ML20141G745
| ML20141G745 | |
| Person / Time | |
|---|---|
| Site: | Arkansas Nuclear |
| Issue date: | 05/19/1997 |
| From: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV) |
| To: | |
| Shared Package | |
| ML20141G724 | List: |
| References | |
| 50-313-97-02, 50-313-97-2, 50-368-97-02, 50-368-97-2, NUDOCS 9705220480 | |
| Download: ML20141G745 (16) | |
See also: IR 05000313/1997002
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ENCLOSURE 2
U.S. NUCLEAR REGULATORY COMMISSION .
REGION IV
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Docket Nos.:
50-313;50-368
License Nos.:
DRP-51; NPF-6
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Report No.:
50-313/97-02; 50-368/97-02
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Licensee:
Entergy' Operations, Inc.
Facility:
Arkansas Nuclear One, Units 1 and 2
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Location:
1448 S. R. 333
Russellville, Arkansas 72801
Dates:
March 16 through April 26,1997
Inspectors:
K. Kennedy, Senior Resident inspector
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S. Burton,' Resident inspector
J. Melfi, Resident inspector
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Appro ted by:
Elmo E. Colline, Chief, Project Branch C
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Division of Reactor Projects
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- Attachment:
Supplemental Information
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EXECUTIVE SUMMARY
Arkansas Nuclear One, Units 1 and 2
NRC Inspection Report 50-313/97-02,50-368/97-02
This routine announced inspection included aspects of licensee operations, engineering,
maintenance, and plant support. The report covers a 6-week period of resident inspection;
in addition, it includes the results of an announced inspection by a regional project
inspector.
Operations
Operators demonstrated good attention to detail and diagnostic skills in identifying
and analyzing a small change in stearn generator levels caused by a malfunction in
the Main Feed Pump B controller circuitry (Section 01.2).
The Unit 2 high pressure safety injection system was properly aligned and in good
material condition. The system engineer demonstrated proper oversight and
ownership of the system (Section 01.3).
The loading of the third dry spent fuel storage cask was performed very well and
with appropriate management's oversight. Radiological controls were very good
during the activity (Section 014).
Maintenance
Maintenance activities were performed well and in accordance with
procedures. Personnel were knowledgeable and generally demonstrated
effective communications, self checking, and peer checking. When
conducted, prejob briefs were comprehensive. The licensee effectively
addressed difficulties encountered during maintenance associated with
Service Water Pump P4A. Unit 2 instrumentation and control technicians
displayed a good questioning attitude when procedural and technical
problems were encountered during the performance of a core protection
calculator surveillance. Appropriate management attention was provided te
address problems and the corrective action process was properly utilized to
address generic concerns. Inspectors found an isolated occurrence in which
documentation of a maintenance activity was inadvertently discarded
(Section M1).
The licensee's failure to perform periodic testing of backup air accumulators
associated with outside air dampers in the control room emergency ventilation
system and the failure to identify a condition adverse to qua!ity was determined to
be a violation. The inspectors found that corrective actions for similar discrepancies
identified by the NRC in 1990, which resulted in a Severity Level 111 violation, were
not fully implemented (Section M8.1).
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Enaineerina
The failure to have administrative controls to ensure that fuel from the Units 1 or 2
cores was not off loaded to the spent fuel pool with service water temperatures in
excess of 85 F was determined to be a noncited violation (Section E8.1).
Plant Support
Locked high radiation areas were properly locked, areas were properly posted, and
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personnel demonstrated proper radiological work practices (Sections 01.4
and R1.1).
Chemistry technicians had a strong familiarity with assigned tasks, demonstrated
good knowledge in their areas of assigned duties, and were performing tasks for
which they were qualified (Section R5.1).
The licensee implemented proper physical security measures associated with the
integrity of protected area barriers, personnel and package access, and personnel
searches (Section S1.1).
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Report Details
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Summary of Plant Status
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Unit 1 began the inspection period at 86 percent power. Power was further reduced to
76 percent on March 16 at the request of the load dispatcher. Following the completion of
repairs to offsite transmission lines damaged as a result of tornados, Unit 1 raised power
and achieved 100 percent power on March 18,1997. Power was reduced to 85 percent
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on April 18 for turbine testing and returned to 100 percent on April 19, where it remained
through the end of the inspection period.
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Unit 2 began the inspection perioo a 97 percent power. On March 18, operators reduced
power to 73 percent to repair a malfunction of the Main Feed Pump B controller. On
March 20, during restoration of Main Feed Pump 8 and escalation to 100 percent power,
an unrelated malfunction in the Main Feed Pump A circuitry resulted in operators
maintaining the power at approximately 84 percent until the deficiency was corrected. On
March 21, power was restored to 97 percent and remained there through the end of the
reporting period.
1. Operations
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Conduct of Operations
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01.1
General Comments (71707)
The inspectors observed various aspects of plant operations, including compliance
with Technical Specifications; conformance with plant procedures and the safety
analysis report; shift manning; communications; management oversight; proper
system configuration and configuration control; housekeeping; and operator
performance during routine plant operations, the conduct of surveillances, and plant
The conduct of operations was professional and safety co'iscious. Emlutions such
as surveillances and plant power changes were well controlled, deliberate, and
performed in accordance with procedures. Shift turnover briefs were
comprehensive and were typically ettended by a chemistry technician, a health
physics technician, and a representative from system engineering. Housekeeping
was generally good and discrepancies were promptly corrected. Safety systems
were found to be properly aligned. Specific events and noteworthy observations
are detailed below.
01.2 Unit 2 - Main Feed Pomo Speed Oscillation
a.
Inspection Scope (71707)
On March 1'7,1997, a malfunction in the Main Feed Pump B controller circuitry was
identified. Operators reduced reactor power to 73 percent to secure Main Feed
Pump B for repairs. The inspectors reviewed the event, logs, trends, and corrective
actions performed by the operations department.
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b.
Observations and Findinas
On May 17 at 12:10 p.m., a control room operator noticed a small perturbation in
Steam Generators A and B level on the computer display. Subsequent investigation
by operations indicated that the Main Feed Pump B speed had decreased by
approximately 240 rpm. Main Feed Pump A automatically compensated to correct
the error in steam generator level. Reactor power was subsequently reduced to
73 percent by the operators and Main Feed Pump B was removed from service to
repair the controller circuitry. The power reduction and transfer to Main Feed
Pump A was accomplished without incident.
The inspectors reviewed the observed indications and associated graphs. The
duration of the transient was less than 3 minutes and steam generator levels
changed by less than 2 percent. Due to the relatively small magnitude and duration
of the event, the event could have gone unnoticed until the next regularly scheduled
logs on the affected equipment.
c.
Conclusions
Operators demonstrated good attention to detail and diagnostic skills in identifying
and analyzing a sma!! change in steam generator levels caused by a malfunction in
the Main Feed Pump B controller circuitry.
01.3 Unit 2 - Hiah Pressure Safety Iniection System Walkdown
a.
Insoection Scone (71707)
The inspectors performed a detailed walkdown of the Unit 2 high pressure safety
injection system. Valve and electricallineups, Safety Analysis Report requirements,
Technical Specifications, system drawings, and associated procedures were
revTew ed.
b.
Observations and Findinas
Valve and electricallineups were consistent with prints and procedures. Breaker
enclosures were clean and free of debris. The inspectors identified a minor
discrepancy on Drawing M-2232, Revision 103, Sheet 1. A test connection on the
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drawing identified as Pressure Indicator 2PI-5094 should have been identified as
Pressure Indicator 2PP-5094.
c.
Conclusions
The inspectors concluded that the Unit 2 high pressure safety injaction system was
properly aligned and in good material condition. The system engineer demonstrated
proper oversight and ownership of the system.
c.
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01.4 - . Unit 2 - Loadina of Drv Fuel Soent Fuel Storaae Cas_k
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Insoection Scope (71707, 71750, 60855)
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Between March 23 and April 2,.1997, the licensee loaded their third dry spent fuel
storage cask and placed it on the storage pad. rhis was the.first cask to be loaded
-with spent fuel from the Unit 2 spent fuel pool. The inspectors observed various
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portions of the cask loading evolution.
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Observations and Findinas
The inspectors found that the loading of the dry spent fuel storage cask was
performed in accordance with procedures and that the licensee complied with the
requirements of the Certificate of Compliance. Radiological controls implemented
during this activity were good. The inspectors observed that the licensee
successfully reduced the amount of time it took to vacuum dry the cask, compared
to the previous two casks, through the use of more effective drying equipment. On
March 26, during the performance of a dye penetrant test following completion of
-the shield lid root pass weld, the licensee discovered a small crack on the
multi-assembly sealed basket wall just above the weld. This issue was the subject
of an NRC specialinspection, the resuits of which are documented in NRC
Inspection Report 50-313/97-12;50-368/97-12,
c.
Conclusions
The loading of the third dry spent fuel storage cask was performed very well and
with appropriate management's oversight. Radiological controls were very good
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during the activity.
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Miscellaneous Observations
The inspectors observed other minor incidental problems with components in the
area of the work activities, which the licensee took correct.ive action on.
Specifically, the licensee took actions to correct a missing jam nut on a steam
generator blowdown line and placed covers around some intake structure electrical
heaters.
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08.1- (Closed) Licensee Event Reoort (LEJ) 50-313/06-004, " Excessive Load Moved Over
Eur! Store'in Soent Fuel Pool"
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This event was discussed in NRC Inspection Report 50-313/96-03;50 368/96-03
and was the subject of a noncited violation. No new issues were revealed by the
LER.
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11. Maintenance
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Conduct of Maintenance
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M 1.1 General Comments
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Lq. oection Scooe (62707)
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The inspectors observed all or portions of the following maintenance activities:
Unit 1 - Job Order (JO) 00961368, "P-153 has Degraded Discharge Pressure
& Flow, investigate, Repair or Replace," performed on March 25,1997.
Unit 1 - JO 00960313, " Corrective Maintenance to Replace Worn Shaft
Sleeve," associated with Service Water Pump P4A, performed on March 31
through April 5.
Unit 1 - JO 00960389, " Preventive Maintenance on P4A Motor, " performed
on March 31 through April 5.
Unit 1 - JO 00923335, "I&C Support for Maintenance on P4A," performed -
on March 31 through April 5.
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Unit 2 - JO 00957988, " Corrective Maintenance to Adjust Local Position
Indicator on 2CV-1076 2," performed on April 15.
Unit 2 - JO 00957627, " Preventive Maintenance on 2CV-1076-2,"
performed on April 15.
Unit 2 - JO 00958413, " Preventive Maintenance on 2CV-1039-1,"
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performed on April 15.
b.
Observations and Findinos
The inspectors found the work performed in these activities to be professional and
thorough. All work was performed in accordance with procedures and the workers
were knowledgeable on their ass:gned tasks. When applicable, appropriate
radiological work permits were followod.
In addition, see the specific discussions of maintenance observed under
Sections M1.2 through M1.4, belovs.
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M 1.2 Unit 1 - Maintenance on Hydroaen-Oxvnen Analyzer
a.
trnpection Scope (62707)
On March 25,1997, the inspectors observed the licensee perform troubleshooting
activities associated with Hydrogen-Oxygen Analyzer C119A Sample Pump P-153.
The licensee believed that the pump had dagraded discharge pressure and flow and
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was determining whether or not the pump needed to be replaced.
b.
Observations and Findinas
On March 25, the inspectors observed the licensee troubleshoot and investigate the
need to replace the Train A hydrogen-oxygen analyzer sample pump. Technicians
found that the sample pump provided the proper discharge flow and pressure as
required by Procedure 1304.184, Revision 4, " Unit 1 Hydrogen / Oxygen Analyzer
Calibration, C119A." The technicians did not replace the pump and canceled the
JO.
The technicians had previously noticed that the suction pipe to this pump was
vibrating and they installed a pipe support which significantly reduced the vibration.
The technicians then performed the surveillance test on the system to verify
operability.
On April 7, the inspectors asked the licensee for the completed JO package. The
licensee discovered that when they discarded the original JO they also inadvertently
discarded the documentation for the work which had installed the pipe support.
The licensee then rewrote the description of the work performed during the
maintenance activity.
c.
Conclusions
The inspectors concluded that the licensee performed the maintenance activity on
the hydrogen-oxygen analyzer sample pump in accordance with the work
instructions. Inspectors found that documentation of the maintenance activity was
inadvertently discarded.
M1.3 . Unit 1 - Maintenance on Service Water Pumo P4A
a.
Inspection Scope (62707)
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The inspectors observed portions of several JOs associated with maintenance on
Service Water Pump P4A, performed between March 31 and April 5. This activity
included the refurbishment of the pump motor due to increased vibrations observed
during previous surveillance tests.
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b.
Observations and Findings
The inspectors observed that the licensee experienced several difficulties during the
reassembly of the service water pump motor. Following a water flush of the motor
stator, the licensee had difficulty in drying out the motor sufficiently to achieve
desired electrical resistance values. The licensee decided to install a spare motor
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assembly. This was performed in accordance with Procedure 1402.061,
R9 vision 12, " Disassembly, inspection, and Reassemb!y of the Unit 1 Service Water
Pumps (P4A, B & C)." Following reassembly, the licensee ran the pump and found
that the motor vibrations remained high. The licensee disassembled the motor and
found that the upper collar on the bearing had an out-of-tolerance clearance on the
upper bearing sleeve. The licensee indicated that this problem was not revealed
when the rotor was balanced because the bearing war not loaded, as is the case
when the rotor is installed in the motor. The licensee had not checked this
clearance prior to installation and the vendor had not specified a tolerance for the
clearances on the upper bearing sleeve. Procedure changes were initiated to ensure
these clearances were checked during future activities.
The licensee reassembled the motor and found that vibra ^ ions were significantly
reduced.
c.
Conclusions
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The licensee effectively addressed difficulties encountered during maintenance
associated with Service Water Pump P4A.
M 1.4 General Comments on Surveillance Activities
a.
Inspection Scope (62707)
The inspectors observed all or portions of the following surveillance activities:
Unit 1 - Procedure 1304.14, " Unit 1 Hydrogen / Oxygen Analyzer
Calibration, C119A," on March 25,1997.
Unit 1 - Procedure 1109.009, Supplement 3, " Unit 1 Governor Valve Test,"
on April 18.
Unit 1 Procedure 1109.009, Supplement 2, " Unit 1 Turbine Valve Test," on
April 18.
Unit 2 - Calibration of Refueling Water Tank Level Transmitter 2LT-5636-1
performed in accordance with Procedure 2304.041, Revision 17, " Unit 2
Plant Protection System Channel A Field Calibration," Supp!ement 1,
" Calibrations Outside Containment," performed on April 25.
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Unit 2 - Calibration of Refueling Water Tank Leve! Transmitter 2LT-5637-2
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performed in accordance with Procedure 2304.042, Revision 17,
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" Unit 2 Plant Protection System Channel B Field Calibration," Supplement 1,
" Calibrations Outside Containment," performed on April 25.
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Unit 2 - Calibration of Refueling Water Tank Level Transmitter 2LT-5639-3
performed in accordance with Procedure 2304.043, Revision 18, " Unit 2
Plant Protection System Channel C Field Calibration," Supplement 1,
" Calibrations Outside Containment," performed on April 25.
Unit 2 - Calibration of Refueling Water Tank Level Transmitter 2LT-5640-4
purformed in accordance with Procedure 2304.044, Revision 18, " Unit 2
Plant Protection System Channel D Field Calibration," Supplement 1,
" Calibrations Outside Containment," performed on April 25.
b.
Observations and Findinas
The inspectors found that the surveillance activities were performed according to
the licensee's procedures by knowledgeable workers. When applicable, appropriate
radiological werk permits were followed.
M 1.5 Unit 2 - 18-Month Calibration of Core Protection Calculator
a.
Inscection Scope (61726)
On March 19, the inspectors observed instromant and control technicians perform
Procedure 2304.182, Revision 1, " Core Protection Calculator 'A' Reactor Coolant
Pump Speed input Loops Calibration." instrument and control technicians
performed a calibration of the pulse shaper modules that mouify the reactor coolant
pump speed input to the core protection calculator,
b.
Observations and Findinas
Due to the introduction of new test equipment, a function generator with a digital
output, the technicians appropriately questioned their supervisor about the readings
being recorded and methodologies utilized to obtain the reading. The function
generator duplicated indications to those found on the oscilloscope and the
technicians questioned which indication to utilize for the surveillance. The
supervisor was consulted and it was determined that the reading from the
oscilloscope was correct. A procedure change form was initiated to clarify the
procedure and a condition report was written to identify and correct procedures that
contained similar vulnerabilities with the use of multiple types of test equipment.
The technicians encountered difficulties integrating the restoration of Core
Protection Calculator A with the rerr. oval of Core Protection Calculator B. A
restoration step for the Core Protection Calculator A requires that the associated
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computer be restored to service, yet the subsequent procedure requires that the
same component be removed from service. The original intent of integrating the
procedures was to leave the computer out of service versus restoring it to service
between procedures. The technicians discussed the integration problem with their
supervisor who contacted the control room. A deviation from the procedure was
authorized in accordance with the guidance in Procedure 1000.006, Revision 45,
" Procedure Control." This allowed the computer to be left out of service and the
work to continue. A procedure farm was initiated to revise the procedure to better
integrate the testing of the core protection calculators.
c.
Conclusions
Instrument and control technicians performed the core protection calculator
surveillance per approved procedures. The technicians displayed a good
questioning attitude when procedural and technical problems were encountered.
Appropriate management attention was provided to address problems and the
corrective action process was properly utilized to address generic concerns.
M1.6 Conclusions on Conduct of Maintenance
Maintenance activities were performed well and in accordance with procedures.
Personnel were knowledgeable and generally demonstrated effective
communications, self checking, and peer checking. When conducted, prejob briefs
were comprehensive. The licensee effectively addressed difficulties encountered
during maintenance associated with Service Water Pump P4A. Unit 2
instrumentation and control technicians displayed a good questioning attitude when
procedural and technical problems were encountered during the performance of a
core protection calculator surveillance. Appropriate management attention was
provided to address problems and the corrective action process was properly
utilized to address generic concerns. Inspectors found an isolated occurrence in
which documentation of the installation of a pipe support on the hydrogen-oxygen
analyzer sample pump was inadvertently discarded.
M8
Miscellaneous Maintenance issues (92902)
M8.1 (Closed) Unresolved item (URI) 60-313/9701-03: 50-368/9701-03. " Failure to Test
Safetv Related Accumulators"
a.
Insnection Scoce (92902)
NRC Inspection Report 50-313/97-01; 50-368/97-01 documented the licensee's
discovery that they had not been performing a procedurally required 18-month test
of the control room emergency ventilation external air dampers to verify that backup
air bottles would maintain these dampers shut upon a loss of instrument air.
Subsequent testing revealed excessive leakage from one of the backup air supplies.
This issue remained unresolved pending further review of a similar finding in 1990
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and resolution of the basis for the test acceptance criteria for the backup air bottles.
The inspectors conducted additional inspection of this issue.
b.
Qbservations and Findinas
NRC Inspection Report 50 313/97-01;50-368/97-01 stated that, in 1990, the
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licensee wrote a condition report to document the fact that they were not
performing tests to verify that Dampers CV-7910 and 2PCD-8607B could be
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maintained closed upon a loss of instrument air. The condition report was written
in response to testing deficiencies identified during an operational safety team
inspection conducted by the NRC in September 1990 (NRC Inspection
Report 50-313/90-24;50-368/90 24). A subsequent followup inspection
conducted in October 1990 (NRC Inspection Report 50-313/90-38;50-368/90-38)
identified that the licensee failed to test certain safety-related instrument air check.
valves in the control room heating, ventilation, and air conditioning system and did
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not provide an accurate response to Generic Letter 88-14, " Instrument Air Supply
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System Problems Affecting Safety-Related Equipment." On December 17,1990,a
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Severity Level lli violation was issued to the licensee for providing inaccurate
information regarding the testing of air-operated, safety-related components and a
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failure to identify a significant condition adverse to quality.
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One of the condition report corrective actions was to provide a procedure for the
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periodic testing of the damper air consumption for Accumulators VRA-1 A
and 2VRA 1B to verify that system integrity was maintained. The periodicity was
specified to be a maximum of 18 months. Procedure 1304.175, "ANO-1 Damper
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Air Consumption Test of VRA-1 A and 2VRA-1B," was written and became effective
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'on October 15,1991. The procedure indicated that the test was to be performed
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at 18-month intervals. However, the procedure was not entered into the licensee's
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repetitive task prcgram and, therefore, was not scheduled to be performed on an
18 month interval, The licensee determined that the procedure was not entered
into the repetitive task program because actions contained in the condition report
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did not clearly define or assign a task to enter the procedure into the repetitive task
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program.
The inspectors found that the licensee failed to implement the corrective actions of
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the condition report in that Procedure 1304.175 had not been performed at
18-month intervals.
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10 CFR Part 50, Appendix B, Criterion XVI, " Corrective Action," requires, in part,
that measures shall be established to assure that conditions adverse to quality, such
as failures, malfunctions, and deficiencies are promptly identified and corrected.
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The licensee's failure to perform tests to verify that backup air accumulators would
maintain outside air dampers in the control room emergency ventilation system
closed upon a loss of instrument air, and the identification that the leakage from
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Accumulator 2VRA-1B was in excess of the acceptance criteria contained in
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Procedure 1304.175, Revision 0, " ANO-1 Damper Air Consumption Test of VRA-1 A
and 2VRA-1B," was determined to be a violation of 10 CFR Part 50, Appendix B,
Criterion XI and XVI" (50-313/9702-01; 50-368/9702-01).
NRC Inspection Report 50-313/97-01; 50-368/97-01 also described an apparent
discrepan y between the design basis of the backup air accumulators and the test
acceptance criteria contained in Procedure 1304.175. The inspectors noted that
Calculation 90 E-0072-02, " Calculation for ANO-1 Control Room Dampers CV 7910
and 2PCD-8607B Allowable Leakage Form High Pressure Accumulators," was used
as a reference in the development of Procedure 1304.175. An assumption made in
the leakage calculation was that the backup air accumulators would provide a
sufficient volume of air to maintain the dampers closed for 30 days on a
loss-of-instrument air. The calculation revealed that the allowable leakage rate to
maintain the damper closed for 30 days was 0.67 psig/hr. The calculation results
also included an acceptable pressure decay of 1.68 psig/ hour to maintain the
damper closed for 12 days. The inspectors noted that the acceptance criteria
contained in Procedure 1304.175,1.68 psig/hr, corresponded to the acceptable
pressure decay to maintain the damper closed for 12 days. However, it appeared to
the inspectors that the design basis for the backup bottles was to maintain the
dampers closed for 30 days. As a result, Procedure 1304.175 did not appear to
provide the correct acceptance criteria to ensure that the backup bottles satisfied
their design requirement,
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The licensee stated that the design basis for the backup air accumulators was to
ensure that an outside air damper can be closed even with the loss-of-instrument
air. The inspectors found that statements in the Safety Analysis Report supported
this design basis and did not include a duration for maintaining the dampers closed.
The licensee stated tl'.it 12 days was sufficient to identify and correct excessive
leakage from an accumulator. The licensee stated that Calculation 90-E-0072-02
was performed to develop appropriate test acceptance criteria in the development of
Procedure 1304.175. The 12-day acceptance criteria was selected for
incorporation into the procedure,
c.
Conclusions
The licensee's failure to perform periodic testing of backup air accumulators
associated with outside air dampers in the control room emergency ventilation
system and the failure to identify a condition adverse to quality were determined to
be a violation. The inspectors found that corrective actions for similar discrepancies
identified by the NRC in 1990, which resulted in a Severity Level 111 violation, were
not fully implemented.
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M8.2' (Closed) Violation 50-368/9508-01, " Operation With inocerable Main Steam Line
Safetv Valves"
(Closed) LER 50-368/95-005, " Main Steam Safety Valve Lift Pressures Not Within
Technical Specification Tolerance Durina Operation Due to a Failure to Adeauatelv
Specifv Environmental Conditions for Use in Vendor P;ocedures for Testina and
Sotooint Adiustment"
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These two items concerned the same issue and the licensee wrote
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LER 50-368/95-005 for this violation of Technical Specifications. The inspectors
verified the corrective actions described in the licensee's response letter, dated
December 15,1995, to be reasonable and complete.
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M8.3 (Closed) Violation 50-313/9601-03, " Failure to Conduct Preventive Maintenance on
Emeraencv Feedwater Initiation and Control Heat Tracina"
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The inspectors verified the corrective actions described in the licensee's response
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letter, dated May 8,1996, to be reasonable and complete. No similar problems
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Miscellaneous Engineering issues (92903)
E8.1
(Closed) URI 50-313/9602-04: 50-368/9602-04, " Review of UFSAR Commitments"
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a.
Inspection Scope
NRC Inspection Report 50-313/96-02;50-368/96-02 documented an apparent
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discrepancy in the licensee's Updated Final Safety Analysis Repart regarding the
design basis of the Units 1 and 2 spent fuel pools and the lack of administrative
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controls to ensure the design basis was not exceeded. Further inspection of the
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unresolved item was conducted during this inspection period.
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b.
Observations and Findinas
The Units 1 and 2 Safety Analysis Reports stated that the spent fuel and spent fuel
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pool cooling system are designed to keep the pool water temperature below 120 F
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for normal refueling operations and 150 F for fut, core discharge situations. This
design basis assumed a service water temperature of 85 F. However, lake
temperatums have routine' exceeded 85 F during the summer months of
l
operation. Since the plant began operating, lake temperatures in excess of 90 F,
but less than 95 F, have been recorded. Lake temperatures in excess of 85 F
L
could cause the spent fuel pool water to exceed the design basis temperatures
stated in the Safety Analysis Reports. NRC Inspection Report 50-313/96-02;
'
50-368/96-02 indicated that, if the service water temperature was assumed to be
,
1
1 -
..
, _
~
_
4
<
e
-12-
95 F and the cores were fully off loaded, the maximum spent fuel pool temperature
would be 168 F on Unit 1 and 162 F on Unit .2.
These maximum' values were well
below the temperature at which boiling of the water in the. spent fuel pool would
occur. However, the inspectors found that the licensee did not have administrative
controls to ensure a core discharge did not occur when service water temperatures
exceeded 85 F.
The inspectors found that the licensee had never off-loaded fuel from either plant
when service water temperatures exceeded 85'F and had never exceeded spent fuel
pool temperatures assumed in the current licensing basis.
To ensure that the maximum licensing basis spent fuel pool temperatures are not
exceeded in the spent fuel pools in the future, the licensee revised the refueling
procedures for both units. As a prerequisite to refueling, procedures require the
licensee to verify that required cocling system components are available and that
the Lake Dardanelle temperature is in a range that would provide sufficient cooling
to maintain spent fuel pool temperatures within design limp.s during the course of
the proposed refueling. Procedure 1502.004, " Control of Unit 1 Refueling," and
Unit 2 Procedure 2502.001, " Refueling Shuffle," were reviewed to verify that the
appropriate precautions were added. The added precautions could preclude the
licensee from performing refuelings during summer months when Lake Dardanelle
temperatures are elevated.
10 CFR Part 50, Appendix B, Criterion Ill, " Design Control," states, in part, that
". . . measures shall be established to assure that applicable regulatory requirements
and the design basis . . . for those structures, systems, and components to which
this appendix applies are correctly translated into specifications, drawings,
procedures, and instructions." The failure to have administrative controls to ensure
a core discharge did not occur with service water temperatures in excess of 85 F
was determined to be a violation. This failure constitutes a violation of minor
significance and is being treated as a noncited violation, consistent with Section IV
of the NRC Enforcement Policy (50-313/9702-02; 50-368/9702-02).
c.
Conclusions
The failure to have administrative controls to ensure fuel from the Units 1 or 2 cores
was not off loaded to the spent fuel pool with service water temperatures in excess
of 85 F was determined to be a noncited violation.
i
,
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.
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-13-
IV Plant SilDDort
,
P
R1
Radiological Protection and Chemistry Controls
R1.1 General Comments'(71750)
During routine tours of the plant and observations of plant activities, the inspectors
-
_
found that access' doors to locked high radiation areas were properly locked, areas
i
were properly posted, and personnel demonstrated proper radiological work
practices.
R5
Staff Training and Qualification
RS.1 Chemistry Technician Qualification (71750)
The inspectors reviewed the training and qualifications of chemistry technicians.
-Technicians. interviewed had a strong familiarity with assigned tasks and
demonstrated good knowledge in their ureas of assigned duties. The chemistry task
to training matrix was reviewed and a sampling of procedures indicated that
technicians were performing tasks for which they were qualified.
S1
Conduct of Security and Safeguards Activities
S 1.1 General Comments (71750_1
During this inspection period, the inspectors observed the licensee implement proper
physical security measures associated with the integrity of protected area barriers,
personnel and package access, and personnel searches.
s
t
.5
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. .
.... _ .-
. . - .
_ - . . - . . _ - -
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,
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'
e
ATTACHMENT
SUPPLEMENTAL INFORMATION
PARTIAL LIST OF PERSONS CONTACTED
Licensee
B. Allen, Maintenance Manager, ui.,
.
-
C. Anderson, Plant Manager, Unit '
G. Ashley, Licensing Supervisor
B. Bement, Radiation Protection and Chemistry Manager
M. Chisum, instrumentation and Control Superintendent, Unit 2
A. Clinkirgbeard, Operations Shift Superintendent, Unit 1
~ M.- Cooper, Licensing
D. Denton, Director, Support
P. Dietrich, Maintenance Manager, Unit 1
R. Edington, General Manager, Plant Operations
C. Eubanks, Mechanical Superintendent, Unit 2
C. Fite, in-House Events Supervisor
R. Hutchinson, Vice President, Operations
J.~ Kowalewski, Manager, Unit 1 System Engineering
J. McWilliams, Modifications Manager
D. Mims, Director, Licensing
T. Mitchell, Manager, Unit 2 System Engineering
T. Russell, Operations Manager, Unit 2
M. Smith, Engirwering Programs Manager
' A_ . South, Licensing
J. Vandergrift, Director, Quality
H. Williams, Jr., Superintendent, Plant Security
C. Zimmerman, Plant Manager, Unit 1
I
INSPECTION PROCEDURES USED
IP 30855:
Plant Operations
IP 61726:
Surveillance Observations
IP 62707:
Maintenance Observations
IP 71707:
Plant Operations
IP 71750:
Plant Support Activities
IP 92902:
Followup - Maintenance
IP 92903:
Folicwup Engineering
)
. .
.
..
..
-
-
. -
.
-
<
' 's
- .
2-
ITEMS OPENED, CLOSED, AND DISCUSSED
Opened
50 313:368/9702-01
Failure to Test Safety Related Accumulators
(Section M8.1)
Opened and Closed
50-313:368/9702-02
Failure to Translate Design Basis of Spent Fuel Pool
into Procedures (Section E8.1)
. Closed
50-368/9505-00
LE9
Main Stearn Safety Valve Lift Pressures Not Within
Technical Specification Tolerance During Operation Due
to a Failure to Adequately Specify Environmental
Conditions For Use in Vendor Procedures for Testing
and Setpoint Adjustment (Section M8.2)
50-368/9508-01
Operation With Inoperable Main Steam Line Safety
Valves (Section M8.2)
50-313/96-004
LER
Excessive Load Moved Over Fuel Store in Spent Fuel
Pool" (Section 08.1)
50-313/9601-03
Failure to Conduct Preventive Maintenance on
{
Emergency Feedwater initiation and Control Heat
Tracing (Section M8.3)
50-313:368/9602-04
Review of UFSAR Commitments (Section E8.1)
50-313:368/9701-03
Failure to Test Safety-Related Accumulators
(Section M8.1)
,
. --
-.
.
.
._.
.
.
.. .-
.
..
.
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. .
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__ _
.
.
.
'
PLANT IPE CORE DAMAGE FREQUENCY lNFORMATION
7
ceo
ree
neye- % a
p.e i.ec=eo ee.r,e ,.n.,perme.w.=ca e-
Innic0F
'
seO
ams
7-
toca
som
ist0ca
w n.e4
seO
ams
1-W=e
toca
som
98tOca w nee 4
Plant IPE
teSees if2
4.7E-05
3.82E-05
1.87E47
7.30E-08
2.83E-08
-
neghgee
3 39E-06
81 %
0%
16%
0%
-
7%
Nme fMe Point 2
3.1E-05
5.50E-06
1.10E-06
2.31E-05
7.40E-07
-
2.50E-08
1.50E-06
18%
4%
75%
2%
-
0%
5%
WNP 2
1.8E-05
1.10E-05
6.25E-07
2.63E-06
5.10E-07
-
neghe &e
2.52E 06
63%
4%
15%
3%
-
0%
14 %
,
C1nton
2.7E-05
1.40E-07
1.40E-05
1.10E-06
-
neghgMe
1.60E-06
38%
1%
53%
4%
-
0%
8%
Grand Gull 1
1.7E-05
7 46E-06
5.56E-08
9.35E-06
5.18E-07
-
neghgMe
JT07
43%
0%
54%
3%
-
0%
1%
Perry 1
1.3E-05
2 25E-06
4.70E-06
4.30E-06
4.50E-07
-
neghgde
1.50E 46
17%
36 %
33%
3%
-
0%
12%
fbver Bond
1.6E-05
1 35E-05 neghge.
2.05E-06 neghg de
-
neghgMe
1.80E-08
87%
0%
13%
0%
-
0%
0%
Babcock and Wilcox PWR 2-loop
ANO 1
4.7E-05
9.93'E-07
1.48E-05
1.57E-05
9.20E-08
6.90E-08
9.34E-0)
34 %
2%
32%
34 %
0%
0%
2%
Cryst.1 Phver 3
1.5E-05
3.28E M negwg&e
9.45E47
9.00E-06
6.70E-07 noghgcle
1.25E-06
21 %
0%
6%
59%
4%
0%
8%
Davis Besse
6.6E-05
3.54E-07
5.71E-05
5.286-06
4.60E-07
8 80E-07
2.00E-06
1%
86 %
8%
1%
1%
3%
i
Oconee 1,2,3
2.3E-05
2.57E-06
1.00E-07
5.33E-06
9.701-06
2.10E-07
4.50E-10
5.50E-06
11%
0%
23%
42%
1%
0%
24 %
!
TMt 1
4.5E-05
1.57E-06 neghg&e
2.36E-05
1.57E-05
8.94E-07
1.80E-07
3.00E-06
3%
0%
52%
35%
2%
0%
7%
Combustion Engineering PWR 2-Loop
ANO 2
3.4E-05
1.23E-06
1.02E-06
2.67E-05
4.804-06
9.53E-08
3.36E-07 neghese
4%
3%
79%
14%
0%
1%
0%
2.40E-05
1.30E-04
6.65E-05
4.49E-06
1.90E-06
1.55E.05
10%
54 %
28%
2%
1%
6%
Calvert Chffs 112
2.4E 04
2.89E-0 7
8.93E 06
1.07E u6
7.67E-07
6.74E-C7
1.87E-06
2%
66%
8%
6%
5%
14%
Fort Calhour 1
1.4E-05
St tucie 1
2.3E-05
2 65E 06
4.13E-07
5.36506
1.22E-05
8.18E-07
1.74E-06
5.00E-07
12%
- %
23%
53%
4%
8%
2%
Sttucie 2
2.6E-05
2.64E-06
1.76E-06
5.31E-06
1.29E-05
8.99E-07
2.72E-06
5.00E-07
10%
7%
20 %
49%
3%
10%
2%
._
Minstone 2
3.4E-05
4.3E 07
1.5E-06
2.5E-06
8.01E-08
5.22E-07
8.60E-08
2.00E-07
1%
4i
74 %
10%
2%
0%
1%
P.hsedes
5.1E-05
9 02E-06
4.00E-06
2.00E-05
1.57E-05
2.54E-06
3E 07
18%
8%
39 %
31 %
5%
0%
0%
,
b
FILE: tPE-CDF.TSL
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PLANT IPE CORE DAMAGE FREQUENCY lNFORMATION
.
Iner. CDF
Core Damage Fueguen~y Por accident CImes
Percent of Care Demeys Fregeancy Pee AW Onee
Plant IPE
so
a1*s
vrer
toCa
sain
istoCa
ii nsed
seo
arws
reer.oinnie
toca
sein
istoCa
b.i nsed
IIsoes en CDF values:
- * For Dans Besse. Calvert Chffs. & Fort Calhoun. seperate 580 CDF was unewedeble. so Transesni
For Turkey Poent, the CDF hsted in the avec summery of the submrttel. which
CDF and % CDF includes SBO contribution
corresponds to *all toyers of recovery," was used
The database values for Oyster Creek do not appear to anchsde the CDF for intemet floods; the
'For Salem 1 & 2. the revesed flood and plant CDFs bsted in the sahenittet letter for the IP1
vetues Ested here include the CDF for intemet Wood
were used
(2)The Surry internet flood CDF is from page 9 of 4/21/92 NMR letter which Ests a revised value
from 19126191 Surry seensiysis submittet
For Watts Bar. the CDFs from the revesed subtruttet were used
Deferred means that hcensee included Interriet flood enelyses in thes IPEEE
.
.
t
,
4
FILE: IPE-CDF.T8t
i
.
PLANT tPE CONTAINMENT FAILURE FREQUENCY INFORMATION
Coes Demoge Freesency Dy Centeinment Fasiste Mede
Percent of Core C.cc. p i
up Por Containment Fenisre r-2
Plant
Plant tPE
Bypese
EF
LF
NCF
Bypese
EF
LF
NCF
Generet Electric - Large Dry
l
5.4E-05l
7.56E-07l
2.32E-06l
neghgesel
5 09E-05l
1%l
4%l.
0%l
94 %
BIO ROCK POINT
General Electric - Merit i
BROWNS FERRY 2
4.8E-05
4.45E 07
2.18E-05
1.25E-05
1.33E-05
1%
45%
26%
28%
BRUNSWICK 1&2
2.7E 05
611E 08
2.38E-06
1.63E-05
8.33E-06
1%
9%
60 %
31 %
COOPER
8 OE-05
neghgtte
1.29E 05
b.7 7E-05
913E-06
0%
16%
72%
11 %
ORESDEN 2&3
1.9E-05
noghgele
5.55E-07
1.59E-05
2.04 E-06
0%
3%
86%
11%
DUANE ARNOLD
7.8E-06
neghgele
3.67E-06
2.49E-06
1.68E-06
0%
47%
32 %
21%
FERMI 2
5.7E 06
2.OOE 07
1.71E-06
2.22E-06
1.57E-06
4%
30 %
39%
28%
FITZPATRICK
1 9E-06
neghg@e
1.20E-06
4.16E-07
3 03E 07
0%
63%
22%
16 %
HATCH 1
2.2E 05
1.85E-07
5.47E 06
5.70E-06
1.10E-05
1%
25%
26%
49%
HATCH 2
2.4E-05
1.94E 07
5 OCE 06
5 91E.06
1.25E-05
1%
21 %
25%
53%
HOPE CREEK
4.6E-05
.neghg &
2.87E-05
1.20E 05
5.56E-06
C%
62%
26%
12%
M RSTONE1
1.1E-05
1.25E-07
3.74E-06
3.2 7E-06
3.87E-06
1%
34 %
3016
35 %
MONTICELLO
2.6E-05
5.20E 09
4.15E-06
6.24E OG
1.56E-05
1%
18%
24%
60 %
NINE MILE POINT 1
5.5E-06
7.48E-08
1.31E-06
3.40E-06
7.12E-07
1%
24 %
62%
13%
OYSTER CREEK
3.7E-06
2.70E-07
5.87E-07
9 69E-07
1.86E 06
7%
16%
26%
61%
PEACH BOTTOM 2&3
5 5E-06
6 64E-09
1.55E-06
1.40E-06
2.5 7E-06
1%
28%
25 %
46%
PtLGRIM 1
5.8E-05
2.32E-07
1.25E-05
3 54E.05
9.86E-06
1%
22%
61%
17%
OUAD CITIES 1&2
1.2E-06
6.OOE-10
2.84E-07
6.62E-07
2.53E-07
1%
24%
55%
21 %
VERMONT YANKEE
4.3E-06
4.30E-08
2.11E-06
9 89E 07
1.16E-06
1%
49%
23%
27%
IPE-CFF.T8L
September 30,1996
-
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..__ .. . _ _ .
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Pt ANT IPE CONTAINMENT FAR.URE FREQUENCY WeFORMATION
!
Case Desusage Fseepsency By Centehunent Fe8mre Mode
Percent et Case Dennage Psegsopey Per - FeAsse Mode
%
Plant IPE
9 ,pese
EF .
LE
feCF
Dypees
EF
LF
90CF
I
,
General Electric - Mark N
!
LA SALLE 1&2- 5305
4.7E-05
neghgede
1.66E-05
2.42E-05
8.64E-06
0%
~ 35 %
51%
14%
LIMERICK 1&2
4.3E-06
noghgede
3.96E-07
1.16E-06
2.75E-06
0%
9%
27%
64 %
.
N!NE MILE POINT 2
3.1E-05
2 79E-08
2.32E46
2.04E-05
8.30E-06
1%
7%
66%
27%
WNP 2
1.8E 05
2.98E-08
5.34E 06
5.30E-06
6.83EM
1%
31 %
30 %
39 %
,
Generet Electric - Meet M
.
CLINTON
2.6E-05
neghedde
8.27E-07
4 84E47
2.4 7E-05
0%
3%
2%
35 %
GRAND GULF 1
1.7E 05
neghgede
8 05E 06
5 66E 06
3 51E-06
0%
47%
33%
20 %
PERRY 1
1.3E-05
neghgede
3.14E-06
4.76E-06
5.30E-06
0%
24 %
36 %
40 %
'
RIVER SEND
1.6E-05
neghgede
4.30E 06
2.14E-06
8 98E 06
0%
28 %
14 %
58%
PWR -Ice Condesiser
CATAWBA 1&2
4.3E-05
7.71E-09
2.31E-07
2.02E-05
2.2 ?E-05
1%
1%
47%
53%
~[
D.C. COOK 1&2
6.3E-05
7.11E-06
9.26E-07
1.13E 06
5.40E-05
11 %
.1%
2%
86 %
[
MCGutRE 1&2
4.0E45
9.60E-07
9.50E-07
1.64E-05
2.20E-05
2%
2%
40%
54 %
SEOUOYAH 1&2
1.7E-04
7.99E-06
2 81E-06
S.32E-05
7.60E-05
5%
2%
49%
46%
i
t
WATTS BAR 1&2
9.0E-05
- 5.95Em
4.03EM
1.72E-05
5.27E-05
7%
5%
22 %
66 %
!
!
PWR - Subetsnospheetc
t
SEAVER VALLEY 1
2.1E-04
1.02E-05
4.73E-05
9.15E-05
6.17E-05
5%
- 23%
44 %
29%
SEAVER VALLEY 2
1.9E-04
9.84E-06
4.74E-05
8 54E 05
4.69E-05
5%
25%
45%
25 %
,
!
NORTH ANNA 1&2
6.8E-05
8 98E-06
1.05E-06
7.68E G
5.03E-05
13%
2%
11 %
74 %
SURRY 1&2
'
MILLSTONE 3
5.9E-05
3.90E47
2.24E-00
1.10E-05
4.47E-05
1%
8%
20 %
g0%
f
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Ft ANT IPE CONTAINMENT FAE.URE FREOUENCY INFORMATION
Core Deenage Frogsency 9y Contabwnent Feeure Mode
Percent et Case Dag Psogneney Per Centehuneset Fe8ese Stede
%
Plant tPE
Sypees
EF
LF
NCF
Bypees
EF
LF
NCF
s
p
PWR - Large Dry
ARKANSAS P.1.lCLEAR O*iE 1
4.9E-05
2.08E-07
3.03EM
5.95EM
3.96E-05
1%
6%
12%
81 %
t
ARKANSAS NUCLEAR ONE 2
3.7E-05
4.07E-07
4 51E-06
5.14E-06
2.69E C5
1%
12 %
14 %
73%
.
6
BRAIDWOOD 1&2
2.7E 05
1.10E-08
5.48E-08
2.54E-06
2.48E-05
1%
1%
9%
90%
.
r
SYRON 1&2
3.1E 45
1.24E-08
2.13E-07
2.50E-06
2.82E-05
1%
1%
8%
91 %
j
CALLAWAY
5.8E-05
1.17E-06
1.17E-07
3.09E-05
2 fi3E-05
2%
1%
53%
45%
.
t
CALVERT CLIFFS 1&2
2.4E-04
7.44EM
2.11E-05
9.53E-05
1.1SE-04
3%
9%
40%
48%
j
COMANCHE PEAK 1&2
5.7E-05
4.67E M
6.75E-07
2.93E-05
2.26E.05
8%
1%
51 %
39%
j
CRYSTAL RIVER 3
1.5E-05
7.39E-C7
5.53E-07
9.56E-06
4.42E-06
5%
4%
63%
29 %
OAVIS-8 ESSE
6.6E-05
.1.725-06
4.16E-06
4 95E-C6
5.52E-05
3%
8%
8%
84 %
DIABLO CANYON 1&2
8 SE-05
1.63E-06
1.01E-05
3 98E-05
3 65E-05
2%
11 %
45%
41%
i
FARLEY 1&2
1.2E-04
4.4 7E-07
7.19E-08
3.90E-06
1.20E-04
1%
1%
3%
96 %
FORT CALHOUN 1
1.4E-05
1.44E-06
2.23E-07
3.80E-06
8.13E-06
11%
2%
28%
60 %
GINNA
8.7E-05
3.71E-05
2.67E-06
1.27E-05
3.50E-05
42%
3%
15 %
40%
H.S. ROBINSON 2
3 2E 04
6.37E-06
4.19E-05
3.20E-05
2.40E-04
2%
13%
10%
75%
HADOAM NECK
1.8E-04
1.16E-05
1.21E-06
9.70E-05
7.01E-05
6%
1%
54 %
39 %
INDIAN POSIT 2
3.1E-05
1.94E-06
5.615-08
2.82EM
2.65E-05
6%
1%
9%
85%
INotAN POINT 3
4.4E-05
2.44E-06
3.12E-07
1.07E-05
3.05E-05
6%
1%
24 %
89%
,
KEWAUNEE
6.6E-05
5.28E-08
1.48E-08
3.22E-05
2.88E-05
8%
1%
49%
43%
>
MAINE YANKEE
7.4E-05
1.21E-06
5.79E-06
3.54E-05
3.18E-05
2%
.8%
,
48%
42%
MILLSTONE 2
3.4E-05
7.66E-07
3.22E-06
1.11E-05
1.91E-05
2%
9%
32%
56 %
OCONEE 1,2.&3
2.3E-05
4.60E-10
2.SIE-07
1.71E-05
5.61E-06
0%
1%
74 %
24%
PALISADES
5.1E-05
2.89E-06
1.67E-06
7.66E-06
2.35E-05
6%
-33%
15 %
48%
PALO VERDE 1.2.&3
9.0E-05
3.20E-06
9.41E-06
1.21E-06
6.53E-05
4%
10%
13%
-
73%
POINT BEACH 1&2
1.0E-04
8.32E-08
3.24E 08
1.81E-06
7.97E-06
8%
1%
17%
77%
,
PRAIRIE 1SL AN01&2
4.9E-05
2.19E 05
4.15E-07
1.11E-05
1.56E 05
44%
1%
22 %
31 %
,
i
'
IPE-CFF.T8L
Sentamher10 1996
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_ _ _ ._ __
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_ . _ _ _ _ _ - . . _ _ _ _ _ . _ . _ .
. . _ . . _ _ . _
i
l
,
1
!-
Pre-Decisional
'
i
Semiannual P1 ant Performance Assessment
i
St. Lucie 1 and 2
i
-
Current SALP Assessment Period: 1/7/96 through 6/97
l
Last SALP Rating
Previous SALP Rating
i
1/2/94 - 1/6/96
5/3/92 - 1/1/94
,
Operations
2
1
Maintenance
2-
1
.
Engineering
1
1
Plant Support
1
1
4
l
I.
Performance Overview
'
Since July 1995, there have been a series of events that led to
,
l
questioning the plant's overall performance. These have included:
i
A Unit 1 turbine trip due to procedural weaknesses,
u
poor operator performance, and weak supervisory
'
oversight.
]
l
The' attempt to restage an RCP seal using inadequate and
inappropriate procedural guidance. The evolution was' compounded
4
i
by failing to follow aspects of the guidance that did exist, which
i
led to the failure of the second and third stage seals.
i
A main steam isolation signal due to an operator failing to block
F
the MSIS signal during a cooldown when an annunciator. indicated
i
that the block was enabled. This failure occurred despite the
fact that the operator's attention was directed to the annunciator
!
.
j'
on at least two different occasions,
i
Both pressurizer power operated relief valves being found
inoperable due to incorrect assembly during a refueling outage.
l
The conditions had existed for approximately 10 months (SL3,CP).
.
[
An loss of RCS inventory (4000 gallons) due to a shutdown cooling
i
relief valve which lifted and then failed to resent due to
'
incorrect setpoint margins (a generic problem involving several
l.
valves). The licensee had sufficient evidence that this generic
condition existed, but had failed to act promptly to evaluate the
conditions (SL4).
l
The spraydown of containment due to an inadequate procedure and
oparator error coupled with an existing operator-work-around.
'
The significant operator inattentiveness which resulted in the
overdilution event on January 22, 1996, highlighted the recent
j
large number of personnel errors and lack of command and control
in the control room.
I
These and several other recent deficiencies involving weak procedures, a
l
.
!
.-
. . - ,
,
. . -
,
---
.
_
_
_ _ _ _ _ _
_._ __.
_ _ _ _ _ _ . _ _ _ _ _ _ _ _ _ _ _ _ . _ _ _ _
.
~
general. lack of procedural compliance, equipment failures, and personnel
errors clearly. indicated that the plant's past high level of performance
had declined. An NRC root cause effort determined that, in addition to
,
procedural adherence / adequacy weaknesses, the licensee suffered from
.
weaknesses in both interfaces across o ganizational lines and corrective
.
{
actions.
II.
Functional Area Assessment - Operations
!
A.
Assessment
i
.
A SALP board convened on January 18, 1996. The board coricluded
a
!
that the licensee's performance in the areas of Operations had
i
declined from an excellent level of performance to good. The
.
,
decline in Operations' performance particularly occurred in the
-
F
final six months of the assessment period. The licensee undertook
<
a number of efforts to reverse declinit;g performance following the
j
j
onset of the operational events descreed above. Verbatim
procedural compliance was established as the norm for the site,
which resulted in the need for literally hundreds of procedural
'!
-
changes and around-the-clock on-site review committee meetings.
An increased emphasis on the initiation of corrective action
documentation resulted in an increase in the number of documents
initiated, but has also resulted in increases in backlogs.
B.
Basis
As basis, the board noted an increase in the. number of operational
events attributable to:
Weaknesses in operator performance
1
Acceptance of long-standing equipment deficiencies
j
Management expectations were not effectively communicated to
personnel and enforced
,
. Weaknesses in procedural adequacy and adherence
Implementation and adequacy of corrective actions
C.
Future Inspections
Increase staffing at St Lucie to N + 1 and focus greater
inspection effort in the areas of: routine operator performance -
professionalism in CR; procedural compliance and enhancements;
operator problem identification and corrective action; management
communication of expectations; interdepartmental interface;
'
resolving impact of operator work arounds; and operation
contribution-to adequacy of safety evaluations.
i
i
--
'
.
-
-
. _
. _ .
. _ . _ . _ _ _ _ . _ . - . _ _ _
_ _ _ . _ ._ ..
._.. _ __ _ . _ _ _ __ _.__.._
_.
i
'
i
!
?
)
L
III.
Functional Area Assessment - Maintenance
A.
Assessment'
,
!
Adverse trends were noted in maintenanc' and the board concluded
e
i-
that the licensee's performance in the area of Maintenance had
declined from an excellent level. of performance to good. The EDG
i
problems indicate a weakness in EDG Maintenance. The number of
!'
problems related to personnel errors and procedure problems may
j.
. indicate possibly attitude problems. Also, Safety Equipment
performance has failed to meet the industry average on all safety
+
system. Maintenance performance has declined.
'
B.
Basis
,
i
1.
Adverse trends were noted on the Site Integration Matrix.
i
!
Recent Equipment Failures:
q
01/23/96 - Elect. arc during maint. caused loss of 25% of control
J
room annunciators
i
i
12/20/95 - Pitting of reactor flange o' ring groove
!
.1/06/95 - Failure of EDG 2A relay sockets
j
l
10/05/95 - EDG 1B fuel oil leak at threaded connection
4
09/20/95 - - EDG 1A/1B governor control problems resulted in load
L
oscillations
u
l
Recent Personnel Errors-
'
4
j.
01/01/96
ICI wiring error during Rx head installation
j
08/31/95 - Damaged cy. head on IB EDG due to loose-lash
!
adjustment
j.
08/09/95 - Inoperable Unit 1 PORV due to maintenance
error / testing inadequacy
4
)
!-
Recent Procedure Problems:
l
12/09/95 - 2A2 RCP seal destaged due to inadequate or weak
procedure-
-
09/15/95 - Failure to have clearance for work on cond. water box
,
08/25/95 - Failure to sign off procedure steps as work completed
j.
2.
Safety Equipment Performance (Availability %) has been below
-
industry a average.
,
i
Actual
Industry Averages
i
Unit 1.
Unit 2
,
1
99.5
97.0
99.6 - 99.1
!
96.0
98.6
99.7 - 99.2
l
95.6
99.8
99.1 - 98.6
,
'
l
- 2C AFW steam admission valve did not open and mechanical
'
j
trip linkage problem
- HPIC 2B Breaker Failure
t
i
e
"
.
-
-
-
. ___ .
-_.__ _ _ _ _ _ _ _ _ _ _ . _ _ .
_.
_ _ _,_ ___._._
f
j
\\
.
3.
Numerous equipment failures have Caused power reductions
'!
4'
-
during the last 6 months.
!
l
- 10/95 Unit 1 Heater Level Control
- 10/95 Unit 1 IB Heater Drain Pump
- 11/95 Unit 1 FW Reg. Viv. Contro'
,
- 11/95 Unit 1 1A Main Transformer
j
- 01/96 Unit 1 FW Viv. LSV-24-A2
- 08/95 Unit 2 Heater Drain Valve
3[
- 08/95 Unit 2 Heater Drain Pump
3
- 08/95 Unit 2 Circ. Water Valve-
1
- 08/95 Unit 2 Htr. Drn. Pop. PCM
' 01/96 Unit 2 Hydrogen Sys. Prob.
j
-
- 01/96 Unit 2 MFW Pump
'
.
!
C.
Future Inspections: Assist the Resident inspector with the
j-
routine Resident Maintenance / Surveillance Inspections program.
i
Conduct Regional Initiative inspection, focus on outage activities
l
BOP and EDG maintenance, procedure adequacy and safety system
i
performance.
Perform maintenance rule inspection in September
i
.!-
1996. Conduct the.ISI inspection.
I
1
l
IV.
Functional Area Assessment - Engineering
A.
Assessment
,
Engineering performance at St. Lucie remained superior during the
i
SALP period ending January 6, 1996, and has not changed since
then.
Continue with core inspections in the engineering area.
i
B.
Basis
The basis for the above assessment was the SALP report issued on
February 8,1996, and a continued low number of engineering
issues. A recent inspection.identifled weakness in engineering-
safety evaluations.
C.
Future Inspection
Conduct the following core inspections:
engineering core
inspection which focus on operability,10 CFR 50.59 evaluations,
engineering support to maintenance and FSAR review; employee
'
concern program due to increased number of allegations in the last
year; and corrective action plan implementation.
V.
Functional Area Assessment - Plant Support
A.
Assessment
Host of the assessment information in the past six months has been
captured in the most recent SALP report 95-99 dated February 8,
1996. There were no specific inspections of the Radiation
Protection (RP) program during the past 6 months. However,
Resident Inspectors observed RP activities throughout the
_ _ .
.
.
.. _
_ . - - - _
__ ..
.
_
.
. _ _ _ _
_
_ _ _ _ _ _ _
l
'
'
assassment period and performance was satisfactory. The RP
i
program continues to adequately maintain external and internal
radiation exposures within regulatory limits. The plant programs
]
for plant chemistry, radiochemical analysis, radiological effluent.
and environmental monitoring, and radioactive waste shipping
'
continued to be effective although some issues were identified.
,
The EP program continued to provide an adequate level of readiness
j
i
to respond to events. Overall, site security has been adequate.
i
Implementation of the fire protection program continued to be
!
satisfactory.
Potential problem exists with " Speak Out" employee
j
concerns program (ECP).
t
B.
Basis
Near the end of the assessment period the licenseer missed
i
The surveillance was missed
4
in October and a NCV 95-18-06 was identified. However the
licensee's corrective actions were not sufficient to prevent
,
{.
a recurrence in November and a VIO 95-21-03 was issued.
'
'
Unit I was suspected of having some leaking fuel that was
not evident prior to this assessment period.
.
No Exercise Weaknesses were identified in the Feb 1996 Full
Participation Exercise.
Site Management expressed concern
that two practice drills were necessary before the NRC
j.
graded exercise to assure no NRC findings.
4
i.
The licensee reported a training and qualification error in
l
which security personnel were qualified using only half the
required rounds, a failure to compensate within 10 minutes
4
and problems with protectoid area barriers.
Fire protection inspections, conducted by resident
-
inspectors, identified overall good performance but-
4
.
l
weaknesses in fire fighting techniques and respirator
qualification program.
4
.
A large number of allegations have been received.
No
4
pattern to organization but some against " Speak Out" program
i
'
C.
Future Inspections
Conduct the following core inspections in the areas of:
occupational exposure to observe RP practices; security - to
review audits, corrective action, plans, management support,
review PA equipment, vital access and alarms; and employee
concerns program implementation due to large number of allegations
dealing with adequacy of employee concern program.
VI.
Attachments
A.
Inspection Schedule
B.
Power Profile (last six months)
C.
Site Integration Natrix
_-_._._ _ , . _ _ . _ . _ _ . _ _ . . _ _ . . . _ _ . _ _ _ _ . . _ _ _ _ _ _ _ _ _ _ . _ . _ . _ . . . _ . _ _ _ _ . _ . . . _ . . . . . . . _ . . _ . - . - . . - . . . _ _ _ . . . _ . _ _ . -
i
i
ST. LUCIE - INSPECTION PLAN
}
.
INSPECTION
NUMER OF
PLAMED
PROCEDURE /
TITLE / PROGRAM AREA
INSPECTORS
INSPECTION
TYPE OF INSPECTION -
i
TEMPORARY
DATES
COMENTS
INSTRUCTION
j
INITIAL OPERATOR EXAMINATION
1
3/11/96
PREPARATION
l
INITIAL OPERATOR EXAMINATON
2
3/25/96
ADMINISTRATION OF EXAM
j
I
71001
LICENSED OPERATOR REQUALIFICATION
1
3/25/96
REQUALIFICATION PROGRAM
PROGRAM EVALUATION
INSPECTION
61726
MAINTENANCE OBSERVATIONS
1
3/25/96
CORE INSPECTION
l
62703
SURVEILLANCE OBSERVATIONS
,
81700
PHYSICAL SECURITY PROGRAM FOR
1
4/1/96
CORE - SAFEGUARDS
POWER REACTORS
.
4XXXX
EMPLOYEE CONCERNS PROGRAM
2
4/29/96
REGIONAL INITIATIVE
i
62700
MAINTENANCE IMPLEMENTATION
2
5/6/96
REGIONAL INITIATIVE -
MAINTENANCE - OUTAGE
i
,
i
'
ACTIVITIES; PROCEDURES
37550
ENGINEERING
1
5/13/96
CORE 50.59 FOCUS
j
73753
INSERVICE INSPECTION
1
5/13/96
CORE - MINTENANCE
i
40500
EFFECTIVENESS OF LICENSEE
3
6/24/96
INSPECT STATUS OF
t
CONTROLS IN IDENTIFYING
PERFORMANCE IMPROVEMENT
RESOLVING,*AND PREVENTING
PROGRAM;
e
!
92720
PROBLEMS; CORRECTIVE ACTION
DILUTION EVENT FOLLOW-UP
l
REVIEW
61726
MAINTENANCE OBSERVATION
1
6/24/96
-
CORE MAINTENANCE AND
62703
SURVEILLANCE OBSERVATION
SURVEILLANCE _
i
37500
ENGINEERING
1
7/22/96
FSAR CORRECTIVE ACTIONS
i
,
!
!
'
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-
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l
l
l
llllI!
.
_ .
__
. . _ _
ST. LUCIE
UNIT
1
Operational
Period
Sep te rn b er
1995
th rough
March
15,
1996
L OO -
-
-
On November 19,1995
80-
Z
End of outage following
a manual reactor trip was
Hurricane E in
initialed to perform MFRV
maintenance.
2
60 -
H
Zy
40 -
On February 24,1996,
.
Z
a manual trip was initiated
p1
cL
wiiile going to a TS required
20-
shuldown
0 ~rrrrri v i t
i i i
i i rr r i i i i
iiiiiiiirrrrriiiiiiiiiiiiiisiii
iiiiiii
S
O
N
D
J
F
M
PERIOD
OF OPERATIdN
Graph
does not include power reductions
for routine
re p airs , waterbox cleaning,
or required repairs.
-
.
- - -
-
-
-
-
- -
.
,-
- ---
-
-
-
. . .
.
, _ -
_ _
,T
LUCIE
I
Operational Period August
1,
-
Tlirough September
12,
1995
1
2
3
4:
.
-
100 -:
-
--
.I
..
(1 0 -
x
1.
On October 26, 1994, the unit tripped from 100 percent power due to a
M
loss of electrical load. This was the result of arc-over la a potential
"5**' '" *** 5"'**hd d"' ** 5 6=d P-
Th' ""' ***"
- at'"d * =a' t r *i 'ai *=t'9' "h'ch **d 6"a 5ch'd=d 6a '
O
6 0 --
days later. The unit was returned to service on flovember 29.
CL
2.
On February 21, 1995, the unit was removed from service for the
b
replacement of pressurizer code safety valves which had been leaking by
.the seat since shortly after startup in Movember, 1994. The unit was
Z
returned to service on March 8.
m
.-1 0 -
U
On July 8, 1995, the unit tripped during turbine valve survelliance
3.
testing. It returned to power on July 12.
M
On August I, 1995, the unit was shutdown as a result of Hurricane Erin.
4.
s
4
Due to a se.les of e
nt problems and personnel performance issues,
.y n
the unit is presenti
utdown.
%U-
0
nniuu,nn u nni,n uo........-,,,
,,,,,,,,,,,,, .n n ninnn,n o,u,u u,uin,n o u,1,o,ou,n,,no,,o,o, nooo,n un,nn,n,oona
-
A
S
O
N
D
J
F
M
A
M
J
J
A
S
l
.
,
PERIOD OF OPERATION
Graph does not include power reductions
for routine repaifs, wat erbox cle;aning,
or required repairs.
.
,
.
.
.-
-
ST. LUCIE
UNIT
2
O pera ti o n al
Period
S e p te rn b er
1995
through
March
27,
1. 9 9 6
100
=
=
,
On October 9,1995, the
,
80-
unit was shut down for
a
m
.'
$
scheduled refueling outage.
,
k
60-
s
$
On January 5,1996, the
40-
'
d
unit was manually tripped
]
E
due to high generator
{
20-
-
hydrogen gas temperature. '
,
O
vivitivtrriviiviivivitivtrr*T-
iiiiiiiiii
S
O
N
D
J
F
M
'
~
PERIOD
OF OPERATION
,
Graph
does
not include power reductions
for routine repairs, waterbox cleaning,
'
or . required
repairs.
.
. -
. -
.-
.
.
.
-.
.-
..
.
-
.
.
-
.
.lTIE 2
.
Operational Peritul August
1,
Through Sepleinber
12,
1995
1
2
.
100
, , _ .
,,
..
II
.
k
80 -
m
N
' = -
.
t
[
60-
,
1.
On February 21, 1995, the unit tripped as a result of low steam
p
generator water level. The condition was the result of a feedwater
Z
regulating valve closure after a steam generator water level centrol
level transmitter failed high. The transmitter was replaced and the
y
40-
. nit was returned to service on rehr arr 25.
W
2.
On August I,1995, the unit was shutdown as a result of ifurricane
M
Erin. It was restarted on August 4,1995 but.
cL
20-
1
0
imi,mi,,,mmimi,mi,mmimimmm,mmmm,mm,,,,m,,,m,m,m,,m,m,,mmmm,,,,mm,,m,,,m.m. ,.,,mm,,,,,,,,,,,,,,,,,m,,,,,,
A
S
0
N
D
J
F
M
A
-M
J
J
A
S
>
PERIOD OF OPERATION
Graph does not include power reduelions
for roittine repairs,' waterbox clearting,
.
- -
-..-....:..-i........:..
- - -
- --- -
-
- -
- -
.
.--..--.
..
-
-
. - . . _ . .
. .
_ _ .
.. -
. _ . _ _ _ < ._
._
.. . . _ . - . . _ _ - .
.
. _ _ . _.
_
__.
-
__.. _ __
..
s
SITE INTEGRATION MATRIX BY DATE
,
~
St. Lucie
I
SFA
-
sEc
APPARENT CAUSE I COMMENTS
DATE
, TYPE
, SOURCE
- ID
, PRIM
, ITEM
3/15/96
LER
IR 96-04
L
PS
Fish kilt identified in intake (great'er than 25 fish
Excessive levels of sitt in waterdue
(pending)
and greater than 100 lbs). NRC notification
to recent rough seas.
required per TS and EPP.
3/14/96
OTHER
1R 96-04
L
PS
Management change. A. Desoiza (human
(pending)
resources manager) replaced by Lynn Morgan
(from TP)
3/13/96
WEAK
IR 96-04
S
M
O
' Unplanned start of 2C AFW Pump. Pump was
Weakness in troubleshooting
(pending)
out-of-service for maintenance and
control. Operations was unaware
troubleshcoting due to the failure of 1 of 2 steam
of the efforts in progress.
!
'
admission valves to open on demand.
Troubleshooting resulted in valve openning and
-
pump starting.
,
3/12/96
OTHER
IR 96-04
S
O
M
Unit 2 standby charging pumps started / stopped
Undetermined.
(pending)
for no reason. Troubleshooting underway for
standby pumps * start controllers.
3/10/96
OTHER
1R 96-04
L
O
. Unit I downpowered to 97.5% due to hot leg
Hot leg stratification.
(pending)
stratification and flow swirl which resulted in
-
higher than actual indicated reactor power.
3/1/96
OTHER
1R 96-04
L
O
Management Changes - T. Plunkett succeeds G.
Goldberg, C. Wood replaces L Rogers as ~
manager of SCE, C. Marple replaces C. Wood
as Ops Supeivisor.
.
,
FROM: 1/1/90 TO: 3/18/96
Page 1 of 11
18-Mar-96
- - .
.
-
.-
. .
-
- . . - - -
-
.
-
-
.
m . . . . . _ . _ . _ . _ _ _ - . _
.. .. _
_ . . .
. _ . ,
-
.
_
..
. _ _ _ _ _
___
-
-i
i
!
'
I
'
SFA
DATE
TYPE
SOURCE
10
PRIM
sEc
ITEM
, APPARENT CAUSE I COMMENTS
(
t
,
2/27/96
WEAK
1R 96-04
S
M
inadvertent start of 1 A EDG occurred when l&C
Poorwork planning. Personnel
(pending)
personnelinstalling a modification in an
were not aware of the proximity of
electrical cabinet bumped the EDG's actuation
the subject relay and EDG was not
relay. No load shedding was required, nor did it
declared out-of-service and isolated
occur.
electrically prior to the
commencement of work.
I
!
2/24/96
WEAK
IR 96-04
t.
PS
O
Unit 1 containment radiation monitor found out-
Failure 10 fcitow procedure on the
(pending)
of-service due to isolation valve which was
part of HP personnel, compounded
closed for a containment entry and not returned
by failure to identify condition by
to the open position.
operators during rounds (the low
-
flow condition of the detector was
,
2/24/96
WEAK
IR 96-04
N
M
Maintenance practices for Steam Bypass and
Poor preventive maintenance and
(pending)
Control System and Feedwater Regulating
work instructions
i
valves found weak in inspection following
2/22/96 Unit 1 trip. Additional weakness found
in the acceptance criteria specified for CEDM
coil resistances.
.
2/22/96
EMERG
IR 96-04
s
O
Dropped CEA (due to SCR failure) leads to TS-
Equipment Failure
T1"W
required shutdown and declaration of NOUE.
. ,
Failure of air supply to FRV leads to operators
tripping reactor from 26%. Good operator
'
performance throughout.
!
I
2/17/96
OTHER
1R 96-01
N
M
PS
Work on 1 A ECCS suction header through-wall
Personnel Work Practices
leak revealed strong FME, but poor HP work
practices observed regarding contamination
,
control.
2/17/96
NEG
IR96-01
N
M
Freeze seal procedure lacked objective criteria
Procedural Weakness
defining when a freeze seat existed.
!
,
.
.
c o n u.1siton T o- 3118/96
Page 2 of 11
18-Mar-96
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. .
, .
.
- .-
-_
,
-
. ..
_
,
6
'
I
1
SFA
APPARENT CAUSE I COMMENTS
DATE
TYPE
SOURCE
ID
PRIM
sEc
ITEM
,
1/7/96
N
O
SALP CYCLE 12 BEGINS
t15/96
NEG
IR 95-22
N
O
Several procedural deficiencies and
inadequate Procedure Review and
calculational errors identified in reload physics
Execution
test procedure.
!
I/5/96
IR 95-22 -
N
O
PS
Several deficiencies in prodecure change
Failure to Properly implement
NCV 95-22-
process implementation identified. Expired or
Procedures
01
cancelled TCs found in control rooms and hol
shutdown panel.
i
t15/96
WEAK
IR 95-22
L
O
M
U2 manual RX trip on high generator H2 temp
Temp Control Valve Failure
'
due to failure of temp control valve. Operator
I
awareness of RPS status post-trip poor.
inspection of post-trip review (for current trip as
,
well as past trips) indicated weaknesses in the
rigor of post-trip reviews
r
12/27/95
NEG
IR 95-22
S
O
E
FRG meeting suffered / items deferred due to
Lack of Attendance at FRG
lack of OPS /Eng*g attendance at meeting.
Majorissues at meeting affected OPS /Eng'g.
-
12/20/95
OTHER
IR 95-22
S
M
RX vessel flange inner O-ring groove pitting
Pitting - Localized Corrosion
resulted in cooldown and head removal for
repair.-
-
.
'
12/9/95
OTHER
1R 95-22
L
M
2A2 RCP seal pkg lower seat destaged da i1
Filling RCS Before Coupling RCP
reverse pressure a:ross seat.
,
r
FROM: 1/1/90 TO: 3/18/96
Page 4 of 11
18-Mar-96
_- _
_
'
'
I
'
SFA
, ITEM
, APPARENT CAUSE / COMMENTS
DATE
TYPE
SOURCE
ID
PRIM
sEc
12/5/95
WEAK
IR 95-22
N
O
M
ESFAS cabinet doors found unlocked following
Poor Logkeeping/Atta to Detail
maintenance work - l&C error. lod entries
associated with work were not complete.
12/1/95
NEG
IR 95-21
N
O
Operators unable to effectively obtain I&C
Inadequate Operator Training
setpoints from computer after hard copies were
removed from control room.
12/1/95
NEG
IR 95-21
N
PS
Rad survey results unavailable for B hot leg
Failure to Document RAD Survey
work. Surveys performed but not documented.
12/1/95
NEG
IR 95-21
N
O
Unit 2 procedures and valve deviation log used
valve Position Administrative
to cycle Unit 1 cross connect valves.
Controls
12/1/95
WEAK
1R 95-21
N
O
SDC procedure contained conflicting values for
Procedural Weakness / Inadequate
RX cavity level requirements. Procedure had
Review
been approved since emphasis on accuracy
stressed.
12/1/95
WEAK
IR 95-21
N
O
CCW sample valve showed dualindication
FTF Procedure
without corrective action documentation initiated.
12/1/95
WEAK
IR 95-21
N
O
Clearance in place to isola *e N2 from CST to
Poor Corrective Actions
facilitate pressure switch rr placement for nine
days without work order bring written.
-
18-Mar-96
FROM: 1/1/90 TO: 3/18/96
Page 5 of 11
- - - .
-
.
.
. . .
.
._. ~....- .-
.
.
.
.
_
.
'
'
SFA
APPARENT CAUSE I COMMENTS
DATE
TYPE
SOURCE
ID
PRIM
sEc
ITEM-
,
12!1/95
NEG
IR 95-21
N
O
Recurrent non-valid alarms when starting fire
FTF Procedure
pumps were not documented as operator
workarounds. Voltage dips associated with such
starts were contributors to a trip previously.
t 2/1/95
WEAK
1R 95-21
N
O
Followup to previous inspection findings
Corrective Actions
indicated a weakness in followthrough in
addressing deficiencies.
!
t 2/1/95
NEG
IR 95-21
N
O
SDC Procedure required natural circ-relatect
Procedural Inadequacy
surveillance prior to estabhshing RCS pressure
boundary Natural circ not possible without
pressurization.
11/27/95
IR 95-21 -
L
O
Missed RCS Boron sample surveillance -
Personnel Error
,
VIO 95-21-03
Repeat from IR 95-18.
.
11/21/95
IR 95-21 -
L
O
Failure to maintain Penetration Log.
FTF Procedure
NCV 95-21-
04
i
11/21/95
Oli:ER
IR 95-21
s
O
Light socket failure during lamp replacement
Equipment Failure
,
results in loss cooling to 1 A Main Transformer.
Unit downpower to ~60%.
11/20/95
IR 95-21 -
N
O
Valve discovered Closed vice Locked Closed as
FTF Procedure
VIO 95-21-01
specified on Equipment clearance Order.
-
FROM: 1/1/90 TO: 3/18/96
Page 6 of 11
18-Mar-96
_
.
.
.
.
. . .
.
. . .
-
-
!
SFA
DATE-
TYPE
SOURCE
ID
PRIM
sEC
ITEM
APPARENT CAUSE I COMMENTS
,
11/16/95
OTHER
IR 95-21
S
O
M
Unit 1 manually tripped when 18 MFRV locked
Long-Standing Equipment Problem
in 50% position. Root cause - degraded power
supply, compounded by voltage dip on starting
both station fire pumps.
11/11/95'
IR 95-21 -
N
O
Tech. Spec. equipmer.1 not specified for IV on
FTF Procedure
VIO 95-21-02
Equipment Clearance Order.
11/6/95
OTHER
1R 95-21
s
M
Fa: lure of EDG 2A relay sockets Potential
Equipment Failure
common mode failure
11/1/95
1R 95-18 -
S
M
ICI wiring error during RX head installation last
Personnel Error
NCV 95-18-
RFO.
,
05
.
10/19/95
IR 95-18 -
3
O
Missed shift CEA position indication surveillance. Personnel Error
l
NCV 95-18-
06
.
10/18/95
IR 95-18 -
L
O
Missed RCS Boron sample surveillance.
Personnel Error
'
NCV 95-18-
07
,
!
.
10/17/95
WEAK
IR 95-18
S
O
Lack of attention to task resulted in overfalling .
Personnel Error
RCS lower cavity during flood up.
L
,
,
FROM: 1/1/90 TO: 3/18/96
Page 7 of 11
18-Mar-96
- - -
- - .
.
.
. - - .
.
_ . .
-. .
. .--
-
..
_.
.
- - . - . . -
.-
.
.
-
I
SFA
DATE
TYPE
SOURCE
ID
PRIM
sEc
ITEM
APPARENT CAUSE f COMMENTS
,
10/12/95
IR 95-18 -
S
E
inserting CIAS signal during safeguards test
Design Error
VIO 95-18-04
shifted EDG 2A to isochronous mode while EDG
paralleled with offsite power.
10/9/95
LER
LER 95-S02
L
PS
Potential route for unauthorized access to
Personnel Error
protected area CWwater piping.
10/7/95
IR 95-18 -
N
O
Did not enter bypass key position in deviation
Failure to Follow Procedures
VIO 95-18-01
log
10/5/95
OTHER
1R 95-18
S
M
DG 18 developed FO leak at threaded
Equipment Failure
connection during surveillance run.
9/30/95
IR 95-18 -
N
O
Did not enter bypass key position in deviation
Failure to Follow Procedures
VIO 95-18-02
log.
9/28/95
OTHER
IR 95-18
s
E
Leaking PZR SVs extended forced outage -
Equipment. Failure
problems with lailpipe alignment.
9/20/95
OTHER
1R 95-18
S
M
EDG 1 A/1B govemor control problems resulted
Equipment Failure
in load oscillations.
.
9/15/95
IR 95-18 -
S
O
M
MaintOps did not provide clearance for work on
Failure to Follow Procedures
VIO 95-18-03
condenserwaterbox cover. When cover pulled
closed, severed worker's finger.
FROM: 1/1/90 TO: 3/18/96
Page 8 of 11
18-Mar-96
5
.
-
-
-
- -
-
-
-
-
-
-
--
- - - ---
-
-
- --.
!
'
SFA
APPARENT CAUSE / COMMENTS
DATE
TYPE
SOURCE
ID
PRIM
sEc
ITEM
9/14/95
WEAK
LER U1/U2
L
pS
Security failed to take correct compensatory
Failure to Follow Procedure
95-S01
action on computer failure
9/10/95
VEAK
IR 95-18
S
O
SG blowdown sent to incorrect system on RAB
Failure to Use Correct Procedrue
roof. Operator used wrong procedure. When
identified did not back out of procedine correctly.
9/9/95
WEAK
IR 95-15
S
M
Leak on SV 1201 flange extended outage,
Weakness in Work Screening and
identified one month earlier but not worked.
Planning
9/7/95
WEAK
IR 95-15
L
O
Unit 2 Main Generator overpressurized while
Personnel Error / Inoperable
filling with H2. Inattention by operators.
Equipment /OWA
'
9/2/95
IR 95-15 -
N
O
Weaknesses identified in logs relating to
Personnel Enor
VIO 95-15-03
abnormal equipment conditions and out of
service equipment not logged (mulitple
' examples).
"
8/31/95
OTHER
1R 95-15
S
M
Damaged cylinder and head on iB EDG due to
Personnel Error
loose lash adjustment.
8/30/95
WEAK
IR 95-15
N
PS
Containment closure walkdowns by
Management and QC Weaknesses
>
management were inadequate and depended
heavity on OC involvement to identify
.
deficiencies.
.
.
!
FROM: 1/1/90 TO: 3/18/96
Page 9 of 11
18-Mar-96
- _ _ _ _ _ - _ _ _ _
.
. . . _ _ - -
-_
_
-__
- _ - _ - _ _ - - - _ - _ _ - - _ _ _ - - _ - _ _ __-_ _ _
- - _ . _ _ _ _ _ _ _ - - _ - _ _ _ - _ _ _ _ - _ _ _ _ _ _ - - _ _ . - - _ - _ _ _ _ _ - - _
I
SFA
DATE
TYPE
SOURCE
ID
PRIM
sEc
ITEM
APPARENT CAUSE / COMMENTS
B/30/95
WEAK
IR 95-15
N
M
Mainte..ance personnel not using procedures for
Supervisory Oversight and Worker
work in progress.
Altitude
8/29/95
IR 95-15 -
N
M
Maintenance joumeyman not signing off
Procedure Use
VIO 95-15-06
procedure steps as work completed (previously
identified as a weakness in May 1995).
8/29/95
IR 95-15 -
L
O
Started 1B LPSI pump with suction valve
Personnel Error
VIO 95-15-04
closed. (No damage 1o pump)
8/23/95
WEAK
IR 95-15
S
M
2A HDP trip due to relay failure. Eight HDP trips
Equipment Failure / inadequate
in past year. Engineering solution available but
Corrective Action
not implemented.
.
8/22/95
IR 95-15
g
PS
QA failed to document a deficiency on
Personnel Error
containment spray valve surveillance identified
in an audit
8/19/95
WEAK
IR 95-15
s
O
Overfill of PWT. Spilled approx.10K gellons on
Operator Error / Operator
ground inside RCA. Operator work around on
Workaround
level control system and inattention to filling
i
'
process by operator caused error.
8/18/95
WEAK
IR 95-15
N
M
Procedural weakness involving supervisory
Procedural Weakness
oversight and joumeyman qualification.
.
FROM: 1/1/90 TO: 3/18/96
Page 10 of 11
18-Mar-96
,
.
.-
..
SFA
APPARENT CAUSE / COMMENTS
DATE
TYPE
SOURCE
ID
PRIM
sEc
ITEM
8/97/95
LER U195-
3
O
Spraydown of Unit 1 containment. STAR
ProceduralInadequacy and
007 - VIO 95-
process did not assign accountability for
Weakness / Operator-Work-Around
15
corrective action. Valve surveillance prelube
!
not documented on STAR.
j
j
B/9/95
IR 95-16 -
L
M
inoperable Unit 1 PORVs due to maintenance
Maintenance / Testing Errors
LER U195-
error / testing inadequacies. (Valves assembled
'
005 - EA 95-
incorrectly) (Used acoustic data only)
180
t
6/6/95
LER U195-
S
E
Lifting of Unit 1 SDC thermal relief due to
Corrective Action / Procedural
006 - VIO 95-
procedural revision from presious corrective
Weakness
!
20-01
action. Inoperable equipment not logged.
l
8/2/95
LER U195-
t
O
1 A2 RCP seal failure due to " restaging" at high
Procedural Weakness / Failure to
004 - VIO 95-
temperature.
Follow Procedures
15-02
8/2/95
LER U195-
3
O
Operator failed to block MSIS actuation dunng
Operator Error _
04 - VIO 95-
cooldown.
15-01
.
SALP Functional Areas:
ID Code:
E
ENGINEERING
L
UCENSEE
M
MABITENANCE
N
NRC
O
OPERA 110NS
S.
SELF-REVEALED
PS
PLANT SUPPORT
sA
SAFETY ASSESSMENT & QV
!
18-Mar-96
conu- ission TO: 3/18/96
Page 11 of 11
.
. -
- .
-
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-
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PI EVENTS FOR 95-1
j
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02/16/95
LERs 33595001
50.728: 28400
PWR HIST: POWER OPERATIONS AT 1005
,
DESC
- WNILE RESTORING A SAFETT BUS TO A MORMAL LINEUP FOLLOWING RELAT REPLACEMENT, THE BUS WAS
l
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LERs 33595003
50.72#: 29039
PWR HIST: POWER OPERATIONS AT 1005
~
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Os/09/95 . LERs 33595005
50.72fs 29175
PWR HIST: COWITION EXISTED IN ALL MODES UP TC 100Y. POWER SINCE 1994
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,
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os/10/95
LERs 33595006 50.72#:
'
PWR HIST EVUT CCCURRED IN COLD SHUTDOWN
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GROUP : RESIDUAL HEAT REMOVAL ST5TEMS GROUP
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RELIEF VALVE. THE ROOT CAUSE WAS INADEOUATE DESIGN MARGIN SETWEEN THE RELIEF AND SLinEMnal SETPotNT
'
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'
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SCRAM c2/21/95
LER# 38995002 50.72#: 28416
PWR HIST POWER OPERAT!DNS AT 1001
DESC
A REACTOR TRIP RESULTED FROM A LOW STEAM GENERATOR LEVEL AFTER A STEAM GENERATOR LEVEL INSTR
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SSF
11/20/95
LERs 3a995005 50.72#: 29626
PWR HIST: CmeITION EXISTED FOR AM INDETERMINATE PERICD OF TIME
Group
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-
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i
.
ST LUCIE MAJOR ASSESSMENTS -
l
DATE
TYPE OF ASSESSMENT
l
i
JULY 1995
INPO ASSESSMENT - CATEGORY 1
AUGUST 1995
DR. CHOU ANALYSIS BY REGION II TO IDENTIFY ROOT CAUSES OF THE RECENT DECLINE IN
.
PERFORMANCE AND MULTIPLE EVENTS
,
i
The team concluded that the predominant root cause for the events observed at St Lucie
!
!
was insufficient detail and scope in site programs and procedures. This causal factor
was found to result in recent events which demonstrated deficiencies in the following
i
areas:
7
!
job skills, work practices, and decision making;
.
interface among organizations as evidenced by a lack of interface formality;.
.
organizational authority for program implementation as evidenced by instances
. .
,
!
of unclear responsibility and accountability.
l
AUGUST 1995
LICENSEE SELF-ASSESSMENT: A SPECIAL TEAM PERFORMED AN ASSESSMENT OF OPERATIONAL PROBLEMS
l
AND IDENTIFIED ROOT CAUSES: MANAGEMENT AND STAFF COMPLACENCY - POOR PERFORMANCE,
i
'
ACCEPTING LONGSTANDING EQUIPMENT PROBLEMS, AND NOT KEEPING UP WITH INDUSTRY IMPROVEMENTS.
-t
!
'
.
t
!
i
1J
I
v
i
!
- .
--
-
-
- -
-
- .
- - - .
-
-
-
.- .
.
.
.
-
.
- 4
p2M4
UNITED STATES
NUCLEAR REGULATORY COMMISSION
l
$
REGloN 11
i
o
101 MARIETTA STREET. N.W., SUITE 2900
k _
[j
7.
ATLANTA. GEORGIA 3GI234199
l
March 27, 1996
%..
Florida Power and Light Company
ATTN: Mr. T. F. Plunkett
'
President - Nuclear Division
P. O. Box 14000
'
Juno Beach, FL 33408-0420
.
SUBJECT:
PLANT PERFORMANCE REVIEW (PPR) - ST. LUCIE 1 AND 2
Dear Mr. Plunkett:
On February 28, 1996, the regional staff completed the semiannual Plant
Performance Review (PPR) of St. Lucie Unit 1 and Unit 2.
The staff conducts
these reviews for all operating nuclear power plants to develop an integrated
understanding of safety performance. The results are used by regional
,
management to facilitate planning and allocation of inspection resources. The
PPR for St. Lucie involved the participation of all technical divisions in
evaluating inspection results and safety performance information for the
period September 1995 through February 1996.
PPRs provide regional management
with a current summary of licensee performance and serve as inputs to the NRC
Systematic Assessment of Licensee Performance (SALP) and senior management
meeting (SMM) reviews.
l
This letter advises you of otr planned inspection effort resulting from the
St. Lucie PPR review.
It is provided to minimize the resource impact on your
staff and to allow for' scheduling conflicts and personnel availability to be
i
resolved in advance of inspector arrival onsite.
The enclosure details our
inspection plan for the next six (6) months. The rationale or basis for each
inspection outside the core inspection program is provided so that you are
aware of the reasons for emphasis in these program areas.
Resident
inspections are not listed due to their ongoing and continuous nature.
During each NRC inspection planned during this period, specific attention will
be given to the verification of selected UFSAR commitments. Applicable
portion (s) of the UFSAR that relate to the inspection activities will be
reviewed and verification made that the UFSAR commitments have been properly
implemented into plant practices, procedures and/or parameters.
The goal is
to determine the accuracy of the UFSAR regarding existing plant practices and
conditions by providing specific attention to the UFSAR when performing
various reactor inspections.
Inspectors will not be judging the overall
completeness of the UFSAR; rather, the inspections will focus on identifying
differences between the UFSAR description and the plant.
,
.
A
9705190225 970512
BINDER 96-485
. . . .
.
. .
. .
.
.
.
-
5
,
2
i
.
We will inform you of any changes to the inspection plan.
If you have any
l
questions, please contact me at 404-331-5509.
Sincerely,
1
i
-
-
!
erry
. La dis, Chief
React r Projects Branch 3
i
"
Division of Reactor Projects
Docket Nos. 50-335, 50-389
Enclosure:
Inspection Plan
cc w/ encl:
.
W. H. Bohlke, Vice President
St. Lucie Nuclear Plant
P. O. Box 128
Ft. Pierce, FL 34954-0128
H. N. Paduano, Manager
Licensing and Special Programs
Florida Power and Light Company
P. O. Box 14000
Juno Beach, FL 33408-0420
J. Scarola
Plant General Manager
St. Lucie Nuclear Plant
P. O. Box 128
Ft. Pierce, FL 34954-0128
E. Weinkam
Plant Licensing Manager
St. Lucie Nuclear Plant
P. O. Box 128
Ft. Pierce, FL 34954-0218
. J. R. Newman, Esq.
1800 M Street, NW
Washington, D. C.
20036
John T. Butler, Esq.
Steel, Hector and Davis
4000 Southeast Financial Center
Miami, FL 33131-2398
cc:
Continued see page 3
.-_
__
. . _ . .
. _ _ _ _ - . . _ _ . _ . _ . - . _ _ _
. _ _
. _ . _ . .
__
. .. _ .-._ ___ _
-.
i
~
FP&L-'
3
cc: Continued
'
Bill Passetti
Office of Radiation Control
Department of Health and
,-
. Rehabilitative Services
d
j
1317 Winewood Boulevard
,
Tallahassee, FL 32399-0700
Jack Shreve-
.,
Public Counsel
-
,
Office of the Public Counsel
-
._c/o.The Florida Legislature
111 West Madison Avenue, Room 812
Tallahassee, FL 32399-1400-
a
' Joe Myers, Director
.
Division of. Emergency Preparedness
'
Department of Community Affairs
2740 Centerview Drive
Tallahassee, FL 32399-2100
Thomas R. L. Kindred
County Administrator
St. Lucie County
2300 Virginia Avenue
,
Ft. Pierce, FL 34982
!
Charles B. Brinkman
' Washington Nuclear Operations
ABB Combustion Engineering, Inc.
12300.Twinbrook-Parkway, Suite 3300
.
]
Rockville, MD 20852
i
.
'I
i
- -
. _ _ . . . . _ - . _ . . _ _ _ . _ _ . _ . . _ . . . . . _ . . _ _ _ _ _ _ . .
_ _ . _ . . . . . _ . _ . . . . _ .
. _ . _ . _ . _ . . _
. _ . _ .
____
'n
l
!
b
4
i
.
ST. LUCIE - INSPECTION PLAN
!
!
-
INSPECTION
NUMER OF
PLAMED
PROCEDURE /
TITLE / PROGRAM AREA
INSPECTORS
INSPECTION
TYPE OF INSPECTION -
l
TEMPORARY
DATES
COMENTS
INSTRUCTION
'
!
INITIAL OPERATOR EXAMINATION
1
3/11/96
PREPARATION
f
r
INITIAL CPERATOR EXAMINATON
2
3/25/96
ADMINISTRATION OF EXAM
i
!
71001
LICENSED OPERATOR REQUALIFICATION
1
3/25/96
REQUALIFICATION PROGRAM
PROGRAM EVALUATION
INSPECTION
J
61726
MAINTENANCE OBSERVATIONS
1
3/25/96
CORE INSPECTION
j
i
62703
SURVEILLANCE OBSERVATIONS
e
81700
PHYSICAL SECURITY PROGRAM FOR
I
4/1/96
CORE - SAFEGUARDS
{
POWER REACTORS
'
I
l
4XXXX
EMPLOYEE CONCERNS PROGRAM
2
4/29/96
REGIONAL INITIATIVE
!
c
62700
MAINTENANCE IMPLEMENTATION
2
5/6/96
REGIONAL INITIATIVE -
!
MAINTENANCE - OUTAGE
!
!
ACTIVITIES; PROCEDURES
l
37550
ENGINEERING
1
5/13/96
CORE 50.59 FOCUS
73753
INSERVICE INSPECTION
1
5/13/96
CORE - MAINTENANCE
l
40500
EFFECTIVENESS OF LICENSEE
3
6/24/96
INSPECT STATUS OF
l
CONTROLS IN IDENTIFYING
PERFORMANCE IMPROVEMENT
l
RESOLVING, AND PREVENTING
PROGRAM;
92720
PROBLEMS; CORRECTIVE ACTION
DILUTION EVENT FOLLOW-UP
4
REVIEW
61726
MAINTENANCE OBSERVATION
1
6/24/96
CORE' MAINTENANCE AND
l
62703
SURVEILLANCE OBSERVATION
SURVEILLANCE
1
,
37500
ENGINEERING
1
7/22/96
FSAR CORRECTIVE ACTIONS
l
!
I
i
I
f
-
--
--- - -
-
--
--
-
---
-
---
- :
. _ _ . - . . _ . _ . _ . . . _ . . -_ . . _ _ _ . _ _ . _ . _ . _ . . - _ . _ _ . _ _ _ . . _ . . . _ . _ . . . . _ _
. - _ _ . . _ _ - _ . _ _
. _ . . _ _ . . _ _ _ _ . .
T
,
!
[
t
t
2
l
INSPECTION
NUMBER OF
PLAlelED
!
PROCEDURE /
TITLE / PROGRAM AREA
INSPECTORS
INSPECTION
TYPE OF IllSPECTI0li -
!
TEMPORARY
DATES
ColWIENTS
l
INSTRUCTI0ll
!
84750
RADI0 ACTIVE WASTE TREATMENT AND
1
8/5/96
CORE
$
EFFLUENT AND ENVIRol#IENTAL
i
MONITORING; SOLID RADI0 ACTIVE
'
86750
WASTE MANAGEMENT AND
l
TRANSPORTATION OF RADI0 ACTIVE
i
MATERIAL
i
62700
MAINTENANCE IMPLEMENTATION
2
8/19/96
I
MAINTENANCE
i
71715
LICENSED OPERATOR REQUALIFICATION
1
9/9/96
PLANT OPERATIONS - FOCUS
i
PROGRAM EVALUATION
ON CopHUID, CONTROL,
!
,
C0091UNICATION AND NORMAL
!
CR OBSERVATION
81700
PHYSICAL SECURITY PROGRAM FOR
1
9/9/96
CORE - SAFEGUARDS
l
'
POWER REACTORS
'
!
83750
DCCUPATIONAL RADIATION EXPOSURE
I
9/9/96
CORE INSPECTIoll
j
'
62706
MAINTENANCE RULE INSPECTION
5
9/16/96
EDG MAINTENANCE PROCEDURE
i
PROCEDURE
ADEQUACY ale) SAFETY
!
'
SYSTEM PERF0lWWICE
40500
EFFECTIVENESS OF LICENSEE
3
10/7/96
INSPECT STATUS OF
,
CONTROLS IN (DENTIFYING,
PERFORMANCE INPROVEMENT
!
RESOLVING, AND PREVENTING
PROGRAM
i
i
PROBLEMS
71001
LICENSED OPERATOR REQUALIFICATION
2
11/18/96
REQOALIFICATION PROGRAM
i
PROGRAM EVALUATI0li
INSPECTI0ll
l
!
I
!
'
!
!
. - . .
-
. - .
.-
--
-
-
-.
-
-
-- - -.-. - -
-- )
_ _ _ . - . . . _ . .
- .
_ . _ _ . _ _
_ _ _ . . _ _ _ _ _ _ _ _ . . _ _ . _ _ _ . _
_m._
_ - _ .
m.-
- . .
UNITED STATES
+#p H: .
NUCLEAR REGULATORY COMMISSION
REGION 11
3
I
$
o
101 MARIETTA STREET. N.W., SUITE 2300
E
j
ATLANTA, GEORGIA 30350100
,
%
March 27, 1996
.
Florida Power and Light Company
ATTN: Mr. T. F. Plunkett
President - Nuclear Division
'
P. O. Box 14000
l
Juno Beach, FL. 33408-0420
!
i
.
SUBJECT:
PLANT PERFORMANCE REVIEW (PPR) - TURKEY POINT 3 and 4
Dear Mr. Plunkett:
,
On February 28, 1996, the regional staff completed the semiannual Plant
Performance Review (PPR) of Turkey Point 3 and 4.
The staff conducts these
,
i
reviews for all operating nuclear power plants to develop an integrated
i
understanding of safety performance. The results are used by regional
management to facilitate planning and allocation of inspection resources. The
PPR for Turkey Point 3 and 4 involved the participation of all technical
,
!
divisions in evaluating inspection results and safety performance information
for the period September 1995 through February 1996.
PPRs provide regional
.,
..
management with a current summary of licensee performance and serve as inputs
to the NRC Systematic Assessment of Licensee' Performance (SALP) and senior
management meeting (SMM) reviews.
This letter advises you of our planned inspection effort resulting from the
e
!
Turkey Point 3 and 4 review.
It is provided to minimize the resource impact
!
on your staff and to allow for scheduling conflicts and personnel availability
i
to be resolved in advance of inspector arrival onsite.
The enclosure details
i'
our inspection plan for the next six (6) months. The rationale or basis for.
I
each inspection outside the core inspection program is provided so that you
.
are aware of the reasons for emphasis in these program areas.
Resident
]
a
inspections are not listed due to their ongoing and continuous nature.
During each NRC inspection planned during this period, specific attention will
be given to the verification of selected UFSAR commitments. Applicable
portion (s) of the UFSAR that relate to the inspection activities will be
reviewed and verification made that the UFSAR commitments have been properly.
implemented 'into plant practices, procedures and/or parameters. ' The goal is
'
to determine the accuracy of the UFSAR regarding existing plant practices and
conditions by providing specific attention to the UFSAR when performing
,
'
various reactor inspections.
Inspectors will not be judging the overall
completeness of the UFSAR; rather, the inspections will focus on identifying
. differences between the UFSAR description and the plant.
4
.
QF
D
.
_,
,,
-
, , , - , , .
,
-_
.. -
,-
- , , .-
.
.
.
.
- - _ _
- _.
_.
~ _ . .
__. .. .
ase
2
We will inform you of any changes to the inspection plan.
If you have any
questions, please contact Kerry Landis at 404-331-5509.
I
'
Sincerely,
,
D
-
erry . Landis, Chief
React
Projects Branch 3
Division of Reactor Projects
'
Docket No. 50-250 and 251
License Nos. DPR-31 and DPR 41
i-
Enclosure:
Inspection Plan
cc w/ encl:
H. N. Paduano, Manager
-
,
Licensing & Special Programs
'
Florida Power and Light Company
,
P. O. Box 14000
Juno Beach, FL 33408-0420
D. E. Jernigan
Plant General Manager
Turkey Point Nuclear Plant
P. O. Box 029100
Miami, FL 33102
R. J. Hovey
Site Vice President
Turkey Point Nuclear Plant
P. O. Box 029100
Miami, FL 33102
T. V. Abbatiello
Site Quality Manager
Turkey Point Nuclear Plant
P. O. Box 029100
Miami, FL 33102
G. E. Hollinger
Licensing Manager
Turkey Point Nuclear Plant
P. O. Box 4332
-
Miami, FL 33032-4332
cc:
Continued see page 3
-
1
.
3
cc: Continued
J. R. Newman, Esq.
1800 M Street, NW
Washington, D. C.
20036
John T. Butler, Esq.
Steel, Hector and Davis
4000 Southeast Financial Center
Miami, FL 33131-2398
Attorney General
Department of Legal Affairs
The Capitol
4
Tallahassee, FL 32304
.
Bill Passetti
Office of Radiation Control
Department of Health and
Rehabilitative Services
1317 Winewood Boulevard
Tallahassee, FL 32399-0700
i
Jack Shreve
Public Counsel
'
Office of the Public Counsel
c/o The Florida Legislature
111 West Madison Avenue, Room 812
Tallahassee, FL 32399-1400
Joaquin Avino
'
County Manager of Metropolitan
,
Dade County
l
)
111 NW lst Street, 29th Floor
,
Miami, FL 33128
,
Joe Myers, Director
,
Division of Emergency Preparedness
i
Department of Community Affairs
2740 Centerview Drive
Tallahassee, FL 32399-2100
-
_._.m._..._._..__-_
.. _ _ ._. _. _ __ _ ._. _ -- _ . _ . .. _. _ .. _ . _ . . _ _ _ _ . _ _ . _ . _ _ . -
- _. . _ _ _ .
'l
i
I
!
-
!
i
TURKEY POINT INSPECTION PLAN
i
I
INSPECTION
ORNBER OF -
PLAMED
i
PROCEDURE /
TITLE /PROGRAN AREA
INSPECTORS
INSPECTION
TYPE OF INSPECTION - ColglENTS
l
TEMPORARY
DATES
!
'
INSTRUCTION
!
I
MAINTENANCE PROGRAM
1
3/25/96
REGIONAL INITIATIVE - OUTAGE
,
IMPLEMENTATION
MAINTAINANCE ISC FOCUS
IP 4XXXX
EMPLOYEE CONCERN PROGRAM
2
4/22/96
REGIONAL INITIATIVE - EMPLOYEES CONCERN
!
PROGRAM
i
i
SURVEILLANCE OBSERVATION
1
5/6/96
CORE - CONCENTRATE ON I&C PROCEDURES
j
MAINTENANCE OBSERVATION
!
!
RADI0 ACTIVE WASTE TREATMENT, AND
1
5/13/96
CORE INSPECTION
EFFLUENT AND ENVIRONMENTAL
MONITORING
SOLID RADI0 ACTIVE WASTE
i
!
MANAGEMENT AND TRANSPORTATION OF
RADI0 ACTIVE MATERIAL
t
,
ENGINEERING
3
5/13/96
CORE INSPECTION- FOCUS ON:
1
5/20/96
- OPERABILITY AND 10 CFR 50.59
i
(2 weeks)
EVALUATIONS
!
-
- ENGINEERING SUPPORT T0
t
OPERATIONS AND MAINTENANCE
!
'
- MANAGEMENT OVERSIGHT
!
- SELF ASSESSMENT
- MODIFICATIONS TO MITIGATE
[
EFFECTS OF GRASS INTRUSION
,
- FSAR REVIEW
- REVIEW SAFET* EVALUATIONS AT
f
CORPORATE HQ
!
- EXTENT OF CONbtIION
l
!
!
.
-- . - - . . - . ~ . ~ . . .
- - . . - - - . - . . . - . - - . - - - - - . . - . . - . - - - . - .
- - . - .
- - - .
. . . . - . - . - .
.
.
!
!
'
!
!
INSPECTION
fluMBER OF
PLAfglED
i
PROCEDURE /
TITLE /PROGRAN AREA
INSPECTORS
. INSPECTION
TYPE OF IIISPECTICII - ColglENTS
!
TEMPORARY
DATES
!
-INSTRUCTICM
ACCESS AUTHORIZATION
1
5/27/96
SAFEGUARDS-ACCESS AUTHORIZATI0ft
i
t
1
5/96
COMPLETE FIRE PROTECTION PROGRAM BY
,
RESIDENT INSPECTORS
j
PILOT
ENGINEERING
3
6/3/96
SPECIAL INSPECTION ON SOFTWARE
f
MODIFICATION (HQ PILOT) INCLUDillG
t
SEQUENCER MODIFICATION
!
4
r
INITIAL OPERATOR EXAMINATION
4
6/3/96
PREPARATION
j
INITIAL OPERATOR EXAMINATION
4
6/17/96
ADMINISTRATION
i
6/24/96
j
SERVICE WATER FlSTEM OPERATIONAL
2
7/22/96
SERVICE WATER FOLLOW UP
f
PERFORNANCE INSPECTION (SWSOPI)
l
FOLLOW UP
l
PHYSICAL SECURITY PROGRAM FOR
1
7/29/96
CORE INSPECTION
l
POWER REACTORS
3 (NRR)
7/30-31/96
j
SUSTAINED CONTROL ROOM AND PLANT
1
7/29/96
INSPECTION OF OPERATOR TRAINING ON
OBSERVATION
NORMAL OPERATIONS
i
t
SURVEILLANCE OBSERVATION
1
8/19/96
CORE - CONCENTRATE ON ISC PROCEDURES
!
MAINTENANCE OBSERVATION
i
,
!
,
!
l
t
1