Letter Sequence Response to RAI |
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MONTHYEARML20141J8811997-08-19019 August 1997 Forwards Proposed Amend to Permit Natural Circulation Test & Issues for Telcon Discussion Project stage: Other ML20216G0951997-09-0202 September 1997 Informs That Addl Info Needed to Complete Review of Licensee Proposed Amend to License of Plant,Unit 1 Revising Section 3/4.1.2 of TS to Permit,On one-time Basis,Performance of Natural Circulation Test Project stage: Approval ML20216H8701997-09-10010 September 1997 Forwards Response to RAI on Proposed Amend Re Natural Circulation Testing Project stage: Response to RAI ML20212G3871997-10-29029 October 1997 Forwards Facsimile from Duke Energy Corp,Signifying Implementation of Amend 162 Project stage: Other 1997-08-19
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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217F8231999-10-13013 October 1999 Informs That on 990930,NRC Completed mid-cycle PPR of Catawba Nuclear Station.Based on Review,Nrc Did Not Identify Any New Areas That Warranted More than Core Insp Program Over Next Five Months.Historical Listing of Issues,Encl ML20217H0041999-10-13013 October 1999 Forwards MOR for Sept 1999 & Revised MOR for Aug 1999 for Catawba Nuclear Station,Units 1 & 2 ML20217F1301999-10-0707 October 1999 Forwards Rev 1 to Request for Relief 99-03 from Requirements of ASME B&PV Code,In Order to Seek Relief from Performing Individual Valve Testing for Certain Valves in DG Starting (Vg) Sys ML20212J3011999-10-0101 October 1999 Forwards Exemption from Certain Requirements of 10CFR54.17(c) Re Schedule for Submitting Application for Operating License Renewal.Se Also Encl ML20217K2651999-10-0101 October 1999 Forwards Retake Exams Repts 50-413/99-302 & 50-414/99-302 on 990921-23.Two of Three ROs & One SRO Who Received Administrative Section of Exam Passed Retake Exam, Representing 75 Percent Pass Rate 05000414/LER-1999-004, Forwards LER 99-004-01,providing Correction to Info Previously Provided in Rev 0 of Rept.Planned Corrective Actions Contain Commitments1999-09-27027 September 1999 Forwards LER 99-004-01,providing Correction to Info Previously Provided in Rev 0 of Rept.Planned Corrective Actions Contain Commitments 05000413/LER-1999-015, Forwards LER 99-015-00 Re Inoperability of Auxiliary Bldg Ventilation Sys That Exceeded TS Limits Due to Improperly Positioned Vortex Damper.Commitments Are Contained in Corrective Actions Section of Encl Rept1999-09-27027 September 1999 Forwards LER 99-015-00 Re Inoperability of Auxiliary Bldg Ventilation Sys That Exceeded TS Limits Due to Improperly Positioned Vortex Damper.Commitments Are Contained in Corrective Actions Section of Encl Rept ML20217A7911999-09-24024 September 1999 Forwards Insp Repts 50-413/99-05 & 50-414/99-05 on 990718- 0828 at Catawba Facility.Nine NCVs Identified Involving Inadequate Corrective Actions Associated with Degraded Svc Water Supply Piping to Auxiliary Feedwater Sys ML20212E6471999-09-24024 September 1999 Discusses GL 98-01 Issued by NRC on 980511 & DPC Responses for Catawba NPP & 990615.Informs That NRC Reviewed Response for Catawba & Concluded That All Requested Info Provided.Considers GL 98-01 to Be Closed for Catawba ML20212F0941999-09-21021 September 1999 Discusses Closeout of GL 97-06, Degradation of Steam Generator Internals for Cns,Units 1 & 2 ML20212M2001999-09-20020 September 1999 Confirms 990913 Telcon Between M Purser & R Carroll Re Management Meeting to Be Conducted on 991026 in Atlanta,Ga to Discuss Operator Licensing Issues 05000414/LER-1999-005, Forwards LER 99-005-00 Re Missed EDG TS Surveillance Concerning Verification of Availability of Offsite Power Sources Resulted from Defective Procedure.Planned Corrective Actions Stated in Rept Represent Regulatory Commitments1999-09-20020 September 1999 Forwards LER 99-005-00 Re Missed EDG TS Surveillance Concerning Verification of Availability of Offsite Power Sources Resulted from Defective Procedure.Planned Corrective Actions Stated in Rept Represent Regulatory Commitments ML20212D5321999-09-15015 September 1999 Informs That Duke Energy Corp Agrees to Restrict Max Fuel Rod Average Burnup to 60,000 Mwd/Mtu,In Order to Support NRC Final Approval & Issuance of Requested Amend ML20212B4641999-09-14014 September 1999 Forwards Monthly Operating Repts for Aug 1999 & Revised Monthly Operating Rept for Catawba Nuclear Station,Units 1 & 2 ML20212A4131999-09-14014 September 1999 Informs That TR DPC-NE-2009P Submitted in 990817 Affidavit, Marked Proprietary,Will Be Withheld from Public Disclosure, Pursuant to 10CFR2.709(b) & Section 103(b) of Atomic Energy Act of 1954,as Amended ML20212M1931999-09-13013 September 1999 Refers to 990909 Meeting Conducted at Region II Office Re Presentation of Licensee self-assessment of Catawba Nuclear Station Performance.List of Attendees & Licensee Presentation Handout Encl ML20212A3751999-09-10010 September 1999 Informs That Postponing Implementation of New Conditions Improved by RG 1.147,rev 12,acceptable Since Evaluation on Relief Based on Implementation Code Case for Duration of Insp Interval ML20212A5191999-09-0808 September 1999 Requests NRC Approval for Relief from Requirements of ASME Boiler & Pressure Vessel Code,Section XI,1989 Edition,App VI,VI-2430(c) & 2440(b).Approval of 99-GO-002 Is Requested by 000301 05000413/LER-1999-014, Forwards LER 99-014-00, Missed Surveillance & Operation Prohibited by TS Occurred as Result of Defective Procedures or Program & Inappropriate TS Requirements. Planned Corrective Action Stated in Rept Represents Commitment1999-09-0101 September 1999 Forwards LER 99-014-00, Missed Surveillance & Operation Prohibited by TS Occurred as Result of Defective Procedures or Program & Inappropriate TS Requirements. Planned Corrective Action Stated in Rept Represents Commitment 05000414/LER-1999-003, Forwards LER 99-003-01, Unplanned Actuation of ESFAS Due to a SG High Level Caused by Inadequate Procedural Guidance. Suppl Rept Provides Info Re Root Cause & Corrective Actions Associated with Event Developed Subsequent to Rev1999-08-31031 August 1999 Forwards LER 99-003-01, Unplanned Actuation of ESFAS Due to a SG High Level Caused by Inadequate Procedural Guidance. Suppl Rept Provides Info Re Root Cause & Corrective Actions Associated with Event Developed Subsequent to Rev 0 of LER ML20211H1741999-08-30030 August 1999 Forwards Comments on Catawba Nuclear Station Units 1 & 2 & McGuire Nuclear Station,Units 1 & 2 Specific Reactor Vessel Info Contained in Rvid.Ltr Dtd 990107,rept ATI-98-012-T005 & Partial marked-up Rept WCAP-14995 Encl ML20211M4451999-08-30030 August 1999 Forwards Summary of Util Conclusions Re Outstanding Compliance Issue Re Staff Interpretation of TS SR 3.0.1,per Insp Repts 50-369/99-03 & 50-370/99-03,as Discussed with NRC During 990618 Meeting 05000413/LER-1999-013, Forwards LER 99-013-00,re RHR Heat Exchanger Bypass Valves Not Verified Per TS Surveillance.Surveillance Procedures Have Been Revised & There Are No Further Planned Corrective Actions or Commitments in LER1999-08-25025 August 1999 Forwards LER 99-013-00,re RHR Heat Exchanger Bypass Valves Not Verified Per TS Surveillance.Surveillance Procedures Have Been Revised & There Are No Further Planned Corrective Actions or Commitments in LER ML20211M8191999-08-25025 August 1999 Confirms 990825 Telcon Between G Gilbert & R Carroll Re Mgt Meeting to Be Held on 990909 in Atlanta,Ga,To Allow Licensee to Present self-assessment of Catawba Nuclear Station Performance ML20211A9641999-08-20020 August 1999 Forwards SE Authorizing Licensee 990118 Request for Approval of Proposed Relief from Volumetric Exam Requirements of ASME B&PV Code,Section XI for Plant,Units 2 ML20211C1191999-08-18018 August 1999 Forwards ISI Rept Unit 1 Catawba 1999 RFO 11, Providing Results of ISI Effort Associated with End of Cycle 11 ML20211B9471999-08-18018 August 1999 Forwards Request for Relief 99-02,associated with Limited Exam Results for Welds Which Were Inspected During Unit 1 End of Cycle 11 RFO ML20211C3651999-08-17017 August 1999 Forwards Rev 25 to Catawba Nuclear Station Units 1 & 2 Pump & Valve Inservice Testing Program, Which Includes Reformatting of Manual & Addl Changes as Noted in Attached Summary of Changes ML20211F2971999-08-17017 August 1999 Forwards non-proprietary & Proprietary Updated Pages for DPC-NE-2009,submitted 980722.Pages Modify Fuel Design & thermal-hydraulic Analysis Sections of DPC-NE-2009. Proprietary Page 2-4 Withheld,Per 10CFR2.790 05000413/LER-1999-011, Forwards LER 99-011-00,re Missed Surveillance on Both Trains of CR Area Ventilation Sys Resulting in TS Violation.Planned Corrective Actions Stated in LER Represent Regulatory Commitment1999-08-16016 August 1999 Forwards LER 99-011-00,re Missed Surveillance on Both Trains of CR Area Ventilation Sys Resulting in TS Violation.Planned Corrective Actions Stated in LER Represent Regulatory Commitment ML20211B1121999-08-16016 August 1999 Forwards Topical Rept DPC-NE-2012, Dynamic Rod Worth Measurement Using Casmo/Simulate, Describing Results of Six Drwm Benchmark Cycles at Catawba & McGuire & Discusses Qualification to Use Drwm at Catawba & McGuire ML20210V0321999-08-13013 August 1999 Forwards Insp Repts 50-413/99-04 & 50-414/99-04 on 990606- 0717.Six Violations of NRC Requirements Identified & Being Treated as non-cited Violations,Consistent with App C of Enforcement Policy ML20210S2751999-08-12012 August 1999 Forwards Monthly Operating Repts for July 1999 for Catawba Nuclear Station,Units 1 & 2.Revised Rept for June 1999,encl ML20210Q3751999-08-0505 August 1999 Informs That NRC Plans to Administer Gfes of Written Operator Licensing Exam on 991006.Authorized Representative of Facility Must Submit Ltr as Listed,Thirty Days Before Exam Date,In Order to Register Individuals for Exam ML20210N9521999-08-0404 August 1999 Forwards Changes to Catawba Nuclear Station Selected Licensee Commitments Manual.Documents Constitutes Chapter 16 of Ufsar.With List of Effective Pages IR 05000413/19980131999-08-0202 August 1999 Discusses Integrated Insp Repts 50-413/98-13,50-414/98-13, 50-413/98-16,50-414/98-16 & NRC Special Repts 50/413/99-11 & 50-414/99-11 Conducted Between Aug 1998 & May 1999.Six Violations Occurred,Based on OI Investigation & Insp ML20210M6411999-07-29029 July 1999 Forwards Request for Relief 99-03 from Requirements of ASME Boiler & Pressure Vessel Code,In Order to Seek Relief from Performing Individual Valve Testing for Certain Valves in DG Starting Air (Vg) Sys 05000413/LER-1999-010, Forwards LER 99-010-01 Which Replaces LER 99-002.Rept Number Has Been Changed in Order to Conform to Numbering Convention Specified in NUREG-1022,since Primary Event Involved Both Units1999-07-22022 July 1999 Forwards LER 99-010-01 Which Replaces LER 99-002.Rept Number Has Been Changed in Order to Conform to Numbering Convention Specified in NUREG-1022,since Primary Event Involved Both Units IR 05000413/19990101999-07-22022 July 1999 Discusses Insp Rept 50-413/99-10 & 50-414/99-10 on 990314- 0424 & Forwards Notice of Violation Re Failure to Comply with TS 3.7.13,when Misalignment of Two Electrical Breakers Rendered SSS Inoperable from 981216-29 ML20217G5241999-07-20020 July 1999 Forwards Exam Repts 50-413/99-301 & 50-414/99-301 on 990524- 27,0603,07-10 & 16.Of Fourteen SRO & RO Applicants Who Received Written Exams & Operating Tests,Eight Applicants Passed & Six Failed Exam 05000413/LER-1999-009, Forwards LER 99-009-00,re Inoperability of Containment Valve Injection Water Sys Valve in Excess of TS Limits.Root Cause & Corrective Actions Associated with Event Are Being Finalized & Will Be Provided in Supplement to Rept1999-07-19019 July 1999 Forwards LER 99-009-00,re Inoperability of Containment Valve Injection Water Sys Valve in Excess of TS Limits.Root Cause & Corrective Actions Associated with Event Are Being Finalized & Will Be Provided in Supplement to Rept 05000414/LER-1999-001, Forwards LER 99-001-01 Re Unanalyzed Condition Associated with Relay Failure in Auxiliary Feedwater Sys,Due to Inadequate Single Failure Analysis.Rev Is Being Submitted to Include Results of Failure Analysis Which Was Performed1999-07-15015 July 1999 Forwards LER 99-001-01 Re Unanalyzed Condition Associated with Relay Failure in Auxiliary Feedwater Sys,Due to Inadequate Single Failure Analysis.Rev Is Being Submitted to Include Results of Failure Analysis Which Was Performed ML20209H4431999-07-14014 July 1999 Forwards Monthly Operating Repts for June 1999 for Catawba Nuclear Station,Units 1 & 2.Revised Rept for May 1999 on Unit Shutdowns Also Encl ML20210A5771999-07-14014 July 1999 Forwards Revsied Catawba Nuclear Station Selected Licensee Commitments Manual, Per 10CFR50.71(e),changing Sections 16.7-5,16.8-5,16.9-1,16.9-3,16.9-5 & 16.11-7.Manual Constitute Chapter 16 of UFSAR ML20216D3941999-07-14014 July 1999 Forwards Revs to Catawba Nuclear Station Selected Licensee Commitments Manual NUREG-1431, Forwards SER Agreeing with Util General Interpretation of TS LCO 3.0.6,but Finds No Technical Basis or Guidance That Snubbers Could Be Treated as Exception to General Interpretation1999-07-0909 July 1999 Forwards SER Agreeing with Util General Interpretation of TS LCO 3.0.6,but Finds No Technical Basis or Guidance That Snubbers Could Be Treated as Exception to General Interpretation ML20196L0371999-07-0808 July 1999 Approves Requested Schedule Change of Current two-year Requalification Examinations to non-outage dates.Two-year Cycle Will Start on 991001 & Will End on 020930 05000413/LER-1999-008, Forwards LER 99-008-00,re Operation Prohibited by TS 3.5.2. Rev to LER Will Be Submitted by 990812 Which Will Include All Required Info About Ventilation Sys Pressure Boundry Breach1999-07-0808 July 1999 Forwards LER 99-008-00,re Operation Prohibited by TS 3.5.2. Rev to LER Will Be Submitted by 990812 Which Will Include All Required Info About Ventilation Sys Pressure Boundry Breach ML20196J9001999-07-0606 July 1999 Informs That 990520 Submittal of Rept DPC-NE-3004-PA,Rev 1, Mass & Energy Release & Containment Response Methodology, Marked Proprietary Will Be Withheld Per 10CFR2.790(b)(5) & Section 103(b) of AEA of 1954 IR 05000413/19990031999-07-0101 July 1999 Discusses Insp Repts 50-413/99-03 & 50-414/99-03 Completed on 990605 & Transmitted by Ltr .Results of Delibrations for Violation Re Discovery of Potentially More Limiting Single Failure Affecting SGTS Analysis Provided 1999-09-08
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML20217H0041999-10-13013 October 1999 Forwards MOR for Sept 1999 & Revised MOR for Aug 1999 for Catawba Nuclear Station,Units 1 & 2 ML20217F1301999-10-0707 October 1999 Forwards Rev 1 to Request for Relief 99-03 from Requirements of ASME B&PV Code,In Order to Seek Relief from Performing Individual Valve Testing for Certain Valves in DG Starting (Vg) Sys 05000414/LER-1999-004, Forwards LER 99-004-01,providing Correction to Info Previously Provided in Rev 0 of Rept.Planned Corrective Actions Contain Commitments1999-09-27027 September 1999 Forwards LER 99-004-01,providing Correction to Info Previously Provided in Rev 0 of Rept.Planned Corrective Actions Contain Commitments 05000413/LER-1999-015, Forwards LER 99-015-00 Re Inoperability of Auxiliary Bldg Ventilation Sys That Exceeded TS Limits Due to Improperly Positioned Vortex Damper.Commitments Are Contained in Corrective Actions Section of Encl Rept1999-09-27027 September 1999 Forwards LER 99-015-00 Re Inoperability of Auxiliary Bldg Ventilation Sys That Exceeded TS Limits Due to Improperly Positioned Vortex Damper.Commitments Are Contained in Corrective Actions Section of Encl Rept 05000414/LER-1999-005, Forwards LER 99-005-00 Re Missed EDG TS Surveillance Concerning Verification of Availability of Offsite Power Sources Resulted from Defective Procedure.Planned Corrective Actions Stated in Rept Represent Regulatory Commitments1999-09-20020 September 1999 Forwards LER 99-005-00 Re Missed EDG TS Surveillance Concerning Verification of Availability of Offsite Power Sources Resulted from Defective Procedure.Planned Corrective Actions Stated in Rept Represent Regulatory Commitments ML20212D5321999-09-15015 September 1999 Informs That Duke Energy Corp Agrees to Restrict Max Fuel Rod Average Burnup to 60,000 Mwd/Mtu,In Order to Support NRC Final Approval & Issuance of Requested Amend ML20212B4641999-09-14014 September 1999 Forwards Monthly Operating Repts for Aug 1999 & Revised Monthly Operating Rept for Catawba Nuclear Station,Units 1 & 2 ML20212A5191999-09-0808 September 1999 Requests NRC Approval for Relief from Requirements of ASME Boiler & Pressure Vessel Code,Section XI,1989 Edition,App VI,VI-2430(c) & 2440(b).Approval of 99-GO-002 Is Requested by 000301 05000413/LER-1999-014, Forwards LER 99-014-00, Missed Surveillance & Operation Prohibited by TS Occurred as Result of Defective Procedures or Program & Inappropriate TS Requirements. Planned Corrective Action Stated in Rept Represents Commitment1999-09-0101 September 1999 Forwards LER 99-014-00, Missed Surveillance & Operation Prohibited by TS Occurred as Result of Defective Procedures or Program & Inappropriate TS Requirements. Planned Corrective Action Stated in Rept Represents Commitment 05000414/LER-1999-003, Forwards LER 99-003-01, Unplanned Actuation of ESFAS Due to a SG High Level Caused by Inadequate Procedural Guidance. Suppl Rept Provides Info Re Root Cause & Corrective Actions Associated with Event Developed Subsequent to Rev1999-08-31031 August 1999 Forwards LER 99-003-01, Unplanned Actuation of ESFAS Due to a SG High Level Caused by Inadequate Procedural Guidance. Suppl Rept Provides Info Re Root Cause & Corrective Actions Associated with Event Developed Subsequent to Rev 0 of LER ML20211H1741999-08-30030 August 1999 Forwards Comments on Catawba Nuclear Station Units 1 & 2 & McGuire Nuclear Station,Units 1 & 2 Specific Reactor Vessel Info Contained in Rvid.Ltr Dtd 990107,rept ATI-98-012-T005 & Partial marked-up Rept WCAP-14995 Encl ML20211M4451999-08-30030 August 1999 Forwards Summary of Util Conclusions Re Outstanding Compliance Issue Re Staff Interpretation of TS SR 3.0.1,per Insp Repts 50-369/99-03 & 50-370/99-03,as Discussed with NRC During 990618 Meeting 05000413/LER-1999-013, Forwards LER 99-013-00,re RHR Heat Exchanger Bypass Valves Not Verified Per TS Surveillance.Surveillance Procedures Have Been Revised & There Are No Further Planned Corrective Actions or Commitments in LER1999-08-25025 August 1999 Forwards LER 99-013-00,re RHR Heat Exchanger Bypass Valves Not Verified Per TS Surveillance.Surveillance Procedures Have Been Revised & There Are No Further Planned Corrective Actions or Commitments in LER ML20211B9471999-08-18018 August 1999 Forwards Request for Relief 99-02,associated with Limited Exam Results for Welds Which Were Inspected During Unit 1 End of Cycle 11 RFO ML20211C1191999-08-18018 August 1999 Forwards ISI Rept Unit 1 Catawba 1999 RFO 11, Providing Results of ISI Effort Associated with End of Cycle 11 ML20211C3651999-08-17017 August 1999 Forwards Rev 25 to Catawba Nuclear Station Units 1 & 2 Pump & Valve Inservice Testing Program, Which Includes Reformatting of Manual & Addl Changes as Noted in Attached Summary of Changes ML20211F2971999-08-17017 August 1999 Forwards non-proprietary & Proprietary Updated Pages for DPC-NE-2009,submitted 980722.Pages Modify Fuel Design & thermal-hydraulic Analysis Sections of DPC-NE-2009. Proprietary Page 2-4 Withheld,Per 10CFR2.790 05000413/LER-1999-011, Forwards LER 99-011-00,re Missed Surveillance on Both Trains of CR Area Ventilation Sys Resulting in TS Violation.Planned Corrective Actions Stated in LER Represent Regulatory Commitment1999-08-16016 August 1999 Forwards LER 99-011-00,re Missed Surveillance on Both Trains of CR Area Ventilation Sys Resulting in TS Violation.Planned Corrective Actions Stated in LER Represent Regulatory Commitment ML20211B1121999-08-16016 August 1999 Forwards Topical Rept DPC-NE-2012, Dynamic Rod Worth Measurement Using Casmo/Simulate, Describing Results of Six Drwm Benchmark Cycles at Catawba & McGuire & Discusses Qualification to Use Drwm at Catawba & McGuire ML20210S2751999-08-12012 August 1999 Forwards Monthly Operating Repts for July 1999 for Catawba Nuclear Station,Units 1 & 2.Revised Rept for June 1999,encl ML20210N9521999-08-0404 August 1999 Forwards Changes to Catawba Nuclear Station Selected Licensee Commitments Manual.Documents Constitutes Chapter 16 of Ufsar.With List of Effective Pages ML20210M6411999-07-29029 July 1999 Forwards Request for Relief 99-03 from Requirements of ASME Boiler & Pressure Vessel Code,In Order to Seek Relief from Performing Individual Valve Testing for Certain Valves in DG Starting Air (Vg) Sys 05000413/LER-1999-010, Forwards LER 99-010-01 Which Replaces LER 99-002.Rept Number Has Been Changed in Order to Conform to Numbering Convention Specified in NUREG-1022,since Primary Event Involved Both Units1999-07-22022 July 1999 Forwards LER 99-010-01 Which Replaces LER 99-002.Rept Number Has Been Changed in Order to Conform to Numbering Convention Specified in NUREG-1022,since Primary Event Involved Both Units 05000413/LER-1999-009, Forwards LER 99-009-00,re Inoperability of Containment Valve Injection Water Sys Valve in Excess of TS Limits.Root Cause & Corrective Actions Associated with Event Are Being Finalized & Will Be Provided in Supplement to Rept1999-07-19019 July 1999 Forwards LER 99-009-00,re Inoperability of Containment Valve Injection Water Sys Valve in Excess of TS Limits.Root Cause & Corrective Actions Associated with Event Are Being Finalized & Will Be Provided in Supplement to Rept 05000414/LER-1999-001, Forwards LER 99-001-01 Re Unanalyzed Condition Associated with Relay Failure in Auxiliary Feedwater Sys,Due to Inadequate Single Failure Analysis.Rev Is Being Submitted to Include Results of Failure Analysis Which Was Performed1999-07-15015 July 1999 Forwards LER 99-001-01 Re Unanalyzed Condition Associated with Relay Failure in Auxiliary Feedwater Sys,Due to Inadequate Single Failure Analysis.Rev Is Being Submitted to Include Results of Failure Analysis Which Was Performed ML20216D3941999-07-14014 July 1999 Forwards Revs to Catawba Nuclear Station Selected Licensee Commitments Manual ML20209H4431999-07-14014 July 1999 Forwards Monthly Operating Repts for June 1999 for Catawba Nuclear Station,Units 1 & 2.Revised Rept for May 1999 on Unit Shutdowns Also Encl ML20210A5771999-07-14014 July 1999 Forwards Revsied Catawba Nuclear Station Selected Licensee Commitments Manual, Per 10CFR50.71(e),changing Sections 16.7-5,16.8-5,16.9-1,16.9-3,16.9-5 & 16.11-7.Manual Constitute Chapter 16 of UFSAR 05000413/LER-1999-008, Forwards LER 99-008-00,re Operation Prohibited by TS 3.5.2. Rev to LER Will Be Submitted by 990812 Which Will Include All Required Info About Ventilation Sys Pressure Boundry Breach1999-07-0808 July 1999 Forwards LER 99-008-00,re Operation Prohibited by TS 3.5.2. Rev to LER Will Be Submitted by 990812 Which Will Include All Required Info About Ventilation Sys Pressure Boundry Breach ML20196G7461999-06-22022 June 1999 Requests Exemption from Requirements of 10CFR54.17(c) That Application for Renewed Operating License Not Be Submitted to NRC Earlier than 20 Yrs Before Expiration of Operating License Currently in Effect ML20196E9541999-06-18018 June 1999 Forwards SG Tube Insp Conducted During Unit 1 End of Cycle 11 Refueling Outage.Attachments 1,2,3 & 4 Identify Tubes with Imperfections in SGs A,B,C & D,Respectively ML20195K4571999-06-14014 June 1999 Forwards MORs for May 1999 & Revised MORs for Apr 1999 for Catawba Nuclear Station,Units 1 & 2 ML20195J1691999-06-10010 June 1999 Forwards Written Documentation of Background & Technical Info Supporting Catawba Unit 1,notice of Enforcement Discretion Request Re TS 3.5.2 (ECCS-Operating),TS 3.7.12 (Auxiliary Bldg Filtered Ventilation Exhaust Sys) ML20217G5771999-06-0909 June 1999 Forwards Post Exam Comments & Supporting Reference Matls for Written Exams Administered at Catawba Nuclear Station on 990603 05000414/LER-1999-002, Forwards Abstract of LER 99-002-00 Re Forced Shutdown of Plant as Result of Flow Restriction Caused by Corrosion of Afs Assured Suction Source Piping Due to Inadequate Testing. Final LER Will Be Submitted No Later than 9907081999-06-0303 June 1999 Forwards Abstract of LER 99-002-00 Re Forced Shutdown of Plant as Result of Flow Restriction Caused by Corrosion of Afs Assured Suction Source Piping Due to Inadequate Testing. Final LER Will Be Submitted No Later than 990708 ML20207F2381999-06-0101 June 1999 Forwards Copy of Catawba Nuclear Station Units 1 & 2 1998 10CFR50.59 Rept, for NRC Files ML20195J1131999-05-26026 May 1999 Requests Approval to Change Cycle Dates for Two Year Requalification Training Program Required by 10CFR55.59,to Improve Scheduling of Requalification Exams to non-outage Periods 05000413/LER-1999-007, Forwards LER 99-007-00,re Operation Prohibited by TS 3.4.7. Commitments Identified in LER Are Listed in Planned Corrective Actions Section1999-05-26026 May 1999 Forwards LER 99-007-00,re Operation Prohibited by TS 3.4.7. Commitments Identified in LER Are Listed in Planned Corrective Actions Section ML20195B4751999-05-24024 May 1999 Forwards Rev 7 to UFSAR Chapter 2 & Chapter 3 from 1998 UFSAR for Catawba Nuclear Station.List of Instructions on Insertion Encl ML20196L1851999-05-20020 May 1999 Forwards Proprietary & non-proprietary Version of Rev 1 to TR DPC-NE-3004, Mass & Energy Release & Containment Response Methodology, Consisting of Finer Nodalization of Ice Condenser Region.Proprietary Info Withheld ML20196L1791999-05-20020 May 1999 Communicates Util Licensing Position Re Inoperable Snubbers. Licensee Has Determined That Structure of ITS Has Resulted in Certain Confusion Re Treatment of Inoperable Snubbers 05000413/LER-1997-009, Forwards LER 97-009-02, Unanalyzed Postulated Single Failure Affecting SG Tube Rupture Analysis, Suppl Revises Planned C/A Described in Suppl 1 to Ler.Current Status of C/As & Addl C/As Planned,Provided in Rept1999-05-17017 May 1999 Forwards LER 97-009-02, Unanalyzed Postulated Single Failure Affecting SG Tube Rupture Analysis, Suppl Revises Planned C/A Described in Suppl 1 to Ler.Current Status of C/As & Addl C/As Planned,Provided in Rept ML20206T4481999-05-13013 May 1999 Forwards Rev 3 to Topical Rept DPC-NE-3002-A, UFSAR Chapter 15 Sys Transient Analysis Methodology, IAW Guidance Contained in NUREG-0390 ML20206R1721999-05-13013 May 1999 Forwards Monthly Repts for Apr 1999 for Catawba Nuclear Station,Units 1 & 2 & Revised Monthly Operating Repts for Mar 1999 ML20206T0281999-05-12012 May 1999 Forwards Changes to Catawba Nuclear Station Selected Licensee Commitments Manual. Document Constitutes Chapter 16 of UFSAR 05000413/LER-1999-006, Forwards LER 99-006-00,re CR Ventilation Sys Inoperability. Root Cause & Corrective Actions for Occurence Are Being Finalized & Will Be Reported in Supplement Rept on 9906071999-05-10010 May 1999 Forwards LER 99-006-00,re CR Ventilation Sys Inoperability. Root Cause & Corrective Actions for Occurence Are Being Finalized & Will Be Reported in Supplement Rept on 990607 ML20206N8201999-05-10010 May 1999 Forwards Revs 15 & 16 to Catawba Unit 1 Cycle 12 COLR, Per TS 5.6.5.Rev 15 Updates Limits for New Catawba 1 Cycle 12 Reload Core & Rev 16 Revises Values Re Min Boron Concentrations for Rwst,Cla & SFP ML20206J4431999-05-0303 May 1999 Forwards Changes to Catawba Nuclear Station Selected Licensee Commitments Manual, Per 10CFR50.71(e).Document Constitutes Chapter 16 of UFSAR ML20206D2141999-04-29029 April 1999 Forwards 1998 Annual Radioactive Effluent Release Rept for Catawba Nuclear Station,Units 1 & 2, Per Plant TS 5.6.3. Rept Contains Listed Documents ML20206E4101999-04-26026 April 1999 Forwards Four Copies of Rev 9 Todpc Nuclear Security & Contingency Plan,Per 10CFR50.54(p)(2).Changes Do Not Decrease Safeguards Effectiveness of Plan.Encl Withheld,Per 10CFR73.21 1999-09-08
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Text
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- Duke Power Company A tu two Gmper Casauha Nudeer Station Atu We 4800 Corwood Road i
York. SC 29745 Gary R. l%reon (803) 831-4251 omCE Yur h nidens (803) 83).3426 fat September 10, 1997 U.S. Nuclear Regulatory. Commission Attention: Document Control Desk Washington, D.C. 20555
Subject:
Catawba Nuclear Station, Unit 1 Docket Number 50-413 Reply to Request for Additional Information on the Proposed Amendment Regarding Natural Circulation Testing (TAC No. M98728)
Reference:
Letter-from Peter S. Tam, NRC, to Gary R.
Peterson, Duke, Request for Additional Information on the Proposed Amendment Regarding Natural Circulation Testing, Septenber 2, 1997 Gentlemen:
Please find attached Catawba Nuclear Station'_s reply to the request for additional information contained in the reference letter. Each NRC question in the reference letter is restated, followed by our response.
If you have any questions concerning this information, please call L.J. Rudy at (803) 831-3084.
Very truly yo rs, t k G.R. Peterson LJR/s CD I ' ,
Attachment 9709170090 970910 -
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Document Control Desk
.Page'2 September 10, 1997 xc (with' attachment):
L.A. Reyes, Regional Administrator Region II D.J. Roberts, Senior Resident Inspector Catawba Nuclear Station P.S. Tam,. Senior Project Manager ONRR
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ATTACHMENT REPLY TO NRC REQUEST FOR ADDITIONAL INFORMATION CATAWBA UNIT 1 NATURAL CIRCULATION TEST FOR REPLACEMENT STEAM GENERATORS
Background
The purpose of this test is to demonstrate the ability of the Nuclear Steam Supply System (NSSS), and more specifically, the BWI Replacement Steam Generators (RSGs),
to remove heat via natural circulation of the primary coolant and to gather information useful in fine-tuning simulators for natural circulation conditions. This test will be performed in Mode 3, during the normal planned shutdown for the Unit 1 End of Cycle 10 (EOC10) refueling outage.
Calculations performed by the Steam Generator Replacement project team showed that natural circulation capabilities of the RSGs should be slightly superior to original SGs. This e~ is due to their greater heat transfer surface area and higher thermal center due to a 1,nger tube bundle. The RSGs are already modeled in approved safety analyses. This test is therefore not being conducted as a requirement, but rather at the direction of the Duke Nuclear Safety Review Board (NSRB) and management to gather data to benchmark the training simulator and to thereby improve operator knowledge of RSG characteristics. As such, the test procedure utilizes equipment most likely to be used in such a scenario, and uses it consistent with existing procedures.
NRC Reactor Systems Branch Position RSB 5-1, which requires the capability to shutdown to cold shutdown from the control room using redundant safety grade equipment, is not adversely impacted, and all such equipment will be verified operable prior to this test.
The positive impact of the RSGs on natural circulation has been confirmed by a RETRAN thermal-hydraulic simulation of a loss of offsite power scenario. The results of this analysis show that, within 5 minutes of the loss of offsite power, a stable reactor coolant system (RCS) flow rate of approximately 5% of the full power value is established with a core delta T of less than 300F.
It should be noted that operators at Catawba Nuclear Station have had recent experience with natural circulation not only on the training simulator, but also during the Unit 2 Loss 1
of Offsite Power (LOOP) Event of February 6, 1996. During
,this event, operators controlled the unit using natural circulation to achieve Mode 4 (hot shutdown). There were no significant problems as a result of this event, and natural circulation proceeded to cool the RCS until the residual heat removal (RHR) system was placed in operation 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br /> later.
This Natural Circulation Verification Test is expected to take only a few hours while in Mode 3 (hot standby) to gather data, meet acceptance criteria, and return reactor coolant pumps to service for normal cooldown.
Answers to the specific NRC questions are provided in the following responses.
NRC Question #1 Describe the test procedure and the major recovery steps in the procedures that will be used for recovery from the test. Include a list of prerequisites for the test including those related to auxiliary feedwater system status, steam generator relief valve status, charging /high head safety injection system status, etc.
Response
Description of the Test Procedure:
- The procedure initially begins with the unit in a stable condition in Mode 3, Hot Standby:
- While the unit is in Mode 3 (557 i 2 F, 2235 i 25 psig), all four reactor coolant pumps (RCPs) will be simultaneously tripped.
Establishment of natural circulation will be verified by observation of wide range loop temperatures as well as core exit thermocouples.
- Pressurizer and SG pressure and level response will be monitored throughout this test.
- Pressurizer auxiliary spray from the chemical volume control system (CVCS) will be actuated if additional pressure control is needed. The procedure specifies that letdown be in service to maintain an acceptable 2
temperature of the auxiliary spray so that the use
, of auxiliary spray is acceptable.
Stable natural circulation will be maintained for approximately 30 minutes while data are gathered to verify that the acceptance criteria have been met.
- The Operator Aid Computer (OAC) transient monitor will be frozen to obtain data of plant parameters during the transition period to natural circulation and during the natural circulation period itself.
- The plant will be recovwred by realigning normal charging and restarting the RCPs per normal operating procedure.
- A detailed evaluation of the data will be performed against certain review criteria.
Major Recovery Steps:
Recovery from this test either from normal or early termination is performed by exiting the test procedure and using preexisting operating procedures:
OP/1/A/6200/01 " Chemical and Volume Control System" OP/1/A/6150/02A " Reactor Coolant Pump Operation" OP/1/A/6100/02 " Controlling Procedure for Unit Shutdown" The following emergency procedures are available to the operator in case of a design basis accident that would make all the RCPs unavailable for continuation of the shutdown:
EP/1/A/5000/ECA-0.1 " Loss of AC Power Recovery without SE Required", and EP/1/A/5000/ES-0.2 " Natural Circulation Cooldown" Test Prerequisites:
- 1) All RCPs are in operation.
- 2) The CVCS is aligned for power operation with letdown and charging in service.
- 3) The following control systems are operable and have been placed in automatic control:
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{
- pressurizer pressure control
- pressurizer power operated relief valve (PORV) control
- pressurizer spray control e secondary steam dump control (pressure mode) to maintain approximately 1092 psig main steam pressure and RCS T-cold at approximately 557*F
- 1NV-294(centrifugal charging pumps A & B flow control)
- 4) Verify the following operable:
- All pressurizer PORVs (with associated block valves open)
- All pressurizer safety valves All main steam PORVs (with associated block valves open)
- 5) OAC RCS system saturation graphics program is operable and outputs are valid.
- 6) SG levels are being maintained using main feedwater pump speed control.
- 7) Conduct shift briefing.
- 8) Establish equilibrium conditions as follows:
- RCS T-avg is stable at 557 i 2 F
- RCS pressure is stable at 2235 i 25 psig
- SG levels are at no-load level 1 3%
- 9) Restrict work in the switchyard area.
- 10) Verify one time change to Technical Specification 3.4.1.2 to allow all four RCPs to be turned off for up to 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> in Mode 3 has been approved by the NRC.
- 11) In addition to the above, the Outage Manager shall ensure the following key safety functions needed to allow natural circulation testing:
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- Two Technical Specification boration flow paths
. operable
- Source range or boron dilutio'n mitigation system (BDMS) operable per Technical Specifications
- Boron concentration 2 cold shutdown concentration
- 1A & 1B centrifugal charging / safety injection trains operable
- Containment integrity established per Technical Specifications
- 4160 volt emergency busses 1 ETA and 1ETB energized from offsite source
- Standby auxiliary transformer SATA or SATB powered from Unit 2
- Unit 1 is not in any Technical Specification action statement of 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> or less duration NRC Question #2: During the initial test, you experienced a problem with the reactor coolant pump that you described as follows: " a reactor coolant pump could not be restarted for a period of time at the completion of the test due to a high standpipe level." Discuss how this problem will be prevented in this test. Discuss this not only fram the perspective of violating technical specifications but from the perspective of being able to start the pump.
Response
During the initial Catawba Unit 1 natural circulation verification performed on January 19-20, 1985, a high standpipe level indication resulted in the inability to restart RCP A while recovering from the test. This test is documented in the Catawba Unit 1 Startup Report, RCP standpipe level problems have been resolved by drain line rerouting some years ago. Some level problems are not 5
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unusual during plant startup following seal maintenance or
, replacement and usually indicate that the seal faces are not in proper contact. Such a problem is unlikely during this test because seal leakoffs will be verified to be within normal range and the RCS will remain hot and pressurized throughout the test. Standpipe levels and other RCP operating parameters during the last two startups were examined and were found to be within acceptable limits.
Plans include having the RCP equipment engineer onsite for the test to assist in monitoring key parameters and resolving any problems if they occur. If a RCP cannot be started for any reason, operators will enter the appropriate procedure for loss of a RCP and proceed as directed by plant procedures and Technical Specifications. Mode 3 Technical Specifications requires 3 of 4 RCPs to be operable and in operation. The RHR system may be placed in service below 3 5 0'F .
In addition to the plant emergency procedures, the safety parameter display system (SPDS) directs the operators along the path for a loss'of heat sink, loss of inventory, etc.
The critical safety functions are then followed along the heat sink " red path", " yellow path", etc. to address the specific function. The test procedure contains termination criteria as well as acceptance criteria. Also, see response
- 4 for a discussion of the training provided to the operators.
NRC Question #3: The initial test was required to be performed at core burnups to ensure that no significant core decay heat levels are present. In this case, a reactor trip would effectively terminate the event. In your proposed test, you will use decay heat to conduct the test and therefore, there will be significant decay heat. Discuss any contingencies that you will have in place to cool the core in case of unexpected system behavior.
Response
This type test was required for initial Unit 1 startup.
Whereas the initial test was performed with the reactor critical (Mode 2) and overtemperature delta temperature (OTAT) and overpower delta temperature (OPAT) trip setpoints bypassed, this procedure is designed to utilize natural decay heat in Mode 3. The initial test was performed during the initial startup program and decay heat was not available, therefore, nuclear heat was used instead.
Performance of this test in Mode 3 instead of Mode 2 has 6
been judged by Engineering and management to have lower
,overall plant risk. No reactor trip setpoint will be bypassed during this test and the possibility of violating the minimum temperature for criticality ( 551*F ) will not be an issue while in Mode 3.
In addition to providing forced cooling, the RCS pumps during Mode 3 are required operable for boron mixing in the event of an inadvertent dilution. The RCS boron concentration will be increased to greater than or equal to the cold shutdown boron concentration prior to shutting down the RCPs. Performing the natural circulation test in Mode 3 with all rods in and cold shutdown boron concentration is considered more conservative from a reactivity management perspective. Temperature control with rods would not provide as good or realistic data to benchmark the training simulators, which is the main purpose of this test. The RSGs have been shown by analysis to perform better than the original SGs, and startup testing and turbine online response has been closely analyzed to assure that expectations were met. The RSGs show good level stability, smooth transition to turbine online, and less shrink and swell during transients. The test implementation plan contains a checklist that specifies that all safety equipment is operable, in addition to the required status of all applicable automatic control systems. Main feedwater and steam dump to the condenser will be employed. Auxiliary feedwater and the SG PORVs will be fully operable as a backup. Redundant trains of emergency core cooling systems (ECCS) and normal RHR cooling will also be required operable.
NRC Question #4 Discuss any special training (class room, briefings, simulator, etc.) that the operators were or will be provided prior to conducting this test.
Response
Training personnel have been involved in the procedure validation using the Catawba simulator. Operators on the shift performing this test will receive "Just in Time" training in the form of a pre-job briefing, simulator exercise, and a second pre-job briefing in the control room immediately prior to the test. It should be noted that
- Catawba Nuclear Station has recent experience with natural circulation not only on the training simulator, but also during the Unit 2 Loss of Offsite Power Event of February 6, 1996. During this event, operators controlled the unit using natural circulation to achieve Mode 4. There were no 7
significant problems as a result of this event, and
, procedures have been optimized to provide better guidance based on lessons learned.
NRC Question #5: In your submittal, you provided a list of example test termination criteria. Provide a complete list of the test termination criteria and a list of expected values for the same parameters. Also, discuss and justify your expectation of system pressure response and primary power-operated relief valve operation.
Response
Specific test termination criteria are provided:
- Lowest RCS subcooling margin s 15'F
- SG 1evel Inarrow range) on any 2 loops < 12%
- Pressurizer level < 17% or > 5% unexplained decrease
- RCS T-hot (wide range) or any valid incore thermocouple reading > 590 F
- RCS AT in any loop > 45*F
- Steam line pressure s 900 psig Dilution of RCS (controlled or uncontrolled)
(Technical Specification 3.4.1.2)
- RCPs have been deenergized for 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> (Technical Specification 3.4.1.2 when approved by NRC)
During the performance of this test, the following parameters are expected to be maintained within the specified limits:
- Lowest RCS subcooling margin 2 25 F
- SG level (narrow range) > 25%
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- Pressurizer pressure > 1955 psig
- Pressurizer level with RCPs running > 25%
- Pressurizer level with RCPs off 2 level at time pumps tripped off ,
- RCS T-hot (vide range) and incore thermocouple readings s 590'F .
i
- RCS T-cold (wide range) 557 i 5*F
- RCS AT in every loop 5 45'F Loops are filled and pressurized to normal operating pressure (2235 psig) in Mode.3, and will remain so throughout the test. SG pressure control is provided by the condenser dumr valves to ensure stable test conditions.
Pressurizer heaters will be operable and will cycle as needed. This will also ensure that the primary side pressure is stable and'that level remains in the pressurizer within the expected range. Letdown is in service and primary pressure control is by pressurizer auxiliary spray since the RCPs-will be secured. During simulator validation of the test procedure, auxiliary spray was capable of preventing a RCS pressure increase up to the PORV setpoint.
Additionally, the PORV controller has anti-windup protection to limit PORV response due to prolonged operation close to,.
but below its 2335 psig setpoint. Pressurizer-PORVs are not expected to open, but plant procedures assure using these as a backup means of pressure control. Chemistry control assures there is no non-condensible gas present. Separation of non-condensible gas does not occur in this mode as it can in Mode 5 when the RCS is depressurized. It is not part of this test to cool the plant down to Mode 5, but rather to restart the RCPs for normal forced flow during the cooldown from Mode 3 to Mode 5.
NRC Question #6 In your submittal, you state that the operators will verify natural circulation by observation of the wide range loop temperatures and core exit thermocouple.
Explain how this verification is accomplished and the type of training operators received in this regard (i.e., how will operators know if there is natural circulation).
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Response
'Oper'ators are trained in the diagnosis of natural circulation as a function of training on emergency i procedures (e.g., Ep/1(2)/A/5000/ECA-0.1 " Loss of AC Power Recovery without SI Required" and EP/1(21/A/5000/ES-0.2
" Natural Circulation Cooldown"). After RCP trip, core exit temperatures will increase and core AT between hot leg and cold leg is expected to increase to approximately 10'F -
40'F depending on the time since shutdown and the number of loops that go into natural circulation. Given the test prerequisites, all 4 loops should go into natural circulation. Operations personnel participating in the simulator validation of this natural circulation test procedure had no problem monitoring core AT, subcooling margin, SG pressure control, and associated parameters using OAC graphics, the SPDS, and control board gauges. Example OAC displays showing core AT and pressurizer pressure and level, taken during the simulator validation of this procedure, will be provided to the shif t as part of the pre- o job briefing.
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