ML20210A915
| ML20210A915 | |
| Person / Time | |
|---|---|
| Site: | Maine Yankee |
| Issue date: | 04/29/1987 |
| From: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| To: | |
| Shared Package | |
| ML20210A912 | List: |
| References | |
| 50-309-85-98, NUDOCS 8705050190 | |
| Download: ML20210A915 (46) | |
See also: IR 05000309/1985098
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ENCLOSURE
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U.S. NUCLEAR REGULATORY COMMISSION
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REGION I
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SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE
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INSPECTION REPORT NUMBER 50-309/85-98
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MAINE YANKEE ATOMIC POWER COMPANY
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MAINE YANKEE NUCLEAR POWER STATION
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ASSESSMENT PERIOD: NOVEMBER 1, 1985 to JANUARY 31, 1987
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BOARD MEETING DATE: MARCH 31, 1987
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8705050190 870429
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ADOCK 05000309
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TABLE OF CONTENTS
PAGE
I.
INTRODUCTION.........................................................
1
II.
CRITERIA.............................................................
2
III. SUMMARY OF RESULTS...................................................
4
A.
Overall
Summary.................................................
4
B.
Background......................................................
4
C.
Facility Performance Analysis Summary...........................
8
D.
Unplanned Shutdowns, Plant Trips and Forced Outages.............
9
IV.
PERFORMANCE ANALYSIS.................................................
11
A.
Plant Operations................................................
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8.
Radiological
Controls...........................................
14
C.
Maintenance.....................................................
17
D.
Survei11ance....................................................
20
E.
Emergency Preparedness..........................................
22
F.
Security and Safeguards.........................................
24
G.
Assurance of Quality............................................
27
H.
Licensing Activities............................................
29
I.
Training and Qualification Effectiveness........................
31
V.
SUPPORTING DATA AND SUMMARIES........................................
33
A.
Investigation and Allegation Review.............................
33
8.
Escalated Enforcement Actions...................................
33
C.
Licensee Conferences Held During Appraisal
Period...............
33
D.
Confirmation of Action Letters..................................
33
E.
Review of Licensee Event Reports
(LERs).........................
33
F.
Licensing Activities............................................
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TABLES
Table 1 - Inspection Report Activities
Table 2 - Inspection Hour Summary
Table 3 - Enforcement Activity
Table 4 - Licensee Event Reports
Table 5 - LER Synopsis
Table 6 - SALP History
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I.
INTRODUCTION
The Systematic Assessment of Licensee Performance (SALP) is an integrated NRC
effort to collect the available observations and data on a periodic basis and
to evaluate licensee performance based on this information.
SALP is supple-
mental to normal regulatory processes used to ensure compliance with NRC rules
and regulations.
SALP is intended to be sufficiently diagnostic to provide
a rational basis for allocating NRC resources and to provide meaningful guid-
ance to the licensee's management to promote quality and safe plant operation.
A NRC SALP Board, composed of the staff members listed below, met on March
31, 1987 to review the collection of performance observations and data to
assess the licensee's performance in accordance with the guidance in NRC
Manual Chapter 0516, " Systematic Assessment of Licensee Performance".
A sum-
mary of the guidance and performance criteria is provided in Section II of
this report.
This report is the SALP Board's assessment of the licensee's safety perform-
ance at the Maine Yankee Atomic Power Station for the fifteen month period
of November 1, 1985 through January 31, 1987.
The SALP Board was comprised of the following:
Chairman
W. F. Kane, Director, Division of Reactor Projects (DRP)
Members
L. H. Bettenhausen, Acting Director, Division of Reactor Safety (DRS)
E. C. Wenzinger, Chief, Projects Branch No. 3, DRP
J. Johnson, Acting Chief, Operations Branch, DRS
L. E. Tripp, Chief, Reactor Projects Section 3A, DRP
C. F. Holden, Senior Resident Inspector
P. Sears, Licensing Project Manager, NRR
M. Shanbaky, Acting Chief, Emergency Preparedness and Radiological Protection
Branch, DRSS
Other Attendees (non-voting)
R. Freudenberger, Resident Inspector, Maine Yankee
D. Limroth, Project Engineer, DRP
W. Troskoski, Senior Resident Inspector, Beaver Valley Unit 1
K. Ferlic, Emergency Response Coordinator, DRSS
W. Bailey, Physical Security Inspector, DRSS
W. Pasciak, Chief, Effluents Radiation Protection Section, DRSS
H. Zibulsky, Safeguards Chemist, DRSS
M. Kamanski, Radiation Specialist, DRSS
P. Polk, Acting Chief, Projects Branch No. 1, DRP
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II.
CRITERIA
Licensee performance is assessed in selected functional areas, depending on
whether the facility is in a construction, preoperational or operational phase.
Functional areas normally represent areas significant to nuclear safety and
the environment.
Some functional areas may not be assessed because of little
-or no licensee activities or lack of meaningful observations.
Special areas
may be added to highlight significant observations.
One or more of the following evaluation criteria were used to assess each
functional area.
1.
Management involvement and control in assuring quality.
2.
Approach to resolution of technical issues from'a safety standpoint.
3.
Responsiveness to NRC initiatives.
4.
Enforcement history.
5.
Operational events (including response to, analyses of and corrective
actions for).
6.
Staffing (including management).
Based upon the SALP Board assessment, each functional area evaluated was
classified into one of three performance categories.
The definitions of these
performance categories are:
Category 1.
Licensee management attention and involvement are aggressive and
oriented toward nuclear safety; licensee resources are ample and effectively
used so that a high level of performance with respect to operational safety
is being achieved.
Reduced NRC attention may be appropriate.
Category 2.
Licensee management attention and involvement are evident and
are concerned with nuclear safety; licensee resources are adequate and reason-
ably effective so that satisfactory performance with respect to operational
safety is being achieved.
NRC attention should be maintained at normal levels.
Category 3.
Licensee management attention or involvement is acceptable and
considers nuclear safety, but weaknesses are evident; licensee reaources
appear to be strained, or not effectively used so that minimally satisfactory
performance with respect to operational safety is being achieved.
Both NRC
and licensee attention should be increased.
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The SALP Board may determine to include an appraisal of the performance trend
of a functional area.
Normally, this performance trend is only used where
both a definite trend of performance is discernible to the Board and the Board
believes that continuation of the trend may result in a change of performance
level.
Improving (declining) trend is defined as: Licensee performance was
determined to be improving (declining) near the close of the assessment period.
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III. SUMMARY OF RESULTS
A.
Overall Summary
The SALP Board assessment confirmed a continuation of a strong management
overview of daily plant activities with emphasis on safe operations.
Most notable were the high performance levels noted in the following
functional areas: plant operations, surveillance, emergency preparedness,
security, and training and qualification effectiveness.
Licensee management exhibited a thorough approach in troubleshooting,
assignment of responsibilities, tracking, and resolution of individual
problems.
Strong individual performance was evidenced by the lack of
personnel errors in all areas.
Significant licensee initiatives were noted during this assessment period
including improved communications through morning plant management meet-
ings, replacement and/or upgrading of major plant components, a compre-
hensive surveillance program augmented by prompt reaction to degraded
surveillance results, a program for the elimination of copper sources
in the condensate and feedwater systems, and utilization of the Quality
Assurance group to aid in improving overall performance.
Based on recent
observations, an improving trend was noted in licensing activities.
Notwithstanding the above, there were eight plant trips, three unplanned
shutdowns and approximately eighteen power reductions / limitations during
this assessment period.
This high incidence of such occurrences was
primarily the result of balance of plant component failures, equipment
performance difficulties, or for the performance of maintenance activi-
ties.
Such performance by balance of plant equipment indicates that im-
provements are needed in the material condition of the plant through
measures such as more aggressive preventive maintenance, reviews of the
effects of aging on plant components, component replacement, or system
redesign.
The radiological controls area was characterized by inconsistent perform-
ance.
While several initiatives indicated strong performance, the re-
sponse to other situations varied in effectiveness.
Additional efforts
in this area are warranted.
As a result of this assessment, NRC activities in Category 1 functional
areas are eligible for reduced inspection effort.
We will consider the
level of performance and initiatives to address identified shortcomings
in our prioritization of the inspection program for the facility.
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B.
Background
1.
Licensee Activities
At the beginning of the assessment period the facility was operating
at 76 percent power and increasing load following the cycle 9 re-
fueling outage and some equipment problems experienced during start-
up following that outage.
Between November 4 and 6, 1985, the plant
reduced power several times because of high stator gas differential
temperature in the main generator.
The plant tripped on November
6 from 81 percent power on loss of load.
This was the result of
a failure of the turbine-driven feedwater pump recirculation valve
controller.
On November 7 the plant was returned to powie opera-
tions reaching full power on November 15.
Power was reduced on
November 15 and 22 to clean r..ain condenser waterboxes and repair
reactor protective system (RPS) temperature detectors. The plant
tripped on November 22 when the turbine generator control system
failed.
Power operations were resumed on November 24.
A power
reduction was made on November 26 to remove the turbine driven
feedwater pump from service following problems with the recircula-
tion valve controller.
On December 4, power was reduced due to a dropped control rod as-
sembly.
On December 24, plant power was reduced to repair a
hydraulic oil leak on a turbine governor valve.
Power was reduced
on December 28 and 31 in order to backwash debris from the main
condenser waterboxes.
On January 3, 1986 the plant reduced power
to place the turbine-driven feedwater pump in service.
On January 4 the plant was manually tripped when an administrative
limit on condenser differential pressure was reached.
The differ-
ential pressure condition was the result of the operator securing
the wrong circulating water pump.
The plant was returned to power
operations on January 5. During early 1986, a number of power re-
ductions to 75 percent were required due to fouling, tube leakage
and eddy current testing of the main condenser.
These occurred on
January 12, 13, 17, 25 and February 1.
Reactor power was reduced below 15 percent on February 15 for tur-
bine governor valve limiter maintenance.
Full power was resumed
on February 16.
Because of main generator hydrogen leakage, power
was limited to 83 percent on February 19, and a plant shutdown was
performed on February 21 to correct the hydrogen leakage.
The plant was taken critical on March 11 and from March 14 a limit
of 98.8 percent power was maintained due to concerns over generator
vibrations.
The plant was shut down on April 16 in order to balance
and shim the main generator.
Upon return to power on April 17,
while switching from electric driven main feedwater pumps to the
turbine-driven main feedwater pump, the plant tripped from 55 per-
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cent.
High level in a steam generator caused a turbine and reactor
trip.
The licensee identified the problem as the speed controller
for the steam-driven main feedwater pump.
The plant remained in
shutdown until April 18 to repair a inverter which grounded on
April 17.
The plant reduced power on April 24 for routine surveillance of
turbine valves.
On April 27, the plant reduced power to 72 percent
and switched to electric driven main feedwater pumps after observing
problems with the steam-driven feedwater pump controller.
The plant
returned to 97 percent power (the maximum power while running elec-
tric driven feedwater pumps) and with the exception of a brief re-
duction in power on April 29 because of grid problems, remained at
that power until May 28.
Two power reductions on May 28 and 31 were required for steam leak
repair and repairs to the heater drain tank level controller.
On
June 12, a rupture disk failure resulted in the inadvertent closure
of a steam generator excess flow check valve (EFCV) and a reactor
trip on low steam generator level.
Following startup on June 13,
power was limited due to chloride cleanup. Power remained at 85
percent while investigations were being conducted on the EFCV rup-
ture disk failure.
The plant was shut down on June 30 to replace
the rupture disks and to perform eddy current inspections of main
condenser tubes.
The tube inspection led to the discovery of addi-
tional problems with a low pressure turbine which extended the shut-
down until July 18.
The plant was phased on the grid July 19 and
power was increased in increments to full power on July 24.
On August 1, a power reduction was initiated to facilitate the
isolation and repair of an electro-hydraulic control oil leak.
Full
power was resumed on August 3.
An automatic reactor trip occurred
on August 10 on low level in a steam generator due to a failure of
- 1 inverter.
A startup was performed on August 11 and the plant
was returned to full power on August 13.
On October 9, a planned 36 hour4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br /> power reduction to 75 percent was
initiated to perform maintenance on a traveling water screen.
The
reactor was manually tripped on October 19 to prevent equipment
damage caused by induced current in the main transformer isophase
bus ducts.
Repairs were completed and a startup was performed the
same day.
On November 7, the plant reduced power to approximately
60 percent in support of maintenance of a distribution substation.
On November 15, a read or trip occurred.
The cause of the trip was
a loss of the steam driven feedwater pump due to low lube oil pres-
sure.
A plant startup was conducted using the electric driven
feedwater pumps on November 16 and power was returned to 97 percent
on November 18.
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On December 2, the plant determined that the control room breathing
air system did not provide the required flowrate and began a shut-
down.
One train of the breathing air system was returned to service
and the plant shutdown was terminated with power at 35 percent.
Power was increased to 100 percent on December 5.
The plant re-
mained at 100 percent power until January 3, 1987 when power was
reduced to 75 percent for turbine valve testing.
Cycle 9 coastdown
operations began January 22 and power was at 95 percent at the end
of the assessment period on January 31, 1987.
2.
Inspection Activities
During this assessment period there were two NRC resident
inspectors assigned to the site.
There were two team inspec-
tions in the quality assurance area and one in the radiological
controls area.
There were a total of 3477 inspection hours, or
2782 hours0.0322 days <br />0.773 hours <br />0.0046 weeks <br />0.00106 months <br /> on a annualized basis.
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C.
Facility Performance Analysis Summary
Last Period
This Period
(7/1/84 -
(11/1/85 -
Recent
Functional Area
10/31/85)
1/31/87)
Trend
A.
Plant Operations
2
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8.
Radiological Controls
2
2
C.
Maintenance
2
2
D.
Surveillance
1
1
E.
Fire Protection
1
N/A**
F.
1
1
G.
Security and Safeguards
1
1
H.
Outages
2
N/A***
I.
Assurance of Quality
2
Improving
J.
Licensing Activities
2
2
Improving
K.
Training and Qualification
1
Effectiveness
L.
Engineering Support
- Assurance of Quality, Training and Qualification Effectiveness, and Engineering
Support are three areas which were not formerly assessed, but are now treated
as separate functional areas.
- This area was not evaluated as a separate functional area during this assess-
ment period.
Pertinent observations are covered in other appropriate functional
areas.
- There were no major planned outages during this assessment period; observations
regarding unscheduled outages are contained in the Maintenance functional area.
- Engineering Support is now considered as a separate functional area.
Due to
limited staff observations in this area, pertinent comments are included in
each of the functional areas.
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D.
Unplanned Shutdowns, Plant Trips and Forced Outages
Power
Root
Functional
Date
Level
Description
Cause
Area
11/06/85
81%
Loss of the steam driven
Aging
Maintenance
feedwater pump following
failure of the recirculation
valve controller led to a
reactor trip on loss of load.
11/22/85
69%
Failure of the main generator Unknown
turbine control system caus-
ing reactor trip because of
turbine trip (loss of load).
01/04/86
75%
Shutdown to prevent equipment Personnel
Operations
damage when an administrative Error
limit on condenser differen- (inattention
pressure was reached.
to detail)
02/21/86
84%
Plant shutdown to repair
Inadequate
Maintenance
hydrogen leakage from main
Corrective
generator.
Maintenance
04/16/86
99%
One day shutdown for balanc-
Inadequate
Maintenance
ing of the main generator.
Corrective
Maintenance
04/17/86
55%
The speed controller for the Aging
Meentenance
steam driven feedwater pump
failed causing reactor trip
on high level in #3 steam
generator.
06/12/86
99%
Rupture disk failure on the
Component
Maintenance
excess steam flow check valve Failure Due
caused a reactor trip on low To Inadequate
SG level.
Preventive
Maintenance
06/30/86
85%
Plant shutdown to upgrade
Inadequate
Maintenance
excess flow check valve rup- Corrective
ture disks and Eddy Current
Maintenance
testing of the main condenser.
Outage was extended when seal
problems in the low pressure
turbine were detected.
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Power
Root
Functional
Date
Level
Description
Cause
Area
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08/10/86
99%
Failure of #1 inverter led
Aging
Maintenance
to a reactor trip on low SG
level,
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10/19/86
100%
Shutdown to prevent equipment Personnel
Maintenance
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damage when isophase support Installation
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structure was discovered
Error
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glowing red.
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11/15/86
100%
Loss of lube oil pressure at Inadequate
Maintenance
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the steam driven feedwater
Preventive
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pump caused a trip of the
Maintenance
feedwater pump resulting in
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a. reactor trip on loss of
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load.
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Note:
The root causes in this Table reflect the opinion of the SALP board based
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on the inspector (s) description of the event and may, in certain instances, differ
from the LER.
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IV.
PERFORMANCE ANALYSIS
A.
Plant Operations (1655 hours0.0192 days <br />0.46 hours <br />0.00274 weeks <br />6.297275e-4 months <br />, 47%)
1.
Analysis
The last SALP report rated performance in the Operations area as
Category 2 with an improving trend primarily as the result of strong
management overview of daily plant activities.
During this assess-
ment period, two resident inspectors were assigned to the site and
were responsible for the majority of inspection effort in the
Operations area.
The licensee continues to exhibit strong performance in the Opera-
tions Area which reflects aggressive management overview of a well
trained highly qualified staff.
The fundamental corporate goal is
safe operations and successive layers of management are accountable
for achieving that goal.
Morning Managers meetings are the primary
mechanism used to focus and direct the staff.
The Plant Shift
Supervisor attends these meetings to provide input about any opera-
tional concerns and coordinate scheduling of daily activities.
All
aspects of plant operations are discussed in an open atmosphere.
A number of systems such as Morning Meeting minutes, Plant Informa-
tion Reports, and Unusual Occurrence Reports are utilized to keep
personnel aware of plant conditions and operational occurrences.
These systems are reviewed weekly at the Morning Managers meeting
for completeness and resolution of issues. When situations arise
that are not well understood, individual assignments are made for
collecting and documenting all related information in an attempt
to understand and resolve the problem.
That information/ resolution
is then reviewed either at a Morning Meeting or during a Plant
Operations Review Committee (PORC) meeting.
Information concerning
problem tracking and resolution is widely distributed through the
use of Morning Meeting Minutes or Plant Information Reports.
This
results in a well informed, coordinated plant staff focused on safe
plant operations and problem resolution.
The Plant Operations Review Committee (PORC) provides an effective
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review function.
The licensee's initiative to use a Procedure Sub-
committee has resulted in a timely, thorough review of procedure
changes and allowed PORC to concentrate on additional issues.
routinely uses Special Meetings to review Operational events and
the results of special reviews of unique or unusually challenging
problems.
PORC reviews are thorough, detailed and timely; there
is good participation and strong leadership.
Senior Corporate Management is frequently involved in plant opera-
tions through routine plant visits and attendance at selected Morn-
ing managers meetings.
Additionally, management development and
planning sessions are periodically held throughout the year to
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measure plant performance in achieving the goals and objectives.
Particular attention has been given in these meetings to the number
of trips, shutdowns, and power reductions / limitations due to equip-
ment failure.
Plant operators are quick to recognize adverse trends and take ac-
tion to resolve them.
Alert and timely response by plant operators
has prevented instrument / equipment failures such as feedwater con-
trol system failures from affecting plant status.
The plant opera-
tors are professional in appearance and maintain an inquisitive
attitude.
Operators routinely coordinate plant evolutions with
other departments such as Engineering and Maintenance.
The plant
demonstrated their conservative approach to resolving technical
issues when they delayed a plant startup pending repairs to an in-
verter in April, 1986.
Control room noise and distractions have been reduced through the
use of a work processing area near the control room entrance.
The
effect of this area has been better control over access to the con-
trol room.
Maine Yankee utilizes a six crew rotation.
Plant Shift Supervisors
are rotated into the Operations Staff for six month assignments in
order to coordinate procedure reviews and special projects.
An
additional position in support of operations on the plant staff has
been authorized and filled.
Plant corrective actions and followup for operational events are
thorough.
When situations arise that are not well understood, the
plant utilizes a variety of methods to identify and correct those
problems including matrix tracking of symptoms and their closeout,
dedicated technicians for troubleshooting and the use of system log
books to track observed causes and effects.
Corrective actions are
also persistent.
When the cause of the excess flow check valve
rupture disk failures was thought to be corrected by controlled
cleanliness and torquing, the plant continued to investigate other
options.
As a result, contact sticking of the associated air com-
pressors along with an out of tolerance relief valve were ultimately
determined to be the root cause of the rupture disk failure.
Plant housekeeping has improved. The plant has released approximately
30 percent of formerly radiological controlled areas for unrestricted
access. Considerable effort was expended to plan for the storage
of refueling tools.
Storage of equipment throughout the plant has
improved during this assessment period through the use of dedicated
storage areas and individual cleaning area assignments.
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One minor violation involving operation of an instrument valve by
an unauthorized licensee engineer was observed.
This evolution
should have been controlled by Operations and is considered an
isolated incident.
The plant scram rate was 0.9 scrams per 1000 critical hours.
One
of the scrams was caused by operator error when the wrong circulat-
ing water pump discharge valve was closed following maintenance.
The operator was quick to recognize his mistake and inserted a
manual scram when condenser differential pressure reached an ad-
ministrative limit. One other partial activation of the engineered
safety features system was attributed to operator error when the
wrong switch was manipulated during a post scram recovery.
Although
these two instances were the result of operator error, the root
cause can be attributed to Human Factor Engineering (similar
switches performing similar functions in close proximity).
The plant has instituted a Human Performance Evaluation System (HPES)
for the review of events and identified deficiencies. The goal of
this system is to identify and correct potential problems through
the review of deficiencies prior to those problems contributing to
operational events.
This program has received management support
based upon the extent of the training conducted and the low thres-
hold of deficiencies reviewed under this system.
Generally the quality of Licensee Event Reports (LERs) continues
to improve.
Maine Yankee's discussion concerning failure mode and
manufacturer information in LERs is good.
Areas for LER improvement
include assessment of safety consequences and corrective actions.
In general, Maine Yankee LERs are judged to be average when compared
to other licensees.
In summary, safe operations continued to receive effective manage-
ment and staff attention.
The overall performance level by the
operations staff was high.
2.
Conclusion
Category 1.
3.
Board Recommendation
None.
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B.
Radiological Controls (382 hours0.00442 days <br />0.106 hours <br />6.316138e-4 weeks <br />1.45351e-4 months <br />, 11%)
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1.
Analysis
In the previous assessment period the licensee was rated Category 2 with
weaknesses noted in the airborne sampling program, personnel contamina-
tion control, sorting of low level waste, and compliance with Radiation
Work Permit (RWP) requirements.
During this assessment period, there
were six inspections by Region I Specialists in the following areas:
three radiation protection inspections, one post accident sampling system
inspection, one non-radiological chemistry inspection and one transporta-
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tion inspection.
The resident inspectors also reviewed selected program
areas.
The licensee has initiated a number of program, policy and procedure up-
grades during this assessment period to improve the Radiological Controls
Program.
Upgrades included the redesign of the radiological controls
check point, development of the Radiological Controls Improvement Program
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and rewrite and reissuance of the Radiation Protection Manual.
The Radiological Controls Improvement Program has been introduced to
identify, track, analyze and resolve radiological incidents. Monthly
reports are issued to management to track progress.
Management support
of this program has been firm and severe disciplinary action has been
taken in a few instances for violations of plant procedures.
The result
has been better adherence to radiological control requirements as evi-
denced by fewer violations and internally identified deviations.
There
is evidence of corporate and site management involvement including fre-
quent meetings, use of feedback and tracking mechanisms, assessment of
activities, etc. with very tight control at all levels.
Decision making
authority regarding radiological controls programs occurs at the depart-
ment manager level or higher reflecting the high level of management
attention to this area.
The licensee has been conducting an effective program for liquid and
gaseous effluent control.
Releases were made in accordance with proce-
dures and Technical Specifications requirements.
Semiannual Radioactive
Effluent Release Reports were comprehensive, accurate and indicate that
releases are well below all regulatory limits.
Effluent control instru-
ments were maintained and calibrated in accordance with regulatory re-
quirements, and ventilation systems were maintained and tested as re-
quired.
Procedures related to the above areas were found to be adequate.
There was an unplanned release of noble gas to the atmosphere as the
result of a leaking flange.
Although this release was a small fraction
of regulatory limits, it was preventable.
The licensee should conduct
a review of plant systems and identify other potential release paths and
take action to prevent such unplanned releases.
There was significant progress in radwaste volume reduction activities
in 1986 including a 47% volume decrease, construction and use of new
waste facilities, and the development of a plan to dispose of the rad-
_ _ _ _ _ _ _ _ _ _ _
.
,
.
15
waste backlog.
The licensee's program for transportation of solid radio-
active waste was adequate with regard to the selection of packaging,
training of personnel, low level waste storage, and use of and adherence
to procedures.
The licensee's ALARA program is well documented and effective at all
levels of the organization.
The ALARA program is controlled and directed
by the ALARA Committee.
This committee includes many of the PORC members
as well as members of the Radiation Protection staff and provides input
to the Plant Manager.
The licensee's exposure goal for 1986, a non-outage
year, was 200 man-rem.
Actual exposure of 92 man-rem reflects good con-
trols in this area.
The ALARA program will be reviewed during the up-
coming refueling outage.
I
Although there were no major weaknesses or programmatic violations iden-
tified, several areas need additional licensee attention.
Long term
records such as dosimetry, training, and physicals are generally complete;
however, short term records such as radiological surveys and air samples
to support RWPs were, at times, incomplete or not retrievable.
Training
for self-monitoring by personnel was inadequate in that it did not pro-
vide adequate instructions for some survey equipment.
Previous techni-
cian experience credit may not be in conformance with industry standards
in some cases.
The comparatively small size of the licensee's staff
appears to limit the ability to react to changes.
There were some weaknesses noted in the chemistry program including a
lack of a measurement quality control program, inadequate equipment to
'
support sulfate analysis, and failure to retrain chemistry technicians.
Little progress has been made in resolving three of nine open issues in
the chemistry area for the post accident sampling system.
The licensee
has taken major steps to resolve these chemistry issues including staff-
ing improvements and hardware changes.
The licensee's reaction to non-routine radiological situations varies
in effectiveness.
Most notable was the sand removed during repairs to
underground piping within the radiologically controlled area.
A portion
of the sand was released into the owner controlled area and was subse-
quently returned to the radiologically controlled area when it was found
partially contaminated.
Better surveys of the sand could have prevented
its initial release.
More aggressive followup of earlier indications
of the contamination problem (some sand material in the pile above back-
ground and employee identification of a potential problem) could have
achieved more timely problem resolution. In contrast, the licensee used
a technically sound and conservative approach in handling and removing
potentially contaminated ceiling tiles from the controlled area.
In summary, although there were many areas of strength and no major pro-
grammatic deficiencies observed in this functional area, there were
several areas where improvements could be realized.
!
. . . _ _ . _ _
_ _ _
_
__._._- _____ __
. _ _ _ _ _
_ ___.,
.
.
16
2.
Conclusion
Category 2.
3.
Board Recommendation
Licensee
Review staff to determine if its size contributes to deficiencies noted
in this area.
NRC
Evaluate chemistry program changes.
.
.
17
C.
Maintenance (447 hours0.00517 days <br />0.124 hours <br />7.390873e-4 weeks <br />1.700835e-4 months <br />, 13%)
1.
Analysis
The previous SALP rated this area category 2 as a result of good
overall management control.
The resident inspectors provided
coverage of this area during routine inspections. Regional inspec-
tors provided input for areas they observed during specialist in-
spections.
The Maintenance Department is_ composed of an experienced, well
qualified staff. Management is actively involved in the prioritiza-
tion of maintenance activities through the morning managers meeting.
During these meetings, input from the Operations Department is re-
ceived and Plant Engineering Department assistance is requested as
necessary. Weekly planning sessions provide for advanced coordina-
tion of surveillances and preventive maintenance.
During this as-
sessment period there were no significant violations identified.
The Deficiency Report / Repair Order (DR/R0) system utilized by the
licensee is an effective and comprehensive system for identifying,
reviewing and correcting off normal conditions. All design changes
and most preventive maintenance items are implemented through the
DR/R0 system. All DR/R0s get Engineering and Quality Assurance
Department reviews.
The Maintenance Department supplies Outage Coordinators to oversee
the repair efforts during outages.
This is a good practice in that
it releases the Plant Shift Supervisor to concentrate on plant
evolutions and status.
The plant maintains a prioritized work list
including items scheduled for unplanned outages which is aggres-
sively pursued.
Coordination and scheduling of additional outage
time was thoroughly planned and reviewed by the licensee.
This has
resulted in effective utilization of outage time.
The Maintenance Department has taken advantage of redundant plant
design features including installed spare components to conduct on-
line preventive maintenance on major equipment, such as, .ipray pump
motors, low pressure safety injection pump motors, condensate pumps
and high pressure drain pumps.
The overall effect is better utili-
zation of planned outage time.
The licensee has embarked on several long term programs to increase
the reliability and safety of the plant.
One particularly effective
program for the reduction of chloride intrusion problems associated
with the Main Condenser was the replacement of the waterboxes with
titanium waterboxes. Although at least 3 power reductions were
necessary in January and June 1986, due to chlorides, the problem
was eventually identified and corrected.
Recent operational data
indicate no chloride intrusion from the main condenser.
In addition,
.
.
18
the licensee continues its program for elimination of copper com-
ponents in the feedwater system.
Upcoming replacement of two sets
of feedwater heaters will result in the elimination of 80 percent
of copper components from the feedwater system.
A spare reactor
coolant pump motor is already in use as a replacement allowing for
routine preventive maintenance on the out of service motor.
Staffing level and training appear to be adequate in the maintenance
area.
During heavy work load periods additional resources are con-
tracted.
Backlogs of outstanding work orders are trended and action
taken to resolve problem areas. Some mechanical maintenance proce-
dures rely primarily on the technicians experience; however, no
deficiencies have been identified as a result of these generic pro-
cedures. In fact, maintenance technicians are knowledgeable in their
field. The licensee has begun a program of converting technicians
experience into plant procedures.
Of the eight reactor trips and three unplanned shutdowns this period,
all but two were attributable to component failures or unscheduled
maintenance.
Two trips involved electronic controllers for the
I
feedwater system.
The licensee has a Comprehensive Reliability
Study underway which addresses the replacement of these controllers
for which repair parts no longer exist.
Some controllers have al-
ready been replaced.
Additional recommendations for upgrades of
other feedwater equipment are scheduled for the upcoming outage.
One trip was attributed to a failure of an inverter.
Age of the
inverter was a contributor to its failure.
One trip appears to be
random failure of the turbine control circuit.
One manual trip
occurred due to faulty installation of the grounding device on the
isophase buswork.
One trip was due to the loss of the operating
steam driven feedwater pump.
A combination of lube oil system leaks
and a loose electrical contact were the cause of the trip.
One trip
attributed to the Excess Flow Check Valve (EFCV) had a number of
root causes including a corroded / sticking relay in an associated
air compressor controller and an out of tolerance relief valve for
the air compressor.
Aggressive followup and root cause determina-
tion resulted in the identification of several of these problems.
In addition to the above, there were numerous (approximately eigh-
teen) power reductions and limitations for a variety of maintenance
related tasks and equipment difficulties as summarized in Section
III.B.
Most of the unplanned trips, shutdowns, and power reductions /limita-
tions were either the direct result of component failure, due to
equipment performance difficulties or for the performance of main-
tenance related activities.
This high incidence of such occurrences
indicates that equipment (primarily balance of plant) performance
at Maine Yankee requires further attention to trend performance
in order to establish root causes to deal with problems in a
_-.
.
--
- - -..
_- -.._._
..
.- - - _ -
.
. - .-
.
.
4
.
19
f
t
i
proactive way.
This high number of trips / shutdowns / power
l
reductions resulted in other undesirable but related consequen-
ces such as added challenges to safety systems and increased
stress for the operating staff due to the needs for added power
i
maneuvering and plant monitoring.
.i
In summary, no programmatic problems were observed during the per-
formance of maintenance activities.
Improvements in the material
condition of the plant are needed through measures such as more
aggressive preventive maintenance, reviews of the effects of aging
l-
on plant components, component replacement, or system redesign.
2.
Conclusion
'
Category 2.
3.
Recommendation
+
<
Licensee:
i
l
Conduct a review of trends of balance of plant equipment performance.
<
'
NRC:
I
J
i
Schedule a special inspection of the balance of plant equipment
'
)
performance per Temporary Instruction 2515/83.
)
!
,
i
,
I
!
k
i
l
'
':
!
!
!
l.
1
i
l
i
i
'
,
i
<
j
!
i
i
l
i
'
-
-
-
-
.
.
.
.
20
t
.
D.
Surveillance (337 hours0.0039 days <br />0.0936 hours <br />5.57209e-4 weeks <br />1.282285e-4 months <br />, 10%)
1.
Analysis
l
The last SALP appraisal rated this area a Category 1 based upon a
well implemented program.
The Resident Inspectors reviewed this
area during routine inspections and Regional Inspectors reviewed
sur/eillances in their respective areas as a part of specialist
inspections.
The licensee's surveillance program is detailed under the Compre-
hensive Equipment Performance (CEP) program.
Under this program
the Technical Specification (T.S.) required surveillances are in-
cluded under the License Enforced Surveillances (LES).
This area
encompasses T.S., Inservice Testing, Inservice Inspection and Code
required surveillances.
Each department maintains their surveil-
lance schedules with coordination of multiple surveillances for the
same equipment provided during the Horning Managers Meeting and
Weekly Planning Meetings.
The CEP also contains the Preventive
Maintenance (PM) program, Production Optimization Program (POP) and
the Operations Routine Instrumentation Surveillance Program (0RIS).
In addition to these, the Supplemental Equipment Reliability Program
(SERP) trends equipment performance and provides monthly reports
for management review.
The combination of these programs in the
CEP provides not only a system which verifies and assures equipment
operability but also trends and reviews equipment performance to
detect potential problems.
The overall affect is a well run program
which provides timely information on plant equipment.
One Technical
Specification required surveillance was late this period but this
is considered an isolated instance.
The licensee's review detected
and corrected the cencition.
The licensee's reaction to failed surveillances is conservative.
As an example, the licensee developed a set of acceptance criteria
for the containment personnel access hatch. When the access hatch
failed the pressurization test, the licensee tagged the hatch to
restrict use.
A special PORC meeting was called to discuss the
surveillance results, operability of the batch and required correc-
tive action.
The resultant corrective mai m eaance and retest in
accordance with PORC direction was timely.
Surveillances are conducted by various licensee departments includ-
ing Engineering, Operations, Maintenance and Technical Support.
Personnel in all departments are knowledgeable of surveillance re-
quirements and the plant equipment involved.
A review of surveil-
lance activities during Generic Letter 83-28 Followup Inspection
(86-07) identified well written, comprehensive procedures and a well
informed Quality Control oversight function.
-
.
_
.
.
21
One LER was issued as a result of an inquiry into a surveillance
testing procedure.
During a routine review of the Control Room
Breathing Air Surveillance procedure, which only checked equipment
operability, an observant operator recommended monitoring the re-
quired air flow.
When test results revealed a discrepancy between
this air flow and refueling interval data, the licensee declared
the system inoperable ar.d began a plant shutdown.
An Engineering
review identified the installed check valves as the source of an
excessive pressure drop.
Repiscement of the check valves terminated
the plant shutdown.
This timely effective resolution of a self-
identified problem is indicative of the licensee's conservative
approach to problem resolution.
One minor violation identified during this assessment period was
that some surveillance readings were marginally outside of the ac-
ceptance criteria and some completion dates for portions of sur-
veillances were not recorded.
Although the cause of the out of
tolerance readings was the result of an indication problem with the
instrument, more attention to detail in the review of completed
surveillances would have found the problem.
In summary, with the exception of the relatively minor problems
discussed above, the surveillance program was particularly well run.
Surveillances were generally accomplished with no adverse impact
on the plant such as trips, inadvertent ESF actuations, or equipment
rendered inoperable.
Personnel involved in surveillances exhibited
good coordination with operations and knowledge of equipment /proce-
dures.
The surveillance program was effective in demonstrating
equipment operability.
2.
Conclusion
Category 1.
3.
Recommendations
None.
.
.
22
E.
Emergency Preparedness (100 hours0.00116 days <br />0.0278 hours <br />1.653439e-4 weeks <br />3.805e-5 months <br />, 3%)
1.
Analysis
1
During the previous assessment period the licensee was rated Cate-
gory 1.
During this assessment period, one routine announced in-
spection was conducted during the licensee's partial scale emergency
exercise on September 23, 1986.
Prior to the exercise, discussions with the Emergency Preparedness
Coordinator, Corporate management representation, and Exercise Con-
{
trollers indicated a high level of upper level management involve-
I
ment in controlling and assuring quality in emergency preparedness.
Two areas requiring licensee attention were identified by the NRC
during the Emergency Exercise.
The first, which was identified
by the licensee, was the coordination and flow of information be-
tween the Control Room, Technical Support Center and Emergency
Operating Facility.
The second was the implementation of an iodine
i
source term prediction capability, a previously identified defi-
ciency.
The licensee has addressed each of these areas but they
have not been evaluated by the NRC during an exercise.
These prob-
lems do not impact on the licensee's ability to protect the health
and safety of the public.
l
l
Emergency positions are identified, and authorities and responsi-
i
bilities are well defined.
Vacant key positions in the emergency
l
organization are filled on a priority bases.
The training and
qualification program makes a positive contribution, commensurate
with procedures and staffing to understanding of work and adherence
to procedures with few personnel errors.
The licensee's audits of the emergency preparedness program were
found to be complete, timely, and thorough.
The licensee's Emer-
gency Plan (EP) and Emergency Plan Implementing Procedures (EPIPs)
are well stated, controlled, and explicit.
Changes to the EP and
EPIPs receive timely, thorough, and technically sound reviews.
The
Plant Operations Review Committee also maintains direct involvement
in program changes and approves revisions to the EP and EPIPs.
Procedures and policies are closely followed.
Corrective action
is generally effective.
The licensee's responses to previously identified items demonstrates
a clear understanding of issues raised.
The resolution of issues
routinely exhibit a conservative approach when a potential for
safety significance exists.
Responses from the licensee concerning
resolution of open items and NRC issues are technically sound,
thorough, and timely in almost all cases.
In summary, the licensee has implemented a strong, effective emer-
gency response program.
The two deficiencies noted last year will
be reviewed during the upcoming exercise.
.
.
23
2.
Conclusion
Category 1.
3.
Board Recommendations
None.
.
.
24
F.
Security and Safeguards (149 hours0.00172 days <br />0.0414 hours <br />2.463624e-4 weeks <br />5.66945e-5 months <br />, 4%)
- 1.
Analysis
During the last assessment period, this area was rated a Category
1 based on a quality program and prompt, thorough corrective actions.
During this assessment period, there was one specialist inspection
of this area in addition to routine resident inspector coverage.
During this assessment period, the licensee's overall performance
in the area of security remained essentially consistent with the
i
previous assessment period.
Corporate management involvement in
the program remained evident by the on-site presence of the Director
of Security.
The incumbent is responsible for licensee oversight
of program implementation, program implementing procedures, security
force training and, through a proprietary site supervisor and a
contractor supervisor, for the contract security force performance
and routine, day-to-day operations.
This oversight provides the
licensee with necessary and current knowledge regarding overall
program performance and demonstrates the licensee's intention to
maintain cognizance of program implementation.
Program implementing procedures and instructions are updated, when
required, to provide the security force with current, clear and
concise directions.
Primary procedures and instructions are re-
viewed and approved by the Plant Operating Review Committee in an
effort to preclude any adverse impacts on plant safety.
Feedback
from routine program implementation is promptly integrated into
procedures, instructions and the training program.
This is indi-
cative of the licensee's desire to implement an effective security
program without compromising safe plant operations.
The training program is administered by two, full-time, experienced
instructors.
Lessons plans have been developed, are current, and
reflect the commitments in the NRC-approved program plans.
Training
facilities are adequate and instructional aids are utilized.
All
security related facilities, e.g., guard house, alarm stations, and
office areas, are well maintained, orderly and clean.
Members of
the security force were found to be generally knowledgeable of their
duties and responsibilities when interviewed by NRC personnel.
The security program is well supported by other plant functional
groups and personnel, and frequent and effective communications
among security and the other plant groups are evident by the lack
of interface problems during this assessment period.
This program
support is also reflected by the high mcrale of the security force
and the dedicated and professional attitude they exhibit in carrying
out their duties.
. . _
_
.
.
25
The turnover rate in the security force remains low and staffing
appears to be adequate, as indicated by the limited use of overtime.
All aspects of the program are maintained reasonably current.
Authority and responsibilities for all members of the security group
are clearly defined and well disseminated.
The licensee submitted two security event reports pursuant to 10 CFR 73.71(c) during the assessment period.
Each report identified
security computer malfunctions.
The licensee took appropriate com-
pensatory action for each event and in each case, the security re-
ports were clear, concise and adequate for NRC analysis.
Because
of the age of the security computer and related equipment, the lic-
ensee is experiencing more frequent malfunctions that have neces-
sitated increased maintenance.
While reither the maintenance nor
the compensatory measures appear to have become burdensome, the
licensee should closely monitor the situation to avoid program de-
gradation in the future.
One concern about meeting NRC requirements occurred during the as-
sessment period from three separate incidents in which security
force members failed to identify encroachment into a plant isolation
zone.
While individually these incidents were not significant,
collectively, they may be indicative of inattention to detail on
the part of security and plant personnel about maintaining clear
isolation zones.
This required management attention.
The licensee
initiated prompt and effective corrective action.
No revisions to the licensee's security program plans were submitted
to the NRC under 10 CFR 50.54(p) or 10 CFR 50.90 during this assess-
ment period.
However, the licensee failed to respond to the Mis-
cellaneous Amendments to 10 CFR 73.55, codified by NRC on August
4, 1986, and requiring that by December 2, 1986, licensees transmit
to the NRC changes to safeguards plans describing how the miscel-
laneous amendments would be met.
The licensee stated that this was
an oversight and that the required response would be submitted as
soon as possible. While this is considered to be an isolated case,
it may indicate that the licensing group does not maintain full
awareness of Safeguards licensing issues and, therefore, management
attention is warranted.
In summary, the licensee has sustained its previous performance
level in the area of security during this assessment period.
Two
minor issues (isolation zone and miscellaneous amendments) were
identified that should receive further management attention.
There
is evidence that the licensee's efforts to maintain a high quality
security program are continuing.
I
.
.
.
26
2.
Conclusion
Category 1.
3.
Board Recommendation
None.
.__ . . _ _ . , .-
_ _ . _ _ _
. _ _ _ _
_ - . _ . - _ , _ . _ _ _ _ _ . _ _ _ _ . _ _ .
__ _ _ _ _ _
-__
.
.
27
G.
Assurance of Quality (407 hours0.00471 days <br />0.113 hours <br />6.729497e-4 weeks <br />1.548635e-4 months <br />, 12%)
1.
Analysis
Management involvement and control in assuring quality is being
considered as a separate functional area in addition to being one
of the evaluation criteria in the other functional areas.
The
various aspects of quality assurance (QA) program requirements have
been discussed as an integral part of each functional area and the
respective inspection hours for quality assurance activities are
included in each one. The hours listed above reflect specific in-
spections of the QA program.
Thfs discussion is a synopsis of the
assessments relating to the assurance of quality for activities in
quality assurance and other functional areas.
The assurance of quality is the stated responsibility of each
employee of Maine Yankee.
All personnel are encouraged to perform
'
their work activities in a quality fashion as evidenced by the low
number of personnel error related events.
Pride in a job well
done is reflected throughout plant personnel.
Employees are also
encouraged to report any indication of differences between expected
plant parameters and observed operating conditions that may suggest
a potential problem.
Plant resources are directed at understanding
these differences.
First line supervisors frequently review in-
progress work.
The overall effect is quality job performance at
all levels within the licensee organization.
Plant Management encourages feedback on methods to improve existing
practices. Management reviews operational problems and deficiencies
during the Morning Managers Meetings and develops lessons learned.
Followup corrective action is implemented as a result of these re-
views.
The plant uses several methods to identify, track and close-
out these issues including matrix tracking of probable causes and
individual action item assignments.
Corporate management support
for quality is evident through their participation in the details
of daily operations and their support of corrective action followup.
The QA/QC organization plays an active role in the assurance of
quality.
In addition to normal QA/QC reviews, inspections, and
monitoring activities, a structured independent inspection program
has been implemented.
These inspections are scoped, planned, and
scheduled for a more thorough verification.
To increase the effec-
tiveness of these inspections, the inspector / auditor is authorized
to modify and increase the scope of the planned inspection.
This
results in meaningful inspection findings which receive management
closecut support.
The technical knowledge level of QA/QC personnel
was found to be high as evidenced by NRC first hand observations.
o
.
28
QA/QC personnel possess experience from other departments including
Operations and Engineering.
Changes in the QA/QC organization have
resulted in an effective utilization of knowledgeable resources.
The Plant Operations Review Committee (PORC) is involved in the re-
view of operational data, Engineering Design Change Requests, and
other pertinent information. Special PORC meetings are frequently
utilized to review timely data and operational problems.
meetings are characterized by an open and free exchange of informa-
tion and questions.
Through their reviews, PORC plays a key role
in the assurance of quality.
Every two weeks the QA/QC managers and the plant management meet
to review QA/QC activities.
All deficiencies, corrective actions
and responses are reviewed and trended.
Additionally, Plant Manage-
ment requests QA/QC involvement in observed problem areas.
As a
result, the QA/QC organization is involved in routine plant activi-
ties, not as strictly compliance, but to determine better methods
and controls for areas reviewed.
Management effectively utilizes
QA/QC to improve performance, not just to identify failures to meet
commitments.
One violation was identified for a lack of administrative controls
applied to the review of concrete block walls.
Because of this lack
of controls, the inspections of block walls conducted in 1980 failed
to identify all block walls covered by Bulletin 80-11.
Further
attention to one-time plant walkdowns appears to be warranted.
In summary, there is evidence of assurance of quality at all levels
in the conduct of work activities at Maine Yankee.
Management
effectively uses various mechanisms including QA/QC in initiatives
to improve overall performance.
2.
Conclusion
Category 2, Improving Trend
3.
Board Recommendation
None.
.. -
.
.
.
.
.
29
1
H.
Licensing Activities
1.
Analysis
.
During the last assessment period this area was rated as Category
?
2. Strengths included management's support and participation in
licensing matters and a weakness was identified in that the licen-
see's responsiveness varied widely on different issues.
During the present rating period, the licensee's management demon-
strated active participation in licensing activities and kept
abreast of all current and anticipated actions.
During the Seismic
Design Review, there was consistent evidence of excellent prior
planning and assignment of priorities.
In general, submittals re-
flected good quality and proper management control to assure quality.
Throughout this assessment period the licensee has dedicated re-
sources to address open licensing issues.
As a result, a signifi-
cant reduction in the backlog of open issue has been realized.
The licensee's management and its staff demonstrated technical
understanding of issues involving licensing actions.
For the
majority of licensing actions, the licensee's submittals were tech-
nically sound, thorough, and well referenced.
They generally ex-
hibited conservatism when considering safety significance.
When information became available that indicated some non-conserva-
tive axial power shapes were possible under the present reload
analysis, the licensee was quick to adopt administrative controls
and brief the staff on the impact on the Loss of Coolant Analysis
'
(LOCA).
As a result, the issue was efficiently resolved.
The lic-
ensee's reload analysis was handled by Yankee Atomic Electric Com-
pany (YAEC) and was of high quality. YAEC personnel were utilized
for a variety of engineering and analysis functions.
They were
available as needed for other special engineering disciplines, such
as, Fire Protection and Seismic Design. The combination of the the
licensee's and YAEC's staff demonstrated their capacity to produce
quality engineering products.
The licensee's timeliness and responsiveness continued to vary
widely on different issues.
For example, the submittal for Tech-
nical Specification change for limiting overtime was listed in the
last SALP report as being significantly delayed by the licensee.
This issue remained open throughout this SALP period despite per-
sistent efforts by the NRC to close the issue.
Resolution of De-
mineralized Water Storage Tank (DWST) level alarm and Inadequate
Core Cooling Instrumentation (ICCI) were similarly difficult to
achieve due primarily to timeliness and responsiveness problems with
>
the licensee.
There were other examples of good responsiveness and
timeliness to resolve questions on licensing submittals, such as,
1
Large Break LOCA and Spent Fuel Pool Reanalysis.
Although the
4
-n-
-
-,
-,,
- - ,
. -
,
.
30
licensee's responsiveness and timeliness has improved during the
latter part of this assessment period, the licensee needs to
review these issues to ensure difficulties that led to stale-
mates as described above are completely resolved.
As mentioned above, the licensee's response to the ongoing Seismic
Design Review was excellent.
This included not only the areas of
making information available to consultants and reviewers and as-
sisting with inspections, but also the licensee's willingness to
make hardware changes to improve the plant. The licensee's initi-
atives and efforts in this area were beyond regulatory r:q>iraments.
In summary, the licensing functions for Maine Yankee are carried
out in an effective manner.
Better coordination and direction of
licensing activities to provide better responses should be pursued.
In general, the licensee's performance in the latter part of the
period exhibited a willingness to be responsive and improve perform-
ance.
2.
Conclusion
Category 2, Improving Trend.
3.
Board Recommendation
None.
.
_
_
._ _ _ .
.
.
31
I.
Training and Qualification Effectiveness
1.
Analysis
During this assessment period, Training and Qualification Effective-
ness is being considered as a separate functional area for the first
time.
The various aspects of this functional area have been con-
sidered as an integral part of other functional areas and the re-
spective inspection hours have been included in those sections.
Licensed Operator Training Program continues to receive full support
of management.
The two license operator exams this period resulted
in a 100 percent pass rate with nine Senior Reactor Operator lic-
enses, three Reactor Operator licenses and one Instructor Certifi-
cation.
License training is available to the Nuclear Shift Engi-
neers (STA) and one third of the engineers currently fulfilling the
Shift Engineer Function hold SR0 licenses,
l
The licensee sets high initial qualification standards by requiring
all newly hired Auxiliary Operator candidates possess a Bachelor
Degree in Engineering or Science. This policy was effectively im-
plemented this SALP period. A Training Review Board is utilized
to review potential license candidates and review and track a can-
didate's progress in the license training program.
The Training
Review Coard provides prompt direction to the training program.
The site specific simulator was effectively utilized for license
candidates training, requalification training and verification of
the new Emergency Operating Procedures which were implemented this
assessment period.
Emergency Plan drills are run in real time on
the simulator providing realism not formerly achievable.
New or
revised procedures are practiced on the simulator prior to imple-
mentation, such as, late in life power reductions and turbine valve
testing utilizing the steam dump system.
Maine Yankee is presently
installing a simulator for the remote shutdown panel in order to
provide specialized training on its use.
As an indication of the
licensee's commitment to training, changes to plant equipment are
i
usually reflected in tne site simulator within six months of imple-
l
mentation.
!
The licensee's Specialty Training provides training for Maintenance,
Chemistry, Radiological Controls Technicians, General Employee
Training and Technical Training.
The training program for techni-
'
cians generally involves classroom lectures.
Future plans call for
a combination of classroom instruction, in plant evaluations and
l
exams.
Throughout this assessment period, technicians have been
observed to be knowledgeable and capable of required job skills.
l
The lack of plant trips or LER's attributed to personnel errors
'
by plant technicians is a significant decrease from the last assess-
ment period which included five (5) maintenance personnel errors.
i
,
_
- - - -
- - - - - --
-
-
- _ -
.-
0-
.
32
Additional positions in the maintenance department have been author-
ized to assist in the observation of work practices and qualifica-
tion of personnel.
The licensee continues to pursue the training program accreditation
through the Institute of Nuclear Power Operations (INP0).
All ten
training programs have completed the Self Evaluation Review process
by the licensee. An INP0 team visit has reviewed the Senior Reactor
Operator, Reactor Operator, Auxiliary Operator and Radiation Ccntrol
Technician training programs and accreditation is expected soon.
Other programs are scheduled for INP0 team evaluation later this
year. The pace of the licensee's efforts in this area have been
slow; however, the licensee continues to implement all aspects of
the training program.
Through the use of the Human Performance Evaluation System (HPES),
the licensee conducts reviews of plant events and potential events.
Lessons learned from these reviews are returned to the Training
Department for incorporation into the Training Program.
A review
of plant events revealed no training deficiencies.
However, two
events required further evaluation because both resulted from
operation of the wrong control switch.
In each case, similar
switches providing the same function are located in close proximity
to each other.
Thus, these events appear to be more closely related
to problems with layout (human factors considerations) rather than
training.
The licensee is evaluating corrective action.
In summary, personnel exhibited good job knowledge with few per-
formance problems.
Licensee standards and success in qualifying
operations personnel was particularly noteworthy; good use was made
of the simulator.
Use of a remote shutdown panel simulator is a
good initiative.
2.
Conclusion
Category 1.
j
3.
Board Recommendation
None.
.
1
!
i
i
s
!
. - ~ . - - . _ - _
- - - , . . . - - . . . - , - _ . . _ _ . _ - _ - , _ - .
-
- - - - _ . , . - ,
.
~ .
- . - . - - -
. - ~ - -
-
.
-
33
V.
Supporting Data and Summaries
A.
Investigations and Allegations Revier
There were four allegations reviewed curing this SALP period.
The first
two involved contractors working in a espirator area without respirators.
The third involved the manner in which eiling tiles were disposed from
the radiological portion of the plant.
The fourth was involved with the
qualification of the computer section head.
All allegations were closed.
No significant health or safety were identified.
B.
Escalated Enforcement Actions
1.
Civil Penalties.
None
2.
Orders.
None
C.
Licensee Conferences Held During Appraisal Period
On February 20, 1986, Region I Management met with Maine Yankee manage-
ment to discuss SALP Report 85-99.
D.
Confirmation of Action Letters
None
E.
Rgview of Licensee Event Reports (LER's)
1.
fabular Listing
Type of Event
a.
Personnel Errors
1
b.
Design / Manufacturing /Const/ Installation
4
c.
External Cause
-
d.
Defective Procedure
-
e.
Component Failure
5
x.
Other
-
Total
10
2.
Causal Analysis
The following sets of common mode events were identified:
a.
LER's 85-18, 85-19, 86-02, 86-03 and 86-05 are events due to
component failures.
Two LER's (85-18 and 86-02) were due to
controller malfunctions in the feedwater system.
__.
- _ - - -
_
. .
. _ - .
_
-_
___
_
.
.
.
34
b.
LER's 86-06, 86-07 and 86-08 involved design or installation
deficiency.
Two of these resulted in plant trips (LER 86-06
and 86-07).
F.
Licensing Activities
1.
NRR/ Licensee Meetings
May 7-8, 1986
First Peer Review Group Meeting concerning
Seismic Design Margins Program
July 21-25,1986
Seismic Design Margins Program
August 25, 1986
Inadequate Core Cooling Instrumentation
September 29,1986
Large Break LOCA Analysis Power Shape
September 30, 1986
Second Peer Review Group Meeting concerning
Seismic Design Margins Program
October 22, 1986
Large Break LOCA Analysis Power Shape
November 18-19, 1986
Third Peer Review Group Meeting concerning
Seismic Design Margins Program
December 16, 1986
Large Break LOCA Analysis Power Shape
December 19-20, 1986
Spent Fuel Pool Masonry Wall Failure Con-
sequence Analysis
2.
Visits to Licensee or Licensee Contractor Facilities
February 18, 1986
Management Meeting at Maine Yankee
April 29, 1986
Participate in Seismic Qualification of
Equipment meeting in San Francisco, CA.
May 7, 1986
Seismic Design Margins Program meeting in
San Francisco, CA.
June 10, 1986
Meeting in Framingham, MA concerning Seis-
mic Design Margins Program
<
June 13-14, 1986
Maine Yankee Plant Inspection
July 21-26,1986
Assist in Seismic Design Margins Review
at Maine Yankee
.
.
35
August 1, 1986
Participate in Seismic Design Margins Pro-
gram Peer Review Group Meeting in San
Francisco, CA.
August 4-6, 1986
Maine Yankee Plant Inspection
November 16-19, 1986
Peer Review Meeting at Maine Yankee
December 18-19, 1986
Participate in Spent Fuel Pool Masonry Wall
Failure Consequence Analysis in Framingham,
MA.
3.
Commission Briefings
None
4.
Schedular Extensions Granted
None
5.
Reliefs Granted
None
6.
Exemptions Granted
None
7.
License Amendments Issued / Denied
December 31, 1986
License Amendment 86 Technical Specifications
on RETS
March 4, 1986
License Amendment 87 Technical Specifications
on Monthly Operability of Turbine Driven
Auxiliary Feedwater Pump
March 17, 1986
License Amendment 88 Technical Specifications
on Auxiliary Turbine Driven Feedwater Pump to
be Operable During Operation
May 27, 1986
License Amendment 89 Technical Specifications
which add Manual Containment Isolation Valves
and Blowdown and Body Vent Valves on Instrument
Lines to List of Manual Combined Intermediate
Valves that may be positioned under Administra-
tive Controls
September 11, 1986
Technical Specifications concerning Introduction
of Peaking Factor Limit, Report - Denied
. _ - .
. - - - - . .
-_ _- _ _ -- -_ -
. . . .
. - - . .
- . _ - . _ . _ . .
.
.
36
.
October 27, 1986
License Amendment 90 Technical Specifications-
which Incorporate Requirements for Iodine Spik-
ing into Annual Report
December 11, 1986
License Amendment 91 Miscellaneous changes to
Technical Specifications for Clarification
January 30. 1986
License Amendment 92 Technical Specifications
for Higher Fuel Enrichment
8.
Emergency Technical Specifications Issued
None
9.
Orders Issued
None
10.
Licensing Actions
Open at beginning of period - 43
Number added during period - 28
Number closed during period - 43
Number open at end of period - 28
..
.
TABLE 1
INSPECTION ACTIVITIES
MAINE YANKEE NUCLEAR POWER STATION
REPORT
HOURS
' AREAS INSPECTED
85-31
58
Radiological Protectior, Activities
85-32
139
Routine Resident Inspection *
85-33
27
Nonradiological Chemistry
85-34
74
PAT Followup
85-35
30
Radiation Protection
85-36
94
Routine Resident Inspection
05-37
N/A
Operator Licensing Exams
-86-01
293
Routine Resident Inspection
86-02
106
Block Wall Bulletin Followup
86-03
355
Routine Resident Inspection
86-04
37
Safeguards
86-05
307
Routine Resident Inspection
86-06
26
Transportation
86-07
135
86-08
286
Routine Resident Inspection
86-09
34
Radiation Protection
86-10
282
Routine Resident Inspection
86-11
32
Radiation Protection / Post Accident Sampling System
86-12
30
Fire Protection
86-13
235
Routine Resident Inspection
86-14
100
T1-1
o
.
REPORT
HOURS
AREAS INSPECTED
86-15
239
Routine Resident Inspection
86-16
N/A
Operator Examinations
86-17
32
Safety Safeguards Interface
86-18
187
Routine Resident Inspection
86-19
115
Radiation Protection
86-20
108
Routine Resident Inspection
87-01
116
Quality Assurance Implementation
l
- Routine Resident Inspection - includes operational activities (logs, records,
plant status); plant tours; physical security; housekeeping / fire protection; sur-
veillance activities; maintenance activities; periodic and special reports; event
"
follow-up; and, operational safety.
l
2
)
T1-2
,
- -
,
--
. .
. - .
.-.--
. - - . . . - . .
. _ _ . -
- _ _ _ _ - . - - . . -
_ _ - - - - .
.
.
.
TABLE 2
INSPECTION HOURS SUMMARY (11/1/85 - 1/31/87)
MAINE YANKEE NUCLEAR POWER STATION
HOURS
HOURS
ANNUALIZED
Percent
1.
Plant Operations
1655
1324
47
1
2.
Radiological Controls
382
305
11
3.
Maintenance
447
358
13
4.
Surveillance
337
270
10
5.
Fire Protection and Housekeeping
N/A
--
--
6.
100
80
3
7.
Security and Safeguards
149
119
4
8.
Outages
N/A
N/A
--
9.
Assurance of Quality
407
325
12
10.
Licensing Activities
N/A
N/A
--
11.
Training and Qualification
Effectiveness
N/A
N/A
--
Total
3477
2782
100
- Allocations of inspection hours vs. Functional Areas are approximations. based upon
inspection report data.
!
1
T2-1
-
--
o
.
t
!
TABLE 3
ENFORCEMENT ACTIVITY
MAINE YANKEE NUCLEAR POWER STATION
A.
Number and severity Level of Violations
Severity Level
0
0
0
'
4
7
TOTAL
II-
B.
Violations vs. Functional Area By Severity Levels
Severity Levels
FUNCTIONAL AREAS
I
II
III
IV
V
1.
Plant Operations
1
2.
Radiological Controls
1
3.
Maintenance
2
4.
Surveillance
1
5.
Fire Protection
6.
7.
Security and Safeguards
1
8.
Outages
9.
Assurance of Quality
1
3
10.
Licensing Activities
11.
Training and Qualification
1
Totals
4
7
T3-1
m
o
Inspection
Severity Functional
Brief
Number
Requirement
Levels
Area
Description
85-31
IV
Training
Chemistry Annual Retraining
Appendix A
not completed
ANSI N18.1
85-34Property "ANSI code" (as page type) with input value "ANSI N18.1</br></br>85-34" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process.
V
Maintenance
Lack of a Control Program
Appendix B
for Test Equipment
V
Anchor bolt installation
Section 4.2
miscalculation
V
Unauthorized Drawings in
Control Room
V
Lack of Shelf Life Program
for Chemicals
86-01
V
Operations
Operations of Valve by an
Unauthorized Person
86-02
IV
Inadequate Masonry Wall
Appendix B
Survey Procedures
86-06
10 CFR
IV
Radiological
Failure to list Radioactive
20.311(b)
Controls
Nuclides in Shipment
86-07
V
Maintenance
Lack of Calibration Control
Appendix B
Program for Dial Indicator
86-15
Security Plan
IV
Security and
Violations of Isolation Zone
Safeguards
87-01
V
Surveillance
Marginal Acceptance Values
Appendix B
and completion dates,
i
T3-2
_ _ _ _ _ _
F
l
0
4
l
l
l
TABLE 4
TABULAR LISTING OF LERs BY FUNCTIONAL AREA
MAINE YANKEE NUCLEAR POWER STATION
AREA
Cause Code
Total
A
g
[
D
{
X
1.
Plant Operations
1
1
2
2.
Radiological Controls
3.
Maintenance
1
5
6
4.
Surveillance
5.
Fire Protection
6.
7.
Security and Safeguards
8.
Outages
,
9.
Assurance of Quality
2
2
10.
Licensing Activities
11.
Training and Qualification
Effectiveness
Total
1
4
5
10
Cause Codes *(Assigned During NRC Review)
A.
Personnel Error
B.
Design / Man./Const./ Install
C.
External Cause
D.
Defective Procedures
E.
Component Failure
X.
Other
LERs reviewed: 85-18 through 85-19
86-01 through 86-08
T4-1
.
__
___
_
o
!
a
TABLE 5
LER SYNOPSIS (85-18 to 86-08)
LER NO.
SUMMARY DESCRIPTION
CAUSE
85-18
Turbine Driven Feed Pump Recirculation Valve Controller Failure
E
85-19
Turbine Control System Failure
E
86-01
Manual Reactor Trip on Condenser Differential Pressure
A
86-02
Controller Malfunction Caused a Feedwater Flow Transient and
E
Subsequent Plant Trip on High Steam Generator Level
86-03
Plant Trip on Low Steam Generator Level Due to Excess Flow Check
E
Valve Closure
86-04
Emergency Feedwater Pump Inoperable Oue to a Faulty Circuit
B
Breaker
86-05
Plant Trip on Low Steam Generator Level due to Static Inverter
E
Failure
86-06
Manual Reactor Trip Af ter Ground Connection Failure on Generator
B
Isophase Bus Duct
86-07
Plant Trip on Turbine Driven Feed Pump Low Control Oil Pressure
B
86-08
Inoperable Control Room Breathing Air Trains
B
.
i
(
,
T5-1
- -
-
-
a
I
O
TABLE 6
Assessment
l
l
l
l
l Fire l
l
l
l
l
l
l
Period
Uh)s RadCon Maint Surv Protect
Sec Outage Lic Trna QA
9/1/80 - 6/30/81
32
2
2
1
1
1
3
1
2
2
1
8/1/81 - 7/31/82
3
2
2
2
1
2
2
2
3
--
--
7/1/82 - 6/30/83
3
2
2
2
1
2
2
1
2
2
7/1/83 - 6/30/84
3
2
2
2
2
1
1
1
2
7/1/84 - 10/31/85
l2l
2
l
2
l
1l
1
l
1l1l
2
l2l
l
l
?
o
.
T6-1