee would perform a root cause analysis prior to return to power and would not perform any additional work on equipment that malfunctioned during the event until the NRC could evaluate the event.
On December 27, 1985, an NRC Augmented Inspection Team (AIT) was sent to the site by the Regional Administrator and started transcribed personnel interviews on December 28. The initial results of this investigation effort indicated that the event was complex and had potentially significant generic implications.
On December 31, 1985, the responsibility for the incident investigation was expanded to a special NRC Incident Investigation Team by the NRC Executive Director for Operations at the re' quest of the Region V Regional Administrator, in conformance with a NRC staff-proposed Incident investigation Program. The Team, composed of six technical experts, was to (1) fact-find as to what happened; (2) identify the probable cause as to why it happened; and (3) make appropriate findings and conclusions to form the i basis for possible follow-on actions. The Team consisted of the AIT members i supplemented by additional staff. It continued the investigation started by -
the AIT at the plant site, The equipment which malfunctioned was quarantined. ;
The Team collected and evaluated information to determine che sequence of I operator, plant, and equipment responses during the event and the causes of equipment malfunctions. The sequence of these responses was determined primarily by interviewing personnel who were at the plant during the event and by reviewing plant data for the period immediately preceding and during' the event. The Team also toured the plant to examine the equipment'which.
malfunctioned, the equipment that was key to mitigating the transient, and the control room instrumentation and controls. The Team also interviewed plant management personnel'and NRC Region V personnel who arrived at the site soon after the plant was stabilized about their knowledge of the plant response and operator actions. By correlating plant records with personnel statement on their actions and observations, the Team was able to compile a picture of the event. 1 1
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. 5 During and subsequent to their onsite activities the Team reviewed and concurred in specific troubleshooting plans developed by the licensee for equipment disassembly, inspection and testing. Several of these activities were witnessed by NRC inspectors, The results of the Team's investigation are contained in NUREG-1195 l' (Reference 4). Problems identified included issues specific to Rancho Seco and several possible generic issues. The Team concluded that design weaknesses and vulnerabilities in the ICS and in the equipment controlled by that system were not adequately compensated by other design features, plant procedures or operator training. These weaknesses and vulnerabilities were largely known to Sacramento Municipal Utility District (SMUD) and the NRC staff by virtue of a number of precursor events and through related analyses and studios. Yet, adequate plant modifications were not made so that this event would be improbable, or so that its course or consequences would be significantly altered.
The NRC continues to be involved in the resolution of this event and related matters. The Executive Director for Operations has directed (Reference 5)
NRC program managers to conduct further generic and plant specific follow-up actions. Development of NRC plant specific action plans commenced while the ;
IIT was on-site in January 1986, and have been expanded subsequently to ;
include a review of the completeness of prior staff and licensee actions j associated with the control systems.
The Executive Director for Operations has also considered this evenc in a ;
January 24, 1986 (Reference 6) request to the B&W Owners Group, to obtain an i industry effort to assess the generic aspects of plant responses to '
i transients, and methods of reduction of the number of plant trips. The Owners l
' Group has been responsive to this request and on April 8, 1986 presented a draft plan of action for conducting the necessary reviews.
l In addition to addressing those issues which have arisen directly as a result '
. of the December 26, 1985 cooldown transient, the NRC regional office has .
re-evaluated the status cf prior Rancho Seco open inspection findings to identify matters which should be resolved prior to restart of the plant.
The licensee and NRR have included these in restart plans. Also, the NRC staff has encouraged the licensee to reexamine the status of all critical plant systems to assure readiness for operation and maximum reliability, so that operation of the plant may be continued with a low probability of disruption from internal causes. Some of these efforts will be observed by NRC inspectors.
These actions outline a program that evaluates the Rancho Seco restart program, and assures that generic aspects are considered.
l Future reports will be made as appropriate.
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Refeesnces
- 1. Letter from R. J. Rodriguez, Assistant General Manager Sacramento Utility District to J. B. Martin, Regional Administrator, NRC Region V .
and F. J. Miraglia Jr. , Director, FWR-B Division, NRC February 19, 1986, forwarding a summary report " Description and Resolution of issues Regarding the December 26, 1985 Reactor Trip".
- 2. Letter from J. B. Martin, Regional Administrator, NRC Region V to R. J. Rodriguez, Assistant General Manager, Sacramento Municipal Utility District, December 26, 1985, requesting that a root cause analysis be completed before return to power.
- 3. Letter from J. B. Martin, Regional Administrator, NRC Region V to R. J. Rodriguez, Assistant General Manager, Sacramento Municipal Utility District, December 26, 1985, requesting the licensee to hold in abeyance l any repair work planned on equipment that malfunctioned l i
- 4. U. S. Nuclear Regulatory Commission, " Loss of Integrated Control System l Power and Overcooling Transient at Rancho Seco on December 26, 1985", !
USNRC Report NUREG-1195, published February 1986. I
- 5. Memorandum, Victor Stello, Jr., Acting Executive Director for Operations to Harold R. Denton, Director, NRR; James E. Taylor, Director IE; John B. Martin, Regional Administrator, Region V, dated March 13, 1986 -
" Staff Actions Resulting from the Investigation of the December 26, 1985 I
Incident at Rancho Seco (NUREG-1195)".
- 6. Letter from Victor Stello, Jr., Executive Director for Operations, to Hal Tucker, Chairman of Babcock and Wilcox Owners Group, dated January 24, 1986 requesting an evaluation of design of B&W plants for reduction of plant trips and mitigating transient response. .
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