ML20196A441

From kanterella
Jump to navigation Jump to search
Forwards 881027 Enforcement Conference Summary Re Insp Repts 50-369/88-24,50-370/88-24,50-369/88-29 & 50-370/88-29.Issues Re Operability of Hydrogen Skimmer Sys & Inoperability of Safety Sys Due to Inadequate post-mod Testing Discussed
ML20196A441
Person / Time
Site: McGuire, Mcguire  Duke Energy icon.png
Issue date: 11/25/1988
From: Ernst M
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To: Tucker H
DUKE POWER CO.
References
NUDOCS 8812060008
Download: ML20196A441 (62)


See also: IR 05000369/1988024

Text

7

.

n

+

-.

-

.

.

-

_

__ _

.}

NOV 2 51988

$,'mau

Gf

.,

!

Docket Nos. 50-369, 50-370

License Nos. NPF-9 NPF 17

.

,

. '

h

h

Duke Power Company

l

f ATTN: Mr. H. B. Tucker, Vice President

C

Nuclear Production Department

i

422 South Church Street

Charlotte, NC 28242

j

!

Gentlemen:

SUBJECT:

ENFORCEMENT CONFERENCE SUMMARY

r

(NRC INSPECTION REFORT NOS. 50-369/88-24, 50-370/88-24 AND

,

50-369/88-29,50-370/38-P.9)

This letter refers to the Enforcement Conference held at our request on

!

t

October 27, 1988.

This meeting concerned activities authorized for your

[

McGuire facility.

The issues discussed at this conference related to

l

l

1

operability of the Hyrdrogen Skimmer (VX) system and inoperability c? safety

systems due to inadequate post modification testing.

A brief sumary, a list

,

j

of attendees, and a copy of your handout are enclosed.

We are continuing our

l

review of these issues to determine the approp"fate enforcement action.

6

1

\\

5

In accordance with Section 2.790 of the NRC's "Rules of Practice," Part 2,

i

T1tle 10, Code of Federal Regulations, a copy of this letter and its enclosures

'

will be placed in the NRC Public Document Room.

]

Should you have any questions concerning this matter, please contact us.

Sincerely,

l

(Original signed by M. Ernst)

I

Malcolm L. Ernst

'

'

Acting Regional Administrator

Enclosures:

1.

Enforcement Conference Sumary

l

2.

List of Attendees

j

3.

Handout

t

t

<gcw/ enc 15:

!

W . 1. McConnell, Station Manager

l

,

f

'

Jenior Resident inspector - Catawba

3

State of North Carolina

i

f

'

bec w/ enc 15:

(See page 2)

l

4

r

GG120f

k

69

j(

j

DR

PDC

JL /

.

-

-

,

' ,

,

'

NOV 2 5 199g

'

Duke Power Company

2

b> r: w/ enc 15:

NRu Resident Inspector

Das Technical A:sistant

  1. Hrnd, NRR

Docun>ent Con *.rol Desk

l

I

I

I

$)n

hv

bh)'f

5 o ',

~

BBonser

t'Peebles

/dN;[,nlee

Jfb,\\/88

< Acyes

ven

s

hr

w

11/A3/88

11/p/88 [/

11/

11/>?/88

11d3/88

11/ ' 88

7

J

/

NOV 2 5 IllW

xffi

' '

ENCLOSURE 1

4

ENFORCEMENT CONFERENCE SU N RY

On October 27, 1988, representatives from Duke Power Company (OPC) met with the

NRC in the Region !! office in Atlanta, Georgia to discuss operability of the

Hydrogen Skimmer (VX) system and the inoperability of sefety systems due to

inadequate post modification testing.

Following opening remarks by J. P. Stohr

NRC, Ri! Acting Deputy Regional

Administrator, DPC gave two presentations (see Enclosure 3) which addressed NRC

concerns on the subjects listed above.

On the VX system, in addition to

covering a system overview, a sequence of events, and causes and contributing

factors, DPC addressed specific NRC concerns regarding preoperational testing

.

of the VX system, a decision to enter Mode 4 on Unit 2 with VX flows below that

given in the FSAR, and OPCs operability determination process.

DPCs

i

presentation on the post modification testing program covered an

'

overview / sequence of events, a safety analysis of each of the valves found to

have problems, and corrective actions to enhance DPCs post maintenance / post

modification testing program.

The NRC is presently considering enforctment action on these issues.

This

meeting served to enhance Region II's understanding of the issues and DPCs

corrective actions.

S

,

!

}-

)

-

-

HOV 2 5 W

'

'

,

f

ENCLOSURE 2

LIST OF ATTENDEES

U.S. Nuclear Regulatory Coninission

J. P. Stohr, Acting Deputy Regional Administrator

C. W. Hehl, Deputy Director, Division of Reactor Projects (DRP)

A. F. Gibson, Director, Division of Reactor Safety (DRS)

1

E. W. Merschoff, Deputy Director, DRS

G. R. Jenkins, Director, Enforcement and Investigation Coordination Staff

(EICS)

V. L. Brownlee, Branch Cr'ef DRP

D. Hood, McGuire Projec ..anager, Office of Nuclear Reactor Regulation (NRR)

F. Jape, Section Chief, uRS

W. T. Orders. Senior Resident Inspector, Catawba, DRP

B. R. Bonser, Project Engineer, DRP

F. K. VanCO)rn, Senior Resident Inspector, McGuire, DRP

D. J. Nelsen, Resident Inspector, McGuire DRP

,

R. P. Croteau, Resident inspector, McGuire, DRP

B. Uryc, Enforcement Coordinator, EICS

Duke Power Company

H. B. Tucker Vice President, Nuclear Production

T. L. McConnell, Station Manager, McGuire

N. Rutherford, Manager, Licensing

B. H. Hamilton, Superintendent of Technical Services. McGuire

W. M. Sample, Superintendent of Maintenance, McGuire

R. O. Sharpe, Compliance Engineer

B. L. Peele, Principal Engineer, Design Engineering

1

,

y

, . ' "

,

..

..

. . . .

.

- - -- - - - .-__.-. _-__.__,.__---...,--.. ._-_______________

-r

.. , , ,

-

NOV 2 5 m

ENCLOSURE 3

o:

'

i

e

O

%

DUKE POWER COMPANY /NRC

ENFORCEMENT CONFERENCE

OCTOBER 27, 1988

VX OPERABILITY

1.

INTRODUCTORY REMARKS

T. L. McCONNELL

11. OVERVIEW

T.

L. McCONNELL

lli. SEQUENCE OF EVENTS

B. H. HAMILTON

IV. ROOT CAUSE AND CONTRIBUTING FACTORS

B. H. HAMi LTON

\\

V. CONCERNS TO BE ADDRESSED

B . H . HAM I LTON

A.

PREOPERATIONAL TESTING OF VX SYSTEM

B. H. HAMILTON

B.

DECISION TO ENTER MODE 4

B. H. HAMILTON

C.

DPCo OPERABILITY DETERMINATION PROGRAM

B. H. HAMILTON

D.

SAFETY ANALYSIS

B. L. PEELE

IV. SUMMARY

T.

L. McCONNELL

FUNCTIONAL VERIFICATION PROBLEMS

1. OVERVIEW

T.

L. McCONNELL

11. SEQUENCE OF EVENTS

T.

L. McCONNELL

lit. ROOT CAUSE/ CORRECTIVE ACTIONS

W.

M.

SAMPLE

IV. SAFETY SIGNIFICANCE

W.

M. SAMPLE

V. SUMMARY STATEMENT

T.

L. McCONNELL

CLOSING REMARKS

T.

L. McCONNELL

s

'

.-

- _ _ _ _ _ - _ - _ _ _ . _ _ _ _ _ _ _ _ _ - _ _

_ _ _ . .

_

_

_.

_

_

_

._

. _ .

._.

-

_ _ _ -

O

.

VX OPERABILITY

'

,

OVERVIEW

,

.

SEE ATTACHED SIMPLIFIED SCHEMATIC OF THE VX SYSTEM (HYDROGEN

SKIMMER PORTION ONLY).

UNIT 1

DURING A UNIT 1 CONTAINMENT CLOSEOUT INSPECTION IN NOVEMBER OF

1987, NRC PERSONNEL NOTICED THAT A HYDROGEN SNIMMER (VX)

SYSTEM DAMPER APPEARED TO BE CLOSED.

OPERATIONS PERSONNEL

INSPECTED AND VERIFIED THAT EACH VX SYSTEM DAMPER WAS IN ITS

CORRECT PRE-OPERATIONAL POSITION WITH THE EXCEPTION OF ONE DAMPER

QUESTIONED BY THE NRC INSPECTOR.

THE CORRECT POSITION 'dAS

VERIFIED BY PAINT SHADOWS ON THE DAMPER ACTUATORS CREATED PRIOR

TO UNIT 1 CRITICALITY.

THE QUESTIONED DAMPER WAS ONLY SLIGHTLY

MISPOSITIONED IN THE CLOSED DIRECTION.

SINCE THERE WAS NO PROCEDURE TO ASSURE PROPER DAMPER POSITIONS ON

THE VX SYSTEM, NRC PERSONNEL WERE CONCERNED ABOUT THE UNIT 2

DAMPER POSITIONS.

STATION PERSONNEL AGREED TO DO VX FLOW BALANCE

TESTS FOR BOTH UNITS DURING THElR NEXT REFUELING OUTAGES.

UNIT 2

AT THE END OF THE JULY 1988 REFUELING OUTAGE, PERFORMANCE

PERSONNEL TOOK "AS FOUND" FLOW MEASUREMENTS USING A HAND HELD

VELOMETER ON BOTH TRAINS OF THE UNIT 2 VX SYSTEM.

SOME VX SYSTEM

DAMPER COMPARTMENT FLOWS DID NOT MEET FSAR REQUIREMENTS AND TWO

DAMPERS, BOTH SERVING THE REACTOR HEAD AREA, WERE FOUND CLOSED,

ALL DAMPERS WERE ADJUSTED IN AN ATTEMPT TO ACHIEVE FLOW RATES

LISTED IN THE FSAR.

THIS WAS UNSUCCESSFUL BECAUSE SETTING THE

.

o

..

HYDROCEN SKINMER

.

AND CONTAINMENT AIR RETURN SYSTEM (VI)

PRESENT ARRANCEMENT

,.,

.,,

s

..

==

/

/

r'

&

$

HSF-1A

BSF-15

,

P

/

/

1

I

1 f

IVX1A

IVX25

l

l

UPPER CONTAINMENT

_

_

_

_

LOWER CONTAINMENT

g

g

,

RING HEADER (EMBEDDED IN CRANE WALL)

I

h'

DAMPERS (TTPICAL)

l

&

/

\\

yW

/

,

\\

/

/

i

\\

/

N

/

/

%

's'%

"'" s

%

,,

!

!

CONTAINMENT

t

..

REACTOO BU1LDING

.-

i

l

l

l

- - - - -

--

. . .

_ ___

__ ~

.

.

.

.

DAMDERS FOR ONE TRAIN TO MEET FSAR FLOWS WOULD CAUSE FLOW RATES

i

FOR THE OTHER TRAIN TO Fall THE FSAR FLOW REQUIREMENTS.

FINAL

FLOWS WERE MEASURED WITH A VELOMETER AND LATER TRAIN A FLOWS WERE

CONFIRMED WITH THE MORE ACCURATE FLOW HOOD.

DESIGN ENGINEERING

(D.E.) PERSONNEL THEN BEGAN AN EVALUATION ON THE NEW VX SYSTEM

FLOW RATES.

PLANT PERSONNEL TERMINATED THE FLOW BALANCE TEST USING THE MORE

ACCURATE FLOW HOOD BEFORE COMPLETING TESTING ON TRAIN B OF THE VX

SYSTEMS AND UNIT 2 ENTERED MODE 4 BASED ON A VERBAL OPERABILITY

DETERMINATION FROM D.E.

RATIONALE FOR THIS DECISION WILL BE

DISCUSSED LATER.

LATER THAT DAY, D.E.

ISSUED A WRITTEN

OPERABILITY DETERMINATION FOR VX BASED IN PART ON THE

AVAILABILITY OF THE OPERABLE HYDROGEN MITIGATION SYSTEM TO

SUPPORT THE OPERABILITY OF THE VX SYSTEM.

IN THClR REVIEW THE

NEXT WEEK, THE NRC JUDGED THE OPERABILITY DETERMINATION BASED ON

THAT ASSUMPTION TO BE INADEQUATE.

WE AGREE WITH THi NRC

DETERMINATION.

PERFORMANCE PERSONNEL COMPLETED THE ACCESSIBLE COMP /RTMENT FLOW

MEASUREMENTS ON TRAIN B OF THE VX SYSTEM USING THE MORE ACCURATE

FLOW HOOD DEVICE.

A NEk UNIT 2 OPERABILITY DETERMINATION WAS

ISSUED BY D.E.

IT CONCLUDED THAT THE PRESENT FLOW BALANCE

CONDITION OF THE VX SYSTEM WAS SUFFICIENT AND WAS CONSIDERED

OPERABLE.

THE NRC HAS SUBSEQUENTLY REVIEWED THIS OPERABILITY

STATEMENT AND HAS AGREED WITH iT.

UNIT 1 FOLLOW-UP

IMMEDIATELY AFTER SHUT 10WN FOR THE CURRENT UNIT 1 OUTAGE, ALL

DAMPERS WERE VERIFIED OPEN AND THElR POSITIONS WERE MARKED.

THE

UNIT 1 VX FLOW BALANCE TEST WAS CONDUCTED USING THE FLOW HOOD

METHOD.

ALL FLOWS MET THE NEW ACCEPTANCE CRITERIA DEVELOPED

EXCEPT FOR TRAIN A OF THE PRESSURIZER CAVITY AND BOTH TRAINS OF

THE REACTOR HEAD AREA.

THE IMPACT OF THESE LOW FLOWS WILL BE

DISCUSSED LATER.

,-

-

- - - - -

_ _ _ _ _ _ _ _

_ - - - - - - -

_ _ _ _

- - - - - - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - - - _ _ _ _ _ _ _ _ .

.

e

!

e

!

,

'

<

VX OPERABILITY

.

.

SEQUENCE OF EVENTS

I

,-

DATE

TIME

EVENT

.

NRC PERSONNEL NOTICED THAT SOME UNIT 1 VX

11/08/87


SYSTEM DAMPERS APPEARED TO BE CLOSED.

,

t

NRC PERSONNEL QUESTIONED OPS PERSONNEL ABOUT

l


THE POSITIONS OF THE UNIT 1 VX SYSTEM DAMPERS.

'

OPS PERSONNEL VERIFIED THAT EACH UNIT 1 VX

11/09/87


,

SYSTEM DAMPER WAS IN ITS PRE-OPERATIONAL

r

POSITION AS EVIDENCED BY PAINT SHADOWS ON THE

i

DAMPER ACTUATORS.

ONE DAMPER WAS MISPOSITIONED

IN THE CLOSED DIRECTION.

IT WAS RETURNED TO

I

ITS PROPER POSITION,

1

NRC PERSONNEL WERE CONCERNED ABOUT THE POSI-


TlONS OF THE UNIT 2 VX SYSTEM DAMPERS, AND

CONSEQUENTLY, STATION PERSONNEL AGREED TO DO A

VX FLOW BALANCE TEST FOR EACH UNIT DURING THEIR

NEXT REFUELING OUTAGES.

PERFORMANCE PERSONNEL TOOK "AS FOUND" FLOW

j

7/19/88


'

MEASUREMENTS USING A VELOMETER ON BOTH TRAINS

OF UNIT 2 OF THE VX SYSTEM.

SOME VX SYSTEM

(

DAMPER COMPARTMENT FLOWS DID NOT MFfT THE

f

MCGUIRE FINAL SAFETY ANALYSIS REPr.RT (FSAR)

[

REQUIREMENTS AND TWO DAMPERS SERVING THE

REACTOR HEAD AREA WERE FOUND CLOSED.

DESIGN

ENGINEERING WAS NOTIFIED OF THESE FINDINGS.

DESIGN ENGINEERING REQUESTED MORE ACCURATE

f

7/20/88


MEASUREMENTS BE TAKEN USING A FLOV HOOD.

f

!

'

l

l

l

-

-

-

,

_ _ _

. _ _ _ _ _ _ _ _ _ _

_ _ _ _ _ _ _

__

_ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ - _ _ _ _ _ _

.

-

.

i

.

,

l

f 5,

7/21/88

~0100

PERFORMANCE PERSONNEL BEGAN THE RF. TEST OF THE VX

.

2A SYSTEM USING A FLOW HOOD.

!

0900

THE TRAIN A VX RETESTS WERE COMPLETED AND

TRAIN 2B RETESTS WERE BEGUN.

'

.

DESIGN ENGINEERING PERSONNEL REEVALUATED THE VX


SYSTEM FLOW RATES THAT WERE LISTED IN THE FSAR.

THEY EXPRESSED CONFIDENCE THAT THEY COULD

f

PROVIDE A TECHNICAL JUSTIFICATION FOR THE

!

OPERABILITY OF THE VX SYSTEM.

!

!

~1430

PLANT PERSONNEL TERMINATED THE 2B VX FLOW

!

BALANCE TEST BEFORE IT WAS COMPLETED.

THIS WAS

{

A MANAGEMENT DECISION WAS BASED UPON D.E.

INPUT

,

TilAT FINAL B TRAIN NUMBERS WERE NO LONGER

ESSENTIAL AND ALL THE INFORMATION REQUIRED FOR

THE OPERABILITY DETERMINATION HAD BEEN

GATHERED.

i

~1500

STATION MANAGEMENT COMMUNICATED THE DECISION

f

TO TERMINATE THE 2BVX FLOW BALANCE TEST TO THE

j

NRC RESIDENT INSPECTOR AS A COURTESY.

THE

j

OPERABILITY DETERMINATION WAS STATED AS THE

,

REASON, HOWEVER, SPECIFICS WERE NOT DISCUSSED

AT THIS TIME.

j

~1700

STATION MANAGEMENT REVIEWED DRAFT OF DESIGN'S

i

VX OPERABILITY DETERMINATION AND EVALUATION.

j

i

AFTER INITIAL DISCUSSION VERBAL AGREEMENT WAS

[

l

REACHED WITH DESIGN.

i

1822

UNIT 2 ENTERED MODE 4 PER MANAGEMENT DECISION.

l

!

[

l

t

!

!

!

!

,

l

l

-

-

- -

,

. _ - - _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ - _ - _ _

_ __.

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

. _ _ _ _ _

.

.

1

.

DESIGN ENGINEERING PERSONNEL ISSUED THE SIGNED

i

7/22/88


,

OPERABILITY DETERMINATION BASED IN PART ON THE

-

OPERABILITY OF THE HYDROGEN MITIGATION SYSTEM.

!

s

AFTER FURTHER REVIEW, THE NRC PERSONNEL JUDGED

8/1/88


THE UNIT 2 OPERABILITY DETERMINATION TO BE

!

INADEQUATE BECAUSE DESIGN ENGINEERING PERSONNEL

TOOK CREDIT FOR THE HYDROGEN MITIGATION SYSTEM

[

TO SUPPORT THE VX SYSTEM OPERABILITY

[

DETERMINATION.

8/2-15/88 ----

DESIGN ENGINEERING PERSONNEL BEGAN

REEVALUATING THE VX SYSTEM FLOW RATES IN A

[

MANNER CONSISTENT WITH REGULATORY GUIDE 1.7,

l

REVISION 2, AND 10CFR50.44, WHICH REDUCED THE

REQUIRED FLOW RATES FOR THE VX SYSTEM.

PERFORMANCE PERSONNEL COMPLETED ON-LINE FLOW

!

8/16/88


MEASUREMENTS ON ACCESSIBLE PORTIONS OF TRAIN B

OF THE VX SYSTEM USING THE FLOW HOOD.

THIS WAS

DOME TO EVALUATE BOTH TRAINS AGAINST THE NEW

i

ACCEPTANCE CRITERIA UNDER DEVELOPMENT.

DESIGN ENGINEERING PERSONNEL ISSUED A NEW UNIT

8/19/88


2 OPERABILITY DETERMINATION AND CONCLUDED THAT

f

THE PRESENT FLOW BALANCE CONDITION OF THE VX

,

SYSTEM WAS SUFFICIENT AND WAS CONSIDERED

OPERABLE.

THIS CONCLUSION ALSO APPLIES TO THE

!

OPERABILITY OF THE SYSTEM ON 7/21/88 WHF.N MODE

!

4 WAS ENTERED.

l

!

A MCGuinE NRC RESIDENT INSPECTOR NOTIFIED

9/16/88


STATION MANAGEMENT THAT NRC HAD FULLY REVIEWED

{

AND ACCEPTED THE OPERABILITY STATEMENT AND

I

EVALUATION.

l

c- ,

'

'

.

.

!

I

'

IO/12/88

PERFORMANCE PERSONNEL ENTERED THE UNIT 1


,

REACTOR BUILDING IMMEDIATELY AFTER S/D AND

-

VERIFIED THE DAMPERS IN THE UPPER HEAD AND

l

'

PRESSURIZER AREAS WERE OPEN AND MARKED THEIR

POSITION.

THIS WAS DONE TO ENSURE "AS FOUND"

DATA.

THESE ARE HIGH TRAFFIC AREAS DURING AN

OUTAGE.

!

PERFORMANCE PERSONNEL CONDUCTED THE UNIT 1 VX

10/18/88


FLOW BALANCE TEST USING THE FLOOD HOOD METHOD.

ALL FLOWS MET THE NEW ACCEPTANCE CRITERIA

DEVELOPED IN THE 8/19/88 OPERABILITY

DETERMINATION WITH THE EXCEPTION OF "A" TRAIN

PRESSURIZER CAVITY AND BOTH TRAINS IN THE

REACTOR HEAD AREA.

I

._

. _ _ _ _ _ _ _ _ _ _ _ _ - ____-_ -_ - _ _

_

_ _ _ _ _ _ _ _ _ _ _ _

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

_ _ - _ _ _ _ _

'

.

.

.-

ROOT CA'USE

,

WO PROBLEMS EVENTUALLY LED TO THIS SITUATION:

(1) THE PREOPERATIONAL TEST PERFORMED ON THE VX SYSTEM WAS

INSUFFICIENT TO PROVE OPERABILITY. THE STATION PERSONNEL'S

DEGREE OF UNDERSTANDING OF THE SYSTEM AND OUR DEPENDENCE UPON

PREVIOUSLY AGREED UPON TESTING COMMITNENTS LED US TO OMIT

FLOW BALANCE TESTING OF THIS SYST M FROM THE PREOPERATIONAL

TEST FROGRAM.

(2) APPROPRIATE MEASURES WERE NOT TAKEN TO ENSURE THE FLOW

BALANCE OF THIS SYST m WAS MAINTAINED EITHER THROUGH PF.RIODIC

TESTING OR CONTROL OF DAMPER POSITIONS.

CONTRIBUTING FACTOR

BY DESIGN, THE VX SYSTEM !!AS A SINGLE HEADER THAT DRAVS AIR FROM

EACH OF THE CONTAINMENT COMPARTMENTS BY USE OF REDUNDANT FANS

LOCATED ON EITHER END OF THE HEADER. EITHER FAN IS CAPABLE OF

DRAWING THE TOTAL DESIGN BASIS FLOWS FROM THE AREAS SERVICED.

HOWEVER. THE EQUIPMENT CONFIGURATION OF THE SYSTEM IS SUCH THAT

BALANCE OF THE INDIVIDUAL COMPARTMENT FSAR FLOW RATES IS

UNOBTAINABLE WHEN OPERATING THE FANS INDEPENDENTLY. THE SYSTEM IS

BEING MODIFIED TO CORRECT THIS DEFICIENCY.

SUBSEQUENT TESTING

WILL VALIDATE THE NEW DESIGN.

A.

PREOPERATIOJAL TESTING OF THE VX SYSTDI

1.

UNIT #1

THE ORIGINAL PREOPERATIONAL TEST PREPARED AND PERFORMED FOR

UNIT #1 WAS BASED ON THE CHAPTER 14 FSAR ABSTRACT.

THE

,,

- - _ - - - - - _ - - _ - _ _ - --

- _ _ _ _ - - - - - - - - - - - - - - - - - - - _

,

.

.

>

.

ABSTRACT INCLUDED NO PROVISIONS FOR FLOW BALANCING THE SYSTEM

.

AND NO BALANCE WAS PERFORMED. STATION PERSONNEL ASSUMED THAT

THE HVAC VENDOR HAD BALANCED THE SYSTEM. THIS WAS THE NORMAL

PRACTICE FOR HVAC SYSTEMS. THIS SYSTEM WAS DIFFERENT. THE

HVAC VENDOR WAS NOT ASSOCIATED WITH THE SUCTION RING HEADER.

LATER IN UNIT #1'S PREOPERATIONAL TEST:lNG, THE PROPER

POSITIONING OF CERTAIN DAMPERS OF THE VX SYSTEM WAS

QUESTIONED.

IN ORDER TO RESOLVE THESE QUESTIONS PLANT

PERSONNEL CONDUCTED A FLOW BALANCE.

THE FLOW BALANCE WAS

INADEQUATE AS A RESULT OF BOTH TRAINS BEING OPERATED

SIMULTANEOUSLY. THIS FLOW BALANCE WAS DOCUMENTED IN A

3/23/81 MEMORANDUM TO FILE AND WAS NOT PART OF THE

PREOPERATIONAL TEST PROGRAM.

IT WAS DONE TO ANSWER SYSTEM

OPERABILITI QUESTIONS.

IT WAS STILL ASSUMED THE HVAC VENDOR

HAD PROPERLY BALANCED THE SYSTEM.

2.

UNIT 2

AFTER REVIEWING THE UNIT 2 PREOPERATIONAL TESTING FOR THE VX

SYSTEM, IT IS DIFFICULT TO DETERMINE EXACTLY WHAT WAS DONE IN

REGARDS TO FLOW BALANCING THE SYSTEM. AGAIN HEAVY DEPENDENCE

WAS PLACED UPON THE HVAC VENDOR PROPERLY BALANCING THE

SYSTEM. WITHOUT FURTHER 'INFORMATION WE CAN ONLY CONCLUDE

THE "A" TRAIN WAS BALANCED. HOWEVER, THE RESULTS ARE NOT

CONSISTENT WITH CURRENT PERFORMANCE OF THE SYSTEM. THOSE

INVOLVED WITH THE UNIT 2 TESTING ARE NO LONGER WITH DUKE

POWER COMPANY AND FOR THIS REASON FURTHER INVESTIGATION IS

RESTRICTED.

.

.

.

3.

INADEQUACY OF THE VX PREOPERATIONAL TEST

.

AT THE TIME OF OUR PREOPERATIONAL TEST PROGRAM, OUR PRIMARY

EMPHASIS WAS ON ECCS SYSTEMS. THE TEST PROGRAM FOR BALANCE

OF PLANT, SAFETY RELATED SYSTEMS WAS NOT AS CAREFULLY

SCRUTINIZED. THIS WAS TRUE OF THE HVAC SYSTEMS WHERE TWO

FACTORS COMBINED TO INHIBIT PROPER TESTING. THE FIRST FACTOR

,

WAS THE CLARITY AND AVAILABILITY OF DESIGN BASIS INFORMATION

ON THESE PARTICULAR SYSTEMS. THE OTHER FACTOR WAS THE

DEPENDENCE ON THE HVAC VENDOR FOR SYSTEM START UP.

'

,

i

ANOTHER FACTOR LEADING TO THE INADEQUATE PREOPERATIONAL TEST

ON THE VX SYSTEM WAS THE FAILURE TO INCLUDE FLOW BALANCE

REQUIREMENTS IN CHAPTER 14 0F THE FSAR. DURING THIS TIME

.

)

PERIOD CHAPTER 14 0F THE FSAR AND THE TECHNICAL

,

SPECIFICATIONS WERE USED AS THE PRIMARY SOURCE OF TESTING

!

t

COMMITMENTS. AT THE TIME OUR PREOPERATIONAL TEST PROGRAM WAS

CONDUCTED WE DID NOT PROGRAMATICALLY LOOK BEYOND THESE

DOCUMENTS FOR OTHER TESTING REQUIREMENTS.

l

l

4.

CORRECTIVE ACTIONS

SPECIFICALLY FOR THE VX SYSTEM:

WE WILL MODIFY THE SYSTEM TO ENRANCE OUR ABILITY TO

1

BAIANCE THE SKIMMER FLOWS.

i

e

WE WILL CONDUCT A TEST TO OPTIMIZE THE FLOW BALANCE

I

OF THE VX SYSTEM.

ll

!

WE WILL ESTABLISH APPROPRIATE CONTROLS TO ENSLTE

l

THE FLOW BALANCE IS MAINTAINED.

'

'

.

.

.

HYDROCEN SKDGER

AND CONTAINNENT AIR RETVEN SYSTEM (VI)

,

.

REVISED ARRANCEMENT

,,,

4qP

k

7

-

-

/

HSF-1A

HSF-1B

O

O

-

NEW CHECK DAMPERS

O

-

O

s

IVX1A

IVI28

)

!

NEW 8" SUCTION CROSS-CONNECT

4

7

i

t

1

_ UPPER CONTAll0ENT

'

'

_

_

_

LOWER CONTAINMENT

g

g

/

\\

/ x

G HEADER (EMBEDDED IN CRANE WALL)

RIN

)

DAMPERS (TTPICAL)

/

'

W

/

\\

/

/

N

/

/

N

%s%w '

- _

,o= #

/

I

t

CONTAINMENT -

~

I

\\

-

!

REACTOR BUILDING -

s=>

a,e

-. .

,

.

.

.

GENERIC ACTIONS:

.

UPON REVIEW WE HAVE CONCLUDED THE PREOPERATIONAL TEST

PROGRAM AT MCGUIRE MAY HAVE BEEN INADEQUATE FOR A

SPECIFIC CLASS OF SYSTEMS: THOSE BEING SAFETY RELATED,

BALANCE OF PLANT SYSTEMS.

IN ORDER TO ADDRESS THIS

CONCERN, WE ARE REVIEWING THE PREOPERATIONAL TESTING FOR

EACH OF T1'ESE SYSTD(S TO ENSURE IT WAS ADEQUATE.

IN

CONJUNCTION WITH THIS WE ARE EVALUATING THE SURVEILIANCE

TESTING CONDUCTED TO ENSURE IT IS SUFFICIENT TO ENSURE

CONTINUED OPERABILITY.

THIS REVIEW HAS BEGUN. THE AUXILIARY FEEDWATER SYSTEM

IS BEING USED AS A "PILOT" SYSTEM. AFTER THIS REVIEW IS

COMPLETE, A SCHEDULE WILL BE ESTABLISHED FOR ALL SYSTEMS

INVOLVED.

IT IS ANTICIPATED THE REVIEW WILL BE DONE BY

MAY OF 1989.

C.

DECISION TO ENTER MODE #4

1.

SITUATION ON JULY 21, 1988

THE VX FLOW BALANCE WAS PERFORMED AT THE END OF THE UNIT #2

REFUELING OUTAGE WHILE IN MODE #5.

IT WAS ONE OF MANY TESTS

PERFORMED, MOSTLY AS A RESULT OF MAINTENANCE AND

MODIFICATIONS, DURING THE LAST WEEKS OF THE OUTAGE. MOST OF

THESE TESTS, INCLUDING THE VX FLOW BALANCE, WERE REQUIRED TO

BE COMPLETED PRIOR TO MODE #4.

TESTING PERSONNEL HAD BEEN

MAINFAINING A VERY INTENSE SCHEDULE FOR APPROXIMATELY 2

WEEKS.

_ _ _ _ _ _ _ _ _ _ _ _

o

.

O

.

2 .'

PERSONS INVOLVED WITH THE DECISION

.

THE DECISION WAS MADE AT THE APPROPRIATE LEVEL OF MANAGEMENT.

THE SUPERINTENDENT OF OPERATIONS, MAINTENANCE. TECHNICAL

SERVICES, AND INTEGRATED SCHEDULING ALL WERE INVOLVED IN THE

DECISION. ALSO INVOLVED WERE THE DESIGN ENGINEERING SITE

OFFICE MANAGER AND OTHER MANAGEMENT PERSONS FROM THE

CORPORATE DESIGN ENGINEERING GROUP.

THE SENIOR RESIDENT INSPECTOR FOR THE NRC WAS MADE AWARE OF

THE DECISION AS A COURTESY.

HIS CONCURRENCE WAS NOT SOUGHT

OR OBTAINED. AT THE TIME THE DECISION WAS COMMUNICATED TO

THE SENIOR RESIDENT, DETAILS OF THE OPERABILITY DETERMINATION

WERE NOT YET AVAILABLE.

_

_ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _

.

,.

.

.

.

3.

FACTORS CONSIDERED IN THE DECISION

.

FOLLOWING THE COMMUNICATION OF TEST RESULTS TO THE CORPORATE

DESIGN ENGINEERING GROUP. THOSE INVOLVED AND RESPONSIBLE FOR

THE DESIGN OF THE VX SYSTEM WERE VERY CONFIDENT THAT THE VX

SYSTEM WOULD STILL PERFORM ITS DESIGN FUNCTION IN ITS

DEGRADED CONDITION. THESE DESIGN EXPERTS CLEARLY BELIEVED

THEY COULD PRESENT A TECHNICALLY CORRECT JUSTIFICATION FOR

THE OPERABILITY OF THE VX SYSTEM. AND EXPRESSED THIS

CONFIDENCE THROUGHOUT THE EVALUATION PERIOD.

THE FLOW BALANCE TESTING HAD GONE THROUGH SEVERAL

UNSUCCESSFUL ITERATIONS. THE ORIGINAL INTENT OF THE TEST HAD

BEEN TO BALANCE THE SYSTEM TO FSAR FLOW VALUES. WE HAD

DISCOVERED THIS WOULD NOT BE POSSIBLE. THE NEW PURPOSE HAD

BECOME TO GATHER ENOUGH DATA TO SUPPORT THE CORPORATE DESIGN

ENGINEERING GROUP'S EFFORT TO JUSTIFY THE OPERABILITY OF THE

VX SYSTM. ONCE THE DESIGN EXPERTS STATED THEY HAD

SUFFICIENT DATA TO SATISTY THIS NEED. FURTHER TESTING WAS

UNNECESSARY. THE LETERMINATION THAT SUFFICIENT DATA HAD BEEN

GATHERED OCCURRED DURING THE FLOW HOOD MEASURD(ENTS ON UNIT 2

"B" TRAIN. THUS A COMPLETE SET OF "B" TRAIN FLOW HOOD

MEASURD(ENTS WAS NOT TAKEN PRIOR TO ENTERING MODE #4.

STATION MANAGD(ENT'S DECISION TO PROCEED TO MODE #4 WAS

PRIMARILY BASED OP.4 INPUT FROM EXPERTS FAMILIAR WITH THE VX

SYSTEM. THESE EXPERTS CLEARLY BELIEVED THE SYSTEM WOULD

PERFORM ITS DESIGN FUNCTION. WITH THIS CONFIDENCE STATION

_ _ _ _ _ _ _ .

.

o

.

.

MANAGEMENT SAW NO REASON TO DELAY THE SCHEDULED START-UP OF

.

UNIT 2 FOLLOWING THE REFUELING OUTAGE.

4.

CORRECTIVE ACTIONS

ALTHOUGH THE OPERABILITY DETERMINATION OF 8/19/88 LATER

CONCLUDED THAT THE VX SYSTEM WAS CAPABLE OF PERFORMING ITS

DESIGN FUNCTION, THE DECISION TO PROCEED TO HODE I/4 ON

7/19/88 WAS BASED ON INCORRECT INFORMATION.

THE DECISION

ITSELF WAS NOT AT FAULT, BUT THE PROCESS BY WHICH IT WAS

ARRIVED AT HAD WEAKNESSES.

THE OPERABILITY DETFAMINATION

PROGRAM WILL BE STRENGTHENED TO HELP PRECLUDE ERRORS SUCH AS

THIS IN THE FUTURZ.

C. OPERABILITY DETERMINATION PROCESS

1.

THE VX OPERABILITY DETERMINATION BROUGHT SEVERAL CONCERNS TO

LIGHT INVOLVING DUKE POWER COMPANY'S JUSTIFICATION FOR

CONTINUED OPERATION /0FFRABILITY DETFAMINATION PROGRAM.

THESE

ARE SUMMARIZED HERE:

+

ALTHOUGH OPERABILITY DETERMINATIONS ARE DOCUMENTED IN

ACCORDANCE WITH ESTABLISHED PROCEDURES AND ARE

TYPICALLY TECHNICALLY STRONG. THEY DO NOT

PROGRAMATICALLY INCLUDE 10CFR50.59 EVALUATIONS.

6

No PROCEDURES EXIST FOR THE REVIEW AND APPROVAL OF

OPERABILITY DETFRMINATIONS BY NUCLEAR PRODUCTION

DEPARIMENT PERSONNEL.

(THE DESIGN ENGINEERING

__

_ _ _ _ _ _

.

,

'

.

DEPARTMENT PERFORMS INTERNAL REVIEWS.) AS A RESULT,

.

OPERABILITY DETERMINATIONS RECEIVE VARYING DEGREES OF

f

REVIEW AND APPROVAL.

l

'

4

NO PROCEDURES EXIST TO CONTROL OPERABILITY

DETERMINATIONS AND TRACK THDi ONCE THEY HAVE BEEN

'

ACCEPTED.

j

e

THE PROCESSES OF PERFORMING A JUSTIFICATION FOR

.

l

CONTINUED OPERATION (JCL), AN OPERABILITY DETERMINATION,

j

L

AND ANSWERING A PROBLD1 IDENTIFICATION REPORT (PIR) HAVE

,

!

BECOME INTERCHANGEABLE. THIS HAS APPARENTLY LED TO A

'

GREAT DEAL OF CONFUSION IN OUR COMMUNICATIONS WITH THE

!

NRC.

RECENT DISCUSSIONS WITH REGION II PERSONNEL HAVE

MORE CLEARLY ESTABLISHED THE DISTINCTIONS BEIVEEN THESE

PROCESSES.

i

,

2.

IN ORDER TO RESPOND TO THESE PROBLEMS, THE FOLLOWING CORRECTIVE

l

ACTIONS ARE BEING PLANNED. THESE CORRECTIVE ACTIONS WILL APPLY To

,

ALL 3 DUKE POWER COMPANY NUCLEAR FACILITIES.

(a.) OUR NUCLEAR PRODUCTION DEPARTNENT DIRECTIVE WILL BE REVISED

i

TO INCLUDE THESE UPGRADES:

,

e

THE JCO, OPERABILITY DETERMINATION, AND PIR RESPONSE

PROCESSES WILL BE CLEARLY DEFINED. EXPECTED LEVELS OF

[

l

NRC INVOLVEMENT WILL BE ESTABLISHED.

l

l

4

REQUIRDtENTS TO CONSIDER THE QUESTIONS ADDRESSED IN

l

10CFR50.59 WILL BE ESTABLISHED.

REVIEW RESPONSIBILITIES BY NUCLEAR PRODUCTION PERSONNEL

I

I

WILL BE ESTABLISHED, APPROVAL LEVELS WILL BE SET.

f

I

i

(

I

t

!

- -

-

__

e

e

4

(b.) PROCEDURES WILL BE ESTABLISHED AT THE STATION TO CONTROL AND

-

TRACK OPERABILITY DETERMINATIONS.

THESE UPGRADES ARE NOW IN PREPARATION AND ARE EXPECTED TO BE

COMPLETE IN THE FIRST QUARTER OF 198'd.

,

i

e

-

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

__

e

.

.

.

UNIT 1 HYDROGEN SKIMMER TAN COMPARTMENT FLOW MEASUREMENT

AS TOUND DATA

10/18/88

Required

compartments

riew

HSF-1A

HSF-18

SG-1A

121

214

916

50-1B

121

671

360

SG-1C

121

521

254

SG-1D

121

300

771

()

283

PZR

121

ACC-1A

4

46

37

ACC-1B

4

36

20

ACC-1C

24

68

86

ACC-1D

24

43

70

Inc. Rs.

15

138

107

(h)

(h)

Rx. Hd.

172

I.

Tan Rs.

29

71

68

W.

Tan Rs.

29

71

57

l

The above flows were measured per TT/1/A/9100/217 and are given

l

in SCTM.

Each of the thirteen compartments above is served by two intake

dampers.

The "as-found" condition for each of the twenty-six

dampers was open or throttled.

Eight dampers (serving the S/Gs)

were 100% cpen, with remaining damper positions varied, throttled

closed by as much as 95%.

Total flow for each HSF was measured by traversing the suction

duct.

Results were

HSF-1A = 3307 SCTM;

HST-1B = 3212 ScrM.

[d /T

7

P. W.

Roberson

NP Engineer, Performance

j

file:dvx.dw4.vxflow.ul.101988

. .

__.

.

l

.

.

.

Table 14.1.3-1 (Page 30)

-

4

CONTAINMENT AIR RETURN AND HYDROGEN SKIMMER SYSTEM FUNCTIONAL TEST

Abstraa.t

Purpose

To descnstrate the capability of the system to operate and to provide design

air flows.

Prerequisites

The .cs condenser inlet doors are blocked closed to prevent operation.

Test Method

Each containment air return fan and hydrogen skimmer fan is operated.

Tests

are performed to demonstrate the proper head and flow characteristics of eacn

fan. Automatic operation of the Containment air return fans is verified for a

simulated high-high containment pressure signal (S ).

System interlocks are

P

also verified.

Acceptance Criteria

Each fan provides air flow as specified in the FSAR and the Containment air

return fans respond properly to a simulated high-high containment pressure

signal (S ).

p

,

O

,

12/83

'

!

..

e.

l

, .-

[

'

VX SAFETY ANALYSIS

-

!

i

!

INADEQUATE VX SYSTEM FLOWS (UNIT 2)

t

!

FLOW BALANCE TESTING PERFORMED DURING THE 1988 UNIT 2 REFUELING

I

OUTAGE BEGAN BY RECORDING "AS-FOUND" FLOW READINGS PRIOR TO

l

ADJUSTING THE BALANCING VALVES,

INLET VALVES FOR THE REACTOR HEAD

l

AREA WERE FOUND IN THE CLOSED POSITION, AND INITIAL' READINGS IN

!

FOUR (4) OTHER COMPARTMENTS WERE FOUND TO BE BELOW THE REVISED

[

MINIMUM FLOW REQUIREMENTS.

IN ADDITION TO THE REACTOR HEAD AREA,

j

THE FOUR (4) AREAS FOUND DEFICIENT IN FLOW WERE THE EAST FAN ROOM,

j

WEST FAN ROOM, ACCUMULATOR ROOM 2C, AND ACCUMULATOR ROOM 20.

!

I

THE AS-FOUND FLOW VALUES HAVE BEEN EVALUATED FOR SAFETY

(

SIGNIFICANCE REGARDING HYDROGEN ACCUMULATION.

THE EVALUATION

(

CONCLUDES THAT SINCE NONE OF THE AFFECTED COMFARTMENTS ARE TRULY

!

l

DEAD-ENDED REGIONS, THE CIRCULATION FORCED BY THE CONTAINMENT AIR

f

l

RETURN FANS ALONG WITH, IN THE CASE OF THE REACTOR HEAD AREA, THE

l

l

SIGNIFICANT NUMBER OF LARGE OPENINGS INSTALLED FOR PRESSURE RELIEF

.

PURPOSES, WOULD LIMIT HYDROGEN CONCENTRATION TO LESS THAN FOUR

j

l

l

VOLUME PERCENT.

l

1

.

FAN ROOMS AND THE AFFECTED ACCUMULATOR ROOMS SERVE AS THE DESIGN

i

t

FLOW PATH FOR THE CONTAINMENT AIR RETURN FANS IN ClRCULATING AIR

l

FROM THE UPPER CONTAINMENT TO THE LOWER CONTAINMENT A*' THROUGH THE

I

ICE CONDENSER.

EACH OF THE REDUNDANT FANS IS RATED AT 30,000 CUBIC

l

FEET PER MINUTE, AND WILL CLEARLY PROVIDE MORE THAN THE MINIMUM

[

VENTILATION REQUIREMENTS NEEDED TO LIMIT HYDROGEN CONCENTRATION TO

f

BELOW FOUR VOLUME PERCENT IN THESE COMPARTMENTS.

f

f

THE REACTOR HEAD AREA IS NOT IN THE DIRECT FLOW PATH FOR THE AIR

RETURN FAN, BUT DOES CONTAIN SEVERAL FEATURES THAT CONTRIBUTE TO

,

LlMlTING HYDROGEN ACCUMULATION.

THE COMPARTMENT CONTA1NS MORE THAN

{

250 SQUARE FEET OF OPENINGS COMMUNICATING WITH OPEN AREAS OF THE

(

LOWER CONTAINMENT.

OPENINGS EXIST BOTH IN UPPER AND LOWER REGIONS

f

t

t

l

>

'

-

-

-

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

_ - _ _ _ _ _ _ _ - - - _ _ _ _ _ _ _ - - _

.

~

.

i

-

<

.

OF THE REACTOR HEAD AREA, THEREBY ENHANCING CIRCULATION DRIVEN BY

-

,

THERMAL EFFECTS DUE TO HEATING OF THE INFLUENT AIR FROM THE LOWER

CONTAINMENT.

FOR EXAMPLE, THE THERMAL HEATING PRODUCED BY A

REACTOR HEAD TEMPERATURE OF 120 DEGREES F WOULD CREATE A

CIRCULATION OF GREATER THAN 1000 cubic FEET PER MINUTE (CFM) BASED

,

ON AN AVERAGE LOWER CONTAINMENT TEMPERATURE OF 100 DEGREES, WHILE

ASSUMING FLOW PATH LOSS COEFFICIENTS AS PRESENTED IN SECTION 6.2 OF

THE FSAR.

THESE CONSERVATIVE TEMPERATURES ARE TYPICAL OF VALUES

WHICH COULD BE EXPECTED LONG TERM IN A POST-ACCIDENT SITUATION.

THIS EXPECTED ,' LOW VALUE COMPARES VERY FAVORABLY WITH A MINIMUM

COMPARTMENT FLOW REQUIREMENT OF 172 CFM FOR LIMITING COMPARTMENT

CONCENTRATION TO BELOW FOUR VOLUME PERCENT.

THE MINIMUM COMPARTMENT FLOW REQUIREMENT IS BASED ON THE PEAK

COMPARTMENT REQUIREMENT FOR A PRIMARY COOLANT BREAK IN THAT

COMPARTMENT.

IF THE EREAK WERE TO OCCUR IN THE REACTOR

CCMPARTMENT, THE ESCAPING FLUIDS WOULD INCREASE TURBULENCE INSIDE

THE COMPARTMENT, THEREBY DECREASING THE POTENTIAL FOR HYDROGEN

ACCUMULATION.

IF A BREAK OCCURRED OUTSIDE THE REACTOR COMPARTMENT,

THE SKlMMER SYSTEM FLOW REQUIREMENT WOULD BE SIGNIFICANTLY LESS

THAN THE 172 CFM VALUE.

IN EARLY STAGES OF THE POST-ACCIDENT

SCENARIO, COMPARTMENT CIRCULATION DRIVEN BE THERMAL EFFECTS WOULD

BE AT ITS GREATEST WHEN NEEDED MOST.

AS THE PRIMARY COOLANT SYSTEM

COOLED TO NEAR AMBIENT TEMPERATURE IN THE LONG TERM AND DECREASED

THE THERMAL EFFECTS IN THE REACTOR COMPARTMENT, HYDROGEN PRODUCTION

BY RADIOLYSIS WOULD DECREASE ACCORDINGLY BASED ON THE DECREASING

RADIOLOGICAL SOURCE TERM.

CONSIDERING THESE FACTORS AFFECTING THE ACTUAL COMPARTMEt.T FLOW

REQUIREMENTS, IT IS HIGHLY UNLIKELY THAT THE CLOSED SKIMMER INLET

VALVES IN THE REACTOR HEAD AREA WOULD HAVE CAUSED THE COMPARTMENT

CONCENTRATION TO EXCEED FOUR VOLUME PERCENT.

IN ADDITION TO THE

NUMEROUS MITIGATING FACTORS, AN ADDITIONAL LEVEL OF PROTECTION IS

PROVIDED BY THE HYDROGEN MITIGATION SYSTEM, WHICH, THROUGH

OPERATION OF THE HYDROGEN IGNITERS, 15 CAPABLE OF LIMITING HYDROGEN

CONCENTRATION TO BELOW DETONABLE LEVELS, TO APPROXIMATELY SIX

VOLUME PERCENT.

_ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ __ ___ ________ ___ __ ____ _____ __ _ __

_

_ _ _ _ _ _ _ _ _ _ _ _ _

.

.

.

.

INADEQUATE VX SYSTEMS FLOWS (UNIT 1)

'

AT THE BEGINNING OF THE OCTOBER, 1988 REFUELING OUTAGE FOR MCGUlRE

UNIT 1, AS-FOUND FLOW READINGS WERE RECORDED USING THE STATIONARY

HOOD DEVICE.

INITIAL READINGS IN TWO (2) COMPARTMENTS WERE FOUND

TO BE BELOW THE MINIMUM FLOW REQUIREMENTS FOR LIMITING

CONCENTRATION TO LESS THAN FOUR VOLUME PERCENT.

THE TWO (2) AREAS

FOUND DFFICIENT IN FLOW WEDE THE REACTOR HEAD AREA AND THE

PRESSURIZER COMPARTMENT.

,

AS PREVIOUSLY DISCUSSED FOR MCGUIRE UNIT 2, THE CIRCULATION

PRODUCED BY THERMAL EFFECTS IN THE REACTOR HEAD AREA, IN

l

CONJUNCTION WITH TIME-DEPENDENT REDUCTION IN RADIOLYTIC HYDROGEN

GENERATION, WOULD LIKELY HAVE PREVENTED THE COMPARTMENT HYDROGEN

CONCENTRATION FROM REACHING FOUR VOLUME PERCENT.

THE PRESSURIZER COMPARTMENT IS A DEAD-ENDED REGION THAT DOES NOT

DIRECTLY BENEFIT FROM CIRCULATirN PRODUCED BY THE C)NTAINMENT AIR

RETURN FANS.

THE CALCULATED MINIMUM SKIMMER SYSTEM FLOW RATE TO

LIMIT COMPARTMENT HYDROGEN CONCENTRATION TO BELOW FOUR VOLUME

,

PERCENT IS 121 CUBIC FEET PER MINUTE (CFM).

MEASURED FLOW RATE

W!TH FAN 1B OPERATING WAS 281 CFM, AND MEASURED FLOW WITH FAN 1A

OPERATING WAS 85 CFM.

BASED ON THE FLOW MEASUREMENT RECORDED FOR FAN 1A, THE PRESSURIZER

I

COMPARTMENT HYDROGEN CONCENTRATION COULD HAVE RLACHED 4.8 VOLUME

PERCENT.

ALTHOUGH 4.8 VOLUME PERCENT EXCEEDS THE CONSERVATION

l

DESIGN BASIS LIMIT OF 4.0 VOLUME PERCENT, IT IS VERY UNLIKELY THAT

l

HYDROGEN AT 4.8 VOLUME PERCENT WOULD IGNITE AND BURN EVEN IN DRY

AIR AND IN THE PRESENCE OF AN IGNITION SOURCE.

HOWEVER, IF BURNING

,

WERE TO OCCUR, ESSENTIAL EQUIPMENT LOCATED IN THE PRESSURIZER

COMPARTMENT HAS BEEN ANALYZED AND DETERMINED ABLE TO SURVIVE EVEN

i

THE BURNING OF HYDROGEN FROM THE 75'$ METAL WATER REACTION OF A

,

l

I

DEGRADED CORE ACCIDENT.

THE ANTICIPATED MAXIMUM CONCENTRATION OF

4.8 VOLUME PERCENT IS CLEARLY WELL BELOW DETONABLE LEVELS, AND IS

NOT CONSIDERED A DETRIMENT TO MAINTAINING CONTAINMENT INTEGRITY AND

TO CONDUCTING A STABLE POST-ACCIDENT RECOVERY.

!

1

- -

-

-

-

- -

_ - - - - - - _ _ -

- - - - - - - - - _ - - - - - - - - - - - - - - -

- - - - - - - - - - - - - - - - - - - - - - - - -


-

---

,

.

<

.

e

.

ANALYSIS OF SAFETY SIGNIFICANCE

METHOD

i

USE REVISED ASSUMPTIONS FOR H SOURCE

'

2

-

TERMS

,

RECOMPUTE REQUIRED FLOW RATES PER

-

,

COMPARTMENT

COMPARE TO AS-FOUND VX SYSTEM

-

CAPABILITY

!

FURTHER ASSESS ANY LOW-FLOW

l

-

COMPARTMENTS

!

,

,

Y

, - . - - - , _ - _ . _ _ - - - - _ _ -

_

_ . - _ _ . . _ - _ . - - - _ . - _ , . - - - - _ - - . , _ . _ , _

-- - _ _

.

.- _ . _ , - _ - ,_.

-

- -

-

---

--

-

- _ - . - - - - - - - - - - _ _ - _ . . _ _ . - . _ _ _ _

e

e

e

9

i

,

COMPARTMENT MODEL

t

I

r

.

X sefm

m

m

V

V

I

t

A N

A k

.

i

1

1

'

t

l

i

[

H,

H 2

,

I

i

l

,

,

l

i

l

l

l

!

!

i

-

1

l

!

!

!

I

i

l

l

!

!

.

!

i

l

I

!

]

.

.

8

l

1

l

4

I

i

- - _ _ __ - -_ _ . _ _ - _

-

- - - _ - _ - - _ - _ . - _ _ _ _-

-

- - -

- . .

-- _

-

- .

_

_ _ ,

- _

_

_

.

.

4

.

t

ORIGINAL,W ANALYSIS

,

I

$

_

X sofm

1.8%

3.5%

'

,

i

i k

J L

4

i

H,

ZlRC REACT

H, - RADIOL

,

(6.0%)

H , - Al

(CONSTANT)

,

i

,

l

1

?

l

l

l'

4

I

- _.

...

-

.

.

.

.

.

REVISED DUKE ANALYSIS

X' s of m

'

0.6%

3.9%

i l

J L

H 2 - ZlRC REACT

H 2- RADIOL

(1.5%)

H 2- Al + Zn

H - PRIM COOL

(TEMP DEP)

2

l

l

.

___ __

.

_--

.--

_

._

.

_ .

_.

._

-

.

.

.

s

.

EXAMPLE FLOW COMPARISON

COMPARTMENT:

SG-1 A

ORIGINAL WESTINGHOUSE

138 SCFM

.

REVISED DUKE

121 SCFM

AS FOUND (VX-A)

214 SCFM

,

AS FOUND (VX-B)

916 SCFM

_ _ - . , _ _ _ - . - , _ _ _ _ _ _ _ . . . _ _

_

.

. -

. . .

.

. _ _ _ _ _ _ _ _ _ _ _ _ . _ _ _ _ . _ . . . _ _ _

_ _ _ _ _ . _ _ _ . _ _ _ _

~

,

,

.

COMPARTMENTS WITH LOW FLOW

'

.

'

(AS-FOUND)

COMPARTMENT

ASSESSMENT

UNIT 1

REACTOR HEAD

THERMAL CONVECTION

PRESSURIZER

COULD HAVE REACHED

4.8% WELL BELOW

DETONABLE

UNIT 2

-

REACTOR HEAD

THERMAL CONVECTION

EAST FAN ROOM

AIR RETURN FAN

VENTILATION

WEST FAN ROOM

AIR RETURN FAN

..

VENTILATION

ACCUM. ROOM 20

AIR RETURN FAN

VENTILATION

ACCUM. ROOM 2D

AIR RETURN FAN

VENTILATION

-

_ - _ _ _ .

. . . - .

-

- -

.

e

e

4

4

ANALYSIS OF SAFETY SIGNIFICANCE

CONCLUSIONS

ONE COMPARTMENT ON ONE UNIT COULD

.

EXCEEDED DESIGN LIMIT.

.

NO SIGNIFICANT SAFETY IMPACT.

-

NEGLIGIBLE EFFECT ON POSTULATED

.

DEGRADED CORE ACCIDENT.

,

- - - - -

- - - -

.

-

_

e

o

.

FUNCTIONAL VERIFICATION PROGRAM

.

DEFICIENCIES

,

DEFINITIONS

POST-MAINTENANCE TESTING - THE POST-MA.NTENANCE iESTING PROGRAM

AT McGUIRE CONSISTS OF A FUNCTIONAL VERIFICATION PROGRAM AND A

RETEST PROGRAM.

FUNCTIONAL VERIFICATION - A CHECK TO ENSURE THAT THE

REQUESTED MAINTENANCE WAS PERFORMED AND THAT THE SUBJECT

EQUIPMENT PERFORMS ALL OF ITS INTENDED FUNCTIONS AND IS

FUNCTIONING PROPERLY PRIOR TO DECLARING THE EQUIPMENT

OPERABLE.

RETEST - THE FORMAL PERFORMANCE OF ALL OR PORTIONS OF

PREOPERATIONAL OR PERIODIC TESTING TO VERIFY THE COMPONENT

OR SYSTEM MEETS APPLICABLE ACCEPTANCE CRITERIA AND/OR

TECHNICAL SPECIFICATION REQUIREMENTS.

SOME MAINTENANCE MAY ONLY REQUIRE A FUNCTIONAL VERIFICATION

WHILE OTHER MAINTENANCE MAY REQUIRE BOTH FUNCTIONAL

VERIFICATION AND RETEST.

POST-MODIFICATION TESTING - THE POST-MODIFICATION TESTING IS

TESTING CONDUCTED TO CONFIRM THAT MODIFICATIONS PERFORM AS EXPECTED

AND THAT OTHER SYSTEMS OR COMPONENTS ARE NOT ADVERSELY AFFECTED.

POST MODIFICATION TESTING MAY CONSIST OF ANY COMBINATION OF

FUNCTIONAL VERIFICATION, RETEST, OR SPECIAL TESTS.

k

e

o

.

OVERVIEW / SEQUENCE OF EVENTS

.

THIS PRESENTATION INVOLVES SEVERAL EVENTS, SOME VERY COMPLEX,

DATING BACK TO FEBRUARY, 1987.

A DRIEF DESCRIPTION OF THE

EVENTS THAT LEAD INTO THE DISCOVERY OF THE NATURE OF THE

PROBLEMS WILL BE PROVIDED AND THEN A HISTORICAL REVIEW AND BRIEF

DESCRIPTION OF ALL THE EVENTS MENTIONED IN THE NRC INSPECTION

REPORT WILL BE PRESENTED.

RECENT EVENTS THAT UNCOVERED THE NATURE OF THE

FUNCTIONAL VERIFICATION PROGRAM DEFICIENCIES

INV-1428

CATAWBA NUCLEAR STATION RECENTLY FOUND SOME LINKS OPEN IN SAFETY

RELATED ELECTRICAL CIRCUITS AND PASSED ON THE CONCERNS TO

,

1

l

McGUIRE, THROUGH DUKE'S OPERATING EXPERIENCE PROGRAM.

McGUIRE

FELT WE MAY BE VULNERABLE TO THE SAME PROBLEM SO WE INSPECTED OUR

SYSTEMS AND FOUND AN OPEN LINK ON A SAFETY RELATED VALVE IN THE

CHEMICAL AND VOLUME CONTROL SYSTEM (VALVE INV-1428).

THIS LINK

,

WAS PART OF THE ELECTRICAL CIRCUITRY WHICH PROVIDED AUTOMATIC

CLOSURE OF THE VALVE.

THE LINK HAD BEEN LEFT OPEN FOLLOWING THE

IMPLEMENTATION OF A MODIFICATION DURING THE UNIT 1 1987 REFUELING

OUTAGE.

PERSONNEL ERROR WAS THE POSSIBLE ROOT CAUSE.

FUNCTIONAL

VERIFICATION OF THE MODIFICATION HAD FAILED TO ENSURE THE LINK

WAS CLOSED.

",

t

O

.

.

.

INS-18(1)

AS A RESULT OF THE INV-142 INCIDENT, PROJECTS PERSONNEL AND ISE

MET AND DECIDED TO REVIEW OTHER SiMILAR MODIFICATIONS ON UNIT 1

AND UNIT 2.

TESTS WERE DEVELOPED AND CONDUCTED TO VERIFY THAT

THE MODIFIED COMPONENTS WERE STILL FULLY OPERABLE.

THIS TESTING

REVEALED THAT 2 OTHER VALVES, INS-18 AND INS-1, IN THE

CONTAINMENT SPRAY SYSTEM, WERE INOPERABLE DUE TO INCORRECT

WlRING.

AS IN THE INV-142B INCIDENT, THESE PERSONNEL ERRORS WERE

NOT DETECTED BY THE FUNCTIONAL VERIFICATION OF THE MODIFICATION.

Dbd

IN JUNE OF 1988 DURING THE IMPLEMENTATION OF A MODIFICATION, IT

WAS DISCOVERED THAT ANOTHER WIRING ERROR HAD OCCURRED MAKING A

VALVE ON THE DECAY HEAT REMOVAL SYSTEM INOPERABLE (VALVE

2NU-48).

THE WIRING HAD BEEN IN THIS CONFIGURATION SINCE THE

PREVIOUS MODIFICATION ON THE VALVE THE YEAR BEFORE.

AGAIN, THIS PERSONNEL ERROR WAS NOT DETECTED BY THE FUNCTIONAL

VERIFICATION CONDUCTED AS PART OF THE POST MODIFICATION TESTING

PROGRAM.

0

s

4

-

.

HISTORICAL OVERVIEW

.

AS A RESULT OF THESE THREE EVENTS, NRC AND DUKE CONDUCTED A

REVIEW TO EVALUATE OUR HISTORY WITH FUNCTIONAL VERIFICATION.

LISTED BELOW, IN CHRONOLOGICAL ORDER, ARE THE EVENTS THAT WERE

JUDGED TO BE ASSOCIATED WITH FUNCTIONAL VERIFICATION, BY DUKE

AND/OR THE NRC.

FEBRUARY, 1987

VALVE INM-26 - A WlRING FAULT IN A NEW

-

ACTUATOR WAS NOT IDENTIFIED BY FUNCTIONAL

VERIFICATION WHEN INSTALLED.

THIS IS AN

EXAMPLE IDENTIFIED IN THE RECENT NRC

INSPECTION REPORT.

APRIL, 1987

INPO IDENTIFIED A FINDING IN THE AREA OF

-

FUNCTIONAL VERIFICATION.

ALTHOUGH THEY DID

NOT FIND SIGNIFICANT EVIDENCE OF FAILURE TO

ADEQUATELY PERFORM FUNCTIONAL VERIFICATION,

THEY FELT OUR PROGRAM WAS TOO DEPENDENT ON

THE INDIVIDUAL JUDGMENT OF THE TECHNICIAN AND

SUPERVISION.

THEY FELT WE SHOULD STRUCTURE

THE PROGRAM AND MAKE IT MORE PRESCRIPTIVE.

DUKE AGREED TO ENHANCE THE PROGRAM BUT AT

THAT TIME DID NOT BELIEVE WE HAD INOPERABLE

EQUIPMENT IN THE FIELD.

VALVE IND-67 - THE WORK CONTROL SYSTEM HAD

AUGUST, 1987

-

INCORRECTLY IDENTIFIED THIS VALVE AS

NON-SAFETY RELATED AND ALSO DID NOT SPECIFY A

FUNCTIONAL VERiflCATION TO BE DONE FOLLOWING

ROUTINE CAllBRATION OF THE INSTRUMENT THAT

CONTROLS THE VALVE.

A PERSONNEL ERROR

OCCURRED IN THE CAllBRATION LEAVING THE VALVE

INOPERABLE.

THIS IS AN EXAMPLE IDENTIFIED IN

THE RECENT NRC INSPECTION REPORT.

's

o

.

.

VALVE 1RN-2358 - REPAlR WORK WAS DONE ON THIS

NOVEMBER, 1987

-

VALVE AND SUBSEQUENTLY FUNCTIONALLY VERIFIED

AND RETESTED PROPERLY.

ADDITIONAL REPAlR

WORK WAS NEEDED SO MAINTENANCE PERSONNEL USED

THE SAME WORK REQUEST TO COMPLETE THE REPAIR

AND AGAIN FUNCTIONALLY VERIFIED THE VALVE

PROPERLY BUT IT WAS NOT RETESTED (STROKE

TIMED).

THE VALVE WAS OPERABLE WHEN LATER

RETESTED.

Tili3 VAS A PERSONNEL ERROR IN THE

WORK CONTROL PROCESS IN IMPLEMENTING POST

MAINTENANCE RETEST.

THIS IS AN EXAMPLE

IDENTIFIED IN THE NRC INSPECTION REPORT.

FEBRUARY, 1988

VALVE 1RN-21 - A MAINTENANCE WORK PLANNER

-

FAILED TO SPECIFY THE REQUIREMENT TO RETEST

THIS VALVE FOLLOWING A PACKING ADJUSTMENT.

THIS WAS A PERSONNEL ERROR IN THE WORK

. K~ROL PROCESS IN IMPLEMENTING POST

40 NTENANCE RETEST.

THIS IS AN EXAMPLE

.9 TIFIED IN THE RECENT NRC INSPECTION

nEF (f.

JUNE, 1988

VALVE 2ND-4 - PREVIOUSLY DESCRIBED.

-

AUGUST, 1988

VALVE INV-142B - PREVIOUSLY DESCRIBED.

-

SEPTEMBER, 1988 -

VALVES INS-18 S INS-1 - PREVIOUSLY DESCRIBED.

ALTHOUGH ALL THESE EVENTS WERE RELATED IN VARYING DEGREES TO THE

FUNCTIONAL VERIFICATION / RETEST PROGRAM, THE LAST 3 EVENTS WERE

THE MOST SIGNIFICANT SINCE THEY HAVE IDENTIFIED A DEFICIENCY IN

THE BASIC STRUCTURE OF THE FUNCTIONAL VERIFICATION PROCESS.

THE

REMAINDER OF THE PRESENTATION WILL FOCUS ON THcSG 3 SPECIFIC

EVENTS, THEIR ROOT CAUSES, OUR CORRECTIVE ACTIONS AND THE SAFETY

IMPACT.

o

'

.

6

.

FUNCTIONAL VERIFICATION PROGRAM

.

SEQUENCE OF EVENTS

,

DATE

TIME

EVENT

AN INPO AUDIT IDENTIFIED DEFICIENCY (MA.3-1)

4/87


IN THE FUNCTIONAL VERIFICATION PROGRAM.

THE

DEFICIENCY STATED THAT THE GUIDELINES FOR

FUNCTIONAL VERIFICATION TESTS 00 NOT SPECIFY

ALL APPROPRIATE TESTS THAT SHOULD BE

CONSIDERED FOLLOWING MAINTENANCE.

5/87-5/88 ----

A NEW MECHANICAL MAINTENANCE PROCEDURE MMP

1.6 WAS BEING DEVELOPED TO PROVIDE MORE

SPECIFIC GUIDELINES ON FUNCTIONAL VERIFICATION

TESTING.

'

A MODIFICATION WAS PERFORMED TO MOVE THE

6/87


TORQUE SWITCH BYPASS TO AN ADD-ON PACK, AND TO

REPLACE ALL JUMPERS WITH QUALIFIED WIRE.

WIRE

NO. 16 WAS NOT PART OF THE JUMPER WIRE CHANGE,

BUT WAS DISCONNECTED AND SUBSEQUENTLY

RECONNECTED TO THE WRONG TERMINAL AFTER THE

JUMPER WIRES WERE REPLACED WITH QUALIFIED

WIRE.

WIRE NO. 16 WAS INDEPENDENTLY VERIFIED

AS BEING ON THE PROPER TERMINAL.

IT WAS LATER

DISCOVERED NOT TO BE THE CASE.

-

~ -

.

.-

- . .

. - .

-- -

-._-

_ _ - . _ . _ _-

-

. - - -

. - -

.

.,

'~

,

,

?F

,-' - .

9/87-10/87 ----

IAE PERSONNEL PERFORMED THE TORQUE SWITCH

BYPASS MODIFICATION ON VALVE ACTUATORS

__

1NI-184B(185A).

THE MODIFICATION INCLUDED

MOVING THE PERMISSIVE INTERLOCK WIRING FOR

VALVES-1NS-1B(18A) TO A PREVIOUSLY UNUSED SET

OF LIMIT SWITCHES TO MAKE ROOM FOR THE BYPASS

,,

/-

WIRING.

CMD PERSONNEL WERE PERFORMING A MODIFICATION

6/15/88


ON 2NI-184 AND FOUND WlRE NO. 16 TO BE

INCORRECTLY CONNECTED TO TERMINAL 42.

t

.

CMD PERSONNEL COMPLETED THE MODIFICATION AND


PLACED WIRE NO. 16 ON TERMINAL 31 AS PART OF

!

THE MORE RECENT MODIFICATION.

QA PERSON DISCOVERED THE MISPLACED WIRE

6/27/88


,

DURING AN AUDIT OF THE MODIFICATION.

QA PERSON RESEARCHED THE ELECTRICAL CIRCUlTRY


FOR THE WIRE AND DETERMINED IT WAS PART OF THE

AUTOMATIC CLOSURE CIRCUlTRY FOR VALVE 2ND-4.

lAE PERSONNEL WERE PERFORMING AN INSPECTION

8/29/88


OF ATC4A AND DISCOVERED LINK l-1 OPEN.

,

l

IAE PERSONNEL RESEARCHED THE ELECTRICAL


CIRCUlTRY FOR LINK l-1 AND FOUND THAT THE LINK

WAS PART OF THE AUTOMATIC CLOSURE CIRCUITRY

'

FOR VALVE INV-142B.

8/29/88

lAE PERSONNEL NOTIFIED OPS CONTROL ROOM


PERSONNEL OF THE OPEN'D LINK IN THE AUTOMATIC

CLOSURE CIRCUlTRY FOR VALVE INV-1428.

.

> 1

.y

.

.

.

IAE PERSONNEL CLOSED LINK l-1 AND FUNCTIONALLY

8/29/88


.

VERIFIED THAT THE AUTOMATIC CLOSURE CIRCUlT

WAS NOT OPEN FOR V'ALVE INV-1428.

~8/30/88- ----

PROJECT SERVICES PERSONNEL REVIEWED ALL

9/1/88

PREVIOUS TORQUE SWITCH BYPASS MODIFICATIONS

FOR DOCUMENTATION OF AN ADEQUATE FUNCTIONAL

VERIFICATION.

9/2/88

PROJECT SERVICES PERSONNEL INITIATED A WORK


REQUEST TO REVERIFY THE INTERLOCKS BETWEEN

VALVES 1NI-184B (185A) AND INS-1B(18A).

9/2/88

IAE PERSONNEL DISCOVERED ELECTRICAL


PERMISSIVE INTERLOCK CONTACT IAS3 BETWEEN

VALVES INI-184B(185A) AND INS-1B(18A) OPEN

WHEN IT SHOULD HAVE BEEN CLOSED AND CONTACTED

OPS PERSONNEL CONCERNING THE DISCREPANCY.

9/3/88

PROJECT SERVICES PERSONNEL INITIATED A

MODIFICATION TO JUMPER THE OPEN CONTACT 1AS3

AND IAE PERSONNEL INSTALLED A JUMPER AROUND

PERMISSIVE INTERLOCK CONTACT lAS3 AND THIS

RETURNED ELECTRICAL CONTROL OF VALVES INS-1B

(18A) TO OPS CONTROL ROOM PERSONNEL.

l

9/9/88

STATION PERSONNEL REVIEWED AN EARLIER


INCIDENT IN WHICH A WIRING ERROR ON 2NI-184B

DISABLED THE REQUIRED SWITCHOVER FUNCTION.

10/1/88

FUNCTIONAL VERIFICATION PROCEDURE MMP 1.3 IS


PHASED OUT AND REPLACED BY MMP 1.6.

,

. , ,

.-

.

.

.

1NV-142

PROBLEM DISCOVERED - 8/29/88

OPEN ELECTRICAL LINK FOUND WHICH DEFEATED AUTOMATIC CLOSURE OF

VALVE 1NV-142.

ROOT CAUSE

DURING MODIFICATION ON VALVE IN 1987 REFUELING OUTAGE TO C)lANGE

OPERATOR MODEL AND ADD ELECTRICAL ANTI-HAMMER CIRCUIT, A WIRING

CHANGE CONNECTED A PREVIOUSLY UNUSED ELECTRICAL LINK.

PERSONNEL ERROR RESULTED IN LINK REMAINING OPEN.

o

,

.

j

.

(

.

'

1NV-142

.,

,

,.,

SAFETY ANALYSIS

A)

THE SAFETY SYSTEM SIGNAL FOR THE AUTOMATIC CLOSURE OF VALVE

1NV-142B HAD BEEN DEFEATED, HOWEVER:

VALVE INV-142B COULD HAVE BEEN CLOSED LOCALLY AS WELL AS

FROM THE CONTROL ROOM.

VALVE INV-141A WAS OPERABLE DURING THIS TIME PERIOD AND

CAPABLE OF ISOLATING THE VCT.

B)

IN THE EVENT OF A SMALL BREAK LOCA DURING THIS TIME PERIOD AND

INV-141A WAS INCAPABLE OF BEING CLOSED:

THE VCT WOULD BE DEPLETED AND ITS HYDROGEN BLANKET COULD

ENTER THE NV PUMP SUCTION LINE, RENDERING THE PUMPS

INOPERABLE IN APPROXIMATELY 18 1/4 MINUTES AFTER SAFETY

ACTUATION.

VALVE INV-142 COULD HAVE BEEN CLOSED LOCALLY IN 15

MINUTES.

THE REACTOR COULD BE SHUTDOWN SAFETY WITH THE CONTROL

RODS.

MAKEUP TO NC SYSTEM WOULL BE PROVIDED BY SI PUMPS

WHEN PRESSURE REACHED 1500 PSIG.

.

.

NY SYSTD(

,

'

s-

NORMAL LETDOWN AND CHARCINC

(!( .

.

.

9,

.

4;

. .,

LETDOWN FROM NC SYSTDI

V

voltam

CONTROL

TAMK

NV-141

-

+

ov

NV PIMP

t

NV-221

MAKEUP TO

< RWST

C

4

SYSTEM

i

NV-222

v

NV PUMP

l

P

, - -

.-n.---

nn,

- --.----,

, , , _ _

- - - - - - - - , - - - -


,,__-.--e

n-

, ,-. -, , - -- - - - - - - -,- - - - --- - , ~ -

-

-

-

.

.

4

.

,

k

CORRECTIVE ACTION

1NV-142

1)

IAE PERSONNEL CLOSED LINK L-1 AND FUNCTIONALLY

VERIFIED AUTOMATIC OPERATION OF VALVE INV-142.

2)

ALL MODIFICATION PACKAGES ON VALVE OPERATORS FOR BOTH

UNITS WERE REVIEWED FOR ADEQUATE FUNCITONAL

VERIFICATION.

TEMPORARY TEST PEOCEDURES WERE

INITIATED WHERE APPROPPIATE.

3)

MAINTENANCE MANAGEMENT PROCEDURE 1.6 ISSUED WHICH

DEFINES THE MINIMUM FUNCTIONAL VERIFICATION

REQUIREMENTS.

REVISION IN PROGRESS AT TIME OF EVENT

DISCOVERY.

4)

CHANGES TO PROCEDURES ON REMOVAL AND INSTALLATION OF

VALVE OPERATORS WHICH INCLUDE FUNCTIONAL VERIFICATION

REQUIREMENTS FOR ALL LIMIT SWITCHES, ASSOCIATED

,

INTERLOCKS AND AUTOMATIC FUNCTIONS.

!

.

. - - -

, < . .

. .

, . ,

.

.

.

.

INS-1, 18

PROBLEM DISCOVERED

9/2/88

.

ELECTRICAL CONTACT FOUND OPEN WHICH BLOCKED OPEN PERMISSIVE

t

NECESSARY TO OPEN INS-1,18 WHEN 1NI-184, 185 REACHED FULL OPEN

POSITION.

ROOT CAUSE

POSSIBLE PERSONNEL ERROR IN TORQUE SWITCH BYPASS MODIFICATION

ON 1NI-184, 185 DURING 1987 REFUELING OUTAGE.

,

.

.

.

.

.

SAFETY ANALYSIS,

THE FUNCTION OF NS-1,18 IS TO ISOLATE THE A(B) NS PUMP FROM REACTOR

BUILDING SUMP LINE A(B).

DURING THE INJECTION PHASE OF A LOCA

NS-1,18 IS CLOSED AND THE NS PUMP IS TAKING A SUCTION FROM THE FWST

VIA NS-20(3).

ON A LOW-LOW FWST LEVEL NS PUMP A(B) IS STOPPED AND

ITS SUCTION IS REALIGNED BY THE CONTROL ROOM OPERATOR FROM THE FWST

TO THE CONTAINMENT SUMP BY CLOSING NS-20(3) AND OPENING NS-18(1)

SINCE NI-185(184) HAS ALREADY OPENED AUTOMATICALLY.

NS PUMP A(B) IS

THEN RESTARTED.

THEREFORE, IN ORDER FOR NS-18(1) TO OPEN,

NI-185(184) MUST BE OPEN AND NS-20(3) CLOSED.

DURING THE ABOVE TIME PERIOD, NS-18(1) COULD NOT HAVE BEEN OPENED

FROM THE CONTROL ROOM IF THE NS-20(3) AND NI-185(184) PERMISSIVES

HAD BEEN MET DUE TO THE 1AS-3 CONTACT SETUP ERROR IN THE SWITCH PACK

ON N1-185(184).

NS-18(1) COULD HAVE BEEN MANUALLY OPENED LOCALLY

IF N1-185(184) WERE TO OPEN.

THE NORMAL ALIGNMENT OF NS IS WITH

NS-20(3) OPEN AND NS-18(1) AND N1-185(184) CLOSED.

THE US SWAP OVER TO THE CONTAINMENT SUMP FROM THE FWST IS PERFORMED

BY CONTROL ROOM OPERATORS USING EMERGENCY PROCEDURE EP/1/A/5000/2.3.

THUS, DURING THE ABOVE TIME PERIOD WHEN THE SUBJECT INTERLOCK WAS

NOT FUNCTIONAL THE NS-18(1) VALVE REALIGNMENT COULD HAVE BEEN

PERFORMED MANUALLY IF REQUIRED.

,

I

f

- - - -

_-

.._.

, ,

.

~

.

.

.

.

5

'

-

I

4

"

8 [::[l I

t

.

.

-

.

E

0

E

l*

I

.

-

5

sa.

-

<CE

=2 I

E

-

l_3

'

g

5

nt

-

-

i

lN g{lv2

I

~

,"

so.1

E

==

wi

i:

=

c=

j

s

8

i

_

EENs

"g i i

[

E!! [g ;

E

i

3R

4

4

p i j

t

3

I

, "A I

o

sc

as

.

hjg

g

  • / -

=

s

CQ

t.t_

r

_

-

,

's l

3

C

-

"

-e,li.l!I

W

i

c

.i -c<

e

'

5

I

,

3G

.d

a)

,

y

i

-

-

7

5

  • T

Sd

d*

c.. . ,

g

l

=

I

R

-

-

--35

n5

c

-

A

/

s

J

[m. O (

f ME

. * NE

'

.

,,

'

3

2

"

R

R

!

1

.

"i

3

l

v

v

.

i

m

,

i

i

,

k.1 .".1

e'.

.l.

.1

'..*2

.-*

.-1

.",

. 2,:;

3*

2

.l_

j_ _

_

,.-l__'_

,

-

-

e

+

-

A

S

1

y

.\\

A

I'

l

i

i

i

4

ZS

.:.,3

IS

ZS 23

IS

h

h

<

4

c

,4

<

<

<

<

c

l4

<

<

<

<

<

<

<

<

4

h

k

<

~

.

em

- - . - - - . - - , ,

, - - , - - , - - - - - - . - . - . - - .

, , - - - - , . _ . , - .

--,

-.--., -

n

-

"

.

.

.

.

.

CORRECTIVE ACTION

INS-1,18

1)

OPS SHIFT PERSONNEL WERE INFCRMED THAT INS-1B AND 18A

WOULD HAVE TO BE MANUALLY OPERATED LOCALLY DURING ACCIDENT

CONDITION.

2)

IAE PERSONNEL IMPLEMENTED MEVN-1454 WHICH RETURNED CONTROL

TO CONTROL ROOM SWITCH BY PLACING JUMPER AROUND OPEN

CONTACT.

3)

MODIFICATION INITIATED TO REMOVE JUMPER AND CORRECT OPEN

CONTACT AT VALVE OPERATOR.

TO BE COMPLETED DURING 1988

REFUELING OUTAGE.

4)

CHANGES TO PROCEDURES ON REMOVAL AND INSTALLATION OF VALVE

OPERATORS WHICH INCLUDES FUNCTIONAL VERIFICATION

REQUIREMENTS FOR ALL LIMIT SWITCHES, ASSOCIATED

INTERLOCKS, AND AUTOMATIC FUNCTIONS.

,

5)

IAE PERSONNEL HAVE REVIEWED ALL WORK REQUESTS WHICH

INVOLVE SAFETY RELATED MOTOR OPERATED VALVE ACTUATOR WORK

SINCE THE LAST ESF TEST ON BOTH UNITS.

6)

IAE PERSONNEL WILL HEAD A REVIEW GROUP TO STUDY THE

STATION'S FUNCTIONAL VERIFICATION, RETEST AND

POST-MODIFICATION TESTING PROGRAMS TO ENSURE PROPER

OVERLAP EXISTS.

,

i

-_

--

-

.

-.

.

.

.

2ND-4

PROBLEM DISCOVERED - 6/27/88

WIRE WAS CONNECTED TO WRONG TERMINAL ON 2NI-184 OPERATOR WHICH

CAUSED THE INTERLOCK THAT AUTO CLOSES 2ND-4 TO BE INOPERABLE.

ROOT CAUSE

PERSONNEL ERROR WAS MADE DURING MODIFICATION ON TORQUE SWITCH

BYPASS IN 1987 REFUELING OUTAGE.

.

Wv

^

9

0

-

%

e

nN

>M

eg

eg

Wg

Wg

i k

J k

[

)g

5

%

Ja

_

J

n-

l

"

"

i ,

.

9

2

5

l:

11:

gp

!i

a

1

a

)

>

n

s8

-

AS

INip :D

p,

k

me

1

- - - _ -

_ _ - _ -

. - -

.

O

.

.

.

SAFETY ANALYSIS

2ND-4

THE RESIDUAL HEAT REMOVAL (ND) AUTOMATIC SWITCH OVER SEQUENCE

FROM THE INJECTION MODE TO THE COLD LEG RECIRCULATION MODE

CAUSES THE CONTAINMENT SUMP ISOLATION VALVE 2NI-184B TO OPEN.

THIS AUTOMATICALLY INITIATES THE CLOSURE OF 2ND-4B.

THIS

OPERATION ISOLATES THE WST ND PUMP SUCTION AND ALIGNS IT TO

THE CONTAINMENT SUMP.

THE MIS-WIRED INTERLOCK WOULD HAVE

PREVENTED THE CLOSURE OF 2ND-4B.

ON VERIFICATION OF SWITCH OVER, THE OPERATOR WOULD NOTE THAT

2ND-4B WAS STILL OPEN AND CLOSE IT.

THE OPERATOR STILL

RETAINED FULL REMOTE CONTROL OF THE VALVE.

ALSO, PER

PROCEDURE, THE UPSTREAM FWST ISOLATION VALVE 2FW-27A, WOULD BE

CLOSP.D BY TTfE OPERATOR AFTER SWITCH OVER.

THI.a ISOLATES FWST.

THE MIS-WIRED INTERLOCK HAD NO ADVERSE EFFECT ON THE SAFETY

INJECTION RECIRUT ATION VALVE ALIGNMENTS AND OPERATOR ACTION TO

CLOSE 2ND-4B IS AVAILABLE.

THEREFORE, THE SAFETY INJECTION

FUNCTION REMAINED OPERABLE.

I.

q

.

.

.

CORRECTIVE ACTION

2ND-4

1)

ALL NSM PACKAGES WERE REVIEWED FOR ADEQUATE FUNCTIONAL

VERIFICATION.

TEMPORARY TEST WERE WRITTEN TO PERFORM

FUNCTIONAL VERIFICATION WHERE APPROPRIATE.

2)

MAINTENANCE MANAGEMENT PROCEDURE

1. 6 ISSUED WHICH DEFINES

THE MINIMUM FUNCTIONAL VERIFICATION RZQUIREMENTS FOR A

PARTICUU R COMPONENT.

REVISION IN PROORESS AT TIME OF

EVENT DISCOVERY.

3)

CHANGES TO PROCEDURES ON REMOVAL AND INSTALLATION OF VALVE

OPERATORS WHICH INCLUDE FUNCTIONAL VERIFICATION

REQUIREMENTS FOR ALL LIMIT SWITCHES, ASSOCIATED

i

'

INTERLOCKS, AND AUTOMATIC FUNCTIONS.

l

l

4)

REVIEW )F ALL WORK REQUEST ON SAFETY RELATED MOV'S

ACTUATORS.

l

5)

REVIEW GROUP TO STUDY FUNCTIONAL VERIFICATION, RETEST AND

POST-MODIFICATION TESTING PROGRAMS.

.

.

o

.

,

GENERIC CORRECTIVE ACTIONS

-

1)

FUNCTIONAL VERIFICATION RE JIREMENTS, MMP-1.6, FULLY

IMPLEMENTED WITH ALL TRAINING COMPLETED.

2)

CHANGES MADE TO THE FOLLOWING PROCEDURES TO GIVE MORE

DETAILED GUIDANCE FOR WORK ON VALVE OPERATORS.

IP/0/A/3066/01A - REMOVAL & INSTALLATION OF LIMITORQUE

,

vPERATORS

-

IP/0/A/3066/02A - REMOVAL & INSTALLAT*0N OF ROTORK

OPERATORS

3)

RELATED INSTANCES WILL BE REVIEWED WITH ALL IAE PERSONNEL

REVIEW IN PROGRESS.

4)

HAVE REVIEWED ALL WORK ON UNIT 2 SAFETY RELATED MOV'S

ACTUATORS SINCE LAST SAFEGUARDS FUNCTIONAL TEST AND

ADEQUACY OF FUNCTIONAL VERIFICATION EXNIINED.

SIX UNIT 2

VALVES HAVE BEEN IDENTIFIED FOR FUFTHER EVALUATION.

ESF

TESTING WILL BE COMPLETED ON UNIT 1 DURING CURRENT

REFUELING OUTAGE.

5)

SPECIAL REVIEW GROUP REVIEWING FUNCTIONAL VERIFICATION,

RETEST, AND POST-MODIFICATION TESTING TO ENSURE ALL AREAS

ARE COVERED.

r

6)

ENGINEERED SAFETY FEATURES ACTUATION TEST WILL BE

CONDUCTED AT END OF FUTURE REFUELING OUTAGES TO ENSURE

E

I

SYSTEMS FUNCTION AS DESIGNED.

,

,

l

i

1

- - -

- -

.

- -

.

-

-

.

.

. - .

.

.

.

.

-

-

.

-

.

WOW

fn'efo@rcDo*

,

WR# ixxpyt

.

Dated /tt/>j

,

Wiring Functional Verification Checklist

'

l Terminals l Device l Function i

l0l IlCl

I

Device

i Method Used for functional

I

i

I

l

Verification

l

l

26 - 27

l

CT/LS ICLars T$ l #P6NGD du 7dAfut au clos ( 5tATI

I V Vl

'

I

l

24 - 25

l

OT/LS 10F(>/ L S 10MNED #M t./MIT TET/f f SPf4 FEAT l V l V I Y l

t

l

6-

7

l

CAS1

lbfbl6Y

l#aNV tYttfD #Ns' 'dY r

-[u$ [

I V I V I V l

y/Aa _j

1

15 - 16

i

OASI

INdT Uf6D l

A//A

l

l

8-

9

i

CAS2

lit C t.lG#T lC.pNTAsL Rsorvi VsRiric.Afte r/

lVI K V[

l

17 - 13

l

OAS2

lGRGtd UGHTICinT(ot. wm VGtiflCAYION

l V l Vi vl

l

10 - 11

l

I AS 1. ' livs4lf. L G H fl $",,'yT ' r#ed $r

//'

I V l V I V"l

l

12 - 13

I

IAS2

lydf tuso l- u/A

-;

l

l

19 - 20

l

IAS3

lut7 uSG l-N/M

'

'

'

l

l

21 - 22

l

IAS4

!N.f7 uJE b lW/A

i

l

'

lurERL*cK TO Cgscx touriauer/ n.sm C1 t 2,1

l

23 - 29

l

IAS5

(2 Alr /W B l

w Tuas As mvt raar exLet. l yl yI yl

l

30 - 31

I

IAS6

l##7 (L1IsD l A//A

i

i

i

-l

Of6M Tot. Qui HELD QVEM T{S SPEN AND 0FGW6D

l

33 - 34

I

IAS7

Intrm. sc _ !steernoun ntrieb t/: usy orsu. I VI VI Vl

'

%uts ron.cas'et.seTareau.v. snrrso gas us t casso.f V l VI jl

Prus cute vis ersH aan cusa vau

-

l

35 - 36

I

I AS o,

rass so.

iurtnoce ro cHEensk churinuort r,um 27- a t

j

l

37 - 33

I

IAS9

lant> 4 3

l/v vuM4 A s VA (.v1f U A y C W s.5 b .

I ,I

l ,l

-

l

40 - 41

l

IAS10 l'"lu'$r $ "l?u s'N ! a ? !! N ? ? c$L N .

I d l #1 V1

1

42 - 43

1

IAS11 INdT M 6D }. - ///A -

l

l

'

l

44 - 39

I

IAS12 l##T d:fGb 4 A /A ---

!

l

/

'

'

Interlocks from Other Devices And/0r Automatic Signals

l

DEVICE

I

!ETH00 USED TO FC';CTIC?! ALLY VERIFY

l

CU lHAMYc! uran $~Y? CP tet corqu7tk luctcsYnH I6/

ALL .T

115'17 o du s

I

Narco s.s coarurc 3.g

cco I'D%Ir*L TotMT 2DNZ13t i CMGcKGD Clee H T& t. IN DICA fto p) IA] A LL 3 is$lfel AS

l

"C U iiusunuu so ra:L +1 Al4-5 (CNecus courinusf y R in1 CA rc X , fen m u u Y < E

l

NAruce L5 Cou T6C71

e

I

l

l

_

I

I

I

I

I

I

E*YA MPL.E. $

l? AlZ ' '

's

ASSU M G O PERA 70R

Wo9s

26m0VED

fRom

7'H6

VA L.VC .

AArHC0

LIMIT

fl)lTCHES TGmov6h ALSD.

OPERArnz

pjn7

I

UWl4tRED' If IT !JAS, FUNcnid V6RIFICKfloN SHel/L1) HAVE EGEs Qjt< yg

rpom

THE ATC, C AS/ME T

nigm wat5.

e

'

O

l

"3

E U :

.

NE {

  • 3 i l

7

7

'

W

g

-

a

==g

Iws

EMI l

l

l

~

w

W

1lI

=

7

7

l

!

=

i

5

-

m

I 5

y

db-

2

I

5

  • O

o

5

o3

gI

-W2

-

w

-

W

>W

EO

H

h

'

L. < M

__

DW

=

W

I

gg

E*>

W

2

$

I

gi

    • W

E

W

3

O

I .,

E42

3

4

d

a

E

u

a

-

f

!

l

l

l

W

!

s

=

e5

0

o@>

5

g5

z

.J

g

w<$

I.

I

E '!!

!

l l

7

7

7

E>o

-

i!!a

e

=

<

=

v

E

W

5

-**

M>

--s1

U

"

-o

W o

s

,

b

!I' l

l

l

$

'

'

"

a

=r-

-

z

-

-

m

-

W

W

l

4

W ,g 4

w

E

E

3 ,.

E

[I

b

Y

k

l

Sh

-

32

g E e.

Z

g

H

Ou

O

O

3

k$g

=

-

O

U

M

-

3

6

JU

'

2

0

I

-

4

l

3

W

1

-

%

.J

I-

EN

E

l

C

W

$ H

W

QQ

>

-

!

w

w

g g

we

'

z

z

=

=

,

.J

U >=

j

d.g

K

W

O

u

<

x .s

<

r

u.

-

Z

33

w]$

4

4

-

Q

we

c-

6

-

g

-

w

3

>

Z2

O

>

=

W.

m

w

O

4

Z .J

-e

ZZ

,$

h

-

-

I

.1

M. $

Z-

.

W

(o

-

-w

!

I

O j

m

Q

OU

-

.

- r

z

-

2

Q

.

. p

WW -

-I

U

w2

W

'De

O

  • (

0

Q

w

ZN

.J W H

>

Q

Q..

OMZ

AJ

w

w

44

UME

=

w

4

e

2

MM-

2U3

QWG

3MW

O

..

O

O '5

.

23:y

gw

35

'

.

e

I-

E

'M

M

EMQ

N

~

"

$

- ee

P4

1

e

.e. k ..

E I

I

'

B

n

x

x

l%

aWX

d

EO

M

  • 2=

g

&UM

E

-

.

e4=

g.

,... . _,

0

E

G. W- >

t2

-g g

a

,

=

-

  • <g

.sgg,

0<=

x

x

x

x

x

x

m

5

lN

.$

a

=

C

    • $

0

l

u

  • >

U

C

5

<d

-

x

x

1.

x

a

u<

r.s

~>

,

=

-

l1

EC

tia I

4

=

vx. ,v

2

_

4

-

x

x

.<

x

x

x

x

-

.

s o.

gs 2

.

wWs

..

.

u:;

i!!

-

-

ssk

2

x

x

x

x

x

x

x

x

x

-

E!=

5 u

g

-

=

__

-

i

l

-

"u

o

l

0*

l

W

Wwd

W*gg

i

w g

,

t o

wg

x

x

x

x

x

x

x

x

x

x

x

x

l

u.

,e w

l

l

EgI

'

-

,

!

.

si

il, l!.li il

d

1 !! 1: li !i il li

n

i

i=

0 D

.i .i

i .i

.

Ja i;

5!

! =lil' !:

ja

at

la

!

-j

I! l.

-

l

i

  1. ,'"

it

su missor:Aiva

333 s

O

0117814 d17

fgg33333

o

. - - - ,

.

- _ .

, , _

-

. _ _ _ _ _ _ _

- _ _ _ _ _ _ _ _ - _ _ _

__

.

o

,

4

FURTHER REVLEW OF POST OCCURRENCES BY NRC AND STATION PERSONNEL

HAVE IDENTIFIED ADDITIONAL POTENTIAL INDICATORS OF INCOMPLETE

FUNCTIONAL VERIFICATION FOLLOWING MAINTENANCE.

EXAMPLE 1:

"lN FEBRUARY 1987, POST MAINTENANCE TESTING ON INM26B

WAS INADEQUATE IN THAT WHATEVER TESTING WAS PERFORMED Dl0 NOT

REVEAL THAT TERMINALS HAD SHORTED, CAUSING THE VALVE TO CYCLE OPEN

ON AN ESF SIGNAL INSTEAD OF CLOSE".

A FAILED ACTUATOR MOTOR WAS REPLACED AND THE VALVE WAS

IT ' LECTRICALLY FROM THE CONTROL

FUNCTIONALLY TESTED BY CYCLING

c

ROOM.

THE VALVE'S INDICATIONS WAS VERIFIED TO WORK CORRECTLY AND

,

THE LEAK TEST AND VALVE STROKE TIMING TEST WERE COMPLETED

]

SATISFACTORlLY.

LATER, THE VALVE CYCLED CONTINUOUSLY DURING A

SLAVE RELAY TEST AND A WIRE TERMINAL WAS FOUND SHORTED AGAINST THE

$

BARREL NUT.

SINCE INM-26B HAD BEEN SUCCESSFULLY CYCLED FROM 1HE

CONTROL BOARD, ITS FUNCTION WAS DEMONSTRATED.

EXAMPLE 2:

"lN AUGUST, 1987, NO RETEST WAS PERFORMED ON THE FLOW

INSTRUMENT CONTROLLING ND PUMP 1B RECIRCULATION VALVE, IND67B,

,

RESULTING IN A VIOLATION".

,

WORK WAS PERFORMED ON THE FLOW INSTRUMENT CONTROLLING ND PUMP 1B

RECIRCULATION VALVE IND678, USING A PROCEDURE THAT DID NOT

i

IDENTIFY THE COMPONENT AS BEING SAFETY RELATED AND DID NOT REQUIRE

FUNCTIONAL VERIFICATION SUBSEQUENT TO MAINTENANCE.

HOWEVER, THE

ROOT CAUSE OF THE INCIDENT WAS DUE TO A FAILURE TO FOLLOW

l

PROCEDURE WHICH LEFT THE INSTRUMENT ISOLATED AND PROPER FUNCTIONAL

!

f

VERIFICATION WAS NOT PERFORMED.

I

EXAMPLE 3:

"ON NOVEMBER 19, 1987, WHILE REVIEWING AN lAE WORK

REQUEST FOR FINAL SIGNOFF, AN lAE STAFF PERSON DISCOVERED THAT

f

f

ADDIT ONAL TESTING WAS NEEDED ON 1RN235B, 1B NS HEAT EXCHANGER

'

COOLING WATER INLET".

I

- _.

,

. .

.

- - - - - - - - - - - - - - - - - - - - - . _ _ _ _ _ _ - - - -

--

o

.

'

A SEAT LEAK ON VALVE 1RN-235B WAS REPAIRED UNDER A WORK REQUEST.

-

A RETEST AND FUNCTIONAL VERIFICATION WERE SUCCESSFULLY COMPLETED

ON THE VALVE.

WHEN A LEAK DEVELOPED, THE NEXT DAY THE ORIGINAL

WORK REQUEST WAS REOPENED TO PERFORM THE WORK.

NO RETEST WAS

PERFORMED ON THIS VALVE.

THE ROOT CAUSE FOR THIS INCIDENT WAS

PERSONNEL ERROR.

A CONTRIBUTING CAUSE WAS DUE TO A PROCEDURAL

DEFICIENCIES (MMP 1.0 AND 1.3) WHICH ALLOWED A WORK REQUEST TO BE

REOPENED ONCE IT HAS BEEN SIGNED COMPLETE.

SUBSEQUENT CHANGES TO

THE WORK CONTROL SYSTEM HAS ELIMINATED THE USE OF A WORK REQUEST

FOR ADDITIONAL WORK AFTER RETEST IS COMPLETED.

AFTER FURTHER REVIEW, THE FOLLOWING ONE EXAMPLE, CITED IN NRC

INSPECTION REPORT 369/88-29, INDICATE A PROBLEM WITH THE WORK

CONTROL SYSTEM.

THIS PROBLEM HAS BEEN ADDRESSED SEPARATELY TO

RCDUCE THE POSSIBILITY OF RECURRdNCE.

EXAMPLE 4:

"ON MARCH 28, 1988, IT WAS DETERMINED 1RN21 UNDERWENT

i

MAINTENANCE WITHOUT A SUBSEQU21T RETEST".

A PACKING ADJUSTMENT WAS PERFORMED ON 1RN21 UNDER A WORK REQUEST.

THE WORK REQUEST INCORRECTLY IDENTIFIED THAT A RETEST WAS NOT

l

REQUIRED AND RN21 IS IDENTIFIED AS A COMPONENT REQUIRING RETEST

l

PER STATION DIRECTIVES.

HOWEVER, THE ERROR THAT OCCURRED WAS THE

RESULT OF PERSONNEL ERROR AND A FAILURE TO FOLLOW PROCEDURES AND

l

WAS NOT DUE TO THE FAILURE OF THE FUNCTIONAL VERIFICATION PROGRAM.

.

e

l

l

l

_ - - _ - - _

2lD/78

'

llIC d'u.Y /$<6x 'c95

-

,ygee;cf

. . -

s*

AMW

r112/

Sf&

&j, ib.u-

^

/Y/Ph/PD23

Ytllo o i

ibson

b i( K U h s N l y h v.

TgJL.

J . f.

v > tt P -

Acvu

pre. 94c. AO,w H

BlE

Sq.I,hm6 N7

0< 91- hell

Oqvi

(OT

kl.A.

(e,

f%A.

bale

&&un

h'CH4

MArv

AMC $&

w 7'd om

se us/anw

&

e

it./. .S<anf

Asbr.d.GGkitP

?.K'. % b ~

su., (-bu r,9

igo,g//ef

'

.0 %

m

h . 3 A/An

fl u .. L f

L + .

ititu R.a

$1b $hlEAU

d

ud

L)Rqc.

6 r.wx&lGcctwk(v

A/RClRE.

e

Rzc

k cef G

Datu,

e ic- r

f

,U. /s

VL.

>-ow n k e

i3ra.,c4 cs, + b e a

fr

12. O . 5 Hrhe PL.

co n p a n c c % w cerz.

y ge./sc %

Bf/hf7mi/bir

Supf e / rec 4mce/ Servicer

puhe/gesei,.e

f,u. 2 G.re.a_

yp duece u heet.

ka

r & . xs e cura u.

su ~~ rev.

harfsuc.via

/ E4t

U it%'//~cs3)

/b /c' =' , A!' m4

bVh~

6L&cle

N opl G 'ew

Dtdu. / pnv

3

,

l

E' W

l

ff,A' f.J.,

d /?$'$%+97 d L C./

/