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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO LER)
MONTHYEARML20151W2321998-09-0808 September 1998 Ro:On 980826,facility Bldg Air Monitor (Fam Channel 4) Failed Daily Fam Alarm Checks Prior to Reactor Operation. Caused by Failed Alarm Relay.Staff Is Preparing Formal Written Procedures for Testing Configurations for Fam Sys ML20217A0891998-03-18018 March 1998 Ro:On 980218,potential Reactor Safety Failure Discovered W/ Reactor Shutdown.Caused by Manual Scram Function Bypassed by Sticking Reset Contact in Console Power key-switch. Protective Action Reset Switches Wired ML20199C5371997-11-11011 November 1997 Ro:On 971030,shim Safety Number 2 Was Found to Be Binding & Became Stuck in Withdrawn Position & Control Rod Failed to Scram.Caused by Incorrect Spacing Between Hold Down Foot & Bundle top-handle.Procedure SOP-II-I Modified ML20129H5191996-10-30030 October 1996 Ro:On 961015,loss of Facility Power Occurred Causing Reactor Scram Due to Lack of Attention to Detail & Excessive Distractions to Operations.Startup Checklist Had Several Individual Instrument Checks Combined Into Single Items ML20079C2481991-06-10010 June 1991 Ro:On 910607,reactor Operated for 30 Minutes at 1 MW W/O Facility Air Monitors in Operation.Operator Removed from Watch Standing Duties.Final Rept Will Be Forwarded Upon Completion ML20066H1401991-02-0808 February 1991 Special Rept 90-01:on 910125,during Annual Fuel Insp of Operational Core VIII-A,fuel Elements 6502 & 8468 Failed to Pass go-no-go Gauge Test for Excessive Transverse Bend. Elements Replaced W/Spare & Fuel Bundles Relocated ML20012E0661990-03-0909 March 1990 RO 90-01:on 900228,reactor Operator Received Servo Fault Alarm.After Directed Shutdown,Complete Loss of Linear Power Channel Noted.Caused by Corroded Connector at Detector Leads.Connector Replaced.Part 21 Related ML20203B0091986-07-10010 July 1986 Ro:On 860708,no Rod Down Indication Received for Transient Rod Until Carriage Driven In,During Performance of Manual Scram for Reactor Shutdown.Caused by Malfunction of Reactor Safety Sys Component.Repairs Underway ML20199B1171986-06-0404 June 1986 Ro:On 860501,improper Handling of Experiment Discovered Which Could Have Resulted in Serious Operational Event. Caused by Insertion of $1.09 Reactivity.Postulated Accidents & Results & Related Info Encl ML20205Q2921986-05-16016 May 1986 Final Ro:On 860501,unanticipated or Uncontrolled Change in Reactivity Greater than One Dollar Occurred.Caused by Removal of Rotisserie from Face Water Notch.Proposed Changes to SOPs Developed as Listed ML20205J9311986-02-18018 February 1986 RO 86-01:on 860204,temp Recorder Providing LSSS Signal to Scram on High Fuel Temp Malfunctioned.Caused by Defective Motor Bearing.Bearing Replaced & Recorder Calibr ML20137Y6291985-09-24024 September 1985 RO-85-04:on 850912,transient Rod Followed Cylinder Out During Positioning of Transient Rod Cylinder.Air Solenoid for Transient Rod Sys Not Functioning as Designed.Air Solenoid Disassembled,Cleaned & Reassembled ML20127M4151985-05-0909 May 1985 Ro:On 850508,during Restart Following Power Failure,Facility Air Monitoring (Fam) Sys Inoperable for 15 Minutes.Caused by Turning Off High Voltage to Detectors.Procedures Revised to Verify Fam Sys After Power Failure ML20113D5681985-01-21021 January 1985 RO 85-2;on 850111,safety Channel 1 Detector Failed During Reactor Operation.Caused by Loose Connector Pin Making Intermittent Contact.New Connector Installed & Detector Verified Operable Prior to Reinstallation ML20134Q1961985-01-11011 January 1985 Ro:On 850111,reactor Shut Down When Safety Channel 1 Did Not Respond Following Annual Reactor Maint.Cause Undetermined. Detector & Cabling Replaced ML20134P7391985-01-10010 January 1985 RO 85-1:on 850108,fuel Temp Recorder Indicated 600 F Instead of 720 F.Caused by Failure of Reactor Safety Sys Channel. Faulty Slide Wire & Contact Arm Replaced ML20134Q2081985-01-0808 January 1985 Ro:On 850108,fuel Temp Recorder Indicated 600 F Instead of 720 F After Reactor Power Returned to 1 MW Following Sample Positioning.Reactor Shut Down & Faulty Slide Wire & Contact Arm Replaced ML20090E1251984-07-0202 July 1984 RO-84-4:on 840626,reactor Operator Noted That Fuel Element Temp Recorder Did Not Correspond to Digital Indication as Shown on Doric Temp Readout.Cause Not Stated.Failure Spurious & Could Not Be Reproduced ML20090D7841984-06-26026 June 1984 Telecopy Ro:On 840626,fuel Elements Temp Recorder Failed to Respond Following Temporary Reduction in Reactor Power.Cause Not Stated ML20090E1241984-06-15015 June 1984 RO 84-3:on 840604,reactor Operator Observed That Safety Power Measuring Channel 2 Not Responding as Reactor Power Level Increased Beyond 30 Kw.Caused by Loose Safety Channel 2 Signal Cable.Connector Replaced ML20090E5141984-06-11011 June 1984 RO 84-2:on 840528,erratic Performance of Reactor Servo Control Not Noted in Log.Caused by Personnel Error.Operator Cautioned to Be More Observant While Taking Log Readings ML20134Q2511984-06-0505 June 1984 Ro:On 840604,during Startup,Reactor Shut Down When Channel 2 Not Indicating in Expected Power Range.Caused by Faulty Connector.Faulty Signal Cable Connector Replaced & Normal Operations Resumed ML20092N9211984-05-29029 May 1984 Ro:On 840528,operator Received Servo Fault Alarm & Linear Power Channel Indication Failed Low.Caused by High Voltage Supply for Linear Defector de-energized ML20084H6171984-04-0202 April 1984 Ro:On 840319,discovered That Performance of Weekly Electronic Maint Checks Not Performed During Previous Wk of Operation.Caused by Inadequate Procedural Controls ML20078P0111983-10-28028 October 1983 Ro:On 831004,high Power Scram Received During Initial Reactor Startup While Banking Shim Safety Control Rods After Reaching 1 MW Power.Caused by Operator Manipulation of Control Rods.Procedures & Proper Documentation Emphasized ML20070N6471983-01-11011 January 1983 Ro:On 830110,fuel Temp Indication Failed to Respond During Reactor Startup.Caused by Shorted Thermocouple Wires in Terminal Box.Reactor Shut Down & Fuel Temp Instrument Connected to More Conservative Indication ML20070M8101983-01-11011 January 1983 Ro:On 830105,during Fuel Element Insp,Elements 7463 & 7486 Failed Go/No Go Test.Both Elements Had Been in Core Since 1973 & Not Inspected Since That Time.Both Elements Removed from Core ML20072A8231982-12-22022 December 1982 Ro:On 821204,power Calorimetric Performed to Determine Agreement Between Indicated Power & Calculated Actual Power Based on Pool Heatup Rate.Results Showed Minus 30.7% Error. on 821206,calorimetric Showed Plus 56.6% Error ML20067C9721982-10-29029 October 1982 Ro:On 821019,power Level Indication Dropped Approx 15% on Both Safety Channels.On 821027,electromagnet Current for Shim Safety 2 Went to Zero.Causes Not Stated.Electromagnet Coil Replaced ML20066A5731982-10-0505 October 1982 Ro:On 820928,during Operation,Fuel Temp Thermocouple Failed. New Instrumented Fuel Element Installed.Thermocouple Readings Normal ML20066A2491982-09-29029 September 1982 Telecopy Ro:On 820928,erratic Readings Noted on Fuel Temp Indicator.Reactor Shut Down Immediately.On 820929,different If Connected to Fuel Temp Channel & Thermocouple Readings Recorded at 300 Watts & 1 MW ML20063H0301982-07-22022 July 1982 Telecopy Message of Ro:On 820722,during Initial & Secondary Reactor Startup,Log Power Channel Rate Meter Failed to Respond.Cleaning of Switch Contacts Returned Instrument to Normal Operation ML20063H0731982-07-22022 July 1982 Ro:On 820722,during Initial Startup,Log Power Channel Rate Meter Failed to Respond.Cause Not Stated.Switch Contacts & Amplifier Boards Cleaned.Close Visual Insps Implemented ML20052B6671982-04-12012 April 1982 Ro:Final Rept Re Possible Loss of self-protection of SNM Ctr.Fuel Bundle May Not Have Decayed Below self-protection Limit as Discrepancies Existed in Readings.Survey Program Improved & Underwater Fuel Surveys Studied ML20050B3531982-02-12012 February 1982 Ro:On 820205,during Initial Startup,Linear Power Channel Did Not Respond.Rod Withdrawal Terminated.Caused by Detector High Detector High Voltages Switch in Off Position.Training Session Implemented on Monitoring of Instrumentation ML20009E4171981-05-15015 May 1981 Ro:On 810507,during Check of Reactor Operator Licenses & Status,Senior Operator License SOP-3478 Found Expired on 810427.Caused by Failure to Follow Administrative Procedures.Operator Relieved of Duties ML19352B1651981-05-0808 May 1981 Ro:On 810507,while Conducting Check of Reactor Operator License & Requalification Status,Found That License SOP-3478 Held by Gw Waldrop Had Expired on 810427.Caused by Defect in Administrative Procedures.Procedures Have Been Corrected ML19352B2101981-04-24024 April 1981 Ro:On 810409 & 14,during Reactor Prestartup Checks,Interlock Used to Prevent Withdrawal of Shim Safety Control Rods Found Not Functioning.Caused by Threshold Change Due to Change in Solid State Switching Device.Capacitor Installed ML20126L4481981-04-15015 April 1981 Ro:On 810409 & 0414,during Prestartup Check of Facility, Interlock to Prevent Withdrawal of Shim Safety Control Rods for Low Source Levels Was Not Functioning.Caused by Defective Relay.Relay Replaced Prior to Reactor Operations 1998-09-08
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20205Q3481998-12-31031 December 1998 Tx A&M Univ Sys Tx Engineering Experiment Station Nuclear Science Ctr 1998 Annual Rept. with ML20151W2321998-09-0808 September 1998 Ro:On 980826,facility Bldg Air Monitor (Fam Channel 4) Failed Daily Fam Alarm Checks Prior to Reactor Operation. Caused by Failed Alarm Relay.Staff Is Preparing Formal Written Procedures for Testing Configurations for Fam Sys ML20217A0891998-03-18018 March 1998 Ro:On 980218,potential Reactor Safety Failure Discovered W/ Reactor Shutdown.Caused by Manual Scram Function Bypassed by Sticking Reset Contact in Console Power key-switch. Protective Action Reset Switches Wired ML20217K1401997-12-31031 December 1997 Tx A&M Univ Sys Tx Engineering Experiment Station Nuclear Science Ctr 1997 Annual Rept ML20199C5371997-11-11011 November 1997 Ro:On 971030,shim Safety Number 2 Was Found to Be Binding & Became Stuck in Withdrawn Position & Control Rod Failed to Scram.Caused by Incorrect Spacing Between Hold Down Foot & Bundle top-handle.Procedure SOP-II-I Modified ML20149F3901997-07-15015 July 1997 Safety Evaluation Supporting Amend 14 to License R-83 ML20137Y0351997-04-16016 April 1997 Rev 4 to Nuclear Science Center Senior Reactor Operator & Reactor Operator Requalification Program ML20137H0541996-12-31031 December 1996 Tx A&M Univ Sys Tx Engineering Experiment Station Nuclear Science Center 1996 Annual Rept ML20129H5191996-10-30030 October 1996 Ro:On 961015,loss of Facility Power Occurred Causing Reactor Scram Due to Lack of Attention to Detail & Excessive Distractions to Operations.Startup Checklist Had Several Individual Instrument Checks Combined Into Single Items ML20115G5511995-08-31031 August 1995 Engineering Analysis of a Power Upgrade for Tx A&M Nuclear Science Ctr Reactor ML20082D5521994-12-31031 December 1994 Thirty-First Annual Progress Rept of Tx A&M Univ Nuclear Science Ctr, for Period of 940101-1231 ML20069H4271993-12-31031 December 1993 Thirtieth Annual Progress Rept of Nuclear Science Ctr Tx Engineering Experiment Station Tx A&M Univ Sys College Station,Tx ML20059G0301993-10-26026 October 1993 Safety Evaluation Supporting Amend 13 to License R-83 ML20094N5431991-12-31031 December 1991 Nuclear Science Center 28th Annual Rept,CY91 ML20079C2481991-06-10010 June 1991 Ro:On 910607,reactor Operated for 30 Minutes at 1 MW W/O Facility Air Monitors in Operation.Operator Removed from Watch Standing Duties.Final Rept Will Be Forwarded Upon Completion ML20066H1401991-02-0808 February 1991 Special Rept 90-01:on 910125,during Annual Fuel Insp of Operational Core VIII-A,fuel Elements 6502 & 8468 Failed to Pass go-no-go Gauge Test for Excessive Transverse Bend. Elements Replaced W/Spare & Fuel Bundles Relocated ML20070U0201990-12-31031 December 1990 Twenty-Sixth Progress Rept of Texas A&M Univ Nuclear Science Ctr,1990 ML20070R9351990-12-31031 December 1990 Twenty-Seventh Progress Rept of Texas A&M Univ Nuclear Science Ctr Jan-Dec 1990 ML20043F4391990-06-0404 June 1990 Revised Page 1 to Reactor Operator & Senior Reactor Operator Requalification Program,Rev Iii.Item 2.1.6 Changed to Include Physical Security Plan ML20012E0661990-03-0909 March 1990 RO 90-01:on 900228,reactor Operator Received Servo Fault Alarm.After Directed Shutdown,Complete Loss of Linear Power Channel Noted.Caused by Corroded Connector at Detector Leads.Connector Replaced.Part 21 Related ML20248J1691988-12-31031 December 1988 Twenty-Fifth Progress Rept of Texas A&M Univ Nuclear Science Ctr,Jan-Dec 1988 ML20151Y9031988-07-15015 July 1988 Review of Texas A&M Univ Nuclear Science Ctr - Beam Port Experiment ML20151L6591988-03-23023 March 1988 Safety Evaluation Supporting Amend 11 to License R-83 ML20148M5691987-12-31031 December 1987 Twenty-Fourth Progress Rept of Texas A&M Univ Nuclear Science Ctr,1987 ML20205Q8241986-12-31031 December 1986 Twenty-Third Progress Rept of Texas A&M Univ,Nuclear Science Ctr for 1986 ML20203B0091986-07-10010 July 1986 Ro:On 860708,no Rod Down Indication Received for Transient Rod Until Carriage Driven In,During Performance of Manual Scram for Reactor Shutdown.Caused by Malfunction of Reactor Safety Sys Component.Repairs Underway ML20199B1171986-06-0404 June 1986 Ro:On 860501,improper Handling of Experiment Discovered Which Could Have Resulted in Serious Operational Event. Caused by Insertion of $1.09 Reactivity.Postulated Accidents & Results & Related Info Encl ML20205Q2921986-05-16016 May 1986 Final Ro:On 860501,unanticipated or Uncontrolled Change in Reactivity Greater than One Dollar Occurred.Caused by Removal of Rotisserie from Face Water Notch.Proposed Changes to SOPs Developed as Listed ML20205J9311986-02-18018 February 1986 RO 86-01:on 860204,temp Recorder Providing LSSS Signal to Scram on High Fuel Temp Malfunctioned.Caused by Defective Motor Bearing.Bearing Replaced & Recorder Calibr ML20199G0441985-12-31031 December 1985 Twenty-Second Progress Rept of Texas A&M Univ Nuclear Science Ctr,1985 ML20137Y6291985-09-24024 September 1985 RO-85-04:on 850912,transient Rod Followed Cylinder Out During Positioning of Transient Rod Cylinder.Air Solenoid for Transient Rod Sys Not Functioning as Designed.Air Solenoid Disassembled,Cleaned & Reassembled ML20127M4151985-05-0909 May 1985 Ro:On 850508,during Restart Following Power Failure,Facility Air Monitoring (Fam) Sys Inoperable for 15 Minutes.Caused by Turning Off High Voltage to Detectors.Procedures Revised to Verify Fam Sys After Power Failure ML20113D5681985-01-21021 January 1985 RO 85-2;on 850111,safety Channel 1 Detector Failed During Reactor Operation.Caused by Loose Connector Pin Making Intermittent Contact.New Connector Installed & Detector Verified Operable Prior to Reinstallation ML20134Q1961985-01-11011 January 1985 Ro:On 850111,reactor Shut Down When Safety Channel 1 Did Not Respond Following Annual Reactor Maint.Cause Undetermined. Detector & Cabling Replaced ML20134P7391985-01-10010 January 1985 RO 85-1:on 850108,fuel Temp Recorder Indicated 600 F Instead of 720 F.Caused by Failure of Reactor Safety Sys Channel. Faulty Slide Wire & Contact Arm Replaced ML20134Q2081985-01-0808 January 1985 Ro:On 850108,fuel Temp Recorder Indicated 600 F Instead of 720 F After Reactor Power Returned to 1 MW Following Sample Positioning.Reactor Shut Down & Faulty Slide Wire & Contact Arm Replaced ML20100C9651984-12-31031 December 1984 Twenty-First Progress Rept of Texas A&M Univ Nuclear Science Ctr,1984 ML20090E1251984-07-0202 July 1984 RO-84-4:on 840626,reactor Operator Noted That Fuel Element Temp Recorder Did Not Correspond to Digital Indication as Shown on Doric Temp Readout.Cause Not Stated.Failure Spurious & Could Not Be Reproduced ML20090D7841984-06-26026 June 1984 Telecopy Ro:On 840626,fuel Elements Temp Recorder Failed to Respond Following Temporary Reduction in Reactor Power.Cause Not Stated ML20090E1241984-06-15015 June 1984 RO 84-3:on 840604,reactor Operator Observed That Safety Power Measuring Channel 2 Not Responding as Reactor Power Level Increased Beyond 30 Kw.Caused by Loose Safety Channel 2 Signal Cable.Connector Replaced ML20090E5141984-06-11011 June 1984 RO 84-2:on 840528,erratic Performance of Reactor Servo Control Not Noted in Log.Caused by Personnel Error.Operator Cautioned to Be More Observant While Taking Log Readings ML20134Q2511984-06-0505 June 1984 Ro:On 840604,during Startup,Reactor Shut Down When Channel 2 Not Indicating in Expected Power Range.Caused by Faulty Connector.Faulty Signal Cable Connector Replaced & Normal Operations Resumed ML20092N9211984-05-29029 May 1984 Ro:On 840528,operator Received Servo Fault Alarm & Linear Power Channel Indication Failed Low.Caused by High Voltage Supply for Linear Defector de-energized ML20084H6171984-04-0202 April 1984 Ro:On 840319,discovered That Performance of Weekly Electronic Maint Checks Not Performed During Previous Wk of Operation.Caused by Inadequate Procedural Controls ML20087N3381983-12-31031 December 1983 Twentieth Progress Rept of Texas A&M Univ,Nuclear Science Ctr,1983 ML20078P0111983-10-28028 October 1983 Ro:On 831004,high Power Scram Received During Initial Reactor Startup While Banking Shim Safety Control Rods After Reaching 1 MW Power.Caused by Operator Manipulation of Control Rods.Procedures & Proper Documentation Emphasized ML20076F0281983-04-30030 April 1983 Nineteenth Progress Rept of Texas A&M Univ Nuclear Ctr, 1982 ML20071H9171983-04-30030 April 1983 Nineteenth Progress Rept of Tx A&M Univ Nuclear Science Ctr 1982 ML20024E1251983-04-30030 April 1983 Nineteenth Progress Rept of Texas A&M Univ Nuclear Science Ctr for 1982 ML20070N6471983-01-11011 January 1983 Ro:On 830110,fuel Temp Indication Failed to Respond During Reactor Startup.Caused by Shorted Thermocouple Wires in Terminal Box.Reactor Shut Down & Fuel Temp Instrument Connected to More Conservative Indication 1998-09-08
[Table view] |
Text
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TEXAS ENGINEERING EXPERIMENT STATION TEXAS A&M UNIVERSITY
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'f COLLEGE STATION TEXAS 77843-3575 M
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NUCLEAR SCIENCE CENTER 409/845-7551 September 8,1998 98-0249 U.S. Nuclear Regulatory Commission ATTN: Document Control Washington, D.C. 20555-0001
Subject:
Reportable Occurrence at Texas A&M University Nuclear Science Center on August 26,1998
Reference:
Facility Operating License R-83, Docket 50-128
Dear Sirs:
The following is a description of the events leading to a Reportable Occurrence at the Texas A&M University Nuclear Science Center Reactor (NSCR) and the corrective i
actions. This event was reported to the NRC on August 27,1998.
Description of Reportable Occurrence On August 26,1998, the Facility Building Air Monitor (FAM Channel 4) failed the daily
]
FAM alarm checks prior to reactor operation. This system is required to be in operation i
as a Limiting Condition of Operation (NSCR Technical Specification 3.5.1). The system was removed from service for troubleshooting and a failed alarm relay was discovered in the NIM module. Spare parts were no longer available from the manufacturer and an i
equivalent relay was ordered from another source. NSC Management considered FAM
\\p Channel 4 to be inoperable and the Reactor Manager was directed to monitor the building using an equivalent but not required channel (FAM Channel 2). The NSC Air Monitor sample transport piping is configured to allow individual detectors to sample from alternate points (Figure 1).
The Duty Health Physicist (DHP) intended to line up the system such that FAM Channel 2 would monitor the reactor building particulates. Although the DHP had performed several Argon-41 calibrations involving the FAM piping, the valve lineup was positioned incon ectly (Figure 2). A cap for a quick connection was missing and the DHP moved a cap from Detector 6 to that location. The combination ofincorrect valve arrangement and the missing cap caused a leakage path that bypassed or significantly reduced flow through all particulate detectors. The air leakage flowed through the building and r?i8 RESEARCH AND DEVELOPMENT FOR MANKIND F
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98-0249 Page 3 L
effluent gas detectors and out through the flow meters. The indications to the DHP appeared normal because the air flow meters (rotometers) indicated normal 350 cfh flow.
l The reactor was operated in this condition for another eight hours. The next day, the L
DHP questioned the abnormally low readings on all FAM meters (<5 cps). The Senior l
Reactor Operator investigated with the DHP and found the incorrect valve line-up. The
[
~ NSC Director, Reactor Safety Board Chairman and the NRC (Marvin Mendonca) were all informed of the Reportable Occurrence.
j l
t Root Cause Analysis J
l Several weaknesses were found during a root cause meeting of the NSCR staff on August
{
l' 27,1998*
- 1. There was no written valve lineup procedure for abnormal conditions of the Facility j
Air Monitoring System.
i 1
- 2. - A certified Duty Health Physicist (DHP) performed valve manipulations without a
-l L
system check by the on-duty Senior Reactor Operator or Reactor Operator. Although j
not formally required, usually the SRO confirms valve alignments.
l
- 3. Readings were logged in the contral room during the eight hour occurrence. These readings clearly indicated a decrease in radioactive counts. The evening shift operators, unfortunately, did not recognize the trend to be a system failure.
l Corrective Actions I
- 1. The Reactor Operations and Health Physics Staff are preparing formal written l
procedures for normal, abnormal and testing configurations of the FAM system.
l-These procedures should be reviewed and approved by the Reactor Safety Board.
l-
- 2. The NSCR Tag-out and Lock-out procedure is being rewritten to require a second check of any tag by a licensed Reactor Operator.
o i
' 3. The NSCR staff will be trained on the new procedures, the necessity for system tag-outs for facility and personnel protection and normal expected indications on all i
facility equipment.
l
. This Reportable Occurrence and the conective actions will be rcviewed at the next p
meeting of the Reactor Safety Board. The Board may make additional requirements l
. necessary.
i
1 98-0249 Page 4 Conclusion This Reportable Occurrence will be documented in the Reactor Safety Board meeting minutes and the facility Annual Report. Please contact Dr. Dan Reece or Mr. Sean O' Kelly at 409-845-7551 if more information is required.
Respectfully, bs LA.
W. D. Reece Director WDR/tll xc:
12110/ Central File 17124/NRC Reportable Occurrence Dr. Ted Michaels, USNRC Mr. Marvin Mendonca, USNRC Dr. Don B. Russell, Reactor Safety Board Chairman