ML20151K541

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Insp Rept 50-344/88-24 on 880508-0618.Violations Noted. Major Areas Inspected:Operational Safety Verification,Maint, Surveillance,Event Follow Up & Open Item Follow Up
ML20151K541
Person / Time
Site: Trojan File:Portland General Electric icon.png
Issue date: 07/12/1988
From: Rebecca Barr, Mendonca M, Suh G
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML20151K510 List:
References
50-344-88-24, NUDOCS 8808030208
Download: ML20151K541 (12)


See also: IR 05000344/1988024

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U.S.-NUCLEAR REGULATORY COMMISSION

REGION V

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. Report No.

50-344/88-24

Docket No.

50-344

License No.

NPF-1

Licensee:

Portland General Electric Company

121 S.W. Salmon Street

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Portland, OR 97204

Facility Name: Trojan

Inspection at:

Rainier, Oregon

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Inspection condu ed:

8-J[ 18, 1988

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Inspectors:

M. C. Barr(/ "

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Approved By:

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Date Signed

Reactor Pr

ts Section 1

Summary:

Inspection on May 8 - June 18,-1988 (Report 50-344/88-24)

Areas Inspected:

Routine inspection of operational safety verification,

maintenance, surveillance (containment incal leak rate testing), event follow

up, and open item follow up.

Inspectic.1 procedures 30703, 41400, 61720,

62703, 71707, 71709, 71881, 92700, 92701 and 93702 were used as guidance

during the conduct of the inspection.

Results:

In the areas inspected, a violation was identified for an apparent failure to

follow procedural requirements for work hour limitations (paragraph 6).

No

general conclusions regarding the strengths or weaknesses of the program areas

inspected were identified during this inspection period.

8808030208 880713

PDR

ADOCK 05000344

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DETAILS

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1.

Persons Contacted

  • D.W. Cockfield, Vice President, Nuclear
  • C.A. Olmstead, Plant General Manager
  • 'R.P. Schmitt, Manager, Operations and Maintenance
  • D.W. Swan, Manager, Technical Services
  • J.K. Aldersebaes, Manager, Plant Modifications
  • J.D. Reid, Manger, Plant Services
  • J.W. Lentsch, Manger, Personnel Protection

R.L. Russell, Operations Supervisor

R.H. Budzeck, Assistant Operations Supervisor

D.L. Bennett, Maintenance Supervisor

R.A. Reinart, Instrument and Control Supervisor

T.O. Meek, Radiation Protection Supervisor

R.W. Ritschard, Security Supervisor

C.H. Brown, Operations Branch Manager, Quality Assurance

The inspectors also interviewed and talked with other licensee

employees during the course of the inspection.

These included shift

supervisors, reactor and auxiliary operators, maintenance personnel,

plant technicians and engineers, and quality assurance personnel.

  • Denotes those attending the exit interview.

2.

Plant Status

The plant was in Mode 6 with fuel assemblies being reloaded into the

reactor core at the beginning of the inspection period.

Near the end of

the previous inspection period on May 5, corporate engineering informed

the plant that the pressurizer surge line was found to be in contact with

one of its pipe whip restraints under cold conditions.

The licensee

initiated a detailed action plan to respond to pipe whip restraint and

pressurizer surge line operability concerns.

On May 13, core reload was

completed.

Following setting of the head on the reactor vessel, reactor

coolant system level was reduced to loop centerline on May 16 in

preparations for eddy current testing of the "A" and "D"

steam

generators.

Following opening of the steam generator primary manways and

installation of nozzle dams, the RCS level was increased to above the top

of the loops.

On May 23, the plant entered Mode 5 as the reactor vessel

head bolts wero tensioned.

On May 27, ultrasonic examination of

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pressurizer surge line welds resulted in relevant indications on the two

welds associated with the 90 degree elbow located below the pressurizer.

The licensee subsequently decided to replace the elbow and adjoining

pieces of piping.

On June 8, reduction of RCS level to slightly above

loop centerline was initiated to support the pressurizer surge line elbow

replacement work.

At the end of the inspection period, the plant was in

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Mode 5.

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3.

Operational Safety Verification (71707, 71709, 41400 and 71881)

During this inspection period, the inspectors observed and examined

activities to verify the operational safety of the licensee's facility.

The observations and examinations of those activities were conducted on a

daily, weekly or biweekly basis.

Daily the inspectors observed control room activities to verify the

licensee's adherence to limiting conditions for operation as prescribed

in the facility Technical Specifications.

Logs, instrumentation,

recorder traces, and other operational records were examined to obtain

information on plant conditions, trends, and compliance with regulations.

On occasions when a shift turnover was in progress, the turnover of

information on plant status was observed to determine that pertinent

information was relayed to the oncoming shift personnel.

Each week the inspectors toured the accessible areas of the facility to

observe the following items:

(a) General plant and equipment conditions.

(b) Maintenance requests and repairs.

(c) cire hazards and fire fighting equipment.

(d) Ignition sources and flammable material control.

(e) Conduct of activities in accordance with the licensee's

administrative controls and approved procedures.

(f)

Interiors of electrical end control panels.

(g)

Implementation of the licensee's physical security plan.

(h) Radiation protection controls.

(1) Plant housekeeping and cleanliness.

(j) Radioactive waste systems.

(k) Proper storage of compressed gas bottles.

Weekly, the inspectors examined the licensee's equipment clearance

control with respect to removal of equipment from service to determine

that the licensee complied with technical specification limiting

conditions for operation.

Active clearances were spot-checked to ensure

that their issuance was consistent with plant status and maintenance

evolutions.

Logs of jumpers, bypasses, caution and test tags were

examined by the inspectors.

Each week the inspectors conversed with operators in the control room,

and with other plant personnel.

The discussions centered on pertinent

topics relating to general plant conditions, procedures, security,

training and other topics related to in progress work activities.

The inspectors examined the licensee's nonconformance reports (NCRs) to

confirm that deficiencies were identified and tracked by the system.

Identified nonconformances were being tracked and followed to the

completion of corrective action.

Routine inspections of the licensee's physical security program were

performed in the areas of access control, organization and staffing, and

control measures used at the entrance to the protected area, verified the

integrity of portions of the protected area barrier and vital area

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barriers, and observed in several instances the implementation of

compensatory measures upon breach of vital area barriers.

Portions of

the isolation zone were verified to be free of obstructions.

Functioning

of central and secondary alarm stations (including the use of CCTV

monitors) was observed.

On a sampling basis, the inspectors verified

that the required minimum number of armed guards and individuals

authorized to direct security activities were on site.

The inspectors conducted routine inspections of selected activities of

the licensee's radiological protection program.

A sampling of radiation

work permits (RWP) was reviewed for completeness and adequacy of

information.

During the course of inspection activities and periodic

tours of plant areas, the inspectors verified proper use of personnel

monitoring equipment, observed individuals leaving the radiation

controlled area and signing out on appropriate RWP's, and observed the

posting of radiation areas and contaminated areas.

Posted radiation

levels at locations within the fuel and auxiliary buildings were verified

by the inspectors using both NRC and licensee portable survey meters,

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The involvement of health physics supervisors and engineers and their

awareness of significant plant activities was assessed through

conversations and review of RWP sign-in records.

The inspectors verified the operability of selected engineered safety

features.

This was done by direct visual verification of the correct

position of valves, availability of power, cooling water supply, system

integrity and general condition of equipment, as applicable.

No violations or deviations were identified.

4.

Maintenance (62703)

Cable Insulation Degradation Near Reactor Coolant Pumps

As a result of electrical preventive maintenance performed on various

valves associated with the reactor coolant pumps, the licensee identified

apparent degradation of their wiring insulation.

The most severe

degradation appeared to be localized to valve components where the wiring

was not protected by a cable outer jacket.

In these cases, portions of

some wiring showed insulation embrittlement.

A program to determine the

extent and cause of the apparent degradation was implemented.

This

program involved examination of cabling in open cable trays and of

cabling accessible upon removal of condulet covers, pull box covers,

terminal box covers, and in some instances disassembly of conduit

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fittings.

Much of the cable degradation wa; associated with non-safety

related cabling and involved various degrees of embrittlement of the

cable outer jacket.

With few exceptions, the enclosed conductors and

associated insulation showed no damage.

This program determined that the

problem was associated with high ambient temperatures caused by air flow

from reactor coolant pump motors.

The licensee developed an action plan

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which included repair and replacement of safety related wiring which

showed degradation, preparation of a safety evaluation which provided the

bases for continued operation with non-safety related cabling which

showed various degrees of degradation, and preparations for potential

replacement of degraded non-safety related cabling in the future.

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addition, the licensee contacted the NSS$ vendor and initiated efforts to

assess the generic implications of the observed conditions.

The inspectors observed portions of the maintenance work performed on

valve CV-8141A which isolated seal leakoff from the "A" reactor coolant

pump.

Some of the wiring which ran from a pull box to the solenoid valve

and to the limit switches of CV-8141A exhibited insulation damage

apparently from high temperature conditions.

The affected wiring was

replaced and necessary in-line splices completed.

Quality control

coverage was present to verify the acceptability of the splices and

completed heat shrink tubing.

The inspectors examined the damaged wiring

which showed brittle insulation.

The portions of the wiring which had

been located in the pull box, solenoid, and limit switches showed a

greater degree of insulation hardness than the portions which were

located in the connecting conduits.

The affected wiring did not have a

protective cable outer jacket.

The outer jacket from the associated

cable was removed at a pull box, and examination of the conductors in the

cable showed no insulation degradation.

The inspectors reviewed the work

instructions of maintenance request MR 88-4206, and the completed work

package which included an electrical termination record.

During a walkdown of cabling in areas around reactor coolant pumps "A"

and "D", the inspectors noted the identity of various cable trays and

conduits.

A review of the work package associated with MR 88-4106 and MR

88-4197 confirmed that licensee personnel had included these cable trays

and conduits in the inspection program to determine the extent and cause

of cable degradation.

Continued licensee actions to determine root cause of observed cable

degradation and implement response actions will be followed in routine

inspection activities.

No violations or deviations were identified.

5.

Containment Local Leak Rate Testing (61720)

Performence of Type B and Type C leak rate tests was controlled by

licensee periodic engineering test PET-5-2, Revision 16, titled

"Containment Local Leak Rate Testing." The inspectors reviewed PET-5-2

and verified that Data Sheet 3 included all containment isolation valves

subject to Type C testing listed in Technical Specification Table 3.6-1

and all electrical penetrations listed in FSAR Table 6.2-33.

Data Sheet

3 was used to calculate the combined leakage rate and compare the result

to the acceptance criteria of 0.6 La (maximum allowable leakage rate

specified for containment ir. the technical specifications).

At the time

of the inspection, local leak rate testing for all but a few penetrations

including the purge system exhaust and supply valves, equipment hatch,

and the 45-foot air lock had been performed.

The r.spectors verified

that the combined leakage rates including estimated (based on recent

results) leakage rates for the penetrations to be done were well below

0.6 La. Review of recent PET-5-2 data sheets showed that local leak rate

testing was performed on a yearly basis and thus met test frequency

requirements specified in the technical specifications and 10 CFR 50

Appendix J.

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The inspectors observed portions of local leak rate tests performed for

the 93-foot air lock and for the equipment hatch tool passageway.

The

tests were performed at 60 psig.

The flow and pressure instrumentation

in the LLRT test panels were verified to be within calibration.

The

inspector reviewed the applicable clearances for the tests.

The work was

performed under Radiation Work Permit RWP 88-131.

No violations or deviations were identified.

6.

Pressurizer Surge Line Elbow Replacement (62703, 93702)

In partial response to unexpected pressurizer surge line movement

discovered during the 1988 refueling outage, the licensee performed

ultrasonic examination of pipe welds on the surge line.

The results

showed relevant indications on the two welds associated with a 90-degree

elbow directly below the pressurizer.

The licensee made the decision to

remove the elbow and adjoining pieces of piping and to rework the surge

line with new components.

The process was controlled in part by Detailed

Construction Package DCP-15 Request for Design Change RDC 87-001.

The

removal of the old elbow and installation of new components was performed

with the assistance of a vendor site services crew.

The inspectors performed an inspection of the elbow replacement work

which included observations of cleanliness controls, weld rod control,

welding, plant operations interface with replacement work, review of weld

procedures, welder qualification records and material documentation.

Cleanliness controls were specified in both the licensee's maintenance

request work instructions and the vendor's procedure which was reviewed

by the Plant Review Board.

These instructions included the cleaning of

the replacement elbow and associated piping and inspection to cleanliness

criteria similar to ANSI N45.2.1 "Cleaning of Fluid System and Associated

Components for Nuclear Power Plants," Class B, conditions; an inspection

for and removal of cutting chips and other debris af ter removal of the

first section of original piping; and cleaning of the piping interior and

inspection after removal of all sections of original piping.

A pneumatic

plug was installed into the horizontal run of piping which connected to

the rest of the reactor coolant system to primarily serve as a barrier to

primary coolant.

A shielded steel plug was also inserted into the

horizontal piping and the end of the piping was covered with a plywood

disc.

On the vertical section of piping connected to the pressurizer, a

shielded steel plug was inserted and the end of the piping was covered

with a plywood disc.

The work instructions provided for tool control

during the period of time the system was open to the environment.

Upon

installation of new components, the pneumatic plug was removed prior to

fit-up of the final section of piping, and a final closeout cleanliness

inspection was performed by both licensee and vendor QC inspectors.

The inspectors reviewed material purchase orders and documentation for

weld rod, replacement elbow and piping used in the elbow replacement

work.

The suppliers were verified to be on the utility's Evaluated

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Contractors and Suppliers List.

Weld rod was stored in a locked metal

container in the vendor's trailer and in the licensee's warehouse on

shelving located off the floor in labeled boxes with controlled access

into the warehouse.

Weld rod was issued with the use of requisition

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slips and tracked on weld history records.

The inspectors observed

portions of the welding performed to install the new elbow and associated

piping and portions of the cutting to remove the original elbow and

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adjoining piping.

For welding, the vendor primarily used an automatic

pipe welding system.

The inspectors verified that a sample of the

operating parameters met the limits of the applicable weld procedure

specification.

Radiation protection and five watch coverage were

observed to be in place.

During the surge line elbow replacement, the reactor coolant system level

was maintained at slightly above the loop centerline.

A temporary

operating instruction, OIT-5-4, "Plant Operations During Surge Line

Repair," was written to control plant operation during the replacement

work and addressed establishment of a RCS overpressure path, level

control of the RCS, and decay heat removal.

The inspectors reviewed the

procedure and verified that the instructions were being followed.

Containment integrity restoration in the event of loss of decay heat

removal capability was addressed in Administrative Order A0-3-11

"Containment Access and Evacuation." The inspectors reviewed A0-3-11

worksheets which presented the restoration plans for applicable

containment penetrations and verified the completion of these plans prior

to RCS cooldown below the top of the loops.

A review was performed of a sample of the weld procedure specifications,

procedure qualification records, welder qualification instructions,

records of welder qualification tests, and specified nondestructive

examination requirements.

No substantive discrepancies were identified.

The inspectors verified that the licensee welding engineers had reviewed

the vendor procedures and had considered sensitization issues in the

review.

Four nonconformance reports had been written at the time of the

inspection.

The inspectors reviewed the reports to verify appropriate

resolutions of the nonconformances had been identified.

During the course of the inspection, it was observed that the vendor was

working seven day weeks.

The inspectors requested a sample of the time

sheets for the welding and machinist shift crews.

For the week of June

11 through June 17, 1988, members of the vendor site service crew

including welders and their immediate supervisors apparently worked in

excess of 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> in a seven day period, taking into account possible

shift turnover time.

No worker showed excessive work hours relative to

the rest of the crew. Work hour limitations were controlled by

Administrative Order A0-3-1, "Shif t Complement and Work Time," which

required the use of deviation sheets if work hours limitations were to be

exceeded.

The licensee project coordinator stated that deviation sheets

had not been completed for the vendor crew.

This is an apparent failure

to follow the procedural requirements of A0-3-1 and an apparent violation

of the workiag hour limits of Technical Specification 6.2.2.g.(50-344/88-24-02).

The inspectors noted that the vendor work

proposal exrlicitly stated that the work schedule would consist of 12

hour shif ts, two shif ts per day, seven days per week.

In discussions

with the inspectors, tne licensee project coordinator indicated that a

nonconforming activity report would be initiated and A0-3-1 deviation

sheets would be promptly processed, as appropriate.

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7.

Event Follow-Up (93702, 92701)

Pressurizer Surae Line Movement

With the plant in Mode _6 and RCS temperature at approximately 80 degrees

F, engineering walkdowns of pipe whip restraints identified that the

pressurizer surge.line was in contact with the upper shim. pack of pipe

whip restraint (WR) 1.2.-

The' inspection of WR's was a result of the

licensee long. term action plan in response to pipe support problems.

identified in the 1987 refueling outage.

No pipe contact was observed

for the seven other WR's on the surge line.

The licensee determined that

approximately 5000 pounds-force was required to push the pipe off the

contact point. After the removal of two shim plates from the WR 1.2

upper shim pack, the pipe moved 3/8 of an inch in the upward direction.

The design cold gap was 9/16 of an inch.

Inspection of the "B" RCS loop

hot leg WR and steam generator upper and lower support ring revealed no

anomalies.

In response, the licensee developed an action plan to assess the cause,

significance, and corrective actions for this event.

One potential cause

which was investigated was the potential for thermal stratification in

the surge line during heatup, particularly when a bubble was being formed

in the pressurizer. At that time, a temperature difference in excess of

300 degrees F could exist between the pressurizer and the RCS hot leg.

The possibility of thermal stratification was apparently not considered

in the NSSS piping analysis.

As part of its action plan, the licensee

planned to make a determination as to the continued operability of the

surge line, make changes to piping supports as appropriate, and planned

to implement a monitoring program for temperature and deflection data for

the surge line.

Problems with RCS thermal expansion at Trojan were

encountered in 1986.

Review of these problems concluded that the RCS had

been over-restrained.

Adjustments were made to the RCS restraints and an

ongoing monitoring program was implemented.

Region V follow-up inspection of licensee actions was documented in

Inspection Report 50-344/88-25, which also dealt ~with pipe whip restraint

design issues.

Pipe Whip Restraint Desian Gaps

Licensee nonconformance report NCR 88-190 dealt with the finding that for

various pipe whip restraints, inadequate gaps existed to accommodate

calculated thermal and seismic movements without contact of the pipe to

the restraint.

Some restraints were reported to be in contact in the

cold condition.

NCR 88-190 was a generic report in that as problems were

identified with additional restraints, they were added onto NCR 88-190.

As of May 12, 1988, the plant onsite quality assurance branch copy of the

NCR showed 22 pipe whip restraints to have inadequate gaps and, of these,

eight pipe whip restraints were observed to be in contact in the cold

condition.

The pressurizer surge line pipe whip restraint 1.2 was not

among the eight or 22 restraints above, but instead was addressed in a

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separate NCR (88-204).

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The inspectors performed an inspection of the eight pipe whip restraints

which were initially reported to be in contact in the cold condition per

NCR 88-190.

In all eight cases, no gross indications of damage to the

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piping or to the restraint'itself was observed.

The as found gap data

shown in NCR 88-190 appeared to be reasonable based on visual observation

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with the following exceptions:

(1) pipe restraint 49.5 - the inspectors

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did not observe contact at the "C" shim pack; instead a slight gap of

approximately 0.020 inches was observed; (2) pipe whip restraint 5.4 -

due to close tolerances the gaps could not be observed due to the

presence of piping insulation; (3) pipe whip restraint 48.3 - this

restraint was inaccessible for close examination; the "C" shim plate

appeared to be in contact as viewed from a distance of approximately 6

feet.

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Region V follow up inspection was documented in Inspection Report

50-344/88-25.

Toward the end of the inspection period, the resident

inspectors reviewed a sample of maintenance request work packages used to

reshim pipe whip restraints to preclude contact with associated piping

during thermal and seismic transients.

The work packages provided

adequate detail and work instructions to the workers and quality control

inspectors.

A production tolerance of one eighth of an inch was

specified for shim gaps, which was verified by QC inspectors and the

results subsequently reviewed by the action engineer. The inspectors

measured shim gaps for two reworked pipe whip restraints - WR 18.3 on the

alternate charging line and WR 48.4 on the letdown line.

The results

closely matched the measurement values reported by the QC inspectors and

were within one eighth of an inch of the specified design values.

No violations or deviations were identified.

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8.

Follow-Up of Open Items (92701, 92700)

Open Item 87-30-01 (Closed) Observed Offset in Piping Supports - In

walkdowns of main feedwater piping inside containment during 1987

refueling outage, the inspectors identified two spring can hangers which

showed large offsets between the pipe clamp stanchion and the load column

attached to the spring can.

The licensee made modifications to the

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hangers (H-3 and H-6 on the "C" and "D" main feedwater lines,

respectively) to reduce the loading to acceptable values.

During the

1988 refueling outage, the licensee staff found that the adjusting rod on

hanger H-3 had sheared off from its load plate.

Nonconformance Report

NCR 88-163 was written.

The cause of the failure was reported to be

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associated either with the pinning of the hanger in preparation for

piping replacement or with hanger offset.

The hanger apparently failed

after plant shutdown for the 1988 refueling outage.

The inspectors reviewed the disposition of NCR 88-163 and discussed

corrective actions with members of the licensee staff.

The load plate on

hanger H-3 was replaced.

To reduce loadings on spring can hanger

components, the baseplate was modified on H-6 to realign the hanger.

In

addition, a 4-inch long pipe was installed between the spring can housing

and the base plate to raise the spring can on H-6.

This allowed the

adjusting rod length to be decreased.

The inspectors performed a

walkdown of all four main feedwater lines, anu noted that the adjusting

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rod for spring can hangers which support the pipe ~from below had been

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reduced to less than one inch in length.

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The inspectors reviewed licensee procedures to verify that hanger offset

was addressed.

A review of the licensee's quality control procedures

(QCP) indicated that QCP-8, Revision 19, "Hanger and Structural Steel

Inspection," did not address hanger offset and the QCP-34, Revision 2,

"Visual Examination," included instructions which would lead to the

identification of excessive hanger offset.

QCP-34 was normally used only

for inservice inspection related activities.

Installation Standard M-6,

Revision 1, which dealt with the procurement, installation, and

adjustment of piping supports, generally addressed piping offset.

It

appeared that the responsible engineer would need to include specific

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instructions in the appropriate work package to provide for the

adjustment and inspection of hanger offset.

Based on the above inspection, this item is considered closed,

LER 88-11 (Closed) Movement of New Fuel Over the Spent Fuel Pool - In

refueling activities, seven new fuel assemblies were moved with the spent

fuel pool bridge crane in the fully raised position over the spent fuel

pool.

The licensee identified this as a violation of Technical Specification 3.9.7.

The inspectors reviewed corrective actions which

included additional training for members of the refueling services

vendor.

LER 88-11 stated procedural non-compliance as the cause of the

event.

The inspectors verified that adequacy of training was discussed

in the licensee's internal event report process.

In addition, review of

the licensee's documentation indicated that the event was within the

design bases of the plant for a postulated fuel handling accident.

This

item is considered closed.

9.

Refuelina Area Material Control (71707)

An inspection was performed of material control in the refueling area

inside containment.

The licensee has implemented a quality control

procedure, QCP-16 "Refueling Area Material Control," which provided

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instructions for controlling material to prevent entry into the reactor

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coolant system.

The inspectors observed the implementation of QCP-16

measures in the refueling cavity area during fuel assembly movement.

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Mcess to the designated work area was controlled through the use of

barriers.

The material control area was designated on the QCP-16

Material Control Barrier Location Form to include the refueling cavity

and an area approximately 15 feet to each side.

General conditions were

observed to be adequate with no loose material stored in the immediate

vicinity of the refueling cavity; objects on the ma.11pulator crane were

either taped in place or attached by lanyards; and personnel in the

material control area observed requirements for securing items.

A

quality control inspector was present to control material entering the

refueling area.

The inspectors reviewed the QCP-16 notebook which

contained in part the Tool and Material Accountability Log Sheet and

found no significant discrepancies in the tool and material

accountability logs and the end of shift material accountability reports.

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The material control measures of QCP-16 were implemented as required by

the licensee's refueling procedures.

The refueling procedures also

required a thorough inspection of the refueling cavity prior to lifting

the reactor vessel head.

The inspectors performed a walkdown of the

refueling upper cavity prior to reactor vessel head lift and visually

inspected the lower cavity for the presence of foreign objects.

The

refueling floor showed good general conditions with a minimum of loose

material.

Discussions with licensee personnel and reviews of various refueling logs

indicated that on several occasions, during refueling activities, small

objects had fallen to the refueling floor from other elevations.

During

the outage, work was progressing on the steam generators and on the

205-foot elevation, as well as other areas of containment, which may have

resulted in material falling onto the refueling floor.

The inspectors

discussed the incidents with members of plant management and shared the

concern of materials potentially falling into the open reactor vessel

during fuel assembly movement, particularly in light of the reported

instances of falling objects.

On one occasion, a plastic tie-wrap

reportedly fell into the refueling cavity onto the upper internals which

was in its stand in the lower cavity.

On another occasion, five small

objects which had the appearance of weld slag reportedly fell into the

refueling cavity and landed near the ladder on the upper refueling

cavity.

The plant was reloading fuel assemblies into the core at the

time.

Plant management expressed the position that (1) controls were in place

to minimize the potential for falling objects and (2) measures would be

taken to inspect for and remove any foreign objects in the refueling

cavity.

The inspectors reviewed the controls prescribed for work

(primarily on pipe supports) performed on the 205-foot elevation inside

containment.

These consisted of the use of lanyards to secure tools and

equipment and the use of-safety belts.

The inspectors performed a

walkdown of work conditions on the 205-foot elevation and observed the

establishment of work areas through the use of scaffolding, herculite and

welding blankets which attempted to minimize the potential for dropping

objects to lower containment elevations.

The inspectors reviewed

refueling logs which indicated that the reactor vessel flange and upper

internals were inspected for foreign objects, the core was inspected

during the course of core mapping, and the refueling cavity was vacuumed

to remove potential foreign material.

No violations or deviations were identified.

10.

Followup on IE Bulletin 85-03 Item e

As requested by Item e. of Bulletin 85-3, "Motor Operated Valve Common

Mode Failures During Plant Transients Due to Improper Switch Settings,"

the licensee identified the selected safety-related valves, the valves'

maximum differential pressures and the licensee's program to assure valve

operability in their letters dated May 8 and July 15, 1986, and November

,

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18, 1987.

Review of these responses indicated the need for additional

information which was contained in Region V letter dated March 9, 1988.

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. . .

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.

Review of the licensee's April 8, 1988, response to this request for

additional information indicated that the licensee's selection of the

applicable safety-related valves to be addressed and the valves' maximum

differential pressures met the requirements of the bulletin and that the

program to assure valve operability requested by action item e, of the

bulletin was acceptable.

The results of the inspections to verify proper implementation of this

program and the review of the final response required by action item f.

have beer. addressed in previous inspections.

This closes IE Bulletin 85-03.

11.

Exit Interview (30703)

The inspectors met with the licensee representatives denoted in paragraph

1 on June 23, 1988, and with licensee management throughout the

inspection period.

In these meetings the inspectors summarized the scope

and findings of the inspection activities.

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