ML20207T628

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Insp Repts 50-369/87-04 & 50-370/87-04 on 861230-870210. Violation Noted:Failure to Maintain Containment Spray Sys Operable Per Tech Spec 3.6.2 or Take Action Required by Tech Spec 3.0.3 & to Take Adequate Corrective Actions
ML20207T628
Person / Time
Site: McGuire, Mcguire  Duke Energy icon.png
Issue date: 02/23/1987
From: Guenther S, William Orders, Peebles T
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20207T613 List:
References
50-369-87-04, 50-369-87-4, 50-370-87-04, 50-370-87-4, NUDOCS 8703240192
Download: ML20207T628 (6)


See also: IR 05000369/1987004

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UNITED STATES

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NUCLEAR REGULATORY COMMISSION

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101 MARIETTA STREET, N.W.

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ATLANTA, GEORGI A 30323

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Report Nos.:

50-369/87-04 and 50-370/87-04

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Licensee: Duke Power Company

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422 South Church Street

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Charlotte, NC 28242

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Docket Nos.:

50-369 and 50-370

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License Nos.: ~NPF-9 ~and NPF-17

Facility Name: McGuire Nuclear Station

Inspection Conducted: December 30, 1986 through February'10, 1987

Inspectors:

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W. T. Orders, Resfdent Inspectop

Date Signed

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2-X7-72

S. F. Guenther, Accompanying Pers6nnel

Date Signed

Approved by:

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T. A. Peebles, Section' Chief

Date Signed

Division of Reactor Projects

SUMMARY

Scope:

This special, unannounced inspection was conducted in the areas of

operations.

Results:

Three violations were identified:

Failure to maintain containment

spray system operable per TS 3.6.2 or take action required by TS 3.0.3; Failure

to take adequate correction actions; Failure to follow procedures. Collectively

these violations may constitute a single violation. These violations are under

consideration for escalated enforcement action.

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REPORT DETAILS

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Licensee Employees Contacted

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  • T. McConnell, Plant Manager
  • B. Travis, Superintendent of Operations

D. Rains, Superintendent of Technical Services

  • B. Hamilton, Superintendent of Technical Services
  • M. Sample, Superintendent of Integrated Scheduling
  • N. McCraw, Compliance Engineer
  • N. Atherton, Licensing and Compliance
  • P. Nardoci, General Office Licensing

Other licensee employees contacted included construction craftsmen,

engineers, technicians, operators, mechanics, security force members,

and office personnel.

  • Attended exit interview

2.

Exit Interview

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The inspection scope and findings were summarized on January 28, 1987, with

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those persons indicated in paragraph 1 above.

The inspector described

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the areas inspected and discussed in detail the inspection findings.

No

dissenting comments were received from the licensee. The licensee did not

identify as proprietary any of the materials provided to or reviewed by the

inspectors during this inspection.

Three violations were identified:

failure to maintain containment spray

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operability; failure to take adequate corrective actions; failure to follow

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procedures (369/87-04-01).

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Another exit was held on February 12 with the plant manager. An additional

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example of failure to provide adequate procedures with respect to

replacement of materials during refueling was discussed (369, 370/87-04-02)

3.

Containment Spray System Inoperability

On the morning of December 30, 1986, both McGuire units were operating at

100% power.

At 9:45 a.m.,

the resident inspector noted in the Unit 1

Technical Specification Action Item Logbook (TSAIL) that train

'B'

of the

Solid State Protection System (SSPS) had been removed from service at

8:39 a.m. to facilitate surveillance testing. It was also noted that train

'A' of Containment Spray (NS) had been removed from service at 9:31 a.m. to

accommodate NS heat exchanger testing.

Since SSPS testing can affect the

automatic actuation of NS, the inspector questioned the shift supervisor

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(SS). The SS informed the inspector that the SSPS testing would not affect

the operability of train 'B' NS (i.e. selected portions of SSPS testing can

be performed without affecting all that train's components). The inspector

documented ,the pertinent information to allow a subsequent, more detailed

review.

During that review, the inspector concluded that the SSPS testing had made

the automatic start of train 'B'

NS inoperable.

As train

'A'

NS was

inoperable with the pump discharge valves closed and power removed, for

the period from 9:31 a.m. until 10:10 a.m. on December 30, 1986, both trains

of NS were inoperable. (Train 'B' was returned to service at 10:10 a.m.).

That conclusion is supported by the following:

(1) The procedure employed to facilitate testing on SSPS train 'B'

was

PT-0-A-4601-08B.

Step 12.1.9 of that procedure instructs the

technician to place the " Mode Selector" in the 'B'

SSPS Output Relay

Test Panel in the " Test" position. This action removes 120V AC from

the coils of the 'B' train output relays, thereby rendering the train

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inoperable.

The 120V AC is not restored until the testing is complete.

(2) The procedure employed to facilitate the train ' A' NS heat exchanger

testing was PT-1-A-4208-03A.

Steps 12.2.11, 12, 13 and 14 respectively,

have the technician close or verify closed pump discharge valves INS-29A

and INS-32A and remove power from them. Thus, train'A' NS was rendered

inoperable.

It is important to note that a very similar situation occurred on the

morning of March 12, 1986, when, at approximately 9:10 a.m.,

while

performing a routine operations safety verification, the inspector detected

in the Unit 1 TSAIL that the 'B' train NS pump and the ' A' train of SSPS

had been taken out of service. The NS pump had been removed from service

at 4:45 a.m. that morning. Train 'A' of SSPS had been removed from service

only moments prior to the inspector's review.

The inspector questioned the control room Senior Reactor Operator (SRO),

who concluded that the work ongoing on SSPS would, in fact, degrade the 'A'

NS pump start logic and was able to stop the work on SSPS prior to the

personnel actually taking the train out of service. The details of this

event and associated enforcement action is detailed in Inspection Report

369, 370/86-08.

The significance of the most recent situation is, therefore, exacerbated by

the fact that it is a repetitive occurrence.

As was the case during the previous event, it appears that certain selected

administrative controls which were established to preclude this type event

appear to have been circumvented.

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The heat exchanger test, procedure PT-1-A-4208-03A, prerequisite 8.4

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requires the technician to " Ensure Train IB of Containment Spray is

fully operable during test if in Modes 1, 2, 3, or 4".

This step was

signed off by the technician ba' sed on permission granted by the Shift

Supervisor. The shift supervisor was under the erroneous impression

that the

'B' train of NS was operable.

Operations Management Procedure (OMP) 2-5, " Technical Specifications

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Action Item Logbook," provides the operating staff instructions for

documenting operation in a degraded condition.

Section 8.1 of that

procedure required that, prior to removing a component from service, an

evaluation be made tc determine what effect the action has on the

operability of other equipment.

The procedure further instructs that

to properly perform the evaluation, the other open items in the TSAIL

must be reviewed to determine if the redundant train component is

inoperable.

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DMP 2-5, step 6.6 requires that the operator ensure that the redundant

train is verified to be operable before removing equipment from

service.

Obviously, the intent of the above requirements is to preclude the removal

of both trains of redundant equipment simultaneously.

The regulatory requirements associated with this event are as follows:

Technical Specification (TS) 6.8.1 requires that written procedures be

established, implemented and maintained covering the operation of safety-

related equipment. As detailed above, it appears that certain procedural

requirements were not complied with.

Technical Specification 3.6.2 requires two independent Containment Spray

Systems be operable in modes 1, 2, 3, and 4.

With one Containment Spray

System inoperable, the inoperable Spray System is to be restored to operable

status within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />. There is no allowable statement in TS 3.6.2 if both

trains are inoperable.

With both trains of NS inoperable, the unit was in TS 3.0.3 which requires

that when a Limiting Condition for Operation (LCO) is not met, except as

provided in the associated ACTION requirements, that within one hour action

shall be initiated to place the unit in a MODE in which the specification

does not apply.

In this particular case, since the operating staff was

unaware of actual plant status, the requisites of TS 3.0.3 were not

considered. However, as they should have known the condition of the system,

the time for entering TS 3.0.3 was taken from when both trains were removed

from service.

Fortunately, the testing on train 'B'

was completed at

10:10 a.m. which precluded exceeding the one hour action requirement.

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In conversation with members of plant' management,' the position was taken

that the unit was not in noncompliance with TS 3.6.2 because the one hour

action statement of TS 3.0.3 had not been exceeded. It is acknow1

the action statement of TS 3.0.3 was not exceeded, howevef, the'ciged that

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position is that the unit was in noncompliance with TS 3.6.2.

The basis for

this position is founded on the following:

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TS 3.0.2 states that . noncompliance with a specification shall exist

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when the requirements of the Limiting Condition for Operation and

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associated ACTION requirements are not met.

The bases of TS 3.0.2

defines those conditions necessary to constitute compliance with the

terms of an individual Limiting Condition for Operation and associated

ACTION requirement.

The bases of TS 3.0.3 specifies that the specification delineates the

measures to be taken for those circumstances not directly provided for

in the ACTION statements of an individual LC0 and whose occurrence

would violate the intent of a specification.

Thus, in this case, with both trains of containment spray inoperable the

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unit was not in compliance with TS 3.6.2, yet no action was taken pursuant

to TS 3.0.3.

The events leading up to the removal of both NS trains involved the

following:

1)

the lack of accurate communication between the performance and

Operations personnel pertaining to equipment operability;

2)

the violation of administrative requirements which, if adhered to,

would have precluded the event; and

3)

apparent inadequate corrective actions to the occurrence of March 12,

19E6.

With respect to the apparent inadequate corrective actions, the event of

March 12, 1986 occurred, as stated in your response, as "...a result of the

failure to realize that "A" Train SSPS work would block the auto start

feature of

"A" Train NS Pump."

You also stated in your response to

Violation 369/86-08-02 that "the incident was covered at the Shi f t

Supervisor's meeting of April 4, 1986." Clearly then, the operations staff

was made aware of the problem and should have known that SSPS testing does

affect the operability of the associated engineered safety features (ESF)

equipment.

4.

Inoperable Containment Air Returr. Fans

On January 30, 1987, at 2:20 p.m., the licensee, in response to a Region II

notification, determined that two sections of curbing were missing from the

refueling floors of both McGuire units.

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The curbing sections (a 3-foot and 6-foot section per unit) form parts of a

dam which is designed to prevent containment spray water from flowing into

the cpntainment air return fan pit area. Without the dam, the water would,

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accorcing to the licensee, result in fan failure.

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requisites of Technical Specification (TS) 3.0.3.

At 3:19

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licensee began shotting both units down. Unit I was at 100% and Unit 2 was

at 58% power at that time. At 4:18 p.m., after discussions with NRC Region

II management, the licensee received an 8-hour discretionary enforcement

extension to the TS 3.0.3 action statement requirements in that the units

could remain stable instead of decreasing in power for the six hours allowed

by the TS and an additional two hours was allowed to conduct the repairs in

a more controlled manner. This additional 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> of reactor criticalit a

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was granted as the work would be done in a total of eight hours and it was

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decided that safety would be better served if the plant was not ramping i.n

power during the repairs. The drawings for the dams were available and the

extension would allow time for the manufacture and installation of the dam

sections. The unit shutdowns were held in abeyance with Unit 1 at 99% and

Unit 2 at 57% power.

The shutdowns were resumed in accordance with the

agreement and TS 3.03 at 11:20 p.m.,

since the work on neither unit was

complete.

The work on Unit 2 was completed at 12:20 a.m.

on January 31, and at

1:54 a.m. on Unit 1. Unit 1 and 2 had reduced power to 80%, and 53%,

respectively. The Unusual Event was cleared at 1:54 a.m.,

and both units

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returned to their previous power levels.

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The air return fans, located in the containment, are designed to return air

from the upper compartment into the lower compartment.

Two full capacity

fans are provided each with the capability to perform the assigned function.

Each fan has a capacity of 30,000 cubic feet per minute.

Both fans are started by a containment spray actuation signal nine (+or-one

minute) minutes after a postulated loss of coolant accident (LOCA) would

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cause containment pressure to reach 3 psig. The fans move air from the

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upper compartment to the lower compartment, thereby returning the air which

would be displaced by the reactor coolant system blowdown to the lower

compartment. After discharge into the lower compartment, the air and steam,

produced by residual heat, would flow through the ice condenser doors into

the ice condenser compartment where the steam portion of the flow would be

condensed. The air flow reta ns to the upper compartment through the vents

in the upper doors of the ice condenscr compartment. The fans operate

continuously after actuation, circulating air through the containment

volume.

The fans, located below the operation deck, discharge into the

equipment annulus outside the crane wall on both sides of the refueling

canal.

Flow enters the lower compartment through ports in the fan room

crane wall.

These ports provide for equalization of pressure between the

lower compartment and dead-ended volumes.

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Preliminary indications reveal that with both containment air return fans

inoperable, the potential would have existed for significant post-LOCA

problems with containment pressure, local hydrogen accumulation and fission

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product scrubbing.

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Since this particular scenario is an unanalyzed condition, the true safety

significance is unknown. The licensee's safety evaluation is forthcoming in

the associated Licensee Event . Report (LER) due by March 1,

1987. The

sections of dam were originally installed on both units, but were removed

during subsequent refueling outages and not replaced.

The root cause of the event appears to be the lack of administrative

controls regarding the removal and re-installation of the components. A

review of pertinent procedures and discussions with licensee personnel

revealed that there were no specific controls concernifig either evolution.

This is an another example of an apparent violation of TS 6.8.1, which

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requires that written procedures be established, implemented and maintained

covering operation and maintenance of safety related equipment. . These

examples question the adequacy of management control over activities

affecting the safe operation of the McGuire nuclear units.

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