ML20209G230

From kanterella
Jump to navigation Jump to search
Insp Repts 50-327/87-02 & 50-328/87-02 on 870106-0205. Violations Noted:Failure to Adequately Control Field Changes & Failure to Establish,Maintain & Implement safety-related Procedures
ML20209G230
Person / Time
Site: Sequoyah  Tennessee Valley Authority icon.png
Issue date: 04/08/1987
From: Harmon P, Jenison K, David Loveless, Mccoy F, Poertner W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20209G174 List:
References
50-327-87-02, 50-327-87-2, 50-328-87-02, 50-328-87-2, NUDOCS 8704300504
Download: ML20209G230 (21)


See also: IR 05000327/1987002

Text

r;

F-

.

UNITED ShATES

A F e ro,S

NUCLEAR REGULATORV COMMISSION

'

o

"

f"

REGION ll

"J

,

,

}g

j

101 MARIETTA STREET, N.W.

  • I

'*

ATLANTA, GEORGn A 30323

....+

y=

Report Nos.:

50-327/87-02, 50-328/87-02

1.-

L

Licensee: Tennessee Valley' Authority

6N38 A Lookout Place

1101 Market Street

Chattanooga, TN 37402-2801

Docket Nos.:

50-327 and 50-328

License Nos.: OPR-77 and DPR-79

Facility Name:

Sequoyah Units 1 and 2

Inspection Conducted:

January 6, 1987 thru February 5, 1987

Inspectors

M

C

Y

/

[

M. M.

iso ~n'- SeM5F~Res ' ~

In}pect r

'Date' Signed

  • 44

$

P. E.

W Re>idlii^

ect

D6te Signed

M=LJ2d

V8/97

'

D. P. Loveless, Resident)Mipec,t r

D' ate Signed

8

7

M

_

x

W. K. Poer

t n ~

forf/

Date Sig ed

,

Approved by:

_W/

//

CN

F. R."NcCoy,' ChieW5est40n 1

D)te# grMr

~

Division of TVA Projects

,

4

SUMMARY'

.

,

3

i

, Scope:

This routine announced inspection involved inspection onsite by the

= resident inspectors in - the areas of:

operational safety verification

(including operations performance, system lineups, radiation protection,

safeguards and . housekeeping inspections); maintenance observations; review of

previous inspection findings; followup of events; review of licensee identified

items; and review of inspector followup items.

A$

Results: Two violations were identified.

$

,

327,328/87-02-01,

failure to adequately control

field changes,

paragraph 7

'

327,328/87-02-02,

failure to establish, maintain and implement safety-

related procedures, paragraphs 9 and 13

hh

$DOOK

$7

G

.

r

-

-

.

4

2

^i

Four unresolved items were identified.

327,328/87-02-03,

modification to control room ceiling, paragraph 5

327,328/87-02-04,

access control, paragraph 5-

327,328/87-02-05,

adherence to Health Physics requirements, paragraph 5

327,328/87-02-07,

two spills of reactor coolant, paragraph 9

No deviations were identified.

.

%

-i ,

t

4'

i

!

,.

. ., -

, . - . _ -

.

. . . . . .

. . , _ _ _ , . . ~ , , _ _ . - . _ _ _ . _ _ , - ~ , _ - _ , . _ . , . _ _ . , _ . . . . _ _ _ _ . . , _ ,

_

_

--___

__-

.

l-

REPORT DETAILS

1.

Licensee Employees Contacted

  • H. L. Abercrombie, Site Director
  • L. M. Nobles, Acting Plant Manager
  • B. W. Willis, Acting Power Plant Superintendent
  • B. M. Patterson, Maintenance Superintendent
  • R. J. Prince, Radiological Control Superintendent
  • M. R. Harding, Licensing Group Manager
  • L. E. Martin,' Site Quality _ Manager
  • D. W. Wilson, Project Engineer

R. W. Olson, Modifications Branch Manager

  • J. M. Anthony, Operations Group Supervisor
  • R.'V. Pierce, Mechanical Maintenance Supervisor

M. A. Scarzinski, Electrical Maintenance Supervisor

  • H. D. Elkins, Instrument Maintenance Group Manager

J. T. Crittenden, Public Safety Service Chief

R. W. Fortenberry, Technical Support Supervisor

  • G. B. Kirk, Compliance Supervisor

-D. C. Craven, Quality Assurance Staff Supervisor

  • J. H. Sullivan, Regulatory Engineering Supervisor

J. L, Hamilton, Quality Engineering Manager

D. L. Cowart, Quality Engineering Supervisor

H. R. Rogers, Plant Operations Review Staff

R. C. Burchell, Compliance Engineer

  • R. H. Buchholz, Sequoyah Site Representative

Other licensee employees contacted included technicians, operators, shift

engineers, security force members, engineers and maintenance personnel.

  • Attended exit interview

2.

Exit Interview

The inspection scope and findings were summarized with the Plant Manager

and members of his staff on February 4, 1987.

The two violations

described in this report's summary paragraph were discussed.

No devia-

tions were discussed.

The licensee acknowledged the inspection findings.

The licensee did not identify as proprietary any of the material reviewed

by the inspectors during this inspection.

During the reporting period,

frequent discussions were held with the Site Director, Plant Manager and

other managers concerning inspection findings.

3.

Licensee Action on Previous Inspection Findings (92702)

(Closed) Violation 327,328/84-38-02, Failure to have Adequate Nonconfor-

mance Report Procedure.

The licensee stated in their response to the

violation dated March 15, 1985, that the violation was not caused by the

- - - _______

_ - ____ _ ____ ___

. _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ - _ _

2

lack of procedure.

They suggested instead that the violation resulted

from a lack of management control which did not ensure the timely

reporting of the potential nonconformance.

The licensee committed to instructing all office of engineering employees

I

at Sequoyah and in Knoxville on the timeliness requirements of documenting

and reporting potential nonconforming conditions.

This information was

presented by memorandum to all Sequoyah engineering project employees on

April 9, 1985.

Knoxville employees were informed during informal meetings

with their supervisors as designated in an April 9,1985 memorandum from

John A. Raulston.

Furthermore, the licensee has committed to training all

office of engineering and nuclear power employees on the use of their new

procedures on conditions adverse to quality in response to NRC Order

85-49. This training was completed in October 1985.

This item is closed.

4.

Unresolved Items

Unresolved items (URIs) are matters about which more information is

required to determine whether they are acceptable or may involve viola-

tions or deviations.

Four unresolved items were identified during this

inspection, and are identified in paragraphs 5 and 9 of this report.

(Closed) URI 327,328/86-60-11, Control of Safety-Related Pumps.

This item

concerned failure of the emergency core cooling system (ECCS) pum

meet the flow balance requirements of Technical Specification (TS) ps to

4.5.2.h

during the performance of the surveillance instructions, failure of the

turbine driven auxiliary feedwater (AFW) pump to reach rated speed and

flow, acceptability of AFW pump dischar

errors in the inservice inspection (ISI)ge piping vibratiori, and technical

procedure for RHR testing.

TS 4.5.2.h requires the performance of a flow balance test during shutdown

following completion of modifications to the ECCS subsystem that alter the

subsystem flow characteristics.

As a result of concerns raised in

Westinghouse bulletin NSD-TB-80-11 concerning pump degradation,llanceSequoyah

began performing the ECCS flow balance on n 18 month survei

interval.

The performance of the flow balance test

indicated that at the

end of the 18 month period the flow balance for the centrifugal charging

pumps would be just below the minimum acceptable value.

The licensee has

received a change to the TS to reduce the required value for the sum of

the injection line flow rates (excluding the highest flow rate) from 346

gpm to 316 gpm.

The flow balance is now conducted with the pump mini-flow

valves open where previously they were closed.

However, discussions with

the mechanical test engineers responsible for conducting the surveillance

determined that the TS change to a lower flow requirement should imarove,

the pass rate of this surveillance activity.

The licensee has a'so

initiated a design change request to replace the positive displacement

charging pump with a centrifugal pump.

This will reduce the run times on

the centrifugal charging pumps therefore the pump degradation between flow

balances would be reduced.

Further review of the licensees performances

.

3

of the ECCS flow balances and the status of the design change request to

replace the positive displacement pump will be inspected during routinely

scheduled NRC ASME Section XI testing inspections. This URI is closed.

Concerning the failures of the turbine driven auxiliary feedwater pump to

reach rated speed and flow, the inspector reviewed the Licensee Event

Reports associated with these events for adequacy. The inspector reviewed

the licensee's potential reportable occurrence (PRO) files to determine if

this constituted a recurring problem when running the turbine driven

auxiliary feedwater pumps. These events appeared to be isolated incidents

and not recurring failures with similar root causes. PR0 1-87-56 has been

issued against the AFW System.

The other items addressed in this URI concerning pump performance were

addressed in NRC Inspection Report 86-71 and are considered to be

resolved. URI 327,328/86-60-11 is closed.

(Closed) URI 327,328/86-71-05, Containment Spray System Field Change

,

Request.

This item is addressed as violation (VIO) 327,328/87-02-01 in

paragraph 7d of this report. This URI is closed.

(Closed) URI 327,328/86-71-06 Control Auxiliary Building and Containment

Isolations. This item is addressed as violation (VIO) 327,328/87-02-02.in

paragraph 9a. This URI is closed.

(Closed) URI 327,328/86-71-04 Adequacy of Surveillance Instruction (SI)

400.1, Liquid Effluent Batch Release

A discrepancy was identified between two different methods used to calcu-

late background radiation on effluent releases.

For the particular

release that the inspector observed, the prccedural discrepancy did not

have any safety significance.

SI 400.1 and Technical Instruction 18,

radiation monitoring, are both under review in the licensee's surveillance

instruction review program.

This URI will be evaluated under the overall

appraisal of the licensee's surveillance instruction review program URI

327,328/86-60-10 described in paragraph 7 of this report.

URI 327,328/

86-71-04 is closed.

(Closed) URI 327,328/86-42-02, Vendor Supplied Requirements

This issue was resolved in subsequent environmental qualification inspec-

tions conducted at Sequoyah nuclear plant and is therefore closed.

5.

Operational Safety Verification (71707)

a.

Plant Tours

The inspectors observed control room operations, reviewed applicable

logs, conducted discussions with control room operators, observed

shift turnovers, and confirmed operability of instrumentation.

The

'

.

'4

inspectors verified the operability of selected emergency systems,

and verified compliance with TS limiting conditions for operation

(LCO). The inspectors verified that maintenance work orders had been

submitted as required and that followup activities and prioritization

-of work was accomplished by the licensee.

Tours of the diesel generator, auxiliary, control, and turbine

buildings, and containment were conducted to observe plant equipment

conditions, including potential fire hazards, fluid leaks, and

excessive vibrations and plant housekeeping / cleanliness conditions.

The inspectors walked down accessible portions of the following

safety-related systems on Unit 1 and Unit 2 to verify _ operability and

proper valve alignment:

_

residual heat removal system

component cooling water system

safety related heat tracing

During a tour of the control room the inspectors observed water

dripping into pans hung in the false ceilings and onto the ceiling

itself.

The licensee stated that they were in the process of

installing drip pans and gutters in the false ceilings to catch the

water from the leaking control building roof. This modification was

being performed under work request (WR) 8214608 with a plant opera-

tion review committee (PORC) approved unresolved safety question

determination (USQD) in place. The inspector questioned the use of a

WR to perform a safety related modification and the corrective action

time frame. These issues will be reviewed during the next inspection

period. This item is considered unresolved and will be identified as

URI 327,328/87-02-03.

No violations or deviations were identified.

b.

Safeguards Inspection

In the course of the monthly activities, the inspectors included a

review of the licensee's physical security program. The performance

of various shifts of the security force was observed in the conduct

of daily activities including protected and vital area access

controls; searching of personnel and packages; badge issuance and

retrieval; patrols and compensatory posts; and escorting of visitors.

In addition, the inspectors observed protected area lighting, and

protected and vital areas barrier integrity. The inspectors verified

various interfaces between the security organization and the opera-

tions and maintenance organizations.

Specifically, the inspectors

inspected security during outages and verified protection of safe-

guards information.

'

.

5

During a tour of the Unit 2 west valve room the inspectors-identified

that a security guard did not appear to have direct control over

access to the open valve room which is a vital area.

This issue was

discussed with Regional management and will be identified as URI

327,328/87-02-04 until resolution by . a security specialist is

effected.

No violations or deviations were identified.

c.

Radiation Protection

The inspectors observed Health Physics-(HP) practices and verified

implementation of radiation protection control.

On a regular basis,

radiation work permits (RWPs) were reviewed and specific work activi-

ties were monitored to ensure the activities were being conducted in

accordance with applicable RWPs.

Selected radiation protection

instruments were verified operable and calibration frequencies were

reviewed.

During a routine tour of the auxiliary building, the inspectors

observed a group of workers gathered around one train of the emer-

gency gas treatment system (EGTS) charcoal tray beds.

The system had

been breached, and one worker had his head and part of his shoulders

within the internal boundary of the system.

The worker inside the

EGTS system appeared to be performing a task with a pair of channel-

lock type pliers.

When questioned, another worker stated that an HP

technician had taken a smear of the area in addition to frisking the

area.

The worker further stated that the HP technician had directed

the workers to wait until he had counted the smear before entering

the internals of the EGTS charcoal tray bed area to commence work.

The inspector questioned the worker who was inside the EGTS system

boundary and he stated that he was aware of the instruction given by

the HP technician.

The outside of the EGTS was not marked poten-

tially contaminated, however, it was marked " notify HP prior to

entry."

Survey number D-87-0162 found no detectable transferable

surface contamination.

Because of the low safety significance of

this particular issue, no violation will be issued at this time.

However, adherence, to directions from HP technicians and compliance

with HP practices will be reviewed as URI 327,328/87-02-05.

No violations or deviations were identified.

6.

Monthly Surveillance Observations (61726)

The inspectors observed / reviewed TS required surveillance testing and

verified that testing was performed in accordance with adequate

procedures; that test instrumentation was calibrated; that LCOs were met;

that test results met acceptance criteria requirements and were reviewed

by personnel other than the individual directing the test; that deficien-

cies were identified, as appropriate, and that any deficiencies identified

during the testing were properly reviewed and resolved by management

personnel; and that system restoration was adequate.

For completed tests,

'

.

6

the inspector verified that testing frequencies were met and tests were

performed by qualified individuals.

The inspector reviewed the performance of SI-244, Periodic Functional

Tests of Radiation Effluent Monitoring Instruments, which was intended

to satisfy TS surveillance requirements for the third quarter of 1986.

The licensee documented that this surveillance had been missed in its

September 1986 monthly report.

The inspector reviewed the recalibration

of flow indicator FI-77-230 and level transmitter LT-27-225.

This issue

was reported by the licensee in LER 327,328/86-37.

The licensee is currently in a large scale surveillance instruction (SI)

review.

The inspector reviewed that process and determined that the

licensee is now in the third iteration of this review effort.

Significant

technical issues have been identified by the site quality assurance (QA)

organization, which may have contributed to this iteration process.

The

following issues were evaluated by the inspector during a review of the

licensee s SI review process:

LER 327,328/86-30 Inadequate TS Procedure

LER 327,328/86-34 Failure to Perform Surveillance on Time

LER 327,328/86-37 Failure to Perform Surveillance on Time

LER 327,328/86-40 Inadequate Isolation Valve Leak Test

LER 327,328/86-43 Inadequate Containment Leak Rate Test

LER 327,328/86-44 Inadequate Emergency Core Cooling System Procedure

LER 327,328/86-48 Inadequate Emergency Core Cooling System Procedure

LER 327,328/86-50 Inadequate Surveillance Instruction

URI 327,328/86-71-04 Procedural Discrepancies

The above issues will be included with the issues identified in inspector

followup item IFI 327,328/86-60-10, and are administratively closed.

7.

Monthly Maintenance Observations (62703)

a.

Station maintenance activities of safety-related systems and compo-

nents were observed / reviewed to ascertain that they were conducted in

accordance with approved procedures, regulatory guides, industry

codes and standards, and in conformance with TS.

The following items were considered during this review:

LCOs were

met while components or systems were removed from service; redundant

components were operable; approvals were obtained prior to initiating

the work; activities were accomplished using approved procedures

and were inspected as applicable; procedures used were adequate to

control the activity; troubleshooting activities were controlled and

the repair record accurately reflected what actually took place; func-

tional testing and/or calibrations were performed prior to return-

ing components or systems to service; quality control records were

maintained; activities were accomplished by qualified personnel;

parts and materials used were properly certified; radiological

_

_

_

_

"

.

7

controls were implemented; QC hold points were established where

required and were observed; fire prevention controls were imple-

mented; outside contractor force activities were controlled in

accordance with the approved quality' assurance (QA) program; and

housekeeping was actively pursued.

b.

On January 7, 1986, the inspectors observed workers replacing Raychem

heat shrinkable tubing following the Raychem inspections.

Workers

discussed with the inspector the color coding of the tags that were

affixed during Raychem signoffs.

The work was covered by special

maintenance instruction (SMI)-2-302-1, Walkdown Procedure for 10 CFR 50.49 Splices Located in Unit 2 Containment Penetrations, R1.

The

procedure was PORC approved and appeared to be adequate.

The speci-

fic work observed involved the preparations and determination of

proper Raychem packages on cables 2-PM-1626-IV and 2-PM-1741-IV.

This specific work was authorized under WR B217558 and B217559

respectively.

,

The inspector witnessed a portion of work plan 12195, AFW system

c.

Cavitating Venturi Post Maintenance Test on MDAFW pump 2A-A.

This

post maintenance test (PMT) plan was being performed because the

cavitating venturi associated with MDAFW pump 2A-A had been replaced

by MR A-522793.

The PMT consists of three parts; performed with the

steam generator (SG) pressure less than 100 psig, with SG pressure at

'

approximately 385 psig and finally with SG pressure at 1005 psig.

The inspector witnessed the performance of the first part of the work

,

plan.

No discrepancies were identified.

i

d.

Portions of design change request (DCR) 2259 were reviewed in order

to resolve URI 327,328/86-71-05.

DCR 2259 was written to change the

'

sequencing time of the containment spray (CS) pumps and other loads

when a loss of offsite power is followed by a need to commence con-

tainment spray.

The closure of this particular issue is consid-

ered by the NRC and TVA to be necessary prior to the startup of

either unit.

A discussion was held with department of nuclear

engineering (DNE) and Sequoyah nuclear plant compliance personnel to

resolve whether certain field generated changes to engineering change

notice (ECN) documents were adequately accomplished.

The following

documents were reviewed:

ECN L6715

DCR 2259

Field Change Request (FCR) 4873

Nuclear Engineering Procedure (NEP) 6.1, Variances / Expansions

,

Sequoyah Engineering Procedure (SQEP) AI-11A, FCR Handling

Sequoyah Administrative Instruction (AI)-19, Part IV, Plant

Modifications After Licensing

Work Plan 12227

l

vrv

-w--

---7-N

y..w-.---w

w

--

4y

ry

~=

%s-a.v._m-.m

-,-~4p.

ygy.p

--vywr4

y

y.-

g.mg

6se4.ey-.smp-g

.

8

After a discussion with the licensee, it was determined that:

(1) The original DCR was not reviewed during the review and approval

process for FCR 4873.

Attachment 2, of NEP-6.1, which is used

during the initial ECN review and approval process, was not used

by either the design engineer or the review engineer to consider

whether FCR 4873 affected certain aspects of ECN L6715.

(2) It is not a normal practice for DNE engineers to review the

affected work plan or other issued FCRs prior to approving a

specific FCR.

(3) The reviews of WP 12227 and FCR 4873 conducted under AI-19 and

SQEP-AI-11A incorrectly determined that FCR 4873 was within the

scope of ECN L6715.

FCR 4873 addressed the removal of admin-

istrative control markings (hold clouds) and electrical circuits

within the hold clouds on certain as-constructed electrical

drawings.

These circuits and hold . clouds were addressed by

another ECN.

ECN L6715 did not address the addition or deletion

of the hold clouds on the affected drawings.

Therefore,

FCR 4873 was not within the original scope of ECN L6715, yet it

was reviewed with respect to ECN L6715.

The FCR was not

reviewed with respect to the ECN to which it really applied, and

consequently, an inadequate review was done prior to implement-

ing the FCR.

10 CFR 50 Appendix B, Criterion III, states that design changes,

including field changes, shall be subject to design control measures

commensurate with those applied to the original design.

NEP-6.1,

states that changes to any design documents which deviate from the

approved scope of work will be evaluated against the original work

scope.

As described above, FCR 4873 was not reviewed and approved

subject to design control measures commensurate with those applied to

the original design.

This is a violation VIO 327,328/87-02-01.

Three additional issues were identified during the review.

(1) SQEP-AI-11A Attachment A sections 12 through 14 were not com-

pleted when the inspector reviewed this completed FCR.

(2)

It was not clear what type of technical review the assigned

approving technical supervisor completed prior to approving this

FCR.

It appeared that the supervisory (DNE management) review

was administrative in nature and did not consider the technical

aspects of the FCR.

(3) The drawings reviewed and approved by the plant oaerations

review committee (PORC) were marked up by modificat ons person-

nel and were not the drawings approved by the DNE engineers.

The drawing revision numbers on the SQEP-AI-11A document did not

match the drawing revision numbers on the AI-19 document.

In

i

. _ _- ___

_

_

.

.

_ _ _ _ _ _ _ _

"

.

9

this case the drawing changes were found to be the same.

However, the FCR process did not ensure the documents were the

same.

These issues will be resolved during a review of the licensee's

corrective action for VIO 327,328/87-02-01.

8.

Licensee Event Report (LER) Followup (92700)

The following LERs were reviewed and closed.

The inspector verified that:

reporting requirements had been met; causes had been identified; correc-

tive actions appeared appropriate; generic applicability had been consid-

ered; the LER forms were complete; the licensee had reviewed the event; no

unreviewed safety questions were involved; and no violations of regula-

tions or TS conditions had been identified.

LERs Unit 1

327/84-070 - Failure of Containment Isolation Valves, due to Sediment

Buildup on the Valve Stems.

During the performance of the weekly portion of SI-3, " Daily, Weekly,

and Monthly Logs," the ice condenser glycol system containment

isolation valves failed to stroke to the fully closed position on

demand.

The obstruction was a sediment buildup on the stem of the

valves.

The stems were cleaned and polished and the 0-rings and

diaphragms replaced.

The licensee was unable to determine the source

of the buildup.

There have been no indications of any similar

buildup on these or other valves on the glycol system prior to the

i

event or to date.

l

l

The inspector determined through

a records review and interview

process, that the event had been discussed with maintenance person-

nel.

The LER states that the results of a further investigation will

be supplied in a supplemental report.

To date this report has not

been issued.

The inspector discussed this discrepancy with licensee

personnel and the report will be issued in the near future.

The

publishing of this supplemental report will be tracked as IFI

327,328/87-02-06.

327/84-42 -

Incomplete Radiation Monitor Modification

327/86-52 -

Administrative Control of High Radiation Areas

LERs Unit 2

328/83-129 -

Loop 3 & 4 Main Steam Line Isolation Valves Would Not Close

Due to Excessive Heating During Operation.

The licensee determined that the valve packing had dried out during

operation.

Subsequent cooling during the refueling outage had caused

the packing to harden around the stem.

This prevented the valve from

)

r

-

.

10

closing properly.

The valve stems were lubricated and the valves

tested satisfactorily.

Licensee review of past events showed that

the valves had been tested during the previous outage.

On the basis

of these tests the licensee determined that no further work was

required on the valves.

The valves are now tested and lubricated

every refueling outage regardless of the valve stroke-time.

This

recommendation was implemented in the Sequoyah preventative

maintenance program.

The inspector reviewed documentation available

to ensure that the problem has not occurred since that time.

This

item is closed.

328/86-08 -

Inadvertent Phase A Isolation As a Result of Personnel

Error In Failing to Follow Procedures.

Events described in

this LER contributed to the issuance of Violation 327,328/

87-02-02, described in Paragraph 9.

This item is closed.

328/86-09 -

Inadvertent Control Room Isolation Resulting from Deficient

Workplan.

Events described in this LER contributed to the

issuance of Violation 327,328/87-02-02, described in

paragraph 9.

This item is closed.

328/86-10 -

Inadvertent Phase B Isolation Occurred During Testing.

Events described in this LER contributed to the issuance of

Violation 327,328/87-02-02, described in Paragraph 9.

This

item is closed.

328/86-11 -

Inadvertent Containment Ventilation Isolation From Electro-

magnetic Interference On A Radiation Monitor

9.

Event Followup (93702, 62703)

During the inspection period covered by Inspection Report 327,328/

a.

86-71, three engineered safety features (ESF) initiations occurred

that were identified as URI 327,328/86-71-06.

The three events have

been determined to constitute a violation of TS 6.8.1.

(1) On November 30, 1986, a containment ventilation isolation (CVI)

was initiated when an instrument mechanic (IM) failed to follow

IMI-99, RT-106A.2, Response Time Test for Containment Lower Rad

Monitor 2-RM-90-106A.

The procedure stipulates that the IM is

required to have the operator place the appropriate channel

block switch in the " block" position prior to inserting a test

lead.

The IM inserted the test leads without having the block

switch in the correct position and a CVI resulted.

(2) On December 1,1986, a control room isolation (CRI) occurred

when a deficient workplan (WP) was used to perform a test on CRI

handswitch 2-HS-31A-7A.

The workplan was in error in that the

test procedure in WP 12268 required that the test personnel lift

one wire at the handswitch.

Subsequent review of wiring diagram

45N631-2 showed that additional parallel wire should have been

,

.

11

specified in the procedure.

When the handswitch was placed in

the " actuate" position, a CRI occurred.

Inclusion of the second

wire in the procedure would have prevented this event.

(3) On December 3,1986, a containment phase "B" isolation occurred

when an inadequate procedure was used to perform instrument

maintenance instruction IMI-99, " Reactor Protection System

Response Time Test for Containment Pressure Channel III,

RT-16.7."

The procedure requires that only the train being

tested be placed in " test" prior to tripping the high-high

containment pressure bistables.

The test did not indicate that

the bistables feed both trains of the reactor protection system.

A phase "B" isolation was initiated by the train not in " test"

when the test was initiated.

TS 6.8.1 requires that written procedures be established, implemented

and maintained for surveillance and test activities of safety-related

equipment.

Contrary to this requirement, the licensee failed to

properly implement the procedure in instance 9.a.(1) above, and

failed to adequately establish and maintain procedures in instances

9.a.(2) and 9.a.(3).

These three examples constitute violation VIO

327/328-87-02-02.

b.

On January 6, 1987, the plant was notified by the division of nuclear

engineering (DNE) tnat a problem existed with the trip settings for

certain safety related breakers.

The significant condition report

(SCR) SQNEEB86124 R0, "SQN Auxiliary Power System class 1E Equipment

Ampacity Study," stated that the calculated maximum loading that

could occur during a loss of coolant accident (LOCA) exceeds the

feeder breaker continuous current setpoints for the control and

auxiliary building ventilation boards 1Al-A, 2Al-A and 2B1-B.

These ventilation boards supply safety related loads such as Emer-

gency Gas Treatment System (EGTS), Auxiliary Building Gas Treatment

System (ABGTS) and control room emergency ventilation fans as well as

various room coolers.

At approximately 4:00 p.m. (EST), the plant

determined that there was not an immediate operability problem

because certain (ESF) signals were blocked in the present mode (cold

shutdown

mode 5).

If the plant were at power, the potential for

maximum LOCA loading would cause the boards to be inoperable.

For

example, board 1Al-A could have a continuous loading of up to 444

amps following a LOCA.

The feeder breaker from the 480V shutdown

board to the vent board 1Al-A is set at 392 amps per the setting

sheets and other plant drawings.

Because the maximum expected

loading on these boards is within the capacities of these breakers,

the plant resolution will be to reset the breakers

to a higher

amperage capacity and change the drawings.

The inspector questioned why the licensee had not discovered this

when the vent boards are tested on a 18 month interval in SI-26.1A,

-26.1B, -26.2A and -26.28, " Loss of Offsite Power with Safety

e

12

Injection - D/G 1A-A,1B-B, 2A-A and 2B-B," respectively.

These

tests, however, do not ensure that cyclic loads (e.g. , room coolers

that cycle on temperature) are running.

Therefore, the maximum LOCA

loading was never experienced.

Resolution of this issue is expected

to be part of the design basis verification program.

This item will be reviewed under URI 327,328/86-60-10.

c.

During the inspection period the licensee began a program to inspect

the feedwater lines in response to the feedwater break event at Surry

Power Station.

d.

During the inspection period two separate spills of reactor coolant

system (RCS) fluid from open steam generator (SG) manways occurred.

Unit 1 SGs are presently undergoing heat treatment of the first two

rows of tubes to relieve stresses induced in manufacturing.

This

necessitates draining down the RCS to a level Lelow the SG primary

nozzles to allow robot aided access to the tube sheets.

A non-

watertight cover is placed over each RCS nozzle to prevent tools and

debris from entering the RCS loops.

The RCS is then placed on RHR

recirculation and the primary access manways are opened.

Proper

water level in the RCS is maintained by use of an installed sight-

glass monitored by a television camera and a TV monitor in the

control room.

The first event occurred on January 28, 1987, and was caused by a

partially plugged sightglass.

The operators in the control room

noticed water level above the maximum allowed and began lowering

level by reducing charging pump flow. Water level in the sightglass

did not respond, and the operators continued to decrease charging

flow rate.

The residual heat removal (RHR) pump amperage began to

fluctuate, indicating pump cavitation.

The operators stop

pump and entered abnormal operating instruction (A01)-14, ped the

Loss of

RHR Cooling."

The operators began to raise water level to restore

adequate pump suction.

This caused actual water level in the RCS to

be increased until the SG channel heads began to fill and water

spilled out the manway.

The operators were alerted and stopped the

evolution.

After blowing down the sightglass, level indication was

restored and proper level attained.

The RHR pumps were then started

and RHR cooling restored.

Approximately 500 gallons of RCS water was

spilled.

The second event occurred on February 1,1987.

The RCS and RHR

system were in the same configuration as in the first event.

The

operators were attempting to perform SI-166.3, " Stroke Time Testing

of FCV-63-1," which is the isolation valve for the normal RHR suction

from the refueling water storage tank (RWST).

When the valve was

opened, water from the RWST began to fill the RCS through the RHR

suction line connected to RCS Loop D, and then spilled from the open

SG manways.

The two series valves in the RCS suction line had not

been shut by the operator prior to opening the RWST suction. With

.

13

the RCS open to atmosphere, the elevation head in the RWST was enough

to cause flow back to the RCS.

The operator could not reclose

FCV-63-1 until the open limit was reached (approximately 25 seconds

stroke time).

After the valve was reclosed, water continued to spill

from the manway.

The operators suspected that valve FCV-63-1 had not

been fully shut by the motor operator, and sent an auxiliary operator

to the valve to manually shut it.

The auxiliary operator reported

that the local handwheel was turned approximately 10 turns in the

shut direction before valve travel stopped.

Total handwheel travel

is approximately 450 turns.

The rapid filling of the RCS displaced 6

of the 8 SG nozzle covers.

Total water spilled was estimated at 3000

to 4000 gallons.

Neither event resulted in personnel contamination.

These issues will be tracked as URI 327,328/87-02-07.

10.

Inspector Followup Items (93701)

Inspector followup Items (IFIs) are matters of concern to the inspector

which are documented and tracked in inspection reports to allow further

review and evaluation by the inspector.

The following IFIs have been

reviewed and evaluated by the inspector.

The inspector has either

resolved the concern identified, determined that the licensee has per-

formed adequately in the area, and/or determined that actions taken by

the licensee have resolved the concern.

(Closed) IFI 327,328/86-31-06, Moisture Entrained in Sense Lines Could

Cause Stress Corrosion Cracking in Bellows of Containment Sump Level

System.

(Closed) IFI 328/84-38-05, Procedure to Address Early Implementation of

Emergency Plan on Inadvertent Safety Injection.

(Closed) IFI 327,328/86-28-03, Component Cooling System Inleakage.

Increasing activity levels in the component cooling system (CCS) have been

observed since early 1985.

Efforts to locate the source of the leak were

not successful until the most recent investigation.

The location of the

leak has been identified as the 2B containment spray (CS) pump seal water

heat exchanger, which was found to have a sheared 0 ring at the inboard

seal.

This 0-ring provides the barrier between the CCS in the seal water

heat exchanger and the fluid in the pump casing.

The leak was found by

comparing cobalt 60/58 ratios from each component served by the CCS

system.

The unit 2 RCS was determined as the source of the radioactive

fluid.

The CS seal water heat exchangers were initially discounted as

possible leak points since the CS pumps are lined up to take suction from

the refueling water storage tank (RWST), and not from the RCS.

Local

samples at the Unit 2 Train B CS pump were conclusive.

The CS pump suction has the capability of switching to the ECCS recircu-

lation sump in the post-LOCA scenario.

This sump suction is by way of the

line common to the RHR Pumps.

Isolation from the sump and RHR system is

through a single valve, 2-FCV-72-20.

When this valve is opened (or leaks

by) the CS pump suction is exposed to RHR suction pressure. With the RHR

system on RCS recirculation, the pressure at this point is approximately

_

-

.

14

100 psig.

The leak was intermittent, which complicated the search.

It

was later determined that leakage only occurred when CCS pressure dropped

below 100 psig, such as when major components were placed in service. The

licensee is presently disassembling the other three CS pumps to inspect

'.

their seals.

IFI 86-28-03 is closed.

(Closed) IFI 327,328/85-27-03, Modifications to Che.nical Volume Control

System (CVCS)

(Closed) IFI 327,328/85-27-05, Flow Induced Vibrations on CVCS

(Closed) IFI 327,328/86-15-04, CVCS line Tee

.(Closed) IFI 327,328/86-20-05, Word Processing Errors

(Closed)IFI 327,328/86-42-04, Vendor Manuals

11. Review of Employee Concern Element Reports (TI251574)

Based on a review the following element reports the following general

areas of interest were identified:

a.

Many of the reports did not completely address the concern as

expressed by the individual,

b.

In some reports the scope and depth of the investigation appeared not

to be acceptable,

c.

There appeared to be a disconnection between some of the element

reports and the document files.

d.

Corrective action in some cases appeared not to resolve the concern

and in others the indicated corrective action did not include ancil-

lary issues.

The following employee concern element reports were reviewed during this

inspection period:

OP308.06 SON

OP307.02 SQN

C015101 SQN

OP308.05 SQN

OP301.05 SQN

OP306.01 SQN

MAS-86-001

OP310.02 SQN

C015109 SQN

OP301.11 SON

'

OP301.07 SQN

OP313.07 SQN

OP301.12 SQN

OP307.08 SQN

OP308.01 SQN

OP309.05 SQN

C015102 SQN

OP313.02 SQN

C01509 SQN

OP307.06 SQN

OP305.01 SQN

OP313.09 SQN

C015105 SQN

OP301.01 SQN

OP301.11 SQN

OP309.01 SQN

-

. _ . . _ . - . . - . -

-

. - - , - - - . _ . .

_ _ ~ - . . -

-_

.

-.

--

-

"

.

15

OP301.08 SQN

OP307.11 SQN

OP313.07 SQN

OP310.03 SQN

OP310.01.SQN

12. Experience Review (93702)

A potentially reportable occurrence report (PRO) 1-87-013, was issued

January 10, 1987.

The report described a condition where water could be

lost from the ECCS recirculation sump area in a post-LOCA event.

The

postulated loss was described as through leak paths at the air-return fans

on the upper containment deck level, and/or through a failed divider deck

seal.

The licensee has made a preliminary evaluation to determine the

amount of water that could be lost from the ECCS path (ref. SCR

SQNNEB8623R0).

The preliminary result of this analysis indicates that

water in the sump could fall below the sump swapover elevation (+13.7

ft.), but would be above the minimum level to prevent pump cavitation

(+8.0).

A second issue involved the possible failure of one of the two air-return

fans during spraydown of the area above the upper deck.

Fan A-A, located

above accumulator room 3, has the potential for having water from the

post-LOCA spraydown pooling above the open fan inlet.

The fan has been

estimated to have a water flow rate of approximately 650 gpm. This value

is in excess of the 50 gpm value guaranteed by the manufacturer.

TVA

personnel have been in informal contact with Duke Power personnel, alert-

ing them to the possibility of an arrangement that could allow water to

pool above their fans.

Resolution of SCR SQNNEB8623R0 is IFI 327,328/

87-02-08.

13. ColdWeatherPreparations(71714)

On January 16, 1987, the inspectors observed work in progress per general

operating instruction (G0I) - 6H, Apparatus Operations - Freeze Protec-

tion.

During this performance the inspector noted several discrepancies.

Step 17.A. and 18. A. both list a number of thermostats to be checked.

These steps require that the following be checked:

"All Circuits greater

than or equal to 75 degrees F - Check thermostats Set at 75 degrees F."

,

The auxiliary unit operator (AV0) conducting the procedure told the

l.

inspector that temperature indications did not exist for these circuits.

Additionally, the thermostats were set ranging from 40-150 degrees F.

They were left at 75-150 degrees F even though the procedure stated that

they were to be set at 75 degrees.

The response received was that the

'

procedure simply meant to make sure the thermostats were set greater than

75 degrees.

The inspector discussed the events with other AU0s and the Unit Operator

on shift.

The responses ranged from the fact that some thermostats were

not good enough to hold the circuit at or above 75 degrees without setting

!

them above that point, to the statement that it really did not matter as

long as the circuit remained above freezing.

i

,

_ . . . . _ __. _ - _ _,_ ,_ ._ _ ~._,_._ _ .., _. _ _ _ . . - - _ _ . _ _ _ . _ . _ _ . _ _ _ . _ - _ _ _ _ _

_

.

16

The inspector found that circuit thermostats for circuits 369P, 367P, 369S

and 367S were not identified in the panels designated in the procedure.

The AU0 accompanied by the inspector could not locate these thermostats.

The inspector was told by other AU0s that they did not exist.

One AVO

informed the inspector that he knew the thermostats did not exist, but

believed that the problem was identified on a WR.

No WR was identified.

Another AVO stated that he had in the past circled the errors and stated

that they were wrong. The inspector reviewed past performances of the G01

performed on December 19, 1987, January 2 and 9, 1987, and found that all

steps were signed off except on January 2, 1987. During this performance

circuits 365S, 363S, 369P and 367P were scribed out with no initials or

justifications.

The inspector went on a second tour with a different AVO on January 27,

1987.

During this tour the AVO showed the inspector the appropriate way

to determine the circuit temperatures.

Also using hand written cabinet

labeling he determined that the circuits were supplied by thermostats that

controlled more than one circuit.

The inspector verified this to be the

case by reviewing the circuit drawings with instrument maintenance person-

nel.

Neither of these points had been addressed by the original perfor-

mance or by the procedure.

The inspector reviewed the January 23, 1987

performance and found that circuits 365S, 3635, 369P, 367P and 367S were

all circled and annotated, "not found or non-existant."

TS 6.8.1 requires that written procedures be established, implemented and

maintained covering activities affecting quality.

G01-6H, Freeze Protec-

tion Checklist, is one such procedure.

Contrary to the above, on January 16, 1987, G01-6H was performed without

verifying the temperatures of circuits as required.

In addition, the

performance did not check certain thermostats as required because they

were not found.

Finally, circuit thermostats were not set to 75 degrees

per procedure specifications.

This is a violation of TS and shall be

identified as another example of Violation 327,328/87-02-02.

In addition, the inspector determined several labeling discrepancies which

included incorrect panel numbers, hand written labeling, and incorrect

switch labeling.

These cases were identified to the licensee personnel,

and will continue to be followed as housekeeping violation VIO 327,328/

85-32-02.

14.

Sustained Control Room and Plant Obcervation (71715)

During the inspection period, meetings were held with the Sequoyah opera-

tional readiness restart group for the purpose of coo-dinating the NRC

restart inspection effort.

The licensee presented, for information, two

operational readiness procedures; standard practice SQA-190, "Sequoyah

Activities List Restart Item Disposition," and standard practice SQA-191,

" Evaluation of Operational Readiness Prior To Plant Restart."

These

procedures establish TVA's restart criteria and describe the closecut

process including independent reviews.

The Sequoyah restart criteria,

. - _ _

- _ - _ - _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _

I

.

(

17

!

Appendix A to SQA-190, is provided below for information:

a.

The item identifies a specific deficiency which has significant

probability of leading to the inoperability of a system required for

startup or operation by the appropriate TS.

b.

The item identifies a programmatic deficiency which has a high

probability of causing or has caused a specific deficiency which

meets No. 1 above.

NOTE:

To assist in the determination of required for restart

relative to TS as in criteria No. I and 2 above, an affir-

mative answer to any or the following questions requires

consideration of the item for restart based on TS

requirements.

(1) Does the item directly and adversely affect safety-

related equipment function, performance, reliability,

or response time?

(2) Does the item indirectly and adversely affect safety-

related equipment power supply, air supply, cooling,

lubrication, or ventilation?

(3) Does the item adversely affect primary containment

integrity?

(4) Does the item adversely affect secondary containment

integrity?

(5) Does the item adversely affect control room

habitability?

(6) Does the item adversely affect systems used to process

radioactive waste?

(7) Does the item adversely affect fire protection or fire

'

loads?

(8) Does the item adversely affect the ability of a system

or component to meet its safety function during a

l

design basis event by impacting the seismic analysis,

i

single failure criteria, separation criteria, high

i

energy line break assumptions, or equipment qualifica-

tion?

(9) Are the programs such as radiological health, secur-

ity, radiological emergency preparedness, or quality

assurance which are necessary for safe conduct of

operations of the plant adversely affected?

_ _ _ _ _ _ - _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

~

,

"

.

18

(10) If not corrected prior to restart, could it lead to an

uncontrolled release or spread of radioactive contarri-

nation beyond the regulated area?

c.

The item identifies a specific deficiency that results in a failure

to comply with NRC regulations and no variance has been approved by

NRC.

d.

TVA has committed to NRC to complete the item prior to restart.

e.

The item identifies a specific deficiency which has a significant

probability of leading to a personal injury during plant operation.

f.

The item identifies a specific condition which has a forced outage

risk (probability X outage length) during the next cycle in excess of

the critical path time to correct the condition prior to restart.

The above restart criteria was evaluated against the criteria established

in volume 2 of the revised Sequoyah nuclear performance plan (SNPP). The

criteria listed in SQA-190 was the same as that in the SNPP with the

exception of items e and f above.

Item e addresses the personnel safety

aspect, where item f addresses schedule considerations.

Item f appears to

place a high degree of importance on schedule; however, when considered

along with the other established criteria it appears to be acceptable.

Additionally, SQA-190 has attempted to define the degree of significar.ce

of an item, where the SNPP implies the item must lead to inoperability of

equipment or systems before it becomes a restart item.

Implementation of

the above criteria will be evaluated during subsequent inspections.

15. Liquid and Gaseous Effluents (90713)

The report listed below was reviewed by Regional inspectors to verify

reporting requirements of technical content, data collection, acceptance

criteria, and handling of deficiencies noted.

Report reviewed was as follows:

Sequoyah Effluent and Waste Disposal Semi-annual Report,1st Half 86,

dated August 29, 1986

No violations or deviations were identified.

16.

IE Bulletins (92703)

(Closed) 327,328/86-BU-03, Potential Failure of Multiple ECCS Pumps Due to

Single Failure of Air Operated Valve in Minimum Flow Recirculation Line.

A review of the licensee response to IEB 86-03 (dated November 14,1986)

was conducted in the region.

In their response, the licensee stated that

.

.

19

the single failure vulnerability discussed in the bulletin did not exist

at Sequoyah due to the following:

The active ECCS consists of the safety injection system (SIS),

residual heat removal system (RHRS), and the centrifugal charging

portion of the chemical and volume control system.

The SIS has two safety injection pumps; each pump has a minimum flow

recirculation line connected to a common return line to the refueling

water storage tank (RWST).

A motor-operated flow control valve is

located in the recirculation line for each pump and in the common

return line to the RWST. The valve on the common return line to the

RWST is normally open and fails "as-is" and is remote-manual con-

trolled. Because it is the only isolation valve on the comon return

line from the safety injection pump discharge to the RWST (minimum

flow recirculation line), the design of the control circuit is such

that no spurious actuation will be able to energize the opening and

closing coils for the valve operator.

Emergency instructions call

for the valve to be closed before transferring SI pump suction to the

containment sump during recirculation mode of accident mitigation to

prevent transfer of radioactively contaminated water to the RWST. As

such, this system does not represent a concern in this area.

The RHRS has two trains and each train has its own separate and

redundant minimum flow recirculation line.

Each recirculation line

has its own normally-closed, fail "as-is," motor-operated globe

valve.

The control logic for each valve is identical.

With the

respective RHRS pump running and switches in the normal / auto posi-

tion, the valve will automatically open for flow below a prescribed

setpoint. The valve can also be opened remote manual.

Two centrifugal charging (CC) pumps share a comon minimum flow

recirculation line which has two motor-operated globe valves in

series.

These valves are normally open with the power removed to

satisfy 10 CFR 50 Appendix R requirements.

This item is closed.