ML20214V718

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Safety Insp Rept 50-341/86-33 on 860930-1110.No Violations or Deviations Noted.Major Areas Inspected:Routine Control Room Operations,Shift Turnovers,Operator Response to Plant Transients & Followup to 861005 & 06 ECCS Actuations
ML20214V718
Person / Time
Site: Fermi DTE Energy icon.png
Issue date: 11/28/1986
From: Wright G
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20214V695 List:
References
50-341-86-33, NUDOCS 8612090801
Download: ML20214V718 (8)


See also: IR 05000341/1986033

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U. S. NUCLEAR REGULATORY COMMISSION

REGION III

Report No. 50-341/86033

Docket No. 50-341

License No. NPF-33

Licensee: Detroit Edison Company

2000 Second Avenue

Detroit, MI 48224

Facility Name:

Fermi 2

Inspection At: Fermi Site, Newport, MI

Inspection Conducted: September 30 through November 10, 1986

Inspectors:

M. J. Farber

D. J. Sullivan

T. S. Rotella

M. R. Johnson

J. A. Isom

W. F. Burton

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L. E. W it

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Approved By:

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Reactor Projects Section 2C

Date

Inspection Summary

Inspection on September 30 through November 10, 1986 (Report

No. 50-342/86033(DRP))

Areas Inspected: Announced special safety inspection by the Augmented Restart

Inspection Team of routine control room operations, shift turnovers, operator

response to plant transients, operator control of maintenance and surveillance,

startup testing, plant maintenance, and followup to the October 5th and 6th

ECCS actuations.

Results:

No violations or deviations were identified.

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DETAILS

1.

Persons Contacted

  • F. E. Agosti, Vice President, Nuclear Operations
  • L. P. Bregni, Compliance Engineer, Licensing
  • L. B. Collins, System Engineer, Nuclear Engineering
  • R. S. Lenart, Plant Manager

R. A. May, Maintenance Engineer

  • G. D. Ohlenmacher, Assistant Maintenance Engineer

G. R. Overbeck, Director, Operator Training

C. V. Phillips, Staff, Maintenance

  • E. Preston, Operations Engineer
  • F. H. Sondgeroth, Region Ill Engineer, Licensing
  • B. R. Sylvia, Group Vice President
  • G. M. Trahey, Director, Quality Assurance
  • W. M. Tucker, Acting Superintendent, Operations
  • Denotes those who attended the exit meeting on November 4,1986.

The inspectors also contacted other licensee administrative and technical

personnel during the course of the inspection.

2.

Routine Control Room Operations

The inspectors monitored routine control operation on a three shift basis

for the majority of plant operating time during the inspection period.

While monitoring control room operations the team focused on communications

among shift personnel, adherence to procedures, recognition or and

response to annunciators, involvement of shift supervisors in plant

operations, and congestion in the control room. Among the evolutions

observed by the team were reactor / plant startups, reactor / plant

shutdowns, turbine / generator operation, and equipment out-of-service and

restoration. The inspectors had comments with respect to the following

evolutions:

a.

Reactor / plant startups

On October 31st, with the reactor at 17% power and pulling control

rods to support operation of the main turbine, a reactor operator

made two control rod manipulation errors, each approximately two

hours apart. The first error resulted from the operator inadvertently

skipping a step in the sequence on his pull sheet. He moved one

control rod one notch out of sequence. He immediately recognized

his error and reported it to his supervisors. With the concurrence

of Reactor Engineering and his supervisors the rod was reinserted

to its proper position and the correct sequence restored.

Approximately two hours later the operator had completed pulling

each of the four rods in the selected group one notch. At this time

an indication problem arose and the operator stopped rod movement

to resolve it. When he started to pull rods again, he failed to

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select the next rod in the sequence and pulled the rod which had

dust previously been moved. The operator, once again, immediately

recognized his error and notified his supervisors. .The shift

supervisor ordered all rod movements stopped and the operator.was

. replaced. With the concurrence of Reactor Engineering,' after a

technical and. safety evaluation, the rod was reinserted to its

proper position. While there was little technical or safety

significance to,these errors, the failure of management programs

to prevent the recurrence of rod manipulation errors was of concern

to the inspectors. Following discussions with the inspectors-and

regional management the licensee implemented a program of double

verification for all rod movements. This program was contained in

a standing. order for all operators. The inspector reviewed the

order,to assess its adequacy, noted that operators were required

to sign for having read it, and attended shift turnover meetings.

where the double verification program was explained to the operators.

Additional actions taken by the licensee include revision of the

rod pull sheets to make them easier to follow and a request to INP0

for a two day Human Performance Evaluation Study (to be conducted

November 10-11,1986).

Review of the revised rod pull sheets and

the INP0 evaluation results is an Open Item (341/86083-01(DRP)).

No further errors were reported or observed during subsequent rod

manipulations; however, the inspectors will continue to monitor this

situation to determine if the program is effective.

b.

Equipment out-of-service and restoration

On October 28th, with the plant in cold shutdown, control room

operators were returning the "A" Reactor Recirculation Pump to

service. When they attempted to start the Motor Generator (MG) set

which provides power to the pump, the operator attending the MG set

heard unusual noises and the sound of electrical arcing. Before

the operators in the control room could shut down the machine, it

tripped.

Inspection revealed that the carbon brushes, used for

transmitting excitation power from the stationary part of the

machine to the rotating element, had been removed from the brush-

holders and were not properly seated on their slip rings. The

attempted start with the brushes removed resulted in damage to

the slip rings, some brushes, and some brushholders. The licensee

determined that after the reactor shutdown on October 23rd, the

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operators lifted the brushes from their holders in order to measure

their length and determine if replacement was in order.

Following

these measurements, the brushes were left out of the holders. When

the operating crew attempted to start the MG set, they were unaware

that the brushes were not installed as required.

The licensee's review of the incident revealed that the operator

who removed the brushes informed the control room that he had not

reinstalled them. He was directed to place a Control Room

Information System (CRIS) Jot on the MG set controls on the panel

as a reminder that the brushes were lifted. He failed to do this.

Review of the control room operator's log showed that an entry,

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stating that the MG set brushes.were lifted, had been made and that

other operators had reviewed the log. ' Fourteen shifts later the

entry was not remembered when the MG set was being' returned to

service.

The key element in this incident appears to be the failure of the

operator to place a CRIS dot on the MG set controls as directed.

Licensee management determined that the administrative controls

in place at the time of the incident were adequate to have prevented

it if they had been followed and an Urgent Required Reading was

issued for all operators which stressed the importance of careful

log reviews and adequate identification of off-normal equipment

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conditions. The inspector reviewed the required reading and

determined that it properly stressed the necessity for adhering

to in-place controls. The inspector reviewed the administrative

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controls discussed in the required reading and agreed that they

were adequate to have prevented the incident, had they been followed.

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Shift Turnover Meetings

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The team monitored shift relief and turnover meetings to assess log

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reviews, panel walkdowns, problem identification, equipment statusing,

proper communications, crew attentiveness, and supervisor effectiveness.

The. team noted that shift turnovers were generally efficient and

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well-run. There were two areas were noted by the-team as needing some

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improvement:

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Some of the individuals providing information at the shift briefings

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spoke so softly that it was nearly impossible to hear them.- This

was not limited to operators; it also included Startup, Reactor

Engineering, Health Physics, and Chemistry personnel.

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During the briefings, it appeared that operators were paying very

little attention to their panels and concentrating on the briefing.

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The shift supervisors were positioning themselves in such a manner

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as to force the operators to turn away from their panels.

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The licensee acknowledged these comments. The inspector noted at the

next shift briefing following the exit meeting that people with

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information spoke up and that the shift supervisor positioned himself

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in the' control room such that his operators could periodically monitor

their panels while he gave his briefing.

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4.

. Operator Response to Plant Transients

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The team monitored operator response during plant transients and abnormal

situations to evaluate operator understanding of plant behavior, operator

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understanding of system interaction, communications under stress, use of

procedures, and integrated shift performance.

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The following transients and abnormal situations were observed:

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Frequent level transients caused by Startup Level Control Valve

problems

120VAC balance of plant instrument power supply transferring from

primary to alternate power feeds

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Intentional scram and plant cooldown caused by continuing problems

with the 120VAC balance of plant instrument power supply

a.

Balance of plant instrument power supply (MPU-3) transfer.

The transfer of MPU-3 between the primary and alternate power feeds

is essentially a dead bus transfer and resulted in the loss of a

considerable amount of equipment and instrumentation. More detailed

information on the equipment lost and the reason for the transfer is

contained in Inspection Report 50-341/86032(DRP). As a result of

this event the operators were faced with a loss of feedwater (loss

of control air to the Startup Level Control Valve), a main turbine

trip, loss of offgas, Division II Standby Gas Treatment actuation,

and shifting of Control Center HVAC to recirculation on loss of

Reactor Building HVAC. After a moment of initial confusion caused

by the number of annunciators which alarmed, the operators

identified their problems, rapidly prioritized them, and then began

addressing these problems. Reactor vessel level control was rapidly

restored using the Standby Feedwater system and then the operators

began to systematically restore the lost equipment. The event was

handled in an exceptionally business-like and professional manner.

The operators were knowledgeable with respect to what had happened

to their plant and what would be necessary to restore it.

b.

Intentional reactor scram and plant cooldown.

Further problems, on the same day, with MPU-3 led the licensee to

decide that the plant should be shut down. Failure of the power

supply appeared imminent and such a failure would result in a plant

trip.

It was decided that a scram, rather than a shutdown, was

warranted due to the potential impact if MPU-3 failed during the

evolution (MPU-3 supplied power for the Rod Sequence Control System

and the Rod Worth Minimizer).

The operators carefully reviewed

their plant status, planned for the expected rapid cooldown due to

lack of decay heat, and developed contingency plans for use in the

event of other possible equipment failures during the evolution.

As a direct result of the planning by the operators the plant was

scrammed and the cooldown completed in a safe, controlled, efficient

manner.

5.

Control of Maintenance and Turveillance

The team monitored operation's control of maintenance and surveillance

activities to assess adherence to procedures, understanding of plant

status, and adherence to technical specifications.

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The team monitored the following maintenance:

Startup Level Control Valve

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Rod Sequence Control System

Reactor Core Isolation Cooling turbine oil leaks

Traversing Incore Probe ball valve

Source Range Monitor "B" cable problem-

Gland Seal Regulator

The team monitored the following surveillances:

Main Steam Isolation Valve Closure

Core Spray Pump and Valve Operability

Main Steam Line "D" Rad Monitor

Drywell Pressure Instrument C71-N050C

Reactor Recirculation Pump Valve Operability Checks

Control Rod Scram Time Testing

The team participated in followup inspections after the licensee reported

that during the performance of HPCI Condensate Storage Tank Level

Calibrations, HPCI and RCIC were both inoperable for two periods of two

hours. Review of.the event revealed that no action had been taken within

one hour to proceed to STARTUP as required by Technical Specification 3.0.3.

This matter is subject to potential escalated enforcement and is

discussed in detail in Inspection Report 50-341/86032(DRP).

The team noted that with the exception of the HPCI/RCIC/ CST event,

operators appeared to be aware of the impacts of maintenance and

surveillances by other departments on plant status.and equipment

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operability.

6.

'Startup Testing

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The team monitored operator involvement in startup testing to evaluate

pre-test briefings, understanding of test conditions, impact of testing

on operability, understanding of-the test procedure, control of the test

evolution, adherence to test procedures, and communications between

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operators and test engineers.

The team monitored the following startup tests:

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STUT.010.022, Pressure Regulator

STUT.01A.023, Startup Level Control Valve

STUT.018.013, Traversing Incore Probe - Process Computer Interface

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Checks

STUT.01G.014, RCIC Vessel Injection

STUT.01A.028, Remote Shutdown Demonstration

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STUT.HUC.014 RCIC System - 150 psig Hot CST Injection

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STUT.HUD.014, RCIC System - 150 psig Vessel Injection

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.The team noted that briefings before tests were generally thorough and

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-well-organized, that the test engineers and operators understood the

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-impact of the testing on the plant, that procedural adherence was

enforced, and that the shift supervisor always remained in control of

the the plant. The operators and test personnel were especially

well-prepared for.the Remote Shutdown Demonstration. A separate shutdown

crew was identified and they spent ~approximately one week preparing for

the test. Equipment locations were reviewed, the procedure was walked

through several times, test engineers and operators met to discuss the

procedure and its intent, the RCIC pump was operated from the Remote

Shutdown Panel for practice, and contingency plans were developed in case

of abnormal occurrences. The intensive preparation resulted in a test

that was performed exceptionally well. On-shift operators, the shutdown

crew, and the test engineers knew their duties and how to carry them out

with little or no confusion or questions. Excellent communications were

maintained between all involved personnel throughout the test and the

Control Room shift supervisor remained in charge of the plant at all

times.

7.

Plant Maintenance

During the inspection period, the team and the resident inspectors became

concerned with the material condition of the plant as evidenced by the

number of CRIS dots on the panels, the backlog of work requests, the

number of leaking valves and_ flanges, and the apparent inability of the

maintenance department to resolve some recurrent equipment problems.

Team members and the residents inspected the plant and reviewed logs to

identify maintenance concerns and then met with licensee management to

discuss them. The licensee has developed a comprehensive program to

restore and improve plant material conditions. Additional information

on this subject is contained in Inspection Report 50-341/86032(DRP).

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ECCS Actuation Followup

On October 5,1986, an I&C technician improperly operated a valve on a

differential pressure transmitter during a Reactor Vessel' Level Channel

Calibration causing a full ECCS actuation. On October 6th, improper

restoration of the transmitter after the event caused an RPS Full Scram

signal to be generated when the calibration was attempted again.

Details

of this event and the licensee's corrective action are contained in

Inspection Report 50-341/86032(DRP). Since the event the Restart Team

Leader has periodically met with I&C supervision to review the

implementation of the corrective action. The licensee appears to be

proceeding adequately, although somewhat slowly. The team will observe

future surveillances involving differential pressure transmitters to

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assess the effectiveness of the licensee's cor?ective actions.

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9.

Open Item

Open items are matters which have been discussed with the licensee, which

will be reviewed further by the inspector, and which involve some action

on the part of the NRC or licensee or both. An open item disclosed

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during the inspection is discussed in Paragraph 2.a.

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10. Exit Interview

The inspectors met with licensee representatives.(denoted in Paragraph 1)

on Novenber 4,1986 and informally throughout the inpsection period and

summarized the scope and findings of the inspection activities. The

inspectors also discussed the likely informational content of the

inspection report with regard to documents or processes reviewed by the

inspectors during the inspection. The licensee did not identify any such

documents / processes as proprietary. The licensee acknowledged the

findings of the inspection.

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