ML20217D169

From kanterella
Jump to navigation Jump to search
Insp Rept 50-382/91-18 on 910514-0617.No Violations Noted. Major Areas Inspected:Plant Status,Followup,Onsite Response to Events,Monthly Maint Observation,Bimonthly Surveillance Observation & Operational Safety Verification
ML20217D169
Person / Time
Site: Waterford Entergy icon.png
Issue date: 07/15/1991
From: Westerman T
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20217D153 List:
References
50-382-91-18, NUDOCS 9107220080
Download: ML20217D169 (15)


See also: IR 05000382/1991018

Text

_ _ _ . . . . - -

, - _ _- ----- -_ _____-.- _ -_ _--- _

.

-

,

\\

-

_

,

APPENDIX

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

NRC !aspectio) Report No:

50-382/91-18

Docket No:

50-382

License No:

NPF-38

Licensee:

Entergy Operations, Incorporated

P. O. Box B

Killona, Louisiana 70066

Facility Name: Waterford Steam Electric Station, Unit 3 (Waterford 3)

Inspection At: Taft, Louisiana

Inspection Corducted: May 14 through June 17, 1991

Inspectors:

W. F. Smith, Senior Resident Inspector

Project Section A, Division of Reactor Projects

S. D. Butler, Resident Inspector

Project Section A, Division of Reactor Projects

7-/P7 /

Approved:

_ _ _ _ _

Chief, Pr6. ject Section A

bate

T. F. West

Inspection Summary

'

Inspection Conducted May 14 through June 17, 1991 (Report 50-382/91-18)

Areas Inspected:

Routine, unannounced inspection of plant status, followup,

onsite response to events, monthly maintenance observation, bimonthly

surveillance observation, and operational safety verification.

Results:

No violations or deviations were identified; however, there were

three unresolved items discussed in this report that have the potential of

becoming violations. An unresolved item is a matter about which more

information is required to ascertain whether it is an acceptable item,

deviation, or violation. These unresolved items and other inspection

highlights are summarized below:

In the plant operations area, house u ping practices were excellent as the

plant transitioned from refueling outage conditions to operating conditions.

Operator performance during startup and physics testing was exemplary; the

operators demonstrated many strengths in the response to events that occurred

during this inspection period. When the reactor coolant system developed a

20 gallon per minute (gpm) unisolable leak on May 17, 1991, the operators

l

followed the appropriate emergency plan, off-normal procedure, and operating

procedures to accomplish a safe and expeditious plant cooldown and

'

9107220000 910715

DR

ADOCK 050

2

l

l~

- . _ _ _ _ _ - - , , _ - , ,

.-

-

.

- _ - _ _ _ _ _ _ .

_

'

.

.

2

depressurization.

To further expedite depressurization, the shift supervisor

first consulted with plant management and then issued an order to isolate

safety injet'Jon tanks, thus entering Technical Specification (TS) 3.0.3.

The

a ._

inspector viewed this ac+1on as prudent; however, it remains unresolved whether

a violation of NRC regulations occurred (paragraph 4.1).

In the radiological controls area, the licensee's handling of the potential

overexposure incident on May 13, 1991, appeared adequate.

Following an

appropriate investigation, the licensee's determination that the individual had

not been overexposed had a sound basis..

The issue remains unresolved, pending

i

followup by a regi nal radiation protection specialist (paragraph 3.2.1).

Radiological work practices and cecontamination efforts at the end of the

refueling outage were a strength.

Maintenance and surveillance conducted during this reporting period did not

reveal any weaknesses, except in the assurance of qua 'ty of replacement parts

I

during repair of the governor on the turbine driven

gency feedwater pump.

An unresolved item was identified regarding this is>we (paragraph 5.1).

During

surveillance testing of High Pressure Safety Injection (HPSI) Pump A, the

licensee took extensive measures to resolve the reduction in recirculation

flow, thus demonstrating lessons learned from previous problems on HPSI Pump B.

This was viewed as a strength.

9

-

4

_

._ _ _ _ _ _ _ _ _ _ _ _ _ _

_

_ _ _ _ _ _

.

-

-3-

DE '

1.

PERSONS {0NTAClcJ

1.1 Principal Licensee Epp.lpyees

D. F, Packei, General Manager, Plant Operations

  • T. R. Leonard, Technical Services Manager
  • R. 5. Starkey, Operations and Maintenance Manager
  • A. 5. Lockhart, Quality Assurance Manager
  • R. E. Allen, Security and General Support Manager
  • D. E. Baker, Director, Operations Support and Assessments

R. G. Azzarelin, Director, Engineering

W. T. Labc.ite, Radiation Protection Superintendent

  • G. M, Davis, Events Analysis Reporting & Response Manager
  • R.

F. Burski, Director, Nuclear Safety

  • T. J. Gaudet, Operational Licensing Supervisor

L. W. Laughlin, licensing Manater

J. G. Hoffpauir, Maintenance Superintendent

D. W. Vinci, Operations Superintendent

A. G. Larsen, Assistant Maintenance Superintendent, Electrical

D. T, Dormady, Assistant Maintenance Superintendent, Mechanical

D. C. Matheny, Assistant Maintenarr.e Superintendent, Instrumentation and

Controls

  • Present at exit interview,

in addition to the above personnel, the inspectors held discussions with

various operations, engineering, technical support, maintenance, and

administrative members of the licensee's staff.

2.

PLANT STATUS (71707)

During the reporting period, plant pressurization and heatup began following

the licensee's fourth refueling outage. The heatup was interrupted on May 17,

1991, when a 20 gpm reactor coolant system (RCS) leak from pressarizer spray

line check Valve RC-303 required the RCS to be cooled down and depressurized to

permit repairs.

Plant heatup was resumed on May 19 and a reactor startup was

performed on May 23 af ter completion of the necessary surveillance testing.

A

reactor trip occurred on May 26, from less than 0.1 percent reactor power,

during troubleshooting of a ground on the plant annunciator system. A second

reactor trip occurred on May 28, from 34 percent power, when nonsafety-related

Bus 381 failed to transfer to offsite power following a manual turbine trip.

The reactor was restarteo on May 29 and reached 100 percent power en June 2,

where it has remained through the end of the reporting Deriod.

_ - _ - _ _ _ _ _ _ _ _ _ __ _ ___- - - _ _

.-

_.4

_ _

-_ _

___ __

_

_ _ . _ _

_ _ _

+,

..

4

.

-

3.

FOLLOWUP

3.1 Followup _ of Previous Inspection Findings (92701)

3.1.1

(Closed) Inspector Followup _ Item (IFI) 382/9005-02

_

.This item was initiated to follow up on the licensee's actions following the

March 29, 1990, reactor trip caused by a power fault at a nearby substation.

Of particular interest was the licensee's consideration of providing a static,

uninterruptible power supply (SUPS) for the reetcar cutback system and the

steam bypass' control system.

The licensee imp Jmented Design Change

Package (DCP) 3320 during the fourth refueling out.ge, which connected those

systems to a SUPS. The systems were placed ta peration after the outage.

In

addition _to the above corrective actions, t.te licenseu d < eloped a 33-item

action tracking list with. Central Engineei ng, fo- the purpose of improving

i

reliability of the offsite power supplies. A few .najor examples of items

included:

control over maintenance by Ccatral Engineeriog, increased awareness

of the- equipment-out-of-service log, disp ,tcher 'rc iain;, a walkdown of the

nearby substation to determine condition, +ae i stab'11ty study of Waterford 3

pcwer busses.

The licensee actions in re>p;1st to the inspector's concerns

have:been satisfactory.

This IFI is clo'ed.

.

3.2 Other Followups (92701)

'

3.2,1 Apparent Overexposure Oue to Misplaced 1 crmoluminescent Dosimeter

On May 13, 1991,-the inspectors were informed that a contractor employee, who

,_

l

had permanently-left the site, may have received radiation exposure of

L

- approximately 3 rem, which was in excess of the limits allowed by 10 CFR 20.

-The initial determination was made by the licensee based on the dose recorded

i

by the employee's thermoluminescent dosimeter (TLD).

The_ licensee initiated

Potentially Reportable Ev'nt-(PRE)91-058 and began an investigation. The TLD

exposure was not consistent with the employee's self reading pocket

-

dosimeter'(SRD) readings, or with the 0.75 rem exposure received by fellow

,'

workers performing similar tasks.

It was subsequently determined that the TLD

reading did not appear to be as realistic as the employee's SRD readings, This

determination was based on interviews with the affected contract employee and

other employees working the same job, a review of work performed by the

employee, and exposure received.by fellow workers. ~lt was also reported that a

'

TLD was found-in the reactor containment building (RCB)'during the time that

the contractor employee was present in the RCB.

The cont ractor employee denied

losing his TLD, however, the licensee health physics personnel recalled that the

l-

individual had earlier lost and then recovered his TLD. A lost TLD report was

not_ initiated.

Since the licensee's administrative requirements for the lost

TLD were not followed, Quality Notice (QN) QA-91-116 was written.

The QN

documented the procedural violation and entered the licensee's corrective

action program.

Based on the licensee investigation, they assigned the worker

en exposure based on the SRD readings.

An NRC regional radiation protection

specialist was kept ir. formed by the licensee of their actions, and the

licensee's-approach to this issue appeared proper, pending further review

L

,

,

m

.,w

,

,e:

- . - - -

--

, - - ,

w

,,

,

--,

~

.

l

.

-5-

during a future inspection to be performed by a regional radiation protection

specialist.

This review shall be tracked by Unresolved Item 382/9118-01.

3.2.2

Low Recirculation Flow During Testing of HPSI Pump A

On May 20, 1991, during an operability verification surveillance test of HPSI

Pump A, the licensee noted that recirculation flow was 28.9 gpm.

This value

was below the " Action Required Limit" of 30.15 gpm per ASME Code,Section XI.

All other parameters recorded during the surveillance test were within

acceptable limits.

The pump was declared inoperable, and the licensee

assembled a cask force including maintenance and engineering personnel to

determine the cause of the low flow and establish corrective actions.

The task

force reviewed previous test data and noted that HPSI Pump A was full-flow

tested during the refueling outage on April 3,1991, and flow was consistent

with previous readings and was acceptable.

The flow measuring instrument was

vented and a calibration check was performed on the instrument.

The flow

instrument orifice had been previously disassembled and verified to be in good

condition and reinstalled properly on April 30, 1991.

Radiography was

performed on potentially blocked components (including the flow limiting

multi-stage orifice), but no obstructions were found.

Vibration data was

collected and reviewed, and no indication of pump damage was noted.

Historical

inservice test data taken since January 1935 was reviewed, and the licensee

noted some variations in recirculation flow that were not attributable to

changing pump performance.

The licenr^e concluded that the pump was operable on the basis of the above

reviews *" tests and attributed the variation in recirculation flow to the

multi-stage flow restricting orifice.

This device contained flow orifice

plates which had off-center orifices in two of the plates.

These plates were

free to rotate within the assembly, thus changing the hydrodynamic

characteristics of the device. With such a design, and based on historical

data, minor variations in recirculation flow could have occurred, which were

not a reflection of pump performance.

New baseline data was established and the pump was declared operable.

In

accordance with the ASME Code, the frequency of testing was doubled,

i.e., HPSI

3

Pump A would be tested every 45 days in lieu of every 90 days.

For the long

term, the licensee indicated that they were developing an alternate test method

for the HPSI pumps, which involved setting up a test loop which would bypass

the flow restricting orifice and provide a reference flow that was greater than

recirculation flow.

In this manner, reference flow would always be achievable

so that pump performance could be consistently evaluated in accordance with the

ASME Code.

This action would require procedure changes.

The inspectors

considered the above actions to be of sufficient depth to adequately address

the HPSI Pump A recirculation flow problem.

The licensee demonstrated

strengths in reflect bg lessons learned from recirculation flow problems

encountered on HPSI Pun.9 B in 1989.

See NRC Inspection Report

No. 50-382/89-09.

.

_ _ _ . _ _ . _ _ . _ _ _ . _ _ _ _ _ _ _ _ _ _ _ . _ _ _

_ _ _ _ _ _ _ _

_

_

_ -

.

- .- _.._ _.__

____

_ ._ _ _ _.__ _ _.

.

4

6-

3.2.3 Stop Screws Missing from Fire Isolation Switch

' On May 18,1931, with the plant in Cold Shutdown (Mode 5), postmodification

testing was being performed on Main Steam Isolation Valve (MSIV) A.

Part of

the testing included closing the valve using Fire Isolation Switch FR-4, in the

auxiliary relay room, to ensure that the MSIV control wiring changes made in

accordance with DC-3217 did not affect the function of the switch. The switch

was intended to be used in the event of a control room evacuation due to a

fire, and would provide control circuit isolation from the contiol room for the

MSIV and several other components and ensure that power is supplied to the

components to maintain them in the desired status. When the switch was

operated, it traveled past the isolate position, allowing two of the adjacent

make-before-break contacts to connect and short the positive side of one

circuit to the negative side of another circuit.

The short circuit caused the

power supply breaker for the switch to trip, but the switch was severely

damaged due to smoke and fire.

The fire was quickly extinguished.

During

replacement of the switch, it was determined that the stop screws that should

have been installed as part of the switch installation, were missing and

allowed the over-rotation of the switch,

The switch was a multi-deck rotary

switch manufactured by Electro-Switch.

It was determined that the stop screws

were supplied with the switch, but the licensee had failec to recognize that

the screws should have been installed. Several other isolatten , switches in

adjacent panels were inspected and at 19ast one other switch wat found to have

the stop screws missing. The licensee wrote a condition identificatior (CI)

report to inspect similar switches and to perform a root cause investigation.

The failed switch was replaced and successfelly tested.

The licensee was

considering notifying the industry via the nuclear repcrt: 1g network, and the

inspectors supplied pertinent data to NRC headquerters for consideration of

generic correspondence.

The licensee's actions wsre appropriate.

3.2.4

Inadvertent lift of Safety Injection Tank Relief Valves

On May 21, 1991, with the unit in Mode 3 at normal operating temperature and

pressure, the licensee entered the action statement for TS 3.5.1 when the

nitrogen relief valve on Safety Injection Tank (SIT) 1A lif ted and

depressurized the tank to approximately 300 psig. An attempt was made to

repressurize the tank, but the valve lifted again at approximately 500 psig.

SIT 1A was subsequently declared inoperable and RCS depressurization was

commenced to less than 1750 psla; a point where Mode 3 operation is allowed

with only three operable SITS maintaining pressure between 235 and 625 psig.

During RCS depressurization, the nitrogen relief lifted on SIT 18, rendering it

inoperable and placing the plant in TS 3.0.3.

The NRC Operations Center was

properly notified in accordance with 10 CFR 50.72. When RCS pressure was

reduced to less than 1750 psia, both TS 3.0.3 and TS 3.5.1 were exited.

SITS IA and IB were singularly isolated and vented and their relief valves

removed for_ inspection and setpoint checks.

The relief for SIT 1A actuated at

about 400 psig on the test bench, and the adjustment locknut was found loose.

It was reset to 700 psig (normal setpoint).

The SIT IB relief valve lifted at

about 710 psig and no adjustment was necessary.

Its locknut was found tight.

__

. .

_

_ _

.__ _ _

_ _ _ _ _ _ _ _

.

l

.

7-

When the relief valves were reinstalled, the tanks were repressurized to normal

operating pressure and monitored.

No additional problems were identified.

The

relief valves-are 3/4 x 1-inch Crosby spring-loaded, nozzle-type relief valves.

At the time the valves lifted, scaffold removal was in progress at both of the

SITS; however, the licensee was not able to initially demonstrate, with

significant confidence, the connection between the scaffolding activity and the

relief valve actuations.

The licensee reviewed logs and alarm princarts,

interviewed operators on duty at the time of tne event, and concluded that an

actual-over pressure condition had not occurred in the SITS. A spare relief

valve of the same type was tested under similar conditions as the SIT relief

valves, and it was demonstrated that mechanical agitation would cause the valve

to lift. Although the scaffold carpenters did not recall hitting the valves or

the tail pipes during scaf fold removal, the licensee concluded that it was

possible that the ,alves could have been inadvertently agitated during the

evolution.

No further problems were experienced with the valves.

The

licensee's actions to solve this problem were satisfactory.

3.2.5

Reactor Trip Breakers Fail to Close_Due to Operating Spring Anomaly

On May 20, 1991, during routine surveillance testing of the reactor trip

circuit breakers (TCB), TCB-4 would not reclose af ter it was tripped open.

Troubleshooting by the electrical maintenance department revealed that one of

two operating springs had become disconnected when the breaker tripped and thus

prevented the breaker from closing properly.

After receiving proper

authorization, the spring was reconnected and the breaker was satisfactorily

tested.

The inspector determined that this was the f ailure mode of General Electric

AK-Series circuit breakers described in NRC Information Notice (IN) 91-15 and

in a 10 CFR 21 report submitted by Maine Yankee on December 28, 1990.

The

inspector discussed the matter with electrical maintenance and system

engineering personnel and learned that they had just completed an inspection of

all of their AK-2-25 TCBs during the recent refueling outage. Based on the

reported TCB problems, they found the springs incorrectly oriented on four of

the eight breakers.

A previous work authorization had been implemented to

correctly install the springs on the four breakers, including TCB-4.

Further

review of the spring installation description in the 10 CFR 21 report and

IN 91-15 revealed that, without diagrams being included, the descriptions were

confusing and appeared to conflict.

The licensee inspected their breakers and

oriented the springs based on the 10 CFR 21. report and verbal discussions with

a vendor representative and concluded that they were installed correctly.

They

intended to contact the vendor with a written request for additional

information and possible design improvements, since it appeared that the

springs could become disconnected even when installed correctly.

In addition,

they were considering procedural changes which would require electrical

maintenance personnel to be present when the breakers were closed to verify

that the springs were properly in place. The apparent conflict between the

10 CFR 21 report and IN 91-15 was reported to cognizant NRC personnel.

The

inspectors will continue to follow up ca this issue until it is resolved.

The

TCBs were capable of performing their intended safety function regardless of

which way the closure springs were oriented.

-

- - _ - _ _ _ _ _ _ _ _ _ _ .

..

_ _ .

_____ _______________ ____

_

_

.

.

_ _ _ _ _ _ _

.

-8-

3.3

In-Office Review Of Licens2e Event Reports (LERsl__{90712J

The following.LERS were reviewed.

The inspectors verified that reporting

requirements had been met, causes had been identified, corrective actions

.ppeared appropriate, generic applicability had been considered, and that the

uER forms were complete. The inspectors confirmed that unreviewed safety

questions and violations of TS, license conditions, or other regulatory

requirements had been adequately described.

The Region IV staff determined

that an onsite inspection followup of the event was not appropriate.

The NRC

tracking status is indicated below.

3.3.1'(Closedl_LER 382/90-003, " Reactor Trip Due_to Grid Disturbance"

_(This LER was closed on the basis of the foflowup inspection of

IFI 382/9005-02 above)

3.3.2

[C_losed) LER 382/91-004, " Failure to Complete Technical Specification

Surveillance due to Inadequate Attention to Detail"~

4.

ONSITE RESPONSE TO EVENTS (93702}

4.1 Unusual Event Due to High RCS Leakage

On May 17, 1991, Waterford 3 declared an Unusual Event (UE) in accordance with

their Emergency Plan, due to an identified RCS leak rate of about 20 gpm. which

was in excess of the TS 3.4.5.2 limit of 10 gpm.

The plant was in Hot Shutdown

(Mode 4), approaching startup from the fourth refueling outage.

RCS temperature

was at 291*F and pressure at about 1600 psia with a steam bubble in the

pressurizer.

During pressurization, minor leakage had been reported coming

from the 4-inch pressurizer spray line check valve (RC-303). Because the

bonnet bolts and the seal had been replaced during the outage, the valve was

being monitored for leakage, with maintenance personnel checking torque on the

bonnet bolts every 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />. Typically, on this type of valve, leakage has

decreased or stopped with increasing pressure, because pressure tends to seat

the seal tighter.

After workers in the RCB reported that a popping sound

occurred, and that it was steam emanating from the pressurizer cubicle,

excessive RCS leakage was confirmed. The RCB was evacuated and operators

commenced depressurization of the RCS in accordance with their operating

procedures.

The differential pressure of the RCB atmosphere increased to about

10 inches water gauge (IWG) due to the leaking RCS flashing to steam, and when

nitrogen venting of the SITS was ccmmenced to reduce SIT pressure, RCB differential

pressure increased to about 20 IWG, with the TS limit being 27 IWG.

In order

to avoid having to purge the RCB, and to expedite depressurization, the shift

supervisor first consulted with plant management and then isolated the SITS

from the RCS.

This placed the plant in TS 3.0.3, because three SITS were

required to be operable by TS 3.5.1, and the action statements did not provide

for all SITS to be isolated.

Since the plant was already shut down and being

cooled down, the required actions of TS 3.0.3 were being met. When RCS

,

pressure was reduced to 392 psia, the pressure at which SITS were no longer

required to be operable, TS 3.0.3 was exited.

Cooldown was accomplished by

steaming to the main condenser until Shutdown Cooling Loop 2 was placed in

service. When the plant reached cold shutdown (Mode 5), the UE was terminated.

_.__ __

.

.

. - - -

.

.

-

-

-

-- .

.

..

.

. - - -

t,

.

+

.g.

The plant was depressurized and drained to 50 percent pressurizer level to

allow disassembly and repair of the valve.

RC-303 was a 4-inch Anchor Darling

i

swing check valve, and had a silver seal ring which was pulled in place _by the

bonnet bolts ~ The licensee disassembled the bonnet and found no damage, but

did find the bonnet seal cocked by about 54 mils, with two of the four bolts

loose,

This type of bonnet was typically installed by applying incremental

torque on the bolts.

No measurements were taken initially to verify alignment.

Subsequently, the licensee, in consultation with the vendor, developed a method

to measure al Snment.

This was applied to the reassembly of RC-303 on May 18,

when a new seal was installed.

Plant heatup and pressu-ization was commenced

on May 19, with no observed leakage from the new seal _ installation.

The NRC and local agencies were notified of the UE by the licensee in

accordance with their Emergency Plan, and pursuant to 10 CFR 50.72. At the

time of the notification, the licensee also informed the NRC headquarters duty

officer that TS 3.0.3 had been entered as a consequence of isolating the SITS.

The inspector was in the control room at the time of this event and observed

the decision process to isolate the SITS. During the event, it was suspected

that the RC-303 bonnet was leaking.

Not knowing the exact location of the-

i

leak, the shift supervisor stated that his decision to isolate the SITS was

based upon the need to expedite RCS depressurization and minimize the

possibility of the condition degrading to a more serious nature.

He was also

concerned that RCB pressure could reach a point that would procedunily require

'

purging the RCB, which would result in a release of activity to the atmosphere.

The shift supervisor consulted with licensee management present in the control

room, and was aware that if an automatic safety injection actuation signal was

received, the SITS would be capable of injecting into the RCS, because the

isolation. valves would open automatically. On May 18, the licensee informed

the NRC that the decision to enter TS 3.0.3 was made pursuant to

10 CFR 50.54(x), which, in part, provides allowance to depart from TS in an

emergency to-protect public health and safety.

This decision was questioned by

the NRC staff, because the circumstances did not appear to meet the intent of

10 CFR 50.54(x).

The licensee subsequently concluded that 50.54(x) was not

utilized during this event.

The licensee informed the hRC of that conclusion

by letter dated June 17,-1991, which transmitted LER 382/91-08. The Basis of

TS 3.0.3 delineates the measures to be taken for circumstances not directly

provided for in the ACTION statements, and whose occurrence would violate the

intent of a specification. This was the case with isolating the SITS when_ they

were required to be operable pursuant to TS 3.5.1; however, it is unresolved as

i.

to whether or not the licensee should have invoked 10 CFR 50.54(x), and whether

l

it was a TS violation when the licensee voluntarily entered, and complied with

L

TS 3.0.3 to mitigate the potential consequences of an off-normal or minor

i

emergency condition that did_not appear to be an immediate threat to public

safety. The Region IV staff has requested assistance from NRR on this issue

'

-and will be tracked as Unresolved Item 382/9118-02.

4.2 Reactor Trip During Startup Testing

On May 26, 1991, with the reactor less than 0.1 percent power, a reactor trip

occurred resulting from an electrical spike during troubleshooting of a ground

L

.

.

. .-

.

_ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _

'

.

'

-10-

on the control room annunciator system. Operators were maintaining the plant

critical at low power and waiting for an emergent design change to be completed

on the process analog cabinets, before increasing reactor power.

Electrical

maintenance was requested to troubleshoot a ground on the annunciator system

while the other work was in progress.

The trip was initiated by high log power

on Channels C and 0 of the plant protection system, and it was concluded that

an electrical spike during the ground isolation procedure caused excore nuclear

instrument Channels C and 0 to increase above the trip setpoint of

.

0.257 percent power.

The plant was stabilized at hot standby using energency

.d.

and normal operating procedures. The NRC Operations Center was notified as

required by 10 CFR 50.72.

Corrective action was taken prior to restarting the

unit, which included hanging a caution tag on the annunciator cabinet and

warning personnel not to open the cabinets with the reactor critical at i.a

power without shift supervisor permission.

A change was to be made to the

electrical maintenance procedure to caution against isolating grounds with the

reactor critical at low power.

The emergant design change was completed and

the annunciator ground cleared.

The reactor was then restarted and startup

testing was resumed.

The actions taken during this event were appropriate, and

,

the operator response to the trip was excellent.

4.3 Reactor Trip Following Turbine Trip

On May 28, 1991, with the reactor at about 34 percent power, a reactor trip

resulted from a turbine trip when the 6.9 Kv Nonsafety Bus 381 failed to

transfer from the unit auxiliary transformer to the unit startup transformer.

Loss of power to the bus caused the IB and 2B reactor coolant pumps (RCPs) to

trip and resulted in a core protection calculator (CPC) auxiliary trip of the

reactor.

Thc unit was in startup testing after the recent refueling outage, and was

holding power for excore calibration and troubleshooting of the digital

i

electro-hydraulic (DEH) control system.

Problems had been experienced earlier

in the day with load swings when attempting to transfer from single valve to

3

sequential valve control on the DEH,

At the time of the trip, the DEH was in

manual valve control while maintenance technicians were running diagnostic

routines on the DEH computer and software,

Shortly before the trip, Governor

Valve (GV) No. I began to open causing turbine load to increase.

The operators

decided to manually trip the turbine, and the reactor trip followed when the

bus transfer failure caused the loss of two of the four operating RCPs.

Following the trip, systems responded normally except that the lack of decay

heat and only two RCPs running resulted in a cooldown to approximately 510 F.

When steam pressure dropped to 764 psia, an automatic main steam isolation

signal (MSIS) occurred.

Prior to the MSIS, attempts were made to throttle feed

flow from the operating main feed pump, which was thought to be a major

contributor to the cooldown.

Once the 381 bus was manually reenergized, the

IB RCp was restarted and the plant was staoilized at hot standby.

The MSIVs

were left shut to allow repair of a steam leak that was identified earlier on

'

the HP turbine.

The cause of GV No. 1 oscillation was found to be an error in

the OEH diagnostic procedure, which failed to specify j'sconnecting the valve's

servo driver card from its digital / analog interface card prior to running the

diagnostic test.

This allowed a signal to be imposed over the manuci signal to

_

___ _ _ _ _ _- _ - _ _ _ _ _ _ - _ _ _ _

-

..,

-11-

the GV, causing it to open.

The cause of the failed bus transfer was found to

be a faulty contact in a follower relay (25x relay) for the synchronous check

relay which prevented the shut signal from reaching the feeder breaker from the

unit startup transformer to the 381 bus.

The 25x relay was replaced.

The unit

was restarted at 1:23 a.m. on May 29, after repair of the HP turbine steam leak

,

i

and replacement of the faulty relay.

Extensive troubleshooting of the DEH with

the unit shut down could not identify the original problem with DEH sequential

valve control, so a plan was developed by the licensee to continue

l

troubleshooting with the turbine online. With the aid of the vendor a ground

was subsequently found, on one position of the DEH test select switch, and

corrected. The DEH was transferred to sequential valve mode without any

problems and startup testing was continued.

Based on the licensee's root cause analysis, the 25x relay failed due to a

'

plastic part disintegrating.

The pieces fell into the relay contactor and

prevented-the contacts from functioning.

The failure mechanism appeared to be

o

!

aging, possibly accelerat'ed by heat.

The 25x relay was manufactured by

!

Struthers-Dunn, Model 602-4-351.

There were also identical relays installed in

!

the plant which were labeled Model 602-4-1007.

The licensee had 348

Struthers-Dunn relays of different types installed-at the plant (nonsafety) and

25 of them were. identical to the one described above that failed. The licensee

,

l

had an exact replacement spare in stock.

Since Struthers-Dunn no longer

L

supplied these relays, the licensee was seeking an alternative source.

The

!

l

licensee implemented a work authorization to inspect similar relays in the

.

other three busses (3A1, 3A2, and 382) for possible defects, so that fast bus

l

transfer won't be impacted again.

They were developing long-term actions, such

l.

as a review of applications of this relay to other circuits in the balance of

I-

plant that ceuld cause unwanted reactor transients upon failure.

Conclusions:

No violations or deviations were identified.

The operator's

,

!

response to events was always timely and appropriate; follewing their

emergency, off-normal, and operating procedures.

One unresolved item was

identified concerning -the voluntary entry into TS 3.0.3- to expedite

d6 pressurization of.the RCS to stop an unisolable leak.

5.

MONTHLY MAINTENANCE OBSERVATION (62703)

l

l:

The station maintenance activities affecting safety-related systems and

L

-components listed below were observed and documentation reviewed to ascertain

l

that the activities were conducted in accordance with approved work

l

authorizations (WAs), procedures, TS and appropriate industry-codes or

standards.

'

l

l

5.1 WA 01058865, 01065885

l

l

On May 21, 1991, the inspector observed work in progress on turbine driven

l_

emergency feedwater (EFW) Pump A/B.

The governor had been replaced and the

,

~

control oil system cleaned to ensure no problems would develop with the turbine

i

control system due to possible contaminants in the oil.

The mechanical

l

overspeed device trip setpoint was being calibrated in accordance with

(

Procedure MM-03-016, Revision 0, " Emergency Feedwater Pump Turbine Mechanical

l

l

l

-

_ ___ - _ _ _ _

'

.

1

'

l

-12-

l

l

t

Overspeed Trip Test and Calibration."

Simultaneously, the turbine speed

control circuitry was being calibrated in accordance with M1-5-425, Revision 2,

,

" Emergency Feedwater Pump Turbine Governing Control System Calibration." The

inspector verified that the work had been properly authorized and was being

performed by qualified individuals in accordance with approved work

instructions.

Equipment operation was being performed by a qualified operator

as directed by the control room.

The inspector learned that an unsuccessful attempt had been made to test run

the pump turbine on the previous day.

Troubleshooting by mechanical

maintenance personnel revealed the oil pump for the replacement governor that

had been installed was not configured to rotate in the direction required by

tnis turbine (i.e., clockwise).

The result was that no oil pressure was being

supplied to the governor valve servo.

The matter was discussed with

maintenance personnel and it was determined that the turbine manufacturer

supplied two different Woodward

vernors for their turbines with either

clockwise (CW) or counterclockwise (CCW) rotating oil pumps. The only

difference in the part numbers was the letter "A"

prefix on the CCW units.

Each governor also has a rotation direction arrow placed on the outside of the

case.

Maintenance personnel originally began governor installation with the correct

governor, as specified in the work instruction. When the old governor was

removed, maintenance personnel observed that the rotation directinn arrow did

not match the arrow for the new governor. Guidance was requested from

maintenance engineering and, after it was found that the second governor in the

warehouse had a rotation direction arrow which matched the installed unit, the

decision was made incorrectly to install the second governor.

This was later

determined to be the wrong unit when the turbine's governor valve would not

function.

It appeared that the installed governor was originally an incorrect

CCW unit that had been field modified during a previous governor repair to

operate as a CW unit, and had the

"A" prefix scratched off of the part number

without reversing the direction of rotation arrow.

There was a second,

incorrect CCW unit in the warehouse that was never identified and properly

dispositioned.

Since the installed ;overnor actually was turning CW but still

had a CCW rotation arrow, the dec'-ion was made, incorrectly, to install the

CCW unit. When the error was ditcovered, after the turbine governor valve

failed to operate properly, the correct CW unit was installed and the turbine

was successfully tested.

Maintenance engineering indicated that the two spare

governor units will be sent to the vender to be refurbished and correctly

ported for CW rotation and then returned to the warehouse for future use.

This

matter will remain unresolved until it can be determined if the field

modification of the previously installed unit was properly authorized and

documented correctly and why the other incorrect spare governor unit in the

warehouse was not properly dispositioned. Additionally, the licensee indicated

that they will address why their quality assurance program did not prevent

installing the incorrect governor during this maintenance activity (Unresolved

Item 382/9118-03).

Conclusions: Although no violations or deviations were identified, the errors

identified during the maintenance on the A/B EFW pump demonstrates a potential

_ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ - -

-

_ _ _ _ _ _ _ _

.

.

.

.

-13-

weakness in a quality aspect of maintenance.

It was unclear why incorrect

parts had been procured for the EFW pump turbine and actually installed on two

different occasions. After the recent occurrence, the error was revealed by

the licensee's maintenance retest program before the pump was returned to

service,

Therefore the safety significance of the error was minimal.

6.

BIMONTHLY SURVEILLANCE OBSERVAT10N__(61726)

The inspectors observed the surveillance testing of safety-related systems and

components listed below to verify that the activities were being performed in

accordance with the TS.

The applicable procedures were reviewed for adequacy,

test instrumentation was verified to be in calibration, and test data was

reviewed for accuracy and completeness.

The inspectors ascertained that any

deficiencies identified were properly reviewed and resolved.

6.1 Procedure OP-903-008, Revision 3, " Reactor Coolant System Isolation

Leakage Test"

On May 22, 1991, the inspector observed the performance of Section 7.4.8 of

OP-903-008 for Valve SI-142B.

The test was performed to satisfy TS

surveillance requirement 4.4.5.2.3.

The test was properly authorized and

performed by qualified individuals in accordance with an approved procedure.

Good coordination was maintained during the test between the control room and

the containment where the leakage was being collected and measured.

The test

acceptance criteria and TS requirements were met for the valve.

No problems

were identified.

6.2 Procedure NE-02-020, Revision 2, " Control Element Assembly (CEA)

Insertion Time Measurement"

On May 22 and 23, 1991, the inspector observed the performance of NE-02-020 to

meet the TS surveillance requirements 4.1.a.3 for CEA reed switch position

transmitter calibration and functional testing and 4.1.3.4 for CEA drop timing.

The tests were properly authorized and performed by qualified individuals in

accordance with an approved procedure.

The inspector verified that the initial

conditions and prerequisites specified in the test procedure were met.

The

test acceptance criteria and TS requirements were both met. No problems were

identified.

6.3 Procedura OP-903-101, Revision 4, "Startup Channel Functional Test"

On May 28, 1991, the inspector observed the performance of OP-903-101, for

nuclear instrument Startup Channel 2, in preparation for a reactor startup

planned for later in the day.

The test was properly authorized and performed

by a qualified individual in accordance with an approved procedure.

The test

acceptance criteria were met and no problems were identified.

Conclusions:

No violations or deviations were identified. The licensee's-

surveillance program continued to perform well.

The licensee expended

considerable ef fort and utilized comprehensive checklists and administrative

controls following the recent refueling, to ensure that the required

i

. -

-

._

-

- _ .

.

-

_ - -

.-

.

_14

surveillances were performed satisfactorily prior to entering operating modes

where the equipment was required to be operable.

7.

OPERATIORAL SAFETY VERIFICATION (71707)

The objectives of this' inspection were to ensure that this facility was being

operated safely and in conformance with regulatory requirements and to ensure

that the licensee's management controls were effectively discharging the

licensee's responsibilities for continued safe operation.

The inspectors conducted control room observations, reviewed logs and reviewed

the equipment out of service log, and noted that plant conditions and equipment

status were being kept up to date.

TS limiting conditions for operation and-

action statements were being followed in an exemplary manner as the plant was

taken through startup and physics testing from the refueling outage.

The

inspectors observed reactor startups following the refueling, noting that

procedures were properly utilized and were current.

The inspectors conducted plant inspection tours on a daily basis, and found

that housekeeping was improving rapidly with the conclusion of the outage.

After the plant had been at full power for just a few days cleanup was

virtuall" completed. The. inspectors did note, however, that the boric acid

makeup' tank rooms did not -improve as a result of the outage.

,;.ere were still

large quantities of unused heat trace and sensing wires draped on the piping

and boric acid deposits were observed in numerous places.

This was brought to

,

the attention of licensee management, who was already aware of the condition

i

from previous tours.

The inspectors attended plan-of-the-day meetings and noted continued excellent

coordination and communications between organizations.

,

l

On May 16, 1991, the inspectors conducted an-inspection tour of the RCB to

'

assess conditions prior to heatup of the plant. _The emergency core cooling

sump was inspected to ensure that no debris was present which could block the

sump screens during an accident, and that the-sump baskets contained sufficient

pH additive as required by .S 4.5.2.d.3

The RCB was generally in good

-

condition but a list of minor discrepancies was provided to the licensee to be

corrected prior to plant startup. The items were corrected as appropriate.

On June 4,'1991, the inspectors performed a test of the Emergency Notification

System in-the control Hoom to confirm operability.

The results were

satisfactory.

On June 4, 8, and 13, the licensee experienced reactor power transients

resulting from a reduction of feedwater heating caused by the inadvertent

,-

isolation of extraction steam (ES) to the high pressure feedwater (FW) heaters.

The ES valves were designed to modulate extraction steam flow and shut

automatically when a high water level is present in the Rd heaters.

The June 4

and 13 events were associated with Ct to the No. 1 FW heaters and the June 8

event resulted when ES was isolate. so the No. 2 FW heaters.

The loss of FW

heating caused-reactor power to increase from 100 percent to as high as

.-

-

_

.

. _ . _ . . _ _ _ . .

___

_ _ _ _

._

_

.

.

,

.

_ _ . . _

__

.

,

-15-

104 percent for about 5 minutes.

The operators took prompt act

power to within the licensed limit in each case by reducing tur

reestablishing ES to the FW heaters.

Although such transients

under t'le circumstances of this incident, NRC does not consider

violation of the licensed steady state power limit of 100 perce

power.

The first two transients were attributed to work that was being

the vicinity of the FW heaters causing physical jarring of the

which actuated the ES isolation.

It was also determined that n

switch mechanisms that were installed in the Magnetrol level co

were very susceptible to actuation by normal system vibration a

physical contact.

The licensee had replaced the older dry cont

mechanisms with the mercury-type mechanisms during the recent r

because of premature aging and heat damage which made the dry c

unreliable.

Initial corrective action for the transients consisted of train

personnel and erecting barriers around the FW heater level cent

physical contact with +he switches.

Since the third transient

associated with actual physical contact, it was concluded that

switch mechanisms were unacceptable, and the vendor was contact

assistance.

The motor operator for the ES valve to the No. 1 F

left deenergized after the third transient.

This was done as a

until the problem could be resolved in order to prevent another

transient.

With the assistance of the vendor, the licensee obtained a diff

mercury-type switch mechanisms that were specifically designed

high vibration applications, and intended to install the new sw

when a spare parts equivalency evaluation report (SPEER) could

work instructions prepared.

The inspectors will continue to moni

activity.

Conclusions: No violations or deviations were identified.

The 1

continued to operate the plant in a safe and professional manner.

j

response to the repeated feedwater transients was considered go~-

taken to prevent further transients were appropriate. Housekee

,

at this plant continue to be excellent.

8.

EXIT INTERVIEW

The inspection scope and findings were summarized on June 20, I

persons indicated in paragraph 1 above.

The licensee acknowled

inspectors' findings. The licensee did not identify as proprie

material provided to, or reviewed by, the inspectors during thi

l

.

.

.-

-_

-. .-

.

.

. - - - . .