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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO LER)
MONTHYEARML20151W2321998-09-0808 September 1998 Ro:On 980826,facility Bldg Air Monitor (Fam Channel 4) Failed Daily Fam Alarm Checks Prior to Reactor Operation. Caused by Failed Alarm Relay.Staff Is Preparing Formal Written Procedures for Testing Configurations for Fam Sys ML20217A0891998-03-18018 March 1998 Ro:On 980218,potential Reactor Safety Failure Discovered W/ Reactor Shutdown.Caused by Manual Scram Function Bypassed by Sticking Reset Contact in Console Power key-switch. Protective Action Reset Switches Wired ML20199C5371997-11-11011 November 1997 Ro:On 971030,shim Safety Number 2 Was Found to Be Binding & Became Stuck in Withdrawn Position & Control Rod Failed to Scram.Caused by Incorrect Spacing Between Hold Down Foot & Bundle top-handle.Procedure SOP-II-I Modified ML20129H5191996-10-30030 October 1996 Ro:On 961015,loss of Facility Power Occurred Causing Reactor Scram Due to Lack of Attention to Detail & Excessive Distractions to Operations.Startup Checklist Had Several Individual Instrument Checks Combined Into Single Items ML20079C2481991-06-10010 June 1991 Ro:On 910607,reactor Operated for 30 Minutes at 1 MW W/O Facility Air Monitors in Operation.Operator Removed from Watch Standing Duties.Final Rept Will Be Forwarded Upon Completion ML20066H1401991-02-0808 February 1991 Special Rept 90-01:on 910125,during Annual Fuel Insp of Operational Core VIII-A,fuel Elements 6502 & 8468 Failed to Pass go-no-go Gauge Test for Excessive Transverse Bend. Elements Replaced W/Spare & Fuel Bundles Relocated ML20203B0091986-07-10010 July 1986 Ro:On 860708,no Rod Down Indication Received for Transient Rod Until Carriage Driven In,During Performance of Manual Scram for Reactor Shutdown.Caused by Malfunction of Reactor Safety Sys Component.Repairs Underway ML20199B1171986-06-0404 June 1986 Ro:On 860501,improper Handling of Experiment Discovered Which Could Have Resulted in Serious Operational Event. Caused by Insertion of $1.09 Reactivity.Postulated Accidents & Results & Related Info Encl ML20205Q2921986-05-16016 May 1986 Final Ro:On 860501,unanticipated or Uncontrolled Change in Reactivity Greater than One Dollar Occurred.Caused by Removal of Rotisserie from Face Water Notch.Proposed Changes to SOPs Developed as Listed ML20205J9311986-02-18018 February 1986 RO 86-01:on 860204,temp Recorder Providing LSSS Signal to Scram on High Fuel Temp Malfunctioned.Caused by Defective Motor Bearing.Bearing Replaced & Recorder Calibr ML20137Y6291985-09-24024 September 1985 RO-85-04:on 850912,transient Rod Followed Cylinder Out During Positioning of Transient Rod Cylinder.Air Solenoid for Transient Rod Sys Not Functioning as Designed.Air Solenoid Disassembled,Cleaned & Reassembled ML20127M4151985-05-0909 May 1985 Ro:On 850508,during Restart Following Power Failure,Facility Air Monitoring (Fam) Sys Inoperable for 15 Minutes.Caused by Turning Off High Voltage to Detectors.Procedures Revised to Verify Fam Sys After Power Failure ML20113D5681985-01-21021 January 1985 RO 85-2;on 850111,safety Channel 1 Detector Failed During Reactor Operation.Caused by Loose Connector Pin Making Intermittent Contact.New Connector Installed & Detector Verified Operable Prior to Reinstallation ML20134Q1961985-01-11011 January 1985 Ro:On 850111,reactor Shut Down When Safety Channel 1 Did Not Respond Following Annual Reactor Maint.Cause Undetermined. Detector & Cabling Replaced ML20134P7391985-01-10010 January 1985 RO 85-1:on 850108,fuel Temp Recorder Indicated 600 F Instead of 720 F.Caused by Failure of Reactor Safety Sys Channel. Faulty Slide Wire & Contact Arm Replaced ML20134Q2081985-01-0808 January 1985 Ro:On 850108,fuel Temp Recorder Indicated 600 F Instead of 720 F After Reactor Power Returned to 1 MW Following Sample Positioning.Reactor Shut Down & Faulty Slide Wire & Contact Arm Replaced ML20090E1251984-07-0202 July 1984 RO-84-4:on 840626,reactor Operator Noted That Fuel Element Temp Recorder Did Not Correspond to Digital Indication as Shown on Doric Temp Readout.Cause Not Stated.Failure Spurious & Could Not Be Reproduced ML20090D7841984-06-26026 June 1984 Telecopy Ro:On 840626,fuel Elements Temp Recorder Failed to Respond Following Temporary Reduction in Reactor Power.Cause Not Stated ML20090E1241984-06-15015 June 1984 RO 84-3:on 840604,reactor Operator Observed That Safety Power Measuring Channel 2 Not Responding as Reactor Power Level Increased Beyond 30 Kw.Caused by Loose Safety Channel 2 Signal Cable.Connector Replaced ML20090E5141984-06-11011 June 1984 RO 84-2:on 840528,erratic Performance of Reactor Servo Control Not Noted in Log.Caused by Personnel Error.Operator Cautioned to Be More Observant While Taking Log Readings ML20134Q2511984-06-0505 June 1984 Ro:On 840604,during Startup,Reactor Shut Down When Channel 2 Not Indicating in Expected Power Range.Caused by Faulty Connector.Faulty Signal Cable Connector Replaced & Normal Operations Resumed ML20092N9211984-05-29029 May 1984 Ro:On 840528,operator Received Servo Fault Alarm & Linear Power Channel Indication Failed Low.Caused by High Voltage Supply for Linear Defector de-energized ML20084H6171984-04-0202 April 1984 Ro:On 840319,discovered That Performance of Weekly Electronic Maint Checks Not Performed During Previous Wk of Operation.Caused by Inadequate Procedural Controls ML20078P0111983-10-28028 October 1983 Ro:On 831004,high Power Scram Received During Initial Reactor Startup While Banking Shim Safety Control Rods After Reaching 1 MW Power.Caused by Operator Manipulation of Control Rods.Procedures & Proper Documentation Emphasized ML20070M8101983-01-11011 January 1983 Ro:On 830105,during Fuel Element Insp,Elements 7463 & 7486 Failed Go/No Go Test.Both Elements Had Been in Core Since 1973 & Not Inspected Since That Time.Both Elements Removed from Core ML20070N6471983-01-11011 January 1983 Ro:On 830110,fuel Temp Indication Failed to Respond During Reactor Startup.Caused by Shorted Thermocouple Wires in Terminal Box.Reactor Shut Down & Fuel Temp Instrument Connected to More Conservative Indication ML20072A8231982-12-22022 December 1982 Ro:On 821204,power Calorimetric Performed to Determine Agreement Between Indicated Power & Calculated Actual Power Based on Pool Heatup Rate.Results Showed Minus 30.7% Error. on 821206,calorimetric Showed Plus 56.6% Error ML20067C9721982-10-29029 October 1982 Ro:On 821019,power Level Indication Dropped Approx 15% on Both Safety Channels.On 821027,electromagnet Current for Shim Safety 2 Went to Zero.Causes Not Stated.Electromagnet Coil Replaced ML20066A5731982-10-0505 October 1982 Ro:On 820928,during Operation,Fuel Temp Thermocouple Failed. New Instrumented Fuel Element Installed.Thermocouple Readings Normal ML20066A2491982-09-29029 September 1982 Telecopy Ro:On 820928,erratic Readings Noted on Fuel Temp Indicator.Reactor Shut Down Immediately.On 820929,different If Connected to Fuel Temp Channel & Thermocouple Readings Recorded at 300 Watts & 1 MW ML20063H0731982-07-22022 July 1982 Ro:On 820722,during Initial Startup,Log Power Channel Rate Meter Failed to Respond.Cause Not Stated.Switch Contacts & Amplifier Boards Cleaned.Close Visual Insps Implemented ML20063H0301982-07-22022 July 1982 Telecopy Message of Ro:On 820722,during Initial & Secondary Reactor Startup,Log Power Channel Rate Meter Failed to Respond.Cleaning of Switch Contacts Returned Instrument to Normal Operation ML20126L4481981-04-15015 April 1981 Ro:On 810409 & 0414,during Prestartup Check of Facility, Interlock to Prevent Withdrawal of Shim Safety Control Rods for Low Source Levels Was Not Functioning.Caused by Defective Relay.Relay Replaced Prior to Reactor Operations 1998-09-08
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20205Q3481998-12-31031 December 1998 Tx A&M Univ Sys Tx Engineering Experiment Station Nuclear Science Ctr 1998 Annual Rept. with ML20151W2321998-09-0808 September 1998 Ro:On 980826,facility Bldg Air Monitor (Fam Channel 4) Failed Daily Fam Alarm Checks Prior to Reactor Operation. Caused by Failed Alarm Relay.Staff Is Preparing Formal Written Procedures for Testing Configurations for Fam Sys ML20217A0891998-03-18018 March 1998 Ro:On 980218,potential Reactor Safety Failure Discovered W/ Reactor Shutdown.Caused by Manual Scram Function Bypassed by Sticking Reset Contact in Console Power key-switch. Protective Action Reset Switches Wired ML20217K1401997-12-31031 December 1997 Tx A&M Univ Sys Tx Engineering Experiment Station Nuclear Science Ctr 1997 Annual Rept ML20199C5371997-11-11011 November 1997 Ro:On 971030,shim Safety Number 2 Was Found to Be Binding & Became Stuck in Withdrawn Position & Control Rod Failed to Scram.Caused by Incorrect Spacing Between Hold Down Foot & Bundle top-handle.Procedure SOP-II-I Modified ML20149F3901997-07-15015 July 1997 Safety Evaluation Supporting Amend 14 to License R-83 ML20137Y0351997-04-16016 April 1997 Rev 4 to Nuclear Science Center Senior Reactor Operator & Reactor Operator Requalification Program ML20137H0541996-12-31031 December 1996 Tx A&M Univ Sys Tx Engineering Experiment Station Nuclear Science Center 1996 Annual Rept ML20129H5191996-10-30030 October 1996 Ro:On 961015,loss of Facility Power Occurred Causing Reactor Scram Due to Lack of Attention to Detail & Excessive Distractions to Operations.Startup Checklist Had Several Individual Instrument Checks Combined Into Single Items ML20115G5511995-08-31031 August 1995 Engineering Analysis of a Power Upgrade for Tx A&M Nuclear Science Ctr Reactor ML20082D5521994-12-31031 December 1994 Thirty-First Annual Progress Rept of Tx A&M Univ Nuclear Science Ctr, for Period of 940101-1231 ML20069H4271993-12-31031 December 1993 Thirtieth Annual Progress Rept of Nuclear Science Ctr Tx Engineering Experiment Station Tx A&M Univ Sys College Station,Tx ML20059G0301993-10-26026 October 1993 Safety Evaluation Supporting Amend 13 to License R-83 ML20094N5431991-12-31031 December 1991 Nuclear Science Center 28th Annual Rept,CY91 ML20079C2481991-06-10010 June 1991 Ro:On 910607,reactor Operated for 30 Minutes at 1 MW W/O Facility Air Monitors in Operation.Operator Removed from Watch Standing Duties.Final Rept Will Be Forwarded Upon Completion ML20066H1401991-02-0808 February 1991 Special Rept 90-01:on 910125,during Annual Fuel Insp of Operational Core VIII-A,fuel Elements 6502 & 8468 Failed to Pass go-no-go Gauge Test for Excessive Transverse Bend. Elements Replaced W/Spare & Fuel Bundles Relocated ML20070R9351990-12-31031 December 1990 Twenty-Seventh Progress Rept of Texas A&M Univ Nuclear Science Ctr Jan-Dec 1990 ML20070U0201990-12-31031 December 1990 Twenty-Sixth Progress Rept of Texas A&M Univ Nuclear Science Ctr,1990 ML20043F4391990-06-0404 June 1990 Revised Page 1 to Reactor Operator & Senior Reactor Operator Requalification Program,Rev Iii.Item 2.1.6 Changed to Include Physical Security Plan ML20012E0661990-03-0909 March 1990 RO 90-01:on 900228,reactor Operator Received Servo Fault Alarm.After Directed Shutdown,Complete Loss of Linear Power Channel Noted.Caused by Corroded Connector at Detector Leads.Connector Replaced.Part 21 Related ML20248J1691988-12-31031 December 1988 Twenty-Fifth Progress Rept of Texas A&M Univ Nuclear Science Ctr,Jan-Dec 1988 ML20151Y9031988-07-15015 July 1988 Review of Texas A&M Univ Nuclear Science Ctr - Beam Port Experiment ML20151L6591988-03-23023 March 1988 Safety Evaluation Supporting Amend 11 to License R-83 ML20148M5691987-12-31031 December 1987 Twenty-Fourth Progress Rept of Texas A&M Univ Nuclear Science Ctr,1987 ML20205Q8241986-12-31031 December 1986 Twenty-Third Progress Rept of Texas A&M Univ,Nuclear Science Ctr for 1986 ML20203B0091986-07-10010 July 1986 Ro:On 860708,no Rod Down Indication Received for Transient Rod Until Carriage Driven In,During Performance of Manual Scram for Reactor Shutdown.Caused by Malfunction of Reactor Safety Sys Component.Repairs Underway ML20199B1171986-06-0404 June 1986 Ro:On 860501,improper Handling of Experiment Discovered Which Could Have Resulted in Serious Operational Event. Caused by Insertion of $1.09 Reactivity.Postulated Accidents & Results & Related Info Encl ML20205Q2921986-05-16016 May 1986 Final Ro:On 860501,unanticipated or Uncontrolled Change in Reactivity Greater than One Dollar Occurred.Caused by Removal of Rotisserie from Face Water Notch.Proposed Changes to SOPs Developed as Listed ML20205J9311986-02-18018 February 1986 RO 86-01:on 860204,temp Recorder Providing LSSS Signal to Scram on High Fuel Temp Malfunctioned.Caused by Defective Motor Bearing.Bearing Replaced & Recorder Calibr ML20199G0441985-12-31031 December 1985 Twenty-Second Progress Rept of Texas A&M Univ Nuclear Science Ctr,1985 ML20137Y6291985-09-24024 September 1985 RO-85-04:on 850912,transient Rod Followed Cylinder Out During Positioning of Transient Rod Cylinder.Air Solenoid for Transient Rod Sys Not Functioning as Designed.Air Solenoid Disassembled,Cleaned & Reassembled ML20127M4151985-05-0909 May 1985 Ro:On 850508,during Restart Following Power Failure,Facility Air Monitoring (Fam) Sys Inoperable for 15 Minutes.Caused by Turning Off High Voltage to Detectors.Procedures Revised to Verify Fam Sys After Power Failure ML20113D5681985-01-21021 January 1985 RO 85-2;on 850111,safety Channel 1 Detector Failed During Reactor Operation.Caused by Loose Connector Pin Making Intermittent Contact.New Connector Installed & Detector Verified Operable Prior to Reinstallation ML20134Q1961985-01-11011 January 1985 Ro:On 850111,reactor Shut Down When Safety Channel 1 Did Not Respond Following Annual Reactor Maint.Cause Undetermined. Detector & Cabling Replaced ML20134P7391985-01-10010 January 1985 RO 85-1:on 850108,fuel Temp Recorder Indicated 600 F Instead of 720 F.Caused by Failure of Reactor Safety Sys Channel. Faulty Slide Wire & Contact Arm Replaced ML20134Q2081985-01-0808 January 1985 Ro:On 850108,fuel Temp Recorder Indicated 600 F Instead of 720 F After Reactor Power Returned to 1 MW Following Sample Positioning.Reactor Shut Down & Faulty Slide Wire & Contact Arm Replaced ML20100C9651984-12-31031 December 1984 Twenty-First Progress Rept of Texas A&M Univ Nuclear Science Ctr,1984 ML20090E1251984-07-0202 July 1984 RO-84-4:on 840626,reactor Operator Noted That Fuel Element Temp Recorder Did Not Correspond to Digital Indication as Shown on Doric Temp Readout.Cause Not Stated.Failure Spurious & Could Not Be Reproduced ML20090D7841984-06-26026 June 1984 Telecopy Ro:On 840626,fuel Elements Temp Recorder Failed to Respond Following Temporary Reduction in Reactor Power.Cause Not Stated ML20090E1241984-06-15015 June 1984 RO 84-3:on 840604,reactor Operator Observed That Safety Power Measuring Channel 2 Not Responding as Reactor Power Level Increased Beyond 30 Kw.Caused by Loose Safety Channel 2 Signal Cable.Connector Replaced ML20090E5141984-06-11011 June 1984 RO 84-2:on 840528,erratic Performance of Reactor Servo Control Not Noted in Log.Caused by Personnel Error.Operator Cautioned to Be More Observant While Taking Log Readings ML20134Q2511984-06-0505 June 1984 Ro:On 840604,during Startup,Reactor Shut Down When Channel 2 Not Indicating in Expected Power Range.Caused by Faulty Connector.Faulty Signal Cable Connector Replaced & Normal Operations Resumed ML20092N9211984-05-29029 May 1984 Ro:On 840528,operator Received Servo Fault Alarm & Linear Power Channel Indication Failed Low.Caused by High Voltage Supply for Linear Defector de-energized ML20084H6171984-04-0202 April 1984 Ro:On 840319,discovered That Performance of Weekly Electronic Maint Checks Not Performed During Previous Wk of Operation.Caused by Inadequate Procedural Controls ML20087N3381983-12-31031 December 1983 Twentieth Progress Rept of Texas A&M Univ,Nuclear Science Ctr,1983 ML20078P0111983-10-28028 October 1983 Ro:On 831004,high Power Scram Received During Initial Reactor Startup While Banking Shim Safety Control Rods After Reaching 1 MW Power.Caused by Operator Manipulation of Control Rods.Procedures & Proper Documentation Emphasized ML20024E1251983-04-30030 April 1983 Nineteenth Progress Rept of Texas A&M Univ Nuclear Science Ctr for 1982. W/830516 Ltr ML20071H9171983-04-30030 April 1983 Nineteenth Progress Rept of Tx A&M Univ Nuclear Science Ctr 1982 ML20076F0281983-04-30030 April 1983 Nineteenth Progress Rept of Texas A&M Univ Nuclear Ctr, 1982 ML20028E6911983-01-11011 January 1983 Telecopy Ro:On 830110,during Reactor Startup,Fuel Temp Not Tracking Although Normal Temp Indication Displayed.Reactor Shut Down.Caused by Failed Fuel Thermocouple.Reactor Switched to Second Thermocouple 1998-09-08
[Table view] |
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A l TEX AS EN GIN EEltlN G EX PERI.t \ ENT STATION TEXAS A&M UNIVERSITY
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_L NUCLEAR SCIENCE CENTER 409'845 7551 November 11,1997 97-0284 Document Control Desk Nuclear Regulatory Commission Washington, DC 20555 SUlUECT: Final Repert of the RepNtable Occurrence of October 30,1997 REF: Texas A&hi University Nuclear Science Center (NSC), Facility License R 83, Docket 50-128
Dear Sirs:
On Thursday, October 30, during an evening Nuclear Engineering Lab (Reactor Calorimetric), Shim Safety No. 2 was found to be binding and became stuck in the withdrawn position The control rod failed to scram; therefore this was considered a reportable occurrence in accordance with the R 83 Technicel Speci0 cations. NSC hianagement informed hir. h1arvin hiendonca (NRIUDRPhi/PDND) of the NRC on October 31. The reactor was inspected and returned to normal operations.
The following is a description of the events and the conclusions.
SecuenccSUhents The reactor was being taken to a power of 500kW for a Nuclear Engineering 405 calorimetric experiment. The SRO instructed the RO to start up the reactor to 500kW.
Upon movement of the shim safeties in " gang," the HO noticed that the Rod Down light never cleared, This meant that the control rod was not coupled to the rod drive and was not withdrawing with the other three shim safeties. On Tuesday, October 28,1997, the control rod drive for shim safety No.2 had been replaced for scheduled annual maintenance. Knowing this, the SRO and RO decided to swap the control rod drives back because the old contial rod drive was known to have worked before the initial swap. ,
Aner the rod drive assembly replacement, startup continued and all indications were normal,
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- Pag'e 2 The reactor was at 500kW and the control rods were in the process of being banked. The control rod positions were at approximately 50.5% and were going to be banked at 60.0%. When shim safety No.2 wa: being moved to 60.0%, the " engaged" light went out and the" rod down" light did not actuate. The RO thought that the wiring behind the light (LED) mi ght be at fault. The shim safety No.2 was driven down and the " engaged" light re energired at approximately 59.8%. A second attempt was made to raise shim safety No.2 to 6( .0%. Shim safety No.2 was raised to M.0% with normal indications. The
" engaged" light blinked ofTand then back on whi. . the RO was taking log readings following the reactor startup.
The SRO veriGed that shim safety No.2 was still in the raised position at the Reactor Bridge. An attempt was made to individually scram shirn safety No.2 to determine its location. The " engaged" light went out momentarily, but the " rod down" light never actuated. The SRO directed to shutdown the reactor and abort the experiment. During the shutdown, shim safety No.2 was found to scram with the " rod down" light actuating between 20.0% and 30.0%. Shim safeiy No.2 was tested with the reactor shutdown. It was determined that the control rod scrammed at a maximum height of approximately 40.5%.
Aner these events, the Director and Assistant Director were notined and the appropriate comments were made in the shin change and RO logs.
SubcauenLEXtats On Friday, October 31,19')7, it was decided that the reactor would be partially unloaded to examine shim safety No.2 and the respective bundle for damage. The Health Physicist obtained a reactor pool sample to determine if there had been any damage to the bundle, fiieled follower or poison section. The results were negative and no fission products detected. The core was examined prior to unloading. It was discovered that the hold down foot, attached to the bottom of the control rod barrel (see attached Ogures), was not positioned properly on the bundle top handle. There was indication that the hold down foot was rotated approximately 45" It was also determined that the top of the control rod drive assembly at the bridge level was higher than the other control rod drives. The control rod was repositioned until the drive motor housing heights matched. The core was re-examined and it was found that the control rod hold down foot was still not properly positioned even though the height was correct. The hold down foot was found positioned on the side of the bundle tor handle and not directly over the handle. The core was then partially unloaid to the point where shim safeties No.2 and No 3 could be removed and inspected. Shim safety No.2 and the respective bundle were inspected and no abnormalities were found. The core was reassembled and the control rods returned to the same locations. The core and control rods were veri 0ed as being properly assembled by the Director and Assistant Director. Scram times were measured on both control rods that were removed. The times were 0.69 and 0.65 seconds for shim safetics ho.2 and
97.Q284 Page 3 No.3 respectively. The Director then gave written permission in accordance with the facility Technical Specifications for a retura to regular reactor operations.
Ro0LCause of thdcPm1Ahic_Qcnincace A root cause analysis meeting was held on November 4 with a representative of the NRC (Mr. Stephen llolmes)in attendance. The cause was identined as incorrect spacing between the hold down foot and the bundle top handle. The fueled control rod followers and hold down feet were installed in the reactor in 1972. The desit ;n was for the hold down foot to be 0.125 inches above the top handle to accommodate possiHe thermal expansion of the fuel bundle. The NSC procedure (SOP 111) for the installation of the control rod calls for the rod to be raised a/ynor/mately 0.250 inches via the control rod barrel support adjusting nuts. This distance was chosen to prevent measurement errors in a limiting direction. A 0.250 inch clearance was intended to insure the 0.125 inch distance while not lifling the hold down foot over the top handle (0.5 inch diameter).
The Shim Safety No.2 rod had been removed during a partial core unload in early October. Scram time was measured as 0.67 seconds at that time. There was no prior indication of rod binding until the rod became stuck on October 30. It is believed that the spacing was incorrect at that time but the rod was correctly aligned. During the change of Shim Safety No.2 drive assemblics the technician (a qualified RO) may have slightly turned the lower rod drive assembly. This misalignment then caused the rod to bind when it was partially withdrawn.
Conchision!LaniIrconnendations The SRO and RO made the correct response to the indications of a stuck rod. The failure of the single control rod to scram did not violate reactor safety. The procedure for removal and insenion of rod drives will be modified to prevent a reoccurrence of the incorrect spacing . The following is the draQ changes to SOP-il 1 to be reviewed and approved at the next Reactor Safety lloard meeting (compare to attached procedure).
- a. Removal and Installation of the Shim Safety Rod (1) Disconnect the electrical connector . ) the rod drive unit.
(2) Using a ruler, determine and record the height, to the nearest 1/16 inch, of the rod drive unit top relative to the upper suppon plate.
(3) Attach the chain liQing device or a .
97-0284-
. Page 4 To install the rod, reverne the above applicable steps, raaking sure that the bottom of the hold down assembly is properly positioned and secured over the fuel
'oundle top handle.
- 1. Lower the assembly until the hold down foot of the hold down assembly rests on the fuel bundle top handle.-
2.. Adjust the barrel support rods for a clearance of between 0.125 to 0.250 inches between the hold down foot and the bundle top handle.-
- 3. Measure height of rod drive unit above upper support plate.
Height should be within 1/16 inch of previous measurement.
4, The control rod should be tes'.ed for operability as per SOP 11 1-6.d.
All Operators have been counseled on attention to procedures and maintaining a questioning attitude during normal and abnormal operations.
- Please contact Mr. Sean O' Kelly or Dr. Dan Reece if you require additional information.
' Thank you for your assistance in this matter. The NSC stafrand management appreciated the concern shown by the NRC in light of this reportable occurrence and the assistance that Mr. Ilolmes provided during his visit.
Respectfully,
/g O'y Dr. W.D. R(e Director Attachments xc: 12212/ Central File 17124/NRC Reportable Occurrence Dr, Ted Michaels, NRC.
Mr. Stephen liolmes, NRC Mr. Blaine Murray, NRC Region IV-Reactor Safety Board
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l NSC Section Page Fcrm 112A Nuclear Science Center II 9 STANDARD TERATING PROCEDURES l Prepared by Subject Procedure Rev,
{ . BFA' REACTOR CORE MANIPULATION I 1 Any11mg a control rod is to be removed, two other scrammable rods (if available in the core) will be cocked at 50%.
- a. Removal and Installation of a Shim Safety Rod During the performance of these procedures, the shim safety rod being removed will be in the scrammed condition.
(1) Disconnect the electrical connector to the rod drive unit.
(2) Attach the chain lifting device or a 1/4 inch nylon lifting rope, with approximately a 3 ft.
loop, to the upper end of the rod drive unit.
(3) Secare the rope to the overhead crano.
(4) Remove the bracket which secures the rod drive unit to the control rod mounting plate.
(5) Carefully raise the control rod assembly approximately one inch using the crane.
(6) Remove the nuts from the top of the control rod barrel support. Remove the barrel support and tie it off to the control rod drive.
-(7) Raise the rod assembly until the shim eniety rod clears the fuel bundle.
NOTP: DO NOT use the overhead crane to phycically extract the rod assembly from the core. Manually lift the assembly from the core and use the crane to support the weight of the assembly during pauses in the lifting process.
(8) Make all necessary entries in the Fuel Log and Reactor Operations Log.
To install the rod, reverse the c.bove steps, making sure that the bottom of the hold down assembly is properly positioned and secured over the fuel bundle top handle. This is done by first lowering the assembly until the crow's foot of the hold down assembly touches the fuel bundle top handle ind then adjusting the barrel support rods for a clearance of approximately 1/4 inch between the crow's foot and the bundle top handle. The control rod should then be tested for operability as per SOP II-I-6.d. i Approved:
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A top handle is represented in Figure 4. Figure 5.is a plan view of the position in the grid plate of a fueled follower element baae. Figuru 6 illustrates a similar plan view of the positioning of the top handle of a fueled follower element.
Figure 7 is an exploded view of a fueled follower-fuel element assembly, I
lloid Down Tube A standard TRIGA control rod operates within a guide tube that currounds the rod and has holes for proper cooling. A fueled-follower control rod can not operate in a guide tube becauce of restrictive cooling. It was necessary to design and fabricate new hold down tubes for the control elements with fueled followers. In the absence of a guide tube, a hold down foot was designed as shown at the top of Figure 7 The foot fits over the top handle cross bar and the blade of the foot extends high enough for clearance of the rod when it is in the full up position. The blade is t2ttached to the sido cf a tube that houses the control rod extension. When the rod drive unit is secured to the reactor support structure, a 1/8" clearance is provided notween the foot and the fuel element top handle cross bar. This clearance permits small thermal expan-sion of the iuel without vertical restriction.
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l l i i i i 7 l l FIGURE 4 FUEL ELEMENT TOP HANDLE i
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E FIGURE 6 FUELED FOLLOWER IN FUEL ELEMENT TOP HANDLE AND ITS RELATION TO ADJACENT ELEMENTS O
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