ML20236N028

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Insp Rept 50-440/98-10 on 980421-0604.Violations Noted.Major Areas Inspected:Operations,Maint & Surveillance,Engineering & Plant Support
ML20236N028
Person / Time
Site: Perry FirstEnergy icon.png
Issue date: 07/09/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20236N019 List:
References
50-440-98-10, NUDOCS 9807140367
Download: ML20236N028 (21)


See also: IR 05000440/1998010

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U. S. NUCLEAR REGULATORY COMMISSION q

REGIONlli

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Docket No: 50-440

License No: NPF-58

Report No. 50-440/98010(DRP)

Licensee: Centerior Service Company

P.O. Box 97, #200

Perry, Ohio 44081

Facility: Perry Nuclear Power Plant

Location: Perry, Ohio

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Dates: April 21 through June 4,1998  ;

inspectors: C. Lipa, Senior Resident inspector

J. Clark, Resident inspector

Approved by: Thomas J. Kozak, Chief

Reactor Projects Branch 4

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9907140367 980709

PDR ADOCK 05000440

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EXECUTIVE SUMMARY

Peny Nuclear Power Plant

NRC Inspection Report 50-440/98010(DRP)

This inspection report included resident inspectors' evaluation of aspects of licensee operations,

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engineering, maintenance, and plant support. The report covers a 6-week period of resident

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inspection.

Operations

e Two operator errors occurred, which were primarily due to inadequate attention-to-detail

during the performance of routine tasks. Both of the errors also represented a failure to

follow a procedure. The inspectors concluded that the failure of operators to

appropriately follow procedures on two occasions led to two personnel errors involving

the removal of an incorrect fuse and installation of an incorrect light bulb. A third operator

enor is discussed in Section M1.2. (Sections 01.2 and 01.3)

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e The inspectors identified four examples of deficiencies that indicate inconsistent operator

attentiveness and awareness of control room panels. The inspectors continue to be

concemed about the varying level of attention to detail and questioning attitude exhibited

' by operators in their routine panel observations. (Section 04.1)

l Maintenance and Surveillance

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The inspectors identified a procedure adherence concern with the performance of a

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surveillance test which resulted in a violation. The inspectors were also concemed that

operations supervision failed to identify an omitted step during review of the data

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package. (Section M1.2)

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e ' The inspectors noted an increase in the number of emergent equipment issues over

recent inspection periods. Some items resulted in distractions to operators or entry into

l Limiting Conditions for Operation. In each case, the licensee resolved the issue promptly.

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e The inspectors identified a procedure adherence violation involving the improper control

of transient combustibles during maintenance activities. The inspectors were also

concemed that supewisory and fire protection personnel did not display adequate

attention to detail in reviewing the administrative control of the transient combustibles.

(Section M2.2)

e The inspectors identified three procedure adherence violations of minor significance

associated with housekeeping and equipment control activities. (Section M2.3)

Enaineerino

e The licensee demonstrated a good questioning attitude in the identification of inadequate

logic testing of radiation monitors. The relay contacts were promptly satisfactorily tested.

(Section E1.1)

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Plant S!Jpport

  • The inspectors were concemed that access control procedures were not uniformly }

followed by station and contract personnel. This procedure adherence concem is l

concurrent with procedure adherence concems seen in other departments throughout this

inspection period. (Section S1.1)

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Report Details

Summary of Plant Status

The plant began this inspection period at 100 percent power and remained at that power level for

most of the inspection period except for a short duration power change to support a control rod

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pattem change.

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l. Operations

! 01 Conduct of Operations

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l 01.1 General Comments

a. Inspection Scope (71707)

l The inspectors followed the guidance of Inspection Procedure 71707 and conducted

frequent reviews of plant operations. This included observing routine control room

activities, reviewing operator logs and system tagouts, attending shift tumovers and crew

i briefings, and performing panel walkdowns.

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b. Observations and Findinas

The conduct of operations was professional The inspectors observed thorough shift

tumovers and good communications. Overall, emergent equipment issues were promptly

addressed and the conduct of operations was appropriately focussed on safety.

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Concems with operator errors during the performance of routine activities and with

! operator attentiveness to control room panels are discussed in Sections 01.2, O1.3, and

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01.4, respectively.

01.2 Operator Error While Removina a Fuse

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a. Inspection Scope (71707)

The inspectors reviewed the circumstances surrounding an operator error during a tagout

activity. This review included Condition Report (CR) 98-1057, Work Order 97-3521,

Tagout No. 30442, and Plant Administrative Procedure (PAP) -1401, " Safety Tagging."

b. Observations and Findinas

On May 6,1998, a licensed operator opened the knife switch for the wrong fuse while

. hanging a tagout on the combustible gas control system. Tagout No. 30442 specified

! which fusa to remove and listed the corresponding wire markings. The operator

incorrectly selected the adjacent fuse, which had a similar wire marking that differed by

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only one character. There was no effect on the plant as a result of this error. The

condition was corrected and the correct fuse was subsequently removed.

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Based on interviews and information provided in the CR, it appeared that the licensed

operator compared the wire markings on the tagout sheet to the markings in the panel

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. while another licensed operator provided dual concurrent verification. Additionally, a Unit

Supervisor (US) provided oversight for this activity. However, this additional review did

not prevent the error.

The inspectors were concemed' that this tagout error was similar to errors in

February 1998 and August 1997 (documented in Inspection Reports 50-440/98007 and

50-440/97012, respectively). The use of dual concurrent verification and US oversight

was an improvement from the' processes in place when the tagout errors occurred in

1997. However, the additional verification as implerrented failed to prevent this error.

The failure to remove the correct fuse while hanging Tagout No. 30442 was a violation for

failure to follow PAP-1401 as required by Technical SpecificaSon (TS) 5.4.1. Although

licensee-identified, this was not a non-repetitive violation and is, therefore, being cited as

a violation of TS 5.4.1.a. (VIO 50 440/fr8010-01(DRP))

01.3 Operator Error While Replacina a Control Panel Liaht Bulb

a. Inspection Scope (71707)

On April 25,1998, a licensed operator replaced a control panel light bulb with a different

type than the prescribed light bulb. This caused a fuse to blow and loss of power to

residual heat removal (RHR) system trains "B" and "C." The inspectors reviewed the

circumstances of the event and the licensee's corrective actions.

b. Observations and Findinas

A licensed operator inadvertently replaced a light bulb with the wrong type. This caused

- a blown fuse in the RHR "B" and "C" control logic. The licensee's investigation

determined that the operator failed to follow the requirements of PAP-0201 and verify that

the replacement bu!b was the same size and type as the one removed. The following

corrective actions were performed:-(1) the correct bulb was installed, the fuse was

replaced, and the circuitry was checked for any potential damage, (2) a Category 3

investigation of Potential Issue Form (PlF) 98-0802 was completed, and (3) a lessons

leamed review was prepared and shared with other operations department personnel.

This non-repetitive, licensee-identified and corrected violation is being treated as a Non-

Cited Violation, consistent with Section Vll.B.1 of the NRC Enforcement Pclicy.

(NCV 50 440/98010-02(DRP))

. 01.4 - Conclusions on Conduct of Operations

Two operator errors occurred, which were primarily due to inadequate attention-to-detail

during the performance of routine tasks. - Both of the errors also represented a failure to

follow a procedure. The inspectors concluded that the failure of operators to

appropriately follow procedures on two occasions led to two personnel errors involving

the removal of an incorrect fuse and installation of an incorrect light bulb.

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02 Operational Status of Facilities and Equipment l

O2.1 General Plant Tours and System Walkdowns (71707)

The inspectors followed the guidance of Inspection Procedure 71707 in walking down

accessible portions of several systems and plant areas, including:

o Control complex ventilation systems

e Emergency batteries

e Emergency diesel generators

e Emergency service water pump house

e Auxiliary building

e Intermediate building

Equipment operability was acceptable in all cases. Concems with materials being

improperly stored or staged to support maintenance activities are discussed in

Sections M2.2 and M2.3. Several minor discrepancies, such as loose or missing labels

on safety-related circuit breakers, were brought to the licensee's attention and were

corrected.

04 Operator Knowledge and Performance

l 04.1 Concems With Operator Attentiveness and Awareness of Control Room Panels

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a. Inspection Scope (71707)

l The inspectors conducted panel walkdowns in the control room and discussed minor ,

l deficiencies with operations personnel.  !

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l b. Observations and Findinas

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e On May 6,1998, the inspectors noted, in the horseshoe area of the control room,

that the green indicating lights for two main turbine bearing oil lift pumps were not

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l" illuminated. All of the adjoining pumps had clearly illuminated green indicatinD

l lights. The inspectors questioned the supervising operator at the controls

l (SO-ATC) about the status of these indicators. The SO-ATC stated that the j

l indicators were in fact illuminated, but dim. The SO-ATC cupped a hand around I

the lens to demonstrate. After the inspectors continued their walkdown, the

SO-ATC brought the inspectors' question to the US. The US performed the same

hand-cupping technique to observe the lights. The US also stated that the

indicators were illuminated, but dim and instructed the SO-ATC to change the two

light bulbs. Afterthe bulbs were changed, there was no apparent change in the

indication. Operations personnel contacted the responsible system engineer and

discovered that the lights should not beve buen illuminated under the plant

conditions. The lights were subsecamly verified to be de-energized.  ;

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I' e On April 24,1998, and on several other occasions throughout the inspection

period, inspectors noted that the drywell equipment drain sump level / rate recorder

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(E31-R619) paper drive was sticking. The inspectors discussed this with several

shift and USs. However, it was not until it was discussed again with a US.on

May 29,1998, that a deficiency tag was initiated,

e On May 8,1998, chemistry department personnel identified that the reactor water

cleanup conductivity chart recorder was not advancing. Upon further review, the

licensee uetermined that the paper had not moved in 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> since the paper had

been replaced. The inspectors were concemed that operators had not identified

the condition because markings on the recorder paper should have alerted the

SO-ATC that the paper was not advancing. The recorder was subsequently

repaired.

o On May 16,1998, the inspectors identified that the " manual" push button for the

"B" reactor recirculation flow control hand station (B33-K603B) was not lit. The

corresponding push button on the "A" hand station was lit. Without the light,

operators could not tell whether the controller was in " manual" or " auto" control.

, The operators explained that this condition had existed for several months. In

j addition, the operators indicated that the push button is always rer;uired to be in

I manual by procedural controls and that it would be a high risk evolution to change

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out the bulb with the plant operating. The inspectors reviewed the open work

j orders on June 3,1998, and identified that no deficiency tag had been written for

this condition. The inspectors were concemed that operations personnel knew of

the deficiency, but had not initiated a deficiency tag.

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During an Operations Assessment Team inspection (Inspection Report 50-440/98007)

earlier this year, similar occurrences of indication anomalies were observed. During that

inspection, the inspectors raised concems that operations personnel exhibited varying

levels of attention to detail on panel walkdowns and that a questioning attitude toward

equipment status was not always evident. The observations with the oil lift pump

indication, recorder paper drives, and unlit manual push button bulb are additional  ;

examples of these concerrsa, j

c. Conclusions

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L Four examples of unidentified or undocumented deficiencies were identified by the

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inspectors that indicated inconsistent operator attentiveness and awareness of control ,

room panels. The inspectors concluded that the level of attention-to-detail and

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questioning attitude used by operators in their routine panel observations varied from

! operator to operator. The inconsistency led to the failure of operators to identify or report

l- four control panel deficiencies that were identified by the inspectors.

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06. . Operations Organization and Administration

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06.1 Chance in Operations Manaaer

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On May 11,1998, Mr. T. Rausch was named as the Operations Manager. He was

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formerly Director of Quality and Personnel Development. Mr. F. Keamey remains as the

Operations Superintendent. The inspectors verified that the Operations ManacGr and

. Operations Superintendent met the qualifications of ANSI /ANS-3.1-1993 as required by

.TS 5.2.2.f and 5.3.1.

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07 Quality Assurance in Operations

07.1; Licensee Self-Assessment Activities (71707)

During the inspection period, the inspectors reviewed multiple licensee self-assessment

activities, including:  !

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e Audit Report 98-01, " Conduct of Operations," l

e Company Nuclear Review Board, April 23,1998

e Daily Management Review of New Condition Reports

The meetings were attended by appropriate personnel and there was sufficient

discussion of items. The inspectors concluded that the self-assessment activities <

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observed were thorough, self-critical, and effective in identifying problems and developing

corrective actions.

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1 08 Miscellaneous Operations issues (92901)

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I' 08.1 (Closed)' Unresolved item 50-440/95002-01(DRP): Locked Valves Not Properly Locked.

On February 18,1995, the licensee identified that two safety-related valves in the nuclear

closed cooling system required to be locked closed were closed, but not locked. The .

l valves were "T" handle valves and the locking device'apparently slipped off the handle.  ;

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The licensee placed instructions in the operations standing instructions to ensure proper  ;

locking by the use of a tight " figure 8"Icop around the handle. Plant Administrative '

i Procedure PAP-0205, " Operability of Plant Systems" was subsequently revised to

l incorporate the instructions. The inspectors conducted a search of other PlFs related to l

l unlocked valves since 1995. There were no other s!milar problems after the corrective l

[ actions were in place. The failure to property lock the valves in this case constitutes a  !

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violation of minor significance and is not subject to formal enforcement action. This item  !

is closed.

! ' 08.2 '(Closed) Violation 50-440/95008-01(DRP): Automatic Reactor Scram Due to Personnel ,

Errors and Failure to Follow Procedure. On September 2,1995, operators failed to verify -

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the Reactor Feed Pump Turbine Flow Control was in manual as required by the System

Operating Instruction. The details of the event are described in Inspection

. Report 50-440/95008.- The licensee's Human Performance Enhancement System

evaluation concluded that this event was caused by operator error. The two operators

j. involved were temporarily removed from licensed duties, were rounseled on their -

improper actions, and received remedial training. A lessons leamed videotape was

L presented to all operating crews which emphasized management's expectations for using

L . self-checking practices. The inspectors determined that corrective actions were

sufficient. This item is closed.

08.3 (Closed) Violation 50-440/95009-01(DRP): Three Examples of inadequate Corrective I

~ Actions. Specific corrective actions to address this violation were reviewed by the

inspectors and considered acceptable, improvements in the Corrective Action Program

were documented in Inspection Report 50-440/98002(DRS). This item is closed.

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II, Maintenance

M1 Conduct of Maintenance

Mi.1 ' General Comments

The inspectors observed or reviewed all or portions of the following work activities:

-e SVI-R45-T2002, " Division 2 Diesel Generator (DG) Fuel Oil Transfer Pump and

Valve Operability Test"

e. Technical Specification Rounds

e SVI-R45-T1320, " Standby Diesel Fuel Oil Receipt Analysis"

.*. SVI-C11-T0044A, * Scram Discharge Volume Water Level High Channel A

Functional"

e SVI-E31-T0374, " Reactor Coolant System Unidentified Leakage Determination"

The inspectors identified several concems with procedural adherence during the

performance of routine activities, as discussed in the following sections.

Mt.2 Procedure Comoliance Concems Durina Diesel Fuel Oil Transfer Pumo Surveillance Test

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a. Inspection Scope (61726 and 71707)

The inspectors observed operations personnel perform a regularly scheduled TS required

sumeillance test (SVI). This included field observation of the test, review of results, and

comparison to TS requirements,

b. Observations and Findinas

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l On May 4,1998, inspectors observed portions of the performance of SVI-R45-T2002, '!

" Division 2 DG Fuel Oil Transfer Pump and Valve Operability Test," Revision 2 l

, (June 1994). During the performance of Step 5.1.2.23, operations personnel experienced
. difficulty in reading the discharge pressure gauge due to pulsations. An in-service testing

l . group representative recommended a technique to the operators to obtain a stable

reading. Based upon this recommendation, the operators closed and then cracked open

l valve 1R45-F501B to obtain a stable reading. Valve 1R45-F501B was directed to be

l opened in Step 5.1.2.19. No other procedure reference was made for operating or

throttling the valve. The operators did not inform their supervision of the valve '

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manipulation, nor was this documented in the data package. The inspectors discussed

this issue with the Shift Supervisor and the Operations Superintendent. While

l manipulation ~of the gauge isolation valve could have been considered a practice within

l the skill-of-the-trade, operations supervision stated that this practice did not meet their

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expectations since the operators appeared unaware of this technique, and because the  !

operators did not stop and request supervisor guidance when unable to complete the SVi

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step as written.

On May 5,' 1998, the inspectors reviewed the completed data package for

SVI-R45-T2002. A comment in the data package indicated that Section 5.1.4 of the SVI, ,

which tested air compressor 1R44-C002B, was not performed due to a tagout. The  :

inspectors noted that the control switch for fuel oil transfer Pump No. 2 (1R45-C002B)  ;

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was incorrectly marked as "N/A" on the system restoration checklist. The inspectors also

noted that the SVI was fully reviewed by operations supervision without noticing the

l discrepancy. This was brought to the attention of the shift and unit supervisors. The

licensee determined that this step was erroneously marked "N/A" due to confusion

between R44 and R45 designations. The control switch was in the correct position.

Technical Specification 5.4.1.a requires, in part, that procedures be implemented

covering applicable procedures recommended in Regulatory Guide (RG) 1.33, Revision 2.

One of the recommendations in RG 1.33 is for written procedures to be implemented to

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conduct surveillance tests. Section 5.2.1 of SVI R45-T2002 required the completion of

L the system restoration checklist. On May 4,1998, operators failed to verify all of the

restoration items specified in the SVI checklist. The NRC identified error in implementing

l the SVI is a violation of TS 5.4.1.a. (VIO 50-440/98010-03(DRP))

c. Conclusions

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The inspectors identified a procedure adherence concem with the performance of a

surveillance test which resulted in a violation. The operators failed to properly verify the

status of an item in the system restoration checklist. The inspectors were also concemed

that operations supervision failed to identify an omitted step during review of the data

package.

M2 Maintenance and Material Condition of Facilities and Equipment .

M2.1 Plant Material Condition

a .- Inspection Scoce (62707)

The inspectors reviewed several emergent work items to ensure appropriate operability

evaluations were performed, TS requirements were met, repairs were made, and root

causes were determined where appropriate.

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b. Observations and Findinas

The inspectors noted that there were several emergent equipment issues during the

inspection period. Although overall plant material condition remained good, the

inspectors noted an increase in sme gent issues over recent inspection periods. The

issues resulted in distractions to operators or entry into Limiting Conditions for Operation

(LCO) in several cases. In each case, the inspectors observed appropriate and timely

resolution. There was effective involvement by engineering personnel and other

departments as necessary. For example,

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e On April 27,1998, the "B" reacto! water cleanup pump tripped. A replacement

pump was installed and retumed to service on April 28,1998.

e On May 17,1998, a scram discharge volume level transmitter failure resulted in a

j half scram. The component was replaced on the same day.

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e On May 18,1998, an annunciator panellost power. This resulted in a loss of

generator hydrogen and stator water cooling annunciators and would prevent

generator runback circuitry on a loss of stator water cooling. The item was -

successfully repaired the next day.

o On May 22,1998, while operators were attempting to transfer the

Division 2125 Vdc battery from the reserve to the normal battery charger, several

alarms were received. The operators transferred the battery back to the reserve

charger and several more alarms came in.. The alarms were caused by a failure

in the alarm circuit. The circuit was successfully repaired the next day,

e On May 23,1998, a Division 2 DG high Jacket water temperature alarm was

received. The heater was not cycling off at the high temperature set point due to

a problem with the temperature switch, which was subsequently repaired.

! e On May 26,1998, a Division 1 DG lowJacket water temperature alarm was

received. The heater was not cycling on at its low set point. The cause was a

problem with the temperature switch, which was subsequently repaired. The

licensee initiated CR 98-1183 as a result of experiencing problems on both

divisions of Jacket water temperature indication within a few days of each other,

j e On May 26,1998, the recorder for drywell unidentified leakage failed. In order to

, meet TS required surveillance requirements, a special surveillance test was

completed each shift for approximately one week until the recorde. was repaired

and retumed to service.

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c. Conclusions

The inspectors noted an increase in the number of emergent equipment issues over

recent inspection periods. Some of the items resulted in distractions to operators or entry 1

into Limiting Conditions for Operation. In each case, the licensee resolved the issue

promptly.  !

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M2.2 Imoroper Control of Transient Combustibles  ;

a. InsDection Scope (62707)

i The inspectors conducted walkdowns in areas of the plant to assess ongoing

safety-related maintenance activities.

b. Observations and Findinas

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On May 8,1998, the inspectors toured the 679-foot elevation of the controls complex.

l The inspectors noted approximately 30 cardboard barrels of charcoal media staged near

safety-related control room heating, ventilating, and air conditioning (HVAC) equipment.

The inspectors noted that a transient combustible permit (TCP) was posted for this rnedia  :

with ongoing control room HVAC work. However, the inspectors noted that the TCP had

expired on March 10,1998. The inspectors notified operations personne! about the

expired TCP, and a new TCP was issued.

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Licensee personnel subsequently determined that the maintenance covered by the TCP

was originally scheduled for February, but had been rescheduled. On March 9,1998, the

TCP was administratively closed. However, the existing TCP was not removed from the

maintenance work package. When the work recommenced in May, workers posted the

TCP from the work package without verifying its status. Maintenance supervision and fire

protection personnel subsequently toured the area and noted a TCP was posted.

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However, they too did not notice that the TCP had expired.

Perry Nuclear Power Plant TS 5.4.1.a. requires that written procedures shall be

implemented covering the applicable procedures recommended in RG 1.33, Revision 2,

Appendix A. Appendix A of RG 1.33 specifies that activities such as fire protection

should be controlled by written procedures.

Part of the plant fire protection program is implemented by Plant Administrative

l Procedure, PAP-1913, " Control of Combustibles," Revision 4. Section 6.4.1 of PAP-1913

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specifies that a Transient Combustible Permit is required to authorize, track, and

document the use of transient combustible materials when the quantity of the

flammable / combustible material exceeds 100 pounds of normal combustibles within

20 feet of safety-related equipment. On May 8,1998, the inspectors identified more than

l 4000 pounds of combustible material, with an expired Transient Combustible Permit, in

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an area within 20 feet of safety-related equipment in the control complex. This NRC

identified failure to follow PAP-1913 is a violation of TS 5.4.1.a.

(VIO 50-440/98010-04(DRP))

c. Conclusions

The inspectors identified a procedure adherence violation involving the improper control

of transient combustibles during maintenance activities. The inspectors were also

concemed that supervisory and fire protection personnel did not display adequate

attention to detailin reviewing the administrative control of the transient combustibles.

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M2.3 Improper Housekeeping md Eauioment Control

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a. Inspection Scope (62707)

The inspectors conducted walkdowns to assess housekeeping and equipment control

- during ongoing safety-related maintenance activities,

b. Observations and Findinas

l The inspectors toured the auxiliary building and the controls complex. Several

l ' housekeeping and material controls issues were identified.

L On May 8,1998, the inspectors identified a large cart in the controls complex

without its wheels locked, blocked, or removed. The cart was near safety-related

control room HVAC equipment on the 679-foot elevation of the controls complex.

Plant Administrative Procedure, PAP-204, " Housekeeping / Cleanliness Control

l Program," requires, in part, minimizing seismic falldown/ interaction concems

related to equipment temporarily stored / staged in safety-related buildings by

adhering to specific requirements. One of these requirements is that cart wheels

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be locked, blocked, or removed. This failure to follow PAP-204 as required by

10 CFR Part 50, Appendix B, Criterion V, constitutes a violation of minor 1

significance and is not subject to formal enforcement action.

On May 8,'1998, the inspectors identified a compressed gas bottle tied to a

safety-related 1" conduit (1R33T218C) on the 620-foot elevation of the auxiliary ,

building. Plant Administrative Procedure -204 also requires that for stored items, l

a clearance of at least 1.5 times the height of the item be maintained from

safety-related items. This failure to follow PAP-204 as required by

10 CFR Part 50, Appendix B, Criterion V, constitutes a violation of minor

significance and is not subject to formal enforcement action.  ;

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On May 8,1998, the inspectors identified a safety-related instrument cable tray

(No.1660) with the radio frequency cover off and tied-back to an adjacent tray in

the 620-foot elevation of the controls complex. Drawing D-214-001, " Cable Tray

Layout," Note 15, specifies that the affected instrument trays have solid covers

throughout the run for radio frequency protection. This failure to follow PAP-204

as required by 10 CFR Part 50, Appendix B, Criterion V, constitutes a violation of

minor significance and is not subject to formal enforcement action. ,

These three examples of procedure violations were quickly corrected after identifying the

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problems to the licensee. Condition reports were also initiated by the licensee to

investigate the causes and for trending purposes. Additional examples of procedure l

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violations in other departments are documented in Sections 01.2, O1.3, M1.2, M2.2, and

S1.1 of this report.

c. Conclusions

The inspectors identified three procedure adherence violations associated with

housekeeping and equipment control activities. This involved equipment that was

improperly staged or stored for maintenance activities.

M8 Miscellaneous Maintenance issues (92903)

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M8.1 (Closed) Violation 50-440/95008-02(DRP): Improper Verification of Equipment Prior to

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Work. No response was requested for this violation. The inspection report documented

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the inspectors' determination that corrective actions were prompt and effective. This item

is closed.

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M8.2 (Closed) Unresolved item 50-440/96006-01(DRP): Past Operability of Division 3 DG with

,

Degraded Air Start Subsystem. The inspectors were concemed that degradation in one

l DG air start subsystem could render the DG inoperable due to the description in the TS

bases. The TS bases states that two air start subsystems are required for operability.

Actual test results indicated that the TS start time limit of 10 seconds was met with the

degraded subsystem. The subsystem was promptly repaired in August 1996. Upon

further review and discussion with the Office of Nuclear Reactor Regulation, the

inspectors concluded that the DG was operable, although degraded. This item is closed.

M8.3 (Closed) Violation 50-44-/97009-04(DRP): Failure to Follow Procedure During

Safety-Related Valve Packing Maintenance. The inspectors had identified that

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maintenance personnel did not follow work order instructions as required. The inspectors

reviewed the licensee's letter dated December 23,1997, in response to the violation.

Corrective actions included a revision to General Maintenance Instruction, GMI-0061,

l " Valve Packing Instruction," and counseling of the maintenance supentisor and

I

maintenance technician involved with the event. No further concems were identified.

This item is closed.

l M8.4 (Closed) Unresolved item 50-440/98009-02(DRP): Jacket Water Level Indicator

l Concems. The inspectors questioned the ability of operators to verify Jacket water level

and DG operability due to repetitive problems with the Jacket water level indicator. In

response to the inspectors' concems, the licensee performed a calculation (as part of

PlF 98-700) that verified DG operability. The DG Jacket water level would be maintained

at an operable level as long as the water level was above the low level alarm setpoint.

Since the alarm setpoint actuated at more than 3 feet above the minimum net positive

suction head requirements for the system, operability is maintained using the alarm as a

minimum levelindication. The licensee's calculation also verified operability considering

evaporation losses. The licensee also initiated other corrective actions as a result of

PlF 90-700. The level indicator was scheduled to be replaced with an indicator of

improved design, the system operating instruction was revised to provide additional

controls on water level in the standpipe, and the operator logs were revised. This item is

closed.

lil Enaineerina

E1- Conduct of Engineering (37551)

The inspectors evaluated engineering staff involvement in resolution of emergent material

condition problems and other routine activities. The inspectors reviewed areas such as

operability evaluations, root cause analyses, safety committees, and self-assessments.

The effectiveness of the licensee's contrels for the identification, resolution, and

prevention of problems was also examined. No concems were identified.  ;

E1.1 Failure to Meet TS Surveillance Requirement Due to inadeouste Loaic Testina

a. Inspection Scope (37551)

On May 6,1998, the licensee identified that four high radiation alarm relay contacts had

not been tested and that TS Surveillance Requirement (SR) 3.3.6.1.5 had not been met ]

since February 8,1994. The licensee reported the condition in a Licensee Event Report

(LER) 50-440/1998-01 as required by 10 CFR 50.73. The inspectors reviewed the

associated condition report, CR 98-1052, the LER, and the results of testing performed

on May 6,1998, to meet TS SR 3.0.3.

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b. Observations and FindinSLs

On May 5,1998, questions were raised by a Licensed Operator Class regarding

containment vent exhaust radiation monitor trip logic. While reviewing the system

drawings on May 6, the procedure writers identified that icsting required by l

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TS SR 3.3.6.1.5 had not been satisfied. Four high radiation alarm relay contacts had not

been tested since 1994. A test document was promptly initiated and the relay contacts l

were satisfactorily tested later the same day. l

Based on an investigation, the licensee determined that an error was made while j

incorporating TS Amendment 77. Corrective actions included: (1)reviewof testing and

drawings for other similar radiation monitors, (2) review of other procedure changes

related to TS Amendment 77, and (3) revision of surveillance test procedures and related

~ drawings. Also, LER 50-440/1998-01 was issued (See Section E8.7 for LER closure).

This non-repetitive, licensee-identified and corrected violation is being treated as a Non-

Cited Violation, consistent with Section Vll.B.1 of the NRC Enforcement Policy.

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(NCV 50-440/98010-05(DRP))

c. Conclusions -

The licensee demonstrated a good questioning attitude in the identification of inadequate

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logic testing of radiation monitors. The relay contacts were promptly satisfactorily tested.

E8 Miscellaneous Engineering issues (92700,92902)

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E8.1 (Closed) Violation 50-440/95004-01(DRP): Slow Corrective Actions Related to On-Site

Vehicle Movements Interfering With Overhead Power Lines. No response was requested

for this violation due to the documentation of sufficient corrective actions in the Inspection

Report. This item is closed.

E8.2 (Closed) Unresolved item 50-440/96002-03: Past Review of Loss of Offsite Power / Loss

of Coolant Accident Test Data Due to Clipping of Data Observed in 1996. During

surveillance testing on February 21,1996, the licensee identified that limitations in

discharge pressure instrumentation prevented the determination of actual time to

discharge pressure stabilization. The licensee reviewed data for the A RHR pump motor

electrical current and determined that response time requirements were met.

Additionally, the licensee reviewed all past performances of surveillance test

SVI-R43-T5366, "LPCS/LPCI A initiation and Loss of EH11 Response Time Test,"

Revision 6 and determined that the discharge pressure stabilization method was

incorrectly used. The licensee did; however, determine that Technical Specification

requirements were met by evaluating recorded electrical current data from past

surveillance tests. The inspectors independently reviewed the electrical current data from

past surveillance tests and agreed TS requirements were met. The licensee's review

was documented in PlF 96-893. This item is closed.

E8.3 (Closed) Inspection Followuo item 50-440/96002-05(DRP): Review of Spent Fuel Pool

Licensing Basis Information. The Project Manager from the Office of Nuclear Reactor

Regulation reviewed procedures, the Updated Safety Analysis Report (USAR), and TS.

No concems were identified. This item is closed.

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E8.4 (Closed) Inspection Followuo item 50-440/96003-07(DRP): NUKON Piping insulation in

the Drywell. The inspectors had identified that the insulation on main steam isolation

valves had been pierced by large bolts. The condition was corrected prior to startup from

the refuel outage. This item is closed.

E8.5 (Closed) Inspection Followuo item 50-440/96003-12(DRP): Main Condenser Evacuation

System. The inspectors reviewed this item and applicable USAR sections and

determined that there were no discrepancies or concems. This item is closed. l

E8.6 (Closed) Violation 50-440/%005-02(DRP): Slow identification of Condition Adverse to

Quality. A containment vacuum breaker valve was discovered to have a bent linkage arm

for position indication, which could have affected the local leak rate testing of the valve. l

The condition was not promptly brought to the attention of control room personnel. The .

licensee's corrective actions for this violation appropriately focused on the importance of l

timely reporting of conditions adverse to quality. This item is closed. '

E8.7 (Closed) LER 50-440/1998-01-00: Instruction Revision Results in inadequate Testing and

Missed TS SR. This item is discussed in Section E1.1 and is closed based on on-site

review of corrective actions.

E8.8 (Closed) inspection Follow-up Item 50-440/%003-08(DRP): Electrical Penetrations

Conformance to USAR. The inspectors had identified an apparent discrepancy between

the USAR description of the electrical penetrations and known degraded c,onditions. 1

There were three separate penetrations that were degraded. Compensatory measures

were established to test and pressurize the degraded penetrations once per week to

ensure that design parameters continued to be met. Repairs were planned for refueling

Outage 7 (Spring 1999). The inspectors determined that there was no USAR discrepancy

as written and that short-term corrective actions were appropriate with long-term actions

scheduled for the next refueling outage. This item is closed.

IV Plant Support

S1 Conduct of Security and Safeguards Activities

31.1 Access Control Procedure Adherence

a. Inspection Scope (71750)

The inspectors reviewed access control facilities and procedures with the licensee's

security supervision. The inspectors also made periodic observations of personnel

entering the plant protected area through the plant access control point (PACP).

b. Observations

The inspectors noted that specific procedures were in place for controlling personnel

access to the protected area through the PACP. These procedures were detailed in the

site security plan and PAP-219, " Personnel and Material Access," Revision 3 (July 28,

1997).

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During the week of May 25,1998, several observations were made of single-guard

l . access control monitoring at the access lanes of the PACP. Single-guard monitoring is l

l permitted by procedure. However, these procedures call for more restrictive control with  ;

L one guard present than when multiple guards are monitoring access. Items of access 1

(explosive monitor, metal detector, and x-ray) are to be performed one step at a time l

during single guard monitoring. The inspectors noted varying levels of performance of l

these steps by single guards. Some officers made very apparent steps in controlling the l

l individual steps of the access lane. However, other guards displayed little difference from

l multiple guard monitoring. l

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On May 26,1998, the inspectors observed an individual approach the access badge 1

window. The individual gave a badge number and a fictitious name. The individual was j

. given the correct badge without stating the correct name because the guard recognized 1

i ' the individual. Plant Administrative Procedure PAP-219 required individuals to give their

l badge number and state their name prior to receiving their badaa The next day, other i

l observations were made by the inspectors of personnel ree N v badge without stating  ;

a badge number and/or name. None of the cases observed by ine inspectors resulted in i

l unauthorized access or issuance of wrong badges to an individual. This failure to follow

PAP-219 constitutes a violation of minor significance and is not subject to formal

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enforcement action. l

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The inspectors' observations were discussed with security supervision. Immediate steps

l were taken by the licensee to reinforce access control requirements. On June 4,1998,

l the inspectors observed another instance of an individual giving a fictitious name at the ,

l badge issue window. The guard issuing badges immediately counseled the individual on  ;

l the procedure and required a name to be given. I

c. Conclusions

i

l The inspectors were concemed that access control procedures were not uniformly

l followed by station and contract personnel. This procedure adherence concem is

[ concurrent with procedure adherence concems seen in other areas throughout this ,

inspection period.

( S8 Miscellaneous Security and Safeguards issues (92904)

S8.1 (Closed) Inspection Follow-up item 50-440/96003-03(DRP): Aberrant Behavior Not

- Reported to Security Department in a Timely Manner. This issue was reviewed by Rlli

security inspectors and determined to be a Non-Cited Violation. This is documented in

Inspection Report 50-440/96004. This item is closed.

P8 Miscellaneous Emergency Preparedness issues (92904)

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P8.1 '(Closed) Unresolved item 50-440/97021-01(DRP): Timeliness of Initial Unusual Event

Declaration on January 23,1998. The licensee declared an unusual event when

' 275 gallons of trichlorethylene leaked from the offgas brine system into the offgas

!

building. The inspectors initially questioned the timeliness of the declaration. This issue

was reviewed by Region lli emergency preparedness inspectors as docume'ited in

Inspection Report 50-440/98003. After a review of the timeline associated with the event,

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the inspectors concluded that the timeliness of the unusual event declaration was

appropriate. This item is closed.

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V. Manaaement Meetinas

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X1 Exit Meeting Summary

The inspectors presented the inspection results to members of licensee management at the i

conclusion of the inspection on June 4,1998. The licensee acknowledged the findings l

presented. The site Vice President disagreed with the inspectors' conclusions regarding

throttling of the gage isolation valve as discussed in Section M1.2. The inspectors asked the i

licensee whether any materials examined during the inspection should be considered proprietary.

No proprietary information was identified.

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PARTIAL LIST OF PERSONS CONTACTED

Licensee

L. Myers, Vice President, Nuclear

H. Bergendahl, Director, Nuclear Services Department

N. Bonner, Director, Nuclear Maintenance Department

]

H. Hegrat, Manager, Regulatory Affairs

T. Henderson, Supervisor, Compliance Unit

W. Kanda, General Manager, Nuclear Power Plant Department

F. Keamey, Superintendent, Plant Operations

T. Rausch, Manager, Plant Operations

R. Schrauder, Director, Nuclear Engineering Department

J. Sears, Radiation Protection Manager

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INSPECTION PROCEDURES USED

IP 37551: Onsite Engineering

j IP 61726: Surveillance Observation

IP 62707: Maintenance Observation

IP 71707: Plant Operations

IP 71750: . Plant Support

. Onsite Followup of Written Reports of Nonroutine Events at Power Reactor

IP 92700:

t Facilities

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IP 92901: Followup - Operations

IP 92902: Followup - Engineering

IP 92903: Followup - Maintenance

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ITEMS OPENED AND CLOSED

Opened

50-440/98010-01 VIO Incorrect Fuse Removed

l 50-440/98010-02 NCV Light Bulb Replaced with Wrong Type

i. 50-440/98010-03 VIO Missed Step in Surveillance Restoration Checklist

! 50-440/98010-04 VIO Expired Transient Combustible Permit

50-440/98010-05 NCV Inadequate Logic Testing of Radiation Monitors '

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i Closed

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L 50-440/95002-01 URI Locked Valves Not Properly Locked j

50-440/95004-01 VIO Slow Corrective Actions Related to On-Site Vehicle Movements

l Interfering With Overhead Power Lines

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50-440/95008-01 VIO Automatic Reactor Scram Due to Personnel Errors

l 50-440/95008-02 VIO Improper Verification of Equipment Prior to Work-

l 50-440/95009-01 VIO Three Examples of inadequate Corrective Actions

50-440/96002-03 URI Past Review of Loss of Offsite Power / Loss of Coolant Accident

Test Data Due to Clipping of Data Observed in 1996

50-440/96002-05 IFl Review of Spent Fuel Pool Licensing Basis Information

l 50-440/96003-03 IFl . Aberrant Behavior not Reported to Security

50-440/96003-07 IFl NUKON Piping insulation in the Drywell

L 50-440/96003-08 IFl Electrical Penetrations Conformance to USAR

l. 50-440/96003-12 IFl Potential USAR Discrepancy

50-440/96005-02 VIO Slow identification of Condition Adverse to Quality

50-440/96006-01 URI Past Operability of Div 3 DG With Degraded Air Start Subsystem

y 50-440/97009-04 VIO Failure to Follow Procedure During Safety-Related Valve Packing

! Maintenance

50-440/97021-01 URI Timeliness of Emergency Declaration

50-440/98001-00 LER Inadequate Testing and Missed TS Surveillance Requirement

, '50-440/98009-02 URI DG Jacket Water Level Concems

l 50-440/98010-02 NCV Light Bulb Replaced with Wrong Type

L 50-440/98010-08 NCV Inadequate Logic Testing of Radiation Monitors

50-440/98010-09 NCV Security Badge issuance Concems

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LIST OF ACRONYMS USED

CFR . Code of Federal Regulations  ;

CR Condition Report '

CRD Control Rod Drive

DG Diesel Generators J

DRP Division of Reactor Projects  !

EA Enforcement Action I

HVAC Heating, Ventilation, and Air Conditioning

IFl Inspection Followup item

IP Inspection Procedure

IR inspection Report

LCO Limiting Condition for Operation

LER Licensee Event Report

NCV Non-cited Violation

NRC. Nuclear Regulatory Commission

PACP Plant Access Control Point

PAP Plant Administrative Procedure

PDR Public Document Room

PIF Potential Issue Form

RG Regulatory Guide

RHR Residual Heat Removal

SO-ATC Supervising Operator at the Controls

sol System Operating Instruction

SR Surveillance Requirements

SVI Surveillance Instruction

TCP Transient Combustible Permit

TS Technical Specification

US Unit Supervisor

USAR Updated Safety Analysis Report

URI Unresolved item

VIO Violation

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