ML20205F733

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SALP Repts 50-282/86-01 & 50-306/86-01 for Dec 1984 - May 1986
ML20205F733
Person / Time
Site: Prairie Island  
Issue date: 08/14/1986
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20205F704 List:
References
RTR-NUREG-0737, RTR-NUREG-737, TASK-1.D.2, TASK-2.A.2, TASK-2.K.3.30, TASK-2.K.3.31, TASK-3.A.1.2, TASK-TM 50-282-86-01, 50-282-86-1, 50-306-86-01, 50-306-86-1, GL-83-28, GL-84-15, IEIN-86-003, IEIN-86-3, NUDOCS 8608190314
Download: ML20205F733 (36)


See also: IR 05000282/1986001

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SALP 6

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SALP BOARD REPORT

U.S. NUCLEAR REGULATORY COMMISSION

REGION III

SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE

50-282/86001; 50-306/86001

Inspection Report No.

Northern States Power Company

Name of Licensee

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Prairie Island Nuclear Generating' Plant

Name of Facility

December 1, 1984 - May 31, 1986

Assessment Period

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I.

INTRODUCTION

The Systematic Assessment of Licensee Performance (SALP) program is an

integrated NRC staff effort to collect available observations and data on

a periodic basis and to evaluate licensee performance based upon this

information. SALP is supplemental to normal regulatory processes used to

ensure compliance to NRC rules and regulations. SALP is intended to be

sufficiently diagnostic to provide a rational basis for allocating NRC

resources and to provide meaningful guidance to the licensee's management

to promote quality and safety of plant construction and operation.

An NRC SALP Board, composed of staff members listed below, met on July 23,

1986, to review the collection of performance observations and data to

assess the licensee performance in accordance with the guidance in NRC

Manual Chapter 0516, " Systematic Assessment of Licensee Performance." A

summary of the guidance and evaluation criteria is provided in Section II

of this report.

This report is the SALP Board's assessment of the licensee's safety,

performance at the Prairie Island Nuclear Generating Plant for the period

December 1, 1984 through May 31, 1986.

SALP Board for Prairie Island Nuclear Generating Plant:

C. E. Norelius, Director, Division of Reactor Projects

J. A. Hind, Director, Division of Radiological Safety and Safeguards

C. J. Paperiello, Director, Division of Reactor Safety

D. Dilanni, Licensing Project Manager, NRR

W. D. Shafer, Chief, Emergency Preparedness and Radiological Protection

Branch

G. Lear, Director, PWR Project Directorate No. 1

C. W. Hehl, Chief, Operations Branch, DRS

1. N. Jackiw, Chief, Reactor Projects Section 2

T. M. Burdick, Chief, Operator Licensing Section

J. E. Hard, Senior Resident Inspector

J. R. Creed, Chief, Safeguards Section

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J. A. Bauer, Reactor Engineer, Technical Support Staff

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M. M. Moser, Resident Inspector

M. A. Ring, Chief, Test Programs Section

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II. CRITERIA

The licensee performance is assessed in selected functional areas depending

whether the facility is in a construction, pre-operational or operating

phase. Each functional area normally represents an area significant to

nuclear safety and the environment, and is a normal programmatic area.

Some functional areas may not be assessed because of little or no licensee

activities or lack of meaningful observations.

Special areas may be added

to highlight significant observations.

One or more of the following evaluation criteria were used to assess each

functional area.

A.

Management involvement in assuring quality.

B.

Approach to resolution of technical issues from a safety standpoint.

C.

Responsiveness to NRC initiatives.

D.

Enforcement history.

E.

Reporting and analysis of reportable events.

F.

Staffing (including management).

However, the SALP Board is not limited to these criteria and others may

have been used where appropriate.

Based upon the SALP Board assessment each functional area evaluated is

classified into one of three performance categories. The definition of

these performance categories is:

Category 1: Reduced IEC attention may be appropriate.

Licensee management

attention and involvement are aggressive and oriented toward nuclear safety;

licensee resources are ample and effectively used so that a high level of

performance with respect to operational safety or construction is being

achieved.

Category 2: NRC attention should be maintained at normal levels.

Licensee

management attention and involvement are evident and are concerned with

nuclear safety; licensee resources are adequate and are reasonably

effective such that satisfactory performance with respect to operational

safety or construction is being achieved.

Category 3:

Both NRC and licensee attention should be increased.

Licensee

management attention or involvement is acceptable and considers nuclear

safety, but weaknesses are evident; licensee resources appear to be

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strained or not effectively used so that minimally satisfactory performance

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with respect to operational safety or construction is being achieved.

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III. SUMMARY OF RESULTS

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The overall regualtory performance of the Prairie Island Plant has

continued at a satisfactory high level during the assessment period.

Rating Last Period

Rating This Period

Functional Area

07/01/83 - 11/30/84

12/01/84 - 05/31/86

A.

Plant Operations

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B.

Radiological Controls

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C.

Maintenance

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D.

Surveillance

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E.

Fire Protection

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2

F.

Emergency Preparedness

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G.

Security

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H.

Outages

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Quality Programs and

Administrative Controls

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Licensing Activities

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K.

Training and Qualification

Effectiveness

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  • Not Rated (new functional area for SALP 6)

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IV. PERFORMANCE ANALYSIS

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A.

Plant Operations

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1.

Analysis

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Evaluation of this functional area is based on the results of

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routine inspections conducted by the resident' inspectors. The

inspections included direct observation of activities, review of

logs and records, verification of selected equipment lineup and

operability, followup of significant operating events, and

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verification that facility operations were in conformance with

the Technical Specifications, administrative procedures, and

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commitments. Five violations were identified during the rating

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period as follows:

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Severity Level V - The boric acid storage tank inventory

a.

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fell below the minimum permitted by Technical Specifica-

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tions with a reactor coolant system temperature above

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200*F. This was a minor violation with no safety

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significance.

(Inspection Report No. 50-282/84-18(DRP)).

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b.

Severity Level IV - A diesel-driven cooling water pump

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control switch was inadvertently left in manual for about

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six hours. The error was detected during a control board

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walkdown and was prontly corrected.

(Inspection Report

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No. 50-282/85003(DRP)).

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c.

Severity Level IV - The level in the Unit 2 caustic addition

tank fell below the required level for about one hour. This

was the result of inadvertently leaving an overflow valve

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open.

(Inspection Report No. 50-306/85003(DRP)).

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d.

Severity Level V - An up-to-date alarm response procedure

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was not available in the control room. This is a relatively

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minor matter which was promptly corrected when pointed out

by the inspector.

(Inspection Report No. 50-282/85014(DRP);

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50-306/85011(DRP)).

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e.

Severity Level IV - This violation is for failure to

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promptly log the discovery of a potentially inoperable

limitorque valve and the correction of the potential

problem.

(Inspection Report No. 50-282/86007(DRP)).

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See also Section I, Quality Programs and Administrative

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Controls, for discussion of an additional violation

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related to this limitorque valve.

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Violations

a.,

b., and c. were the result of errors in

judgement by the operating staff. Violation d. was the result

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of an administrative oversight.' Violation e. seems to have

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been caused by a misunderstanding of what needs to be, recorded

in the permanent plant logs. Appropriate corrective action has

been or is being taken by the licensee.

During the assessment period,.the licensee took corrective

actions tc reduce the number and severity of violations noted

in the last SALP report. The status of these corrective

actions and additional measures being taken to improve plant

operation is reviewed below:

1.

Positive Discipline _ Program - The disciplinary

aspects of this program are being used for hunun

errors involving gross negligence or deliberate

actions. The positive aspects of the program, such

as the Employee-of-the-Quarter awards, are being

used for high level performance.

2.

Study of personnel / procedural errors - An Error

Reduction Program has been instituted which relates

to many different aspects of plant operation. No

significant reduction in violations is yet noted.

3.

Outside management audit by Delian Corp. - Delian

reported their findings to the licensee in April

1985. The findings focus principally'on areas where

management, both in plant _and corporate, can signifi-

cantly improve their roles. Action is being taken by

NSP in the identified areas.

There were six reactor trips during the assessment period:

two

were < 15% power; four were > 15% power. The first four trips

were on Unit I and the last two on Unit 2.

The first trip was

the result of a broken instrument air line which occurred

during Appendix R work. This caused a main feedwater valve to

close, resulting in a low steam generator level trip. During

recovery from that trip, a second trip resulted when a feedwater

valve malfunctioned. This time, a feedwater pump motor-operated

discharge valve tripped off while being opened. The third

reactor trip occurred while troubleshooting instabilities in the

main generator regulator. A generator lockout during trouble-

shooting caused the generator trip-reactor t' rip. The fourth trip

on Unit 1 occurred from low power as a result of mismatch of

feedwater flow and steam flow while in manual operation.

The Unit 2 trips occurred late in the assessment period. The

first of these was the result of a technician error during

surveillance testing and was the first trip on Unit 2 in nearly

three years.

(Also discussed in Section D. Surveillance). The

second trip resulted from steam generator level control problems

during the subsequent startup.

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There were six LERs involving personnel errors by operations

personnel during the assessment period; four of these errors

were made by licensed operators.

The six errors included two

valving mistakes, an error in interpreting technical specifica-

tions, two switching mistakes, and a computational error. None

of these had any major safety significance.

In addition to the

LERs, there was one Significant Operating Event (SOE) during

the period which is of particular note because of its poter,tial

safety significance. This SOE was the contamination of crankcase

lube oil in one diesel generator because of improperly marked

oil drums. The contaminated lube oil made a diesel-generator

inoperable. Though the investigation failed to disclose the

specific source of contamination, controls instituted by the

licensee over oil drums should prevent future problems from this

source. Unlicensed operators were involved in this SOE.

Despite the difficulties discussed above, the plant operating

record is outstanding.

Cumulative availabilities were more

than 80% for Unit I and more than 85% for Unit 2.

For the

period 1983-85, the Unit I capacity factor was the best in

the nation at 84.1% and Unit 2 was fifth best at 80.2%.

2.

Conclusion

The licensee continues to be rated Category 2 in this area.

3.

Board Recommendations

The board notes that since the end of the SALP rating period,

NRC has become aware of a matter which should be mentioned.

That matter involves the request for transfer away from Prairie

Island of about two-thirds of the licensed operators on the

operating crews. The immediate plant loss will only involve

three operators since a limited number of other jobs are

available. Management attention is being focussed on the

causes of operator dissatisfaction.

Plans to replace the

personnel being transferred are also being discussed.

B.

Radiological Controls

1.

Analysis

Three inspections were conducted during this assessment period

by region based inspectors. These inspections included

operational and outage radiation protection, radiological

waste management, and transportation activities. The resident

inspectors also reviewed this area during_ routine inspections.

One violation was identified as follows:

Severity Level IV - Failure to follow procedures requiring valve

restoration to normal position following maintenance and

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requiring valve position verification before making a liquid

radwaste release which resulted in an inadvertent release from

a radwaste tank.

(50-282/85019-01;50-306/85018-01)

The licensee was responsive to the violation; corrective actions

were timely and appear to be effective. The violation appears to

be an isolated incident and not indicative of a programmatic

weakness.

Staffing continued to be a licensee strength. The staff is

stable and well organized with no significant turnover other

than career progression.

Management involvement in this functional area is evident. There

is consistent evidence that managers and supervisors are involved

in the day-to-day activities of the plant.

Procedures and

policies are adhered to and records are complete, well maintained,

and available. Corrective actions, when necessary are prompt and

consistently recognize and address concerns. Annual audits of

this functional area are conducted by both onsite and corporate

groups. The audits of radiation protection, chemistry and

transportation activities completed in 1985 were comprehensive,

timely and thorough.

A conservative approach to resolution of radiological control

issues is routinely exhibited. Personal radiation exposures for

this assessment period, which included refueling outages for both

units and a 10 year ISI for Unit I were 136 person-rem in 1984

and 390 person-rem for 1985. This was well below the average of

U.S. pressurized water reactors. An effective ALARA program,

with good management and worker support, contributes to the low

exposures. Several improvements were made during this assessment

period which helped reduce radiation exposures, including

underwater replacement of the antivibration bars (AVB) in the

steam generators which reduced the radiation level to the workers

by a factor of about 15, mockup training for AVB work, and mockup

training for reactor head modifications.

Total liquid and airborne radioactive releases and solid

radioactive waste volume and ' activity remained well below the

average for U.S. pressurized water reactors. No radioactive

material transportation problems were reported. The liquid

radwaste release referenced in the above violation, although

unplanned, was within technical specification radioactivity

limits.

Examination of the Radiological Environmental Monitoring Program

(REMP) was limited'to a review of the licensee's 1984 annual

report. This program continuts to be acceptable with'no signi-

ficant anomalies noted.

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2.

Conclusion

The licensee is. rated Category 1 in this area. Licensee

performance has remained essentially constant over the course

of the SALP assessment period.

3.

Board Recommendations

None.

C.

Maintenance

1.

Analysis

Evaluation in this area is based on routine inspections by the

resident inspectors. Areas examined during these inspections

included: major and minor plant modifications, calibrations,

repairs, equipment overhauls, preventative maintenance, and

maintenance organization and administration. No viola' ions

were identified in this area.

During the assessment period there was one LER attributed to

personnel error. This event involved a reactor trip which

occurred during troubleshooting work being done on the Unit 1

main generator voltage regulator. The error was the pulling

of a regulator card without adequate review of the possible

consequences.

The licensee's preventative maintenance program shows consistent

evidence of prior planning and assignment of priorities; it is

well-defined, controlled, and has explicit procedures for

control of preventative maintenance activities which is

evidenced by the plant's high availability factor. Records of

maintenance activities are well maintained and readily available.

Special maintenance work continues to be performed in a very

impressive manner.

An example of this high level of performance

was the removing and. replacing of the Unit I reactor upper

internals. This job required careful planning and attention to

details because of the size of the internals packages and the

radiation levels associated with the old internals. The job

was performed smoothly and without significant delay even though

this had not been done previously at Prairie Island.

Other significant mainienance efforts during the period included

rebuilding of the safeguards traveling screens, upgrading of the

caustic addition systems, installation of'new level indicators on

boric acid storage tanks, and rebuilding of a heater drain tank

and pump.

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An organizational change made during the period involved the

replacement of the Maintenance Superintendent, who has retired,

with one of the Lead Production Engineers. Since the new

Superintendent is also a long time Prairie Island employee, and

since the maintenance group remains extremely stable with very

little attrition, the experience level continues to be very high.

2.

Conclusion

The licensee continues to be rated Category 1 in this area.

3.

Board Recommendations

None.

D.

Surveillance

1.

Analysis

Evaluation of this functional area is based on routine assessments

by the resident inspector during implementation of the resident

inspection program and four inspections by region based special-

ists. Six violations were identified as follows:

a.

Severity Level IV - Containment Integrated Leak Rate Test

(CILRT) procedures were not a

(Inspection

50-282/85011(DRS))ppropriate.

Report No.

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b.

Severity Level IV - CILRT supplemental verification test

not long enough.

(Inspection Report No. 50-282/85011(DRS)).

c.

Severity Level V - Failure to add pre and post-repair

differential leakage to CILR.

(Inspection Report

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No. 50-282/85011(DRS)).

d.

Severity Level V - Pump not allowed to run five minutes

before taking data. Pump speed not measured.

(Inspection-

Reports No. 50-282/85012(DRS); 50-306/85009(DRS)).

e.

Severity Level V - Failure to use controlled, traceable

instruments for vibration testing.

(Inspection Report

No. 50-282/85012(DRS); 50-306/85009(DRS)).

f.

Severity Level IV - During performance of the surveillance

associated with the Nuclear. Power Range Daily Calibration

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Procedure a calculational error was made; consequently,

the required recalibration of the nuclear power range

instruments was not performed and, as a result, the

licensed power level was exceeded by approximately three

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megawatts thermal (0.16%) based on a calculation of

average power level during an eight-hour shift (Inspection

Report No. 282/85008).

Violations

a.,

b., and c. were the result of a Region III

specialist inspection of data accumulated during the Unit 1

CILRT. While the three violations represent difficulties

with the licensee's performance of the CILRT, the CILRT itself

was, in fact, found to have acceptably low containment leakage.

With regard to Violation c., the inspection noted that the

licensee was unaware of the Type A CILRT as found requirements

and in their response NSP noted that these requirements were

different from what had been NSP's long-standing practice.

NSP has taken corrective actions for all three violations.

Containment Integrated Leak Rate Testing is a unique

specialized area and as such is not necessarily reflective of

the plant's surveillance program as a whole.

Violations d. and e. were also the result of a Region III

specialist inspection. Prompt and appropriate action was taken

by the licensee; in the case of Violation d., corrective action

was taken prior to the exit meeting. Violation f. appeared to

be an isolated occurrence.

The number of violations in this assessment period shows a slight

increase as compared to the previous period. However, severity

levels and safety significance are reduced.

The number of LERs attributed to personnel error has been reduced

from tive in SALP 4 to four in SALP 5 to two in the current

period. The first one involved a surveillance test on the

turbine overspeed system which was performed two days late.

The other event was a Unit 2 reactor trip because of technician

error during surveillance testing.

Approximately 8,000 surveillance. tests are performed annually

at Prairie Island. This extensive program is coordinated by

one of the more experienced Lead Production Engineers in the

Operations Engineering group. A variety of computer generated

lists are distributed to the plant forces responsible for test

. performance. Many different groups are involved in performing

the tests. The test procedures themselves are generally

written by the engineers or others to whom the system being

tested is assigned. Review of test results is performed by

several individuals including the test author. A cover page on

each test identifies the individuals who performed the test and

who reviewed and approved the test results. After the reviews

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are complete, the entire test document is reduced to microfilm

for permanent storage. This system of administering the

surveillance test system works quite well as evidenced by

the extremely low rate of missed or late surveillances.

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During this period the licensee paid considerable attention to

performance in the surveillance area. This is evidenced by the

following activities:

a.

A computer program has been developed for trending leakage

through "Section XI valves." This subject had been

addressed by a Region III inspector.

b.

An independent (out-of pl nt) review was conducted of

selected surveillance procedures examining clarity of

intent, conformance to technical specifications, and

adequacy of communications.

c.

Specific improvements were made in the procedures for

caustic standpipe and component cooling system; areas in

which regulatory difficulties have been experienced in the

past.

d.

The Procedures Committee has been reactivated and currently

is involved in a major ongoing effort aimed at improving

all procedures.

It appears that as a result of the licensee's special efforts

in the Surveillance area, improvements in performance are being

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seen.

2.

Conclusion

The licensee continues to be rated Category 2 in this area.

An improving trend in performance has been noted by NRC.

3.

Board Recommendations

None.

E.

Fire Protection

1.

Analysis

Evaluation of this functional area is based on routine assess-

ments by the resident inspectors. No violations were identified.

Similarly, no LERs were filed in this area.

Work required to be performed per 10 CFR 50, Appendix R, Fire

Protection Program, was completed within the time schedule

approved by NRR. This job was a massive effort requiring careful

' scheduling and the employ of many tradesmen from outside the

plant. At one time during this effort, approximately 70 people

at the plant were working solely to meet the Appendix R

requirements.

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One small fire occurred during the assessment period. This was

caused by a hot electrical connection which ignited a plastic

sheet in contact with it. No significant damage resulted.

All operators and shift supervisors are members of the Fire

Brigade.

In order to maintain an active status in the Brigade,

each member must attend 16 hours1.851852e-4 days <br />0.00444 hours <br />2.645503e-5 weeks <br />6.088e-6 months <br /> of classroom training and

participate in eight hours of hands-on " smokehouse" training

every year. The Brigade members learn to fight all types of

fires which conceivably could occur at the plant. Quarterly

fire drills are performed by each of the six crews. These

drills have demonstrated the ability to mobilize within seconds

and the general preparedness of Brigade members to handle

unannounced emergencies.

In the area of housekeeping, licensee performance is judged to

be about average. Although the licensee has expended considerable

effort in painting, cleaning, and general organization of storage

areas, much more needs to be done, particularly in the auxiliary

building. As noted by the Regional Administrator during his

recent plant tour, the turbine building appears reasonably good

but the auxiliary building is cluttered, has graffiti on the

walls, and needs improvement in the identification of equipment.

Observers from NRR have commented favorably on the clean and

well ordered appearance of the plant simulator, training

facilities and the control room. These same observers also

noted that in-plant laboratories, tool rooms and storage areas

were clean, bright, and well laid out. The Licensee is

continuing his effort to improve housekeeping where further

improvement is necessary.

2.

Conclusion

The licensee is rated Category 2 in this area. This is a

decline from the last assessment period rating of Category 1,

due primarily to housekeeping practices at the plant.

3.

Board Recommendations

None.

F.

Emergency Preparedness

1.

Analysis

Two inspections were performed during the assessment period.

One

of these was an evaluation of the annual emergency preparedness

(EP) exercise conducted on May 14, 1985. The other was a routine

inspection, resulting in no violations, that included a review of

training, changes to the program, license audits, maintenance of

emergency preparedness, and activations of the emergency plan.

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No weaknesses were identified during the exercise. The scenario

was somewhat unique in that a simulated radioactive release never

occurred outside the plant and the emergency never exceeded the

Alert level throughout the exercise. The quality of scenario

data was much improved over the 1984 scenario. All nine objec-

tives of the exercise were met by the licensee. While it was a

good exercise and well performed, it was not a very challenging

scenario.

It was recommended that the licensee use more alter-

nates in filling key emergency positions in the Technical Support

Center (TSC) and the Emergency Operations Facility (EOF) to

expand the emergency experience level of the staff and provide

a broader base of qualified emergency response personnel.

The routine inspection involved a finding relating to the lack

of required training for four individuals with emergency response

positions. The licensee identified this omission and took

appropriate corrective action to prevent a violation from being

issued. Licensee management was advised to periodically review

the number of individuals assigned emergency functions, particu-

larly for lower echelon support positions, to ensure that all

will be trained annually as required.

A computerized list of emergency preparedness issues has been

incorporated into the training lesson plans. This list includes

items from NRC inspection reports, audit findings, and drill and

exercise critiques. Documentation for individual participation '

in drills, exercises and table-top discussions has been improved

and is included as part of the training records. This had been

identified as a weak area in the previous SALP report. Overall,

training related items have improved during this SALP period.

Shift augmentation drill records were reviewed and found to be

satisfactory. The tone alert radio system used to notify

off-duty emergency response personnel, has had some operating

problems, and was being replaced by the Automatic Dialing Alert

System (ADAS). The ADAS should be in operation by the Fall of

1986; and it is expected to be a more effective communications

system than the present one.

Management involvement in decision making has been consistently

at a level which ensures adequate management review.

Responsiveness to NRC initiatives has been technically sound,

and where noted, acceptable resolutions have been provided in a

professional and timely manner. Events that have resulted in

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the activation of the emergency plan have been properly identi-

fied, classified, and resulting notifications made within the

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required times. Staffing of key emergency personnel is well

identified and described adequately in both corporate and plant

implementing procedures.

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In summary, the licensee is continuing its effort to improve the

emergency preparedness program. Corporate and plant management

are continuing to demonstrate their concern by being involved in

emergency preparedness policy making and making improvements in

the program, whether suggested by the Region III inspection teams

or by their own initiatives.

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Conclusion

The licensee continues to be rated Category 1 in this area.

3.

Board Recommendations

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G.

Security

1.

Analysis

During the assessment period, one routine inspection was

performed by region-based inspectors in the early part of the

assessment period. The resident inspectors made periodic

observations of security activities. Three violations were

identified.

Severity Level IV - The licensee failed to adequately

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implement' compensatory measures for a failed security

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system.

(Inspection Reports No. 50-282/85009;

50-306/85007.)

r

b.

Severity Level IV - The licensee's assessment aids were not

adequate in providing surveillance of the protected area

perimeter barrier.

(Inspection Reports No. 50-282/85009;

50-306/85007.)

c.

Severity Level IV - The protected area intrusion detection

system failed to detect attempted penetrations in one zone.

(Inspection Reports No. 50-282/85009; 50-306/85007.)

The number and severity level of the violations remain

essentially unchanged from the previous SALP assessment period.

Although the violation noted in Item a. was the only specific

instance observed of the licensee's failure to meet minimum

requirements for compensatory measures, the quality of

implemented compensatory measures, in general, was not

representative of above average performance.

Item b. was

indicative of a deteriorating security system that had not

been adequately maintained.

Item c. represented a design

deficiency in the protected area intrusion alarm system which

.

had existed since the inception of the program. During the one

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inspection conducted by region based inspectors, weaknesses or

concerns were noted in several areas including managment's

role in assuring quality (lack of an in-depth audit program),

Access Control - Packages (marginally acceptable equipment);

and Safeguards Contingency Plan Implementation Review (limited

security drill program). Based on the violations and the

observed weaknesses during that specific inspection, the

licensee's representatives were informed that their performance

,

had declined.

'

In response to the referenced inspection findings, corporate

security conducted a comprehensive team audit of the security

program. Additionally, the licensee contracted with another

experienced nuclear utility's security organization to conduct

an independent in-depth audit of the design and implementation

of all aspects of their security program. Site security manage-

ment enhanced the Quality Assurance (QA) audit program by

developing and implementing a program of security officers

performing specific and periodic internal audits on a continuing

basis. The above noted reviews were thorough and technically

sound, and were indicative of increased attention by management

in assuring quality in the security program. Management's

support for the security program was evidenced by the procurement

and installation of state-of-the-art search equipment; improve-

ments in the Protected Area intrusion detection system; the

employment of both a full and part-time engineer to work on

security modifications; the employment of a full time security

specialist to administrative 1y assist the Supervisor of Security

in order that he will be more able to provide more direct manage-

ment of tha program; and the installatien of new state-of-the-art

assessment aids and the replacement of other deteriorating

equipment. These measures have clearly demonstrated a more

effective role of managers in~ assuring quality.

The licensee took prompt action in resolving the issues which

were noted during the region-based security inspection. The

licensee has been cooperative in providing the resi<'

.t inspector

with periodic updates concerning the progress in rewiving NRC

initiated issues; however, the licensee should also communicate

more frequently with the region based safeguards staff. The

licensee's approach to resolving identified weaknesses / concerns

has been comprehensive.

Solutions to technical safeguards problems were sound, timely and

conservative, indicating a clear understanding of the issues, as

demonstrated by the high quality and scope of specific equipment

replacement.

The multiple minor violations and security concerns / weakness

identified in the early security inspection were indicative of

a program that had regressed from the previous SALP evaluation.

Since the identification of these issues by the NRC, they have

16

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been resolved in a timely and extremely extensive manner during

the remainder of the assessment period.

The licensee's perfor-

mance significantly improved during the second half of the

assessment period.

During this period, there were nine safeguards events that were

reported as required. Most of the reportable events were

attributable to causes not under the licensee's control such as

equipment failures during the early part of the SALP period.

Only one reported event was under the licensee's control and

involved a plant staff member badged without a formal background

check. The event was promptly and completely reported.

Security organization positions and responsibilities are well

defined. The size of the security staff and the contract

security force was increased during the assessment period to

provide improved efficiency. The security force is considered

to be ample to implement the facility's physical protection

program.

The occurrence of only a few personnel errors shows that security

training and qualification program has made a positive contribu-

tion to the security organization's understanding of their duties

and responsibilities. The training program is well defined and

administered by a dedicated and resourceful staff.

2.

Conclusion

The licensee's performance is considered to be Category 1 in this

area. Although performance declined during the first quarter

of the evaluation period, the licensee's corporate and site

security management team significantly improved their system

and performance. The current trend of performance is improving.

3.

Board Recommendations

None.

H.

Outages

1.

. Analysis

Inspections of outage activities were conducted by the resident

inspectors during the following refueling outages:

Unit 1

January 11 - March 10, 1985

March 4 - April 10, 1986

Unit 2

September 6 - November 1, 1985

During the assessment period, there were also six inspections

of outage activities conducted by region based inspectors.

Inspection activities during the period included:

review of

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procedures, tests, and surveillances involving refueling tools

and equipment; witnessing core unloading and loading operations,

review of cutage inservice inspection results and modification

QA, review of reload safety evaluations, and witnessing of many

other outage activities. A few of the major activities witnessed

were:

a.

Replacement of Unit I upper internals

b.

Replacement of boric acid lines

c.

Control board modifications

d.

Installation of Reactor Vessel Level Indication

System (RVLIS)

e.

Steam generator snubber testing and rebuilding

f.

Limitorque EQ inspections and modifications

Two violations were noted during these inspections:

a.

Severity Level IV - Failure to investigate snubber seal

deterioration and possible fluid contamination.

(Inspection

Reports No. 50-282/85015(DRS); 50-306/85012(DRS)).

b.

Severity Level IV - Failure to. submit LER on snubber

performance.

(Inspection Reports No. 50-282/85015(DRS);

50-306/85012(DRS)).

These two violations related to performance of the large-bore

steam generator snubbers. The licensee has committed to and

initiated corrective action on these items. These violations

are not repetitive of violations identified during the previous

assessment period and they do not appear to have generic or

programmatic implications.

One LER is assigned to the Outage category. This event was the

accidental actuation of one train of safety injection during

simultaneous electrical and instrument maintenance. Thaugh this

potential problem had been recognized in the planning phase,

administrative controls over the work were not adequate.

Refueling activities generally are conducted in a well-organized

and efficient manner, however, some problems have been

experienced. A delay of several days during the Fall 1985

refueling outage was the result of mispositioning 11 fuel

assemblies on the grid plate during core reloading. These

assemblies had been positioned such that they straddled the

grid plate alignment pins.rather than being positioned on the

,

pins. As a result of the mispositioning, an assembly being

reloaded later became stuck and was damaged while being

extracted. Two other assemblies were also damaged during the

removal effort. These damaged assemblies were replaced. The

root cause of this problem was inadequate lighting in the

,

reactor vessel because of burned-out underwater lights.

Appropriate corrective action has been taken.

18

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At the end of each outage comprehensive testing is performed

to assure that the unit has been returned to a satisfactory

operating condition. Adequate time is scheduled to permit

this testing. This testing is generally detailed in the work

requests and also is followed personally by the individual

who requested the outage work. This personal attention by the

plant technical support staff assures project continuity from

design to testing and represents a strength in-the management

of the plant.

Scheduling of outage activities receives high priority at Prairie

Island. These planning efforts make possible_the performance of

outage tasks on a very compressed schedule.

For example, the

Unit I refueling outage in 1986, which-included replacement of

reactor upper internals, 100% eddy-current inspection of steam

generator tubes, antivibration bar replacement in both steam

generators, and major overhaul of the turbine-generator, in

addition to removal and reinstallation of all feel assemblier,

was completed in only 36 days.

Detailed planning is accomplished by a three person full-time

scheduling group. This group spends manths working on detailed

agenda to assure that critical paths are properly identified

and that other work can be accomplished althin the confines

1

which exist in time and space. During the actual performance

of outage work, this scheduling group supervises the outage,

conducts daily status and work planning seetings, and adjusts

the scheduled work as necessary to assure that the outage does

not become bogged down in any way. Meinbers of the planning

group have been selected for their ccmprehensive knowledge of

the facility and their extensive experience at Prairie Island.

2.

Conclusion

The licensee continues to be rated Category 1 in this area.

3.

Board Recommendations

None.

I.

Quality Programs and Administrative Controls

1.

Analysis

Quality programs (QA and QC) and administrative controls were

routinely assessed by the resident inspectors. 'In addition, one

routine and three special inspections were conducted durirg the

period by region-based inspectors.

i

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Three violations were noted during these inspections:

a.

Severity Level IV - Violation of 10 CFR 50.59 as a

result of inverter upgrading.

(Inspection Reports

No. 50-282/85024(DRP); 50-306/85022(DRP)).

b.

Severity level IV - Unplanned start of a diesel generator

because of failure to follow relay testing procedures.

(Inspection Reports No. 50-282/86007(DRP);

50-306/86007(DRP)).

i

c.

Severity Level IV - Electrical cover left off motor-operated

containment isolation valve and failure to adequately

control modification work in the control room.

(Inspection

Report No. 50-282/86007(DRP)).

All of these violations are indicative of weaknesses in plant

'

administrative controls. The number of violations has increased

to three from the two noted in the last SALP report.

'

One LER submitted during the report period is assigned to this

area. This LER discussed the diesel generator start reviewed

in Violation b. above.

An area of safety concern, related to Violations c. and d., was

identified by the resident inspectors during the assessment

period. This concern addressed the control of facility

modifications.

(Inspection Reports No. 50-282/85014(DRP);

50-306/85011(DRP)). Plant events which occurred and which

illustrate the concern are as follows:

a.

During Appendix R work in May 1985, an instrument air line

solder joint failed because of the line being moved. This

instrument air failure caused a reactor trip.

b.

In July 1985 a temporary cable splice failed thus disabling

many diesel generator auxiliaries. The splice may have been

stepped on during modification work.

c.

In August 1985 breaker 228, which provides safety-related

loads, was tripped accidentally by construction forces

working in the area.

d.

In October 1985 breaker 12 M, which supplies a large number

of safety-related motor control centers, was accidentally

tripped by personnel working on a plant modification.

e.

In May 1986 an electrical cover was left off a

motor-operated containment isolation valve.

(See

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Violation c. above). The conditions which resulted in

-

this error currently are being investigated and are

probably related to modifications made to the valve.

f.

Also in May 1986, during electrical work in the control

room, damage was done to the Unit I contrql rod step

'

counter wiring.

(See Violation d. above). This matter

.

was being investigated at the end of the assessment period.

A special inspection in the modification process area was

requested by the resident inspectors and was conducted by

,

region based specialists in October and November 1985. Their

inspection report (50-282/85021(DRS); 50-306/85019(DRS))

contained six specific recommendations for the licensee.

Although the licensee has devoted much management attention,

including corporate attention, to the reconnendations, final

resolution had not been achieved at the end of the report period.

t.

The NRC considers this subject to be a matter of continuing

high priority, and notes that management of modifications has

'

also been highlighted by licensee's consultant, Delian Corp.,

as an area needing some improve. ment.

l-

As a result of questions raised at the Kewaunee Plant regarding

environmental qualification of Limitorque valve wiring, the

resident inspectors notified the licensee in a meeting on

December 13, 1985 of the concerns which had been raised. The

i

licensee promptly made plans for visual inspection of all valve

operators during upcoming outages.

(Licensee considered and

q

rejected the approach of taking safety-related valves out of

service for inspections during plant operation.) As of the end

'

of the appraisal period, all Unit I valves had been inspected

and wiring of questionable qualification had been replaced.

Unit 2 inspections are scheduled to be performed during the

next outage. Region based inspectors reviewed the status

of this subject during a special inspection on February 6 and 7,

1986.

Potential enforcement action remains under NRC review.

,

During this assessment period the licensee instituted a program

to help shift supervisors obtain their college degrees. As of

the end of the period, two supervisors had been degreed and three

1

others were well along in their studies. When adequate numbers

have been so trained, the licensee plans to assign Shift Managers

to each shift. These Managers would supervise the operating

crews and by virtue of their technical degrees, would simultan-

eously satisfy the Shift Technical Advisor requirements. These

changes should significantly strengthen the Operations staff.

Two other areas in which licensee has taken special efforts to

improve plant safety are:

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a.

Review of Davis-Besse event - NSP formed a special task

force to study the event and to develop lessons-learned for

application to NSP plants. This is a continuing effort.

b.

Reliability Study of Auxiliary Feedwater System - In

cooperation with a number of consultants, licensee used

Probabilistic Risk Assessment (PRA) methods to evaluate the

reliability of the Prairie Island AFW system. The report of

this study was provided to for NRR review in April 1986.

General conclusions from the report are favorable.

2.

Conclusion

The liceasee continues to be rated Category 2 in this area.

3.

Board Recommendations

None.

J.

Licensing Activities

1.

Analysis

This evaluation represents the integrated inputs of the Project

Manager (PM) and those technical reviewers who expended signifi-

cant amounts of effort on PINGP licensing actions during the

assessment period.

The basis for this appraisal was the licensee's performance in

support of licensing actions that were either completed or had

a significant level of activity during the assessment period.

There were a total of 25 active actions at the beginning of the

assessment period. Twenty-one actions were added for a total of

46 actions by the end of the assessment period. We have closed

33 actions during the assessment period and have 13 active

actions at the end of this assessment period. These actions and

a partial list of completions consisting of amendment requests,

exemption requests, responses to generic letters, TMI items, and

licensee initiated actions are:

21 Multi-Plant Actions (15 completed). Some of the completed

.

actions in this category are:

!

Equipment Qualifications of Safety Related Electrical

Equipment (MPA B-60)

'

Control of Heavy Loads Phase II (MPA C-15)

<

Instrumentation to follow the course of an accident

i

Reg Guide 1.97 (MPA A-17)

Many Salem ATWS items (i.e., Items 4.3, 4.2.1, 4.2.2, 3.2.1,

etc.)

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Diesel Generator Reliability (GL 84-15) (MPA D-19)

14 Plant-Specific Actions (11 completed).

Some of the completed

actions in this category are:

Reload Safety Evaluation method for Control Rod Drop

Analysis

Schedular Exemption Request for Requirement of Appendix R

of 10 CFR 50.48c

ECCS Error and Core Height Fq (Kz curve verification only)

Rod Cluster Control Guide Thimble Plug Removal

Capsule Surveillance Summary Report Exemption

11 TMI (KUREG-0737) Actions (7 completed). Some of the completed

actions in this category are:

Small break LOCA Analysis item II.K.3.30

Safety parameter Display System Item I.D.2

Compliance with 10 CFR 50.46 Item II.K.3.31

Technical support center Item III.A.1.2

Meteorological Data Upgrade Item II.A.2.2

Emergency Operations Facility Item A.I.2

This appraisal also considers the remaining number of backlog

licensing issues that are carried over to the next assessment

period. The remaining backlog reflects all existing issues for

which the review effort has not yet been completed by the staff

and may need additional input by the licensee in order to

achieve a satisfactory resolution. At the end of this assessment

period the breakdown of unresolved licensing issues for Prairie

Island stands as follows:

MPA

6

Plant Specific

3

TMI (issues)

4

Total

13

There has been a 52.2% reduction in the backlog of licensing

issues during this assessment period. The 52.2% reduction

exceeds by far the performance of all past assessment periods

and the 13 remaining issues is the lowest for all licensed

'

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operating plants in the country. The low number of remaining

open issues demonstrates the company wide aggressive

participation with the NRC Project Manager to resolve safety

issues.

a.

Management Involvement and Control in Assuring Quality

During this assessment period, the licensee's management

actively participated in licensing activities and kept

abreast of all current and anticipated licensing actions.

Management participation was evident in the response to

our Generic Letter 83-28 and the scheduling and planning

of the plant modifications associated with this issue.

In

addition, management involvement in licensing activities

assured timely response to the Commission's requirements

related to TMI NUREG-0737 issues and preparing the new

upper plenum ECCS injection model. The licensee's

management has consistently exercised good control over

its internal activities and contractors and has maintained

effective communication with the NRC staff. This was

exemplified in the manner in which the verification of

the K(Z) curve was handled.

In addition, the licensee's

management actively participated with the NRC Project

Manager to reduce the backlog of licensing actions within

NRR. The 33 actions completed attest to the licensee's

management. involvement and represent 72% of the total

number of PINGP licensing actions in force during the

period. The licensee's management maintained effective

communication with the staff. The licensee has met

schedules or informed the Project Manager at an early

date of schedular problems.

One area where management attention could be increased is

in the timeliness of submittals for amendment requests

that are tied to plant restart after a refueling outage.

The amendment request dated January 13, 1986 which was

tied to the Unit No. 1 startup scheduled for the first

week in April 1986 is the case in point; two months were

available for the staff and licensee to review, interact,

notice and prepare documentation. A minimum lead time of

five months should be allowed to permit adequate processing.

b.

Approach to Resolution of Technical Issues from a Safety

Standpoint

The licensee's management and its staff demonstrated sound

technical understanding of issues involving licensing

actions. The licensee demonstrated extensive technical

expertise in technical areas involving the resolution of

technical areas associated with licensing actions. Sound

technical approaches are taken by the licensee when

meeting with the NRC. These attributes were demonstrated

l

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in the resolutions of issues related to the authorization

of steam generator tube sleeving, the safety evaluation of

the reload analysis method for control rod drop and the

environmental qualification of safety-related electrical

equipment.

When the licensee deviated from the staff guidance as in

the implementation of the inadequate core cooling instru-

mentation and the review of the diesel generator reliability

requirement, the licensee consistently provided good

technical justification for such deviations. The NRC

technical reviewers were able to complete their Safety

Evaluations on the basis of the original submittals with

no more than telephone questions for clarification.

In

the case of the amendment request associated with steam

generator tube sleeving, the submittal was complete and

required only telephonic discussions for clarifying minor

staff comments in order to complete the safety evaluation

and issue the amendment.

The licensee's visit to NRC to discuss forthcoming requests

for staff actions prior to formal submittals demonstrates

the licensee's desire to minimize potential problem areas

that could arise during the NRC staff reviews. This

approach has been consistently found to be beneficial to

both the staff's and licensee's efficiency in processing

such actions.

c.

Responsiveness to NRC Initiatives

The licensee has been consistently responsive to NRC

initiatives. Throughout the rating period, the licensee

exhibited a superior effort to meet or exceed established

commitments which contributed to the reduction of open

issues (i.e., MPA's, plant specifics, and TMI NUREG-0737

actions). When the NRC desired clarification or additional

information during the review of the licensee's submittals,

the responsiveness by the licensee has been judged as

excellent.

In addition, when clarification or additional

information could not adequately be resolved by conference

calls and/or correspondence, the licensee has met on short

notice with the NRC as soon as they were made aware of our

concerns. Typical examples of such performances occurred

when the NRC expressed concern with the preparation of

amendment package dealing with upgrading the technical

specification and the upper Plenium Injection Evaluation

Model to meet the requirement of 10 CFR 50.46 Appendix K.

In these examples, the licensee gave oral presentations

that exhibited thoroughocss and sound technical judgement.

25

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The licensee is waiting for NRC to take positions on most

j

submittals related to the remaining open issues at the end

of the assessment period. The licensee committed to

reasonable schedules for those open issues where additional

information is needed in order to complete the NRC review.

d.

Staffing

The licensee has a sufficient staff to provide adequate and

timely response to our safety concerns. The staff is

knowledgeable of our regulations, and the engineering

aspects of the plant which results in a satisfactory

resolution of licensing issues.

In addition, the licensee's

scheduled dates for completion of NRC items are rarely

missed. This is an indication that adequate staffing

exists.

2.

Conclusion

The licensee continues to be rated Category 1 in this area.

3.

Board Recommendations

None.

K.

Training and Qualification Effectiveness

1.

Analysis

During the assessment period, examinations were administered to

six Reactor Operator and six Senior Reactor Operator candidates.

Five Reactor Operators and three Senior Reactor Operators passed

the examinations. This passing rate is below the national

passing average. Also, in March 1985, a requalification exami-

nation was conducted by Region III at Prairie Island. Five of

the ten Senior Reactor Operators and two of the three Reactor

Operators examined failed the written requalification examination.

As a result of these failures, Region III issued a Confirmatory-

Action Letter dated April 26, 1985, to Northern States Power

Company stating that the individuals who failed the requalifica-

tion examination would be prohibited from independently performing

licensed duties until they have satisfactorily completed an

accelerated requalification program and passed a written

, examination approved by the Nuclear Regulatory Commission.

)

At a June 12, 1985, meeting, NSP personnel presented the results

of their review of the retraining program and the measures they

-

planned to take to improve it.

26

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In September 1985, Region III Operator Licensing Section staff

reviewed the final results of the accelerated requalification

efforts for those who failed the Region III examination in

March 1985 and found that effort to be acceptable.

In the previous assessment period, 23 Senior Reactor Operators

and 11 Reactor Operators were examined. Of these, 15 Senior

Reactor Operators and 6 Reactor Operators passed. The current

trend in this area is unchanged.

Based on this history of examination results, the operator

licensing training and retraining program at Prairie Island

would be considered marginal. However, since the events of 1985,

the licensee has instituted a set of actions intended to address

the NRC concerns. These actions include:

a.

Requiring all licensed personnel to attend eight to 12

requalification lectures per year.

b.

Requiring quizzes each training cycle (every six weeks) and

providing feedback to all trainees regarding their quiz

results.

c.

Tailoring the annual requalification exams in a format

similar to the NRC requalification exam format.

d.

Updating the reference systems descriptions (B Sections),

e.

Improving the effectiveness of feedback from the plant

forces to the training forces.

f.

Updating the simulator to reflect plant changes.

g.

Improving training methods and instructor qualifications.

Progress has been made in these areas to improve the

effectiveness of training efforts.

In addition, NSP has been participating in the INP0 accreditation

process for their training program. At the end of the assessment

period, INP0 had accredited the Prairie Island Maintenance and

Operations training programs.

A good measure of training effectiveness and the qualification

.

of the operating crew is the superb operating record at Prairie

Island. As noted in Section A above, Unit I was the best in

the nation in capacity factor for the period 1983-85 and Unit 2

was fifth best for the same period. The operating crews

represented by the shift supervisors, lead operators, other

licensed operators, and unlicensed outplant operators, plus the

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support groups have demonstrated their ability to get the job

done and to handle all problems, both routine and unexpected,

in exemplary fashion. This ability is a reflection of both

pride of work and qualification to do the job.

2.

Conclusion

The licensee is rated Category 2 in this functional area. The

trend during the assessment period clearly has been toward

improvement.

3.

Board Recommendations

None.

,

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4

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V.

SUPPORTING DATA AND SUMMARIES

,

A.

Licensee Activities

1.

On January 12, 1985, Unit I was shut down for the ten year

in-service inspection and refueling outage. Major activities

performed during the outage included:

reactor vessel weld

inspection, steam generator tube eddy current inspection,

refueling, reactor vessel level indicating system (RVLIS)

installation, and control room panel modifications. Unit I

was restarted on March 10, 1985.

2.

On May 8, 1985, with Unit I at 100% power, an instrument air

line joint separated and the resulting loss of air caused a steam

generator feedwater regulating valve to close. This resulted in

a reactor trip. The unit was off-line for approximately 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

3.

On May 9, 1985, with Unit I restarting after tripping on May 8,

Unit I again experienced a reactor trip. This second trip was

caused by low steam generator level plus feedwater flow / steam

flow mismatch. Return to the power grid was delayed an

additional four hours.

4.

Extensive 10 CFR 50 Appendix R work was completed during this

SALP period. This work involved wrapping cable trays and

conduits in certain fire areas with an approved one-hour fire

barrier. This work was completed on June 14, 1985.

5.

On September 6, 1985, Unit 2 was shut down for the ten year

in-service inspection and refueling outage. Major activities

performed during the outage included:

reactor vessel weld

inspection, steam generator antivibration bar (AVB) installation,

steam generator snubber removal testing and reinstallation,

reactor vessel level indication system (RVLIS) installation,

boric acid line replacement, and control room panel modifications.

Unit 2 was restarted on November 1, 1985.

6.

On September 15, 1985, with Unit 1 at 100% power, troubleshooting

activities in the main generator voltage regulator produced a

voltage transient which resulted in a reactor trip. Cause of the

trip was incorrect troubleshooting techniques. The unit was

off-line for approximately 14 hours1.62037e-4 days <br />0.00389 hours <br />2.314815e-5 weeks <br />5.327e-6 months <br />.

7.

On March 4, 1986, Unit I was shut down for a routine refueling

outage. Major activities performed during the outage included:

steam generator tube eddy current inspection; refueling; replace-

ment of upper internals; steam generator snubber removal, testing,

and reinstallation; and steam generator antivibration bar

installation. Unit I was restarted on April 10, 1986.

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8.

On April 10, 1986, during a restart of Unit 1 after refueling,

a reactor trip occurred at low power level caused by low steam

generator level plus feedwater flow / steam flow mismatch. The

reactor was restarted and the generator was placed on line

approximately six hours later.

9.

Improvements made to facilities and plant systems during this

assessment period included:

Phase 2 expansion of spent fuel

storage capacity; reactor vessel level indicating system (RVLIS)

installation; relocated steam inlet valves for 11 and 22

auxiliary feedwater pumps; modernization of main steam reheaters;

turbine generator emergency and auto stop trip DC power separa-

tion; and upgrading of plant protected area security equipment

including main vehicle gate, personnel screening, and

surveillance cameras.

.

B.

Inspection Activities

1.

During the period of August 19 through August 23, 1985, a special

security regulatory effectiveness review (RER) was conducted to

evaluate and analyze the effectiveness of the licensee's safe-

guards program.

2.

A special safety inspection was conducted during the period of

October 28 to November 15, 1985 by region based specialists.

This inspection was an in-depth assessment of the licensee's

modification program and related activities and was prompted

when modification activities began impacting plant operating

equipment.

3.

A special reactive inspection was conducted on February 6 and 7,

1986 by region-based specialists to investigate the use of

non qualified wires in 10 CFR 50.49 designated environmentally

qualified (EQ) limitorque valve operators identified in IE

Information Notice No. 86-03.

)

1

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30

_. _

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~

.

.

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INSPECTION ACTIVITY AND ENFORCEMENT

PRAIRIE ISLAND NUCLEAR GENERATING PLANT DOCKET NOS. 50-282 AND 50-306

Inspection Reports

Unit 1 - 84013, 84016-18, OL-85001-02, 85001-05, 85007-24, 86002-05,

86007

Unit 2 - 84015, 84017-19, 85001, 85003-22, 86002-05, 86007

FUNCTIONAL

NO. OF VIOLATIONS IN EACH SEVERITY LEVEL

AREA

I

II

III

IV

V

DEV.

.

Plant Operations

3

2

Radiological Controls

1

Maintenance

'

Surveillance

3

3

Fire Protection

Emergency Preparedness

Security

3

Outages

2

Quality Programs and

Administrative Controls

3

Licensing Activities

Training and Qualification

Effectiveness

'

Totals

0

0

0

15

5

0

1

1

4

+

b

31

_ _ _ _ _ - . _

_

. - _ _ . _ .

'.

C.

Investigations and Allegation Review

An allegation was made in an anonymous call to the Region III office

on April 23, 1986. A letter has been sent requesting the licensee

to review this matter.

,

D.

Escalated Enforcement Actions

-

1.

Civil Penalties

No civil penalties were issued during this assessment period.

2.

Orders

A confirmatory Action Letter (CAL) was issued by the NRC on

April 26, 1985 after the poor performance on the NRC administered

operator annual requalification examination. The licensee

removed the affected operators from performing licensed duties

and placed them on an accelerated training program. The NRC

reviewed and approved the June 14 and July 1 re-examinations

prior to administration by the licensee. A review of the

examination grading resulted in passing grades for all the

individuals and the CAL is considered closed.

E.

Licensee Conferences Held During Appraisal Period

1.

On February 25, 1985, a management conference was held at

Region III to present the licensee with the findings

of the SALP 5 report.

2.

On June 12, 1985, a management meeting was held at Region III

to discuss the poor performance exhibited during the annual

licensed operator requalification examination and the measures

the licensee planned to take to ensure improved performance in

this area.

3.

On April 18, 1986, the NRC Region III Regional Administrator,

the NRC Director of BWR Licensing, and the NRC Region III

Director of Division of Reactor Projects met with plant and

corporate officials at Corporate Headquarters to discuss the

modified inspection program.

Prairie Island was one of three

plants selected in Region III by virtue of exceptional past

performance and SALP ratings for this program.

32

- - _ .

_. - _.

_ -.

_ _ _ _ _

__

'.

.

F.

Review of Licensee Event Reports and 10 CFR 21 Reports

1.

Licensee Event Reports (LERs)

New LER reporting requirements have been implemented since the

previous SALP period which incorporated changes in the proximate

cause codes and definitions of the proximate causes. Therefore,

be aware that a comparison of the number and proximate cause

codes of LERs submitted during this assessment period with the

submittals during previous periods would not provide meaningful

comparative information.

a.

The LERs for this evaluation period include 1-85-01 through

1-86-05 for Unit 1 and 2-85-01 through 2-86-02 for Unit 2.

PROXIMATE CAUSE*

SALP 6

Personnel Error

12 (0.67)**

Design, Manufacturing,

Construction / Installation

7 (0.39)

External

0

Defective Procedure

1 (0.06)

Management / Quality

Assurance Deficiency

3 (0.17)

Other

3 (0.17)

TOTAL

26 (1.44)

  • Proximate Cause is the cause assigned in accordance with

NUREG-1022, " Licensee Event Report System."

    • Numbers in parenthesis are the average number of events

per month,

b.

Evaluation

The monthly rate of LERs is slightly reduced from 1.88 in

the previous SALP rating period to 1.44 in the current

period.

In addition, those events attributed to personnel

error have been reduced in rate from 0.82 to 0.67.

These

improvements are due in part to licensee efforts at error

reduction during the rating period. We encourage the

licensee to continue efforts to reduce the number of LERs

'

especially those related to personnel errors.

.

4

l

'

33

!

'.

.

Review of the LERs indicated that the information given,

particularly later in the assessment period, generally

provided a clear and adequate description of,each event;

the entries reviewed were correct and the codes agreed

with the information in the narrative. The. licensee

voluntarily submitted three reports (LERs 1-85-03, 1-85-16,

1-86-2) that were not required by reporting requirements

of 10 CFR 50.73 but which are included in the table above.

The NRC Office for Analysis and Evaluation of Operational

Data (AE0D), reviewed several LERs early in the SALP

period and noted a number of deficiencies. The principle

identified weaknesses' involve lack of adequate discussion

of root cause, lack of adequate safety assessment,

inadequate discussion of corrective actions and personnel

errors, and failure to reference previous similar events.

Discussions have been held with the licensee on this

,

matter and improvements in LERs have already been seen.

2.

10 CFR 21 Reports

a.

In an April 15, 1985 letter to the licensee, Chicago Tube

and Iron (CT&I) transmitted Part 21 notifications that CT&I

had received from their suppliers Hub, Inc. and Phoenix

Steel Corporation. The problem related to the identification

of a small length (21'7") of 8" Schedule 120 pipe as being

1

Schedule 160. Reanalysis of the support constructed of this

pipe was done by Teledyne Engineering Services who concluded

that Schedule 120 pipe was adequate for the service.

b.

In a letter dated November 26, 1985, Region III informed the

licensee of the results of an inspection of the implementa-

tion of Exo-Sensors, Inc., Quality Assurance program that

was conducted by the Vendor Program Branch. This inspection

was initiated as a result of allegations that Exo-Sensors,

Inc., had failed to report a deficiency under 10 CFR Part 21

and that serious deficiencies existed with their Quality

Assurance program. The licensee responded in a letter dated

December 10, 1985 indicating that hydrogen analyzers had

been purchased from Exo-Sensors, Inc. A maintenance history.

for the instruments was also provided.

It was concluded by

licensee and resident inspectors that the Exo-Sensors, Inc.,

equipment is meeting procurement requirements and technical

specifications and that the equipment maintenance history is

<

also acceptable.

G.

Licensing Actions

.

1.

NRR/ Licensee Meetings

Upper Plenum Injection - Evaluation Model

January 10, 1985

Reactor Upper Internal (Top Hat Design)

June 26, 1985

,

34

.

4

s

_.

. _ _ __ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _

'

.

Upper Plenum Injection Evaluation Model

June 28, 1985

Upper Plenum Injection Evaluation Model

and Technical Specification Upgrade

November 22, 1985

2.

NRR Site Visits / Meetings

SALP 5 Meeting and Site Visit

Feb 25 - Mar 1, 1985

Site Visit / Meeting / Resident Inspector

June 19-20, 1985

Site Visit / Meeting / Resident Inspector

Unit 2 Refueling Outage

October 7-10, 1985

Site Visit / Meeting / Resident Inspector

March 11-14, 1985

Unit 1 Refueling Outage

3.

Commission Meetings

None.

4.

Schedular Extensions Granted

Fire Protection Appendix R 10 CFR 50.48c

May 7, 1985

Surveillance Capsule Summary Report

Extension

.

March 17, 1986

i

Confirmatory Order Supplement 1

NUREG-0737

February 5, 1986

5.

Reliefs Granted

None.

6.

Exemptions Granted

None.

7.

License Amendments Issued

Amendment No.

Title

Date.

72/65

Operability period of

February 15, 1985

cooling H2O header

73/66

Thirteen chanc% i)

June 25, 1985

technical 94 ifb . tion

74/67

Spent Fue; anip,...aj

June 26, 1985

Cask Movement over

Spent Fuel Pool No. 1

75/68

Shunt trip and Manual

June 26, 1985

reactor trip circuitry

GL 83-28 Item 4.3

35

-

' ;

-

.

,

'

/

,

I

J

76/69

Steam Generator Tube

October 11, 1985

. ,

Sleeving

1 ,

77/70,'

Fuel Reload Technical

April 3, 1985

Specification Change

8.

Emergency Technical Specification

-

None.

}

,

9.

Orders Issued

'

,

None.

'

10.

NRR/ Licensee Management Conference

None.

.

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i

.

4

6

8

1

f

4

l

i -

6

3

_ . . . .

--

-

- - -