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MONTHYEARML17299B3221985-11-0606 November 1985 Forwards Preliminary Case Study Rept, Effects of Ambient Temp on Electronic Equipment in Safety-Related.... Rept Initiated by 840604 Event Re Total Loss of Control Area Ventilation Sys at Plant.Comments Requested within 30 Days Project stage: Other ML17299B3241985-11-30030 November 1985 Preliminary Case Study Rept, Effects of Ambient Temp on Electronic Equipment in Safety-Related Instrumentation & Control Sys Project stage: Other ML20137X7791986-02-28028 February 1986 Confirmatory Action Ltr Re 860228 Telcon W/Jw Lynch Outlining Listed Actions to Be Taken to Assure Operability of Reactor Control Room Emergency Ventilation Sys,Per Tech Specs & GDC 19 Project stage: Other ML20141C7141986-03-21021 March 1986 Notice of Deviation from Insp on 860128-30 & 0224-28 Project stage: Other ML20197F2511986-05-0707 May 1986 Forwards Request for Addl Info Re Control Room Habitability. Control Room Ventilation Sys Functioning Inconsistent W/Tmi Action Plan Item III.D.3.4 or Updated FSAR Project stage: RAI ML20198A1601986-05-14014 May 1986 Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $80,000.Violation Noted:Control Room Emergency Ventilation Sys Inoperable & Not Independent Due to Excessive Makeup Flow Rate in Train CB-1B Project stage: Other ML20198A1351986-05-14014 May 1986 Discusses Insp on 860128-30 & 0224-28 & Forwards Notice of Violation & Proposed Imposition of Civil Penalty.Violation Involves Licensee Failure to Maintain Control Room Emergency Ventilation Sys in Operable Status Project stage: Other ML20155J9501986-05-19019 May 1986 Forwards Addl Info Re Adequacy of Control Room Emergency Ventilation Sys & Control Room Habitability,Per Tl Chan 860507 Concerns.Complete Reanalysis of NUREG-0737,III.D.3.4 Requirements Will Be Completed Prior to Startup Project stage: Other ML20195F0061986-06-0404 June 1986 Forwards Revised Dose Calculation Analysis & Schedule for Completion of Control Room Emergency Ventilation Sys & Revised CB-1 Action Plan,Per 860528 Request Project stage: Other IR 05000344/19860211986-06-13013 June 1986 Insp Rept 50-344/86-21 on 860522-0606.No Violations or Deviations Noted.Major Areas Inspected:Activities Re Periodic Containment Integrated Leak Rate Test,Including Review of Procedures & Personnel Interviews Project stage: Request ML20205T6301986-06-13013 June 1986 Forwards Revised CB-1 Action Plan,Control Room Pressurization Test Results & Summary of Control Bldg HVAC Operation,Per 860609 Telcon Re Control Room Emergency Ventilation Project stage: Other IR 05000344/19860271986-07-14014 July 1986 Enforcement Conference Rept 50-344/86-27 on 860709.Major Areas Discussed:Apparent Violation Noted During Special Insp of QC Activities (Insp Rept 50-344/86-24) Project stage: Request ML20212K5051986-08-14014 August 1986 Forwards Notice of Withdrawal of Portions of 850419 Application for Amend to License NPF-1,per Util 860714 Request Project stage: Withdrawal ML20212K5131986-08-14014 August 1986 Notice of Withdrawal of Portions of 850419 Application for Amend to License NPF-1,revising Tech Specs to Permit Performance of Surveillance Testing of Control Room Emergency Ventilation Sys Project stage: Withdrawal ML20214Q8211986-09-19019 September 1986 Summary of 860528 Meeting W/Util & Bechtel in Bethesda,Md Re Control Room Emergency Ventilation Sys,Per TMI Action Item III.D.3.4 on Control Room Habitability.List of Attendees Encl Project stage: Meeting ML20215C2151986-09-30030 September 1986 Forwards Revised Toxic Gas Analysis Re NUREG-0737,III.D.3.4, Control Room Habitability, Justifying Deletion of Ammonia & Sulfur Dioxide Detectors.Implementation Plan for Design Changes & Related Info Encl Project stage: Other ML20207C6791986-12-24024 December 1986 Requests Expedited Review & Approval of Control Room Emergency Ventilation Sys (CB-1) Testing Changes Requested in Re TMI Action Item III.D.3.4, Control Room Habitability. Control Room Cooling Design Change Described Project stage: Other 1986-05-19
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l APPENDIX A NOTICE OF DEVIATION Portland General Electric Company Docket No. 50-344 121 S. W. Salmon Street License No.NPF-1 Portland, Oregon 97204 As a result of the inspection conducted during the period January 28-30, and February 24-28, 1986, a deviation from your commitments to the NRC was identified. In accordance with the General Statement of Policy and Procedure-for NRC Enforcement Actions, 10 CFR Part 2 Appendix C, as revised, 49 FR 8583 (March 8, 1984), the deviation was set forth below:
A.
FSAR sections 6.4.4.1 and 9.4.1.3 and PGE III.D.3.4 submittal for TMI item III.D.3.4 January 2, 1981, state that, system CB-1 complies to Regulatory Guide 1.52, March 1972 (with few exceptions), which endorses ANSI /ASME N509. N509 states that: the heater stage shall be sized on the basis of reducing the maximum relative humidity to 70 percent and in 1.52 that:
"...A low flow air bleed system should satisfy the single failure j
criterion for providing low humidity (Jess than 70 percent relative humidity) cooling air flow."
Contrary to the above, at the time of the inspection, the system humidistat was set at 85 percent during normal lineup, rather that at the 70 percent value indicated in the FSAR.
This is a Deviation.
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l Portland General Electric Company is hereby requested to submit to this office within thirty days of the date of this Notice, a written statement regarding the above deviation, describing the corrective steps taken, the results achieved (or corrective steps that are planned), and the date when corrective action will be completed.
MAR 2119es j-Dated T. Young,Jr.,Chpf
{j Engineering Sectiun 1
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