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| 05000280/LER-1985-001, :on 850101,safe Signal Placed in Loop B Channel 2 of Overtemp Delta T W/O Cognizance of Operations or Instrumentation Staff.Caused by Lack of Administrative Controls.Event Will Be Reviewed |
- on 850101,safe Signal Placed in Loop B Channel 2 of Overtemp Delta T W/O Cognizance of Operations or Instrumentation Staff.Caused by Lack of Administrative Controls.Event Will Be Reviewed
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| 05000281/LER-1985-001-02, :on 850106,auxiliary Feed Pump Operated During Monthly Reactor Protection Logic Test,Contrary to Planned Evolution.Caused by Failure to Perform Test in Proper Sequence |
- on 850106,auxiliary Feed Pump Operated During Monthly Reactor Protection Logic Test,Contrary to Planned Evolution.Caused by Failure to Perform Test in Proper Sequence
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| 05000281/LER-1985-002-03, :on 850215,svc Water Isolated to Charging Pump Intermediate Seal Cooler & Component Cooling Water Isolated.Caused by Valve Misposition Due to Operator Error. Valve Repositioned & Personnel Counseled |
- on 850215,svc Water Isolated to Charging Pump Intermediate Seal Cooler & Component Cooling Water Isolated.Caused by Valve Misposition Due to Operator Error. Valve Repositioned & Personnel Counseled
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| 05000280/LER-1985-002-01, :on 850113,lo-lo Level in Steam Generator B Caused Reactor Scram.Caused by Failure of Personnel to Adequately Control Steam Generator Level.Feedwater Bypass Flow Indication Design Installed |
- on 850113,lo-lo Level in Steam Generator B Caused Reactor Scram.Caused by Failure of Personnel to Adequately Control Steam Generator Level.Feedwater Bypass Flow Indication Design Installed
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| 05000281/LER-1985-002, :on 850215,charging Pump Intermediate Seal Coolers Discovered Improperly Aligned.Caused by Personnel Error.Proper Intermediate Seal Cooler Placed in Svc. Personnel Reinstructed Re Following Procedures |
- on 850215,charging Pump Intermediate Seal Coolers Discovered Improperly Aligned.Caused by Personnel Error.Proper Intermediate Seal Cooler Placed in Svc. Personnel Reinstructed Re Following Procedures
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| 05000281/LER-1985-003, :on 850423,outside Recirculation Spray Pump a Suction Valve Found Degraded & Pump B Valve Found Inoperable.Caused by Inadequate Sector Gear & Sheared Pins in Extension Shafts.Pins Replaced |
- on 850423,outside Recirculation Spray Pump a Suction Valve Found Degraded & Pump B Valve Found Inoperable.Caused by Inadequate Sector Gear & Sheared Pins in Extension Shafts.Pins Replaced
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| 05000280/LER-1985-003, :on 850126,reactor Tripped Due to Voltage Transient Induced on Vital Bus I When Momentary Overload Condition Caused Circuit Breaker 13 to Trip Open.Cause Unknown.Plant Returned to Stable Condition |
- on 850126,reactor Tripped Due to Voltage Transient Induced on Vital Bus I When Momentary Overload Condition Caused Circuit Breaker 13 to Trip Open.Cause Unknown.Plant Returned to Stable Condition
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| 05000281/LER-1985-003-03, :on 850428,Type C Testing Revealed Both Outside Recirculation Spray Pump Suction Valves MOV-RS-255A, B(Eiis 20) Inoperable.On 850510,outside Recirculation Spray Pump Discharge Valve Inoperable |
- on 850428,Type C Testing Revealed Both Outside Recirculation Spray Pump Suction Valves MOV-RS-255A, B(Eiis 20) Inoperable.On 850510,outside Recirculation Spray Pump Discharge Valve Inoperable
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| 05000281/LER-1985-004-01, :on 850501,discrepancies Noted W/Rosemount Model 1153 Transmitters & Conax Environ Seal Assemblies. Caused by Overtorqued Hollow Screws in Transmitters & Improper Installation of Connectors |
- on 850501,discrepancies Noted W/Rosemount Model 1153 Transmitters & Conax Environ Seal Assemblies. Caused by Overtorqued Hollow Screws in Transmitters & Improper Installation of Connectors
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| 05000281/LER-1985-004-03, :on 850501,degraded Terminal Screws Used to Terminate Field Wiring Inside Rosemount Transmitters & Conax Seal Assemblies Did Not Provide Positive Environ Seal. Caused by Overtorquing Hollow Screws |
- on 850501,degraded Terminal Screws Used to Terminate Field Wiring Inside Rosemount Transmitters & Conax Seal Assemblies Did Not Provide Positive Environ Seal. Caused by Overtorquing Hollow Screws
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| 05000280/LER-1985-004, :on 850127,reactor Tripped Due to Closing of Four Turbine Stop Valves.Caused by Insufficient Consideration of Steam Leakage Effect on Plant Parameters. Plant Parameters Returned to Stable Conditions |
- on 850127,reactor Tripped Due to Closing of Four Turbine Stop Valves.Caused by Insufficient Consideration of Steam Leakage Effect on Plant Parameters. Plant Parameters Returned to Stable Conditions
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| 05000281/LER-1985-005-03, :on 850514 & 15,automatic Initiation of Hazard Zones 8 & 4,respectively,locked Out W/No Fire Watch Present. Caused by Lack of Procedure & Training.Procedure for CO2 Sys Lockouts Will Be Implemented |
- on 850514 & 15,automatic Initiation of Hazard Zones 8 & 4,respectively,locked Out W/No Fire Watch Present. Caused by Lack of Procedure & Training.Procedure for CO2 Sys Lockouts Will Be Implemented
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| 05000280/LER-1985-005-01, :on 850403,operator Discovered Lockout of Automatic Initiation of CO2 for Fire Zone 7 W/O Required Fire Watch.Caused by Misunderstanding Between Personnel Re Fire Zone Tagging |
- on 850403,operator Discovered Lockout of Automatic Initiation of CO2 for Fire Zone 7 W/O Required Fire Watch.Caused by Misunderstanding Between Personnel Re Fire Zone Tagging
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| 05000280/LER-1985-006, :on 850128,reactor Trip Occurred Due to Differential Pressure anti-motoring Turbine Trip.Caused by Isolation of Exhaust Pressure Sensing Line Root Valve in anti-motoring Instrumentation.Plant Returned to Svc |
- on 850128,reactor Trip Occurred Due to Differential Pressure anti-motoring Turbine Trip.Caused by Isolation of Exhaust Pressure Sensing Line Root Valve in anti-motoring Instrumentation.Plant Returned to Svc
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| 05000281/LER-1985-007-02, :on 850612,spurious Safety Injection Occurred During Periodic Functional Test.Caused by Procedure Deficiency.Function Test Will Be Modified to Provide Separate Steps & Signoffs |
- on 850612,spurious Safety Injection Occurred During Periodic Functional Test.Caused by Procedure Deficiency.Function Test Will Be Modified to Provide Separate Steps & Signoffs
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| 05000280/LER-1985-007, :on 850429,turbine/reactor Trip Occurred as Result of Main Feed Pump a Trip.Caused When Valve Open Signal Not Sent to Feed Pump Trip Logic.Valve Position Actuator Arm Modified |
- on 850429,turbine/reactor Trip Occurred as Result of Main Feed Pump a Trip.Caused When Valve Open Signal Not Sent to Feed Pump Trip Logic.Valve Position Actuator Arm Modified
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| 05000281/LER-1985-008-01, :on 850619,auxiliary Ventilation Damper I-VS-MOD-58A Drifted Closed.Cause Undetermined.Unit 2 Containment Purge Stopped & Damper Manually Opened.Parts Needed to Repair Actuator Ordered |
- on 850619,auxiliary Ventilation Damper I-VS-MOD-58A Drifted Closed.Cause Undetermined.Unit 2 Containment Purge Stopped & Damper Manually Opened.Parts Needed to Repair Actuator Ordered
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| 05000281/LER-1985-008, :on 850619,auxiliary Ventilation Damper 1-VS-MOD-58A Drifted Closed.Caused by Short in Damper Actuator Relief Valve Coil.Actuator Sent to Mfg for Overhaul |
- on 850619,auxiliary Ventilation Damper 1-VS-MOD-58A Drifted Closed.Caused by Short in Damper Actuator Relief Valve Coil.Actuator Sent to Mfg for Overhaul
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| 05000280/LER-1985-008, :on 850318,tag Inadvertently Placed on Fire Zone 5,locking Out Automatic Initiation of CO2 W/O Fire Watch as Required by Tech Specs.Caused by Operator Error.Sys Returned to Automatic.Red Tags Used in Future |
- on 850318,tag Inadvertently Placed on Fire Zone 5,locking Out Automatic Initiation of CO2 W/O Fire Watch as Required by Tech Specs.Caused by Operator Error.Sys Returned to Automatic.Red Tags Used in Future
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| 05000280/LER-1985-009, :on 850512,PORV PCV-1455C Cycled Twice Due to Overpressure Condition.Caused by Failure of Normal Letdown Pressure Control Valve PCV-1145 Due to Positioner Misadjustment.Part Adjusted |
- on 850512,PORV PCV-1455C Cycled Twice Due to Overpressure Condition.Caused by Failure of Normal Letdown Pressure Control Valve PCV-1145 Due to Positioner Misadjustment.Part Adjusted
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| 05000281/LER-1985-009-03, :on 851107,six Individual Rod Position Indicators in Controlling Bank D & One Indicator in Bank C Declared Inoperable Due to Incorrect Positions.Caused by Instrumentation Drift.Indicators Calibr |
- on 851107,six Individual Rod Position Indicators in Controlling Bank D & One Indicator in Bank C Declared Inoperable Due to Incorrect Positions.Caused by Instrumentation Drift.Indicators Calibr
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| 05000281/LER-1985-009, :on 851107,individual Rod Position Indicators for Six Rods in Controlling Bank D & One Rod in Controlling Bank C Indicated More than 12 Steps from Bank Demand Position.Caused by Instrument Drift |
- on 851107,individual Rod Position Indicators for Six Rods in Controlling Bank D & One Rod in Controlling Bank C Indicated More than 12 Steps from Bank Demand Position.Caused by Instrument Drift
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| 05000281/LER-1985-010-02, :on 850813,unit Experienced Turbine Runback to Approx 48% Power Resulting in Partial Loss of Emergency Bus. Caused by Tripped Series Breaker to Vital Bus 2-1 Sola Transformer.Breakers Reset |
- on 850813,unit Experienced Turbine Runback to Approx 48% Power Resulting in Partial Loss of Emergency Bus. Caused by Tripped Series Breaker to Vital Bus 2-1 Sola Transformer.Breakers Reset
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| 05000281/LER-1985-010-01, :on 850813,turbine Runback to Approx 48% Power Occurred,Initiating Loss of Vital Bus 2-I.Caused by Tripped Transformer Breaker.Breakers Replaced |
- on 850813,turbine Runback to Approx 48% Power Occurred,Initiating Loss of Vital Bus 2-I.Caused by Tripped Transformer Breaker.Breakers Replaced
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| 05000280/LER-1985-010, :on 850515,intermediate Range High Flux Trip Bistables NI-35 & NI-36 Tripped at 30% & 31% Power, Respectively.Apparently Caused by Lack of Experience in Developing Intermediate Setpoints |
- on 850515,intermediate Range High Flux Trip Bistables NI-35 & NI-36 Tripped at 30% & 31% Power, Respectively.Apparently Caused by Lack of Experience in Developing Intermediate Setpoints
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| 05000281/LER-1985-011-02, :on 851023,emergency Diesel Generator (EDG) Automatically Started.Caused by Inadequate Design Change Test Procedure.Control of EDG 2 Transferred to Main Control Room Panel & Diesel Shut Down |
- on 851023,emergency Diesel Generator (EDG) Automatically Started.Caused by Inadequate Design Change Test Procedure.Control of EDG 2 Transferred to Main Control Room Panel & Diesel Shut Down
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| 05000280/LER-1985-011, :on 850626,while Racking Charging Pump B Breaker 15J5 Out for Pump Maint,Normal Feeder Breaker 15H6 for Operating Charging Pump C Tripped Due to Electrical Interlock.Caused by Inadequate Precautions |
- on 850626,while Racking Charging Pump B Breaker 15J5 Out for Pump Maint,Normal Feeder Breaker 15H6 for Operating Charging Pump C Tripped Due to Electrical Interlock.Caused by Inadequate Precautions
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| 05000281/LER-1985-012-01, :on 851026,results of RCS Sample Indicated Drop in Boric Acid Concentration from 2,217 Ppm to 1,952 Ppm. Caused by Out of Calibr Flow Transmitter That Inputs to Boric Acid Integrator.Flow Transmitter Calibr |
- on 851026,results of RCS Sample Indicated Drop in Boric Acid Concentration from 2,217 Ppm to 1,952 Ppm. Caused by Out of Calibr Flow Transmitter That Inputs to Boric Acid Integrator.Flow Transmitter Calibr
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| 05000280/LER-1985-012, :on 850609,during Testing of Discharge Valves, Chemical Addition Tank Water Level Decreased.Caused by Failed Closed Contact,Resulting in Valve Reopening.Flow Path Isolated & Failed Contacts Replaced |
- on 850609,during Testing of Discharge Valves, Chemical Addition Tank Water Level Decreased.Caused by Failed Closed Contact,Resulting in Valve Reopening.Flow Path Isolated & Failed Contacts Replaced
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| 05000280/LER-1985-013, :on 850721,containment Temp Exceeded 120 F for Approx 3 H.Caused by Loss of Component Cooling Chiller Unit. Component Restarted & Chiller Condenser Svc Water Tubes Cleaned |
- on 850721,containment Temp Exceeded 120 F for Approx 3 H.Caused by Loss of Component Cooling Chiller Unit. Component Restarted & Chiller Condenser Svc Water Tubes Cleaned
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| 05000280/LER-1985-013-01, :on 850721,containment Temp Exceeded 120 F for Approx 3 H.Caused by Loss of Component Cooling Chiller I-CD-REF-IA Due to Tube Fouling on Water Side Causing High Chiller Condenser Pressure |
- on 850721,containment Temp Exceeded 120 F for Approx 3 H.Caused by Loss of Component Cooling Chiller I-CD-REF-IA Due to Tube Fouling on Water Side Causing High Chiller Condenser Pressure
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| 05000281/LER-1985-013-02, :on 851107,turbine Trip/Reactor Trip Occurred as Result of High Steam Generator Level.Caused by Operator Inexperience W/Manual Feed Control During Low Power Startup Conditions.Status Tree Reviews Performed |
- on 851107,turbine Trip/Reactor Trip Occurred as Result of High Steam Generator Level.Caused by Operator Inexperience W/Manual Feed Control During Low Power Startup Conditions.Status Tree Reviews Performed
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| 05000281/LER-1985-014-01, :on 851226,control Rod Urgent Failure Alarm Occurred as Rods Stepping in Automatic.Caused by Problem in Logic Cabinet Pulser Card A101.Card Replaced & Sys Tested Satisfactorily |
- on 851226,control Rod Urgent Failure Alarm Occurred as Rods Stepping in Automatic.Caused by Problem in Logic Cabinet Pulser Card A101.Card Replaced & Sys Tested Satisfactorily
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| 05000280/LER-1985-017-01, :on 850911,following Reactor trip,I-131 Level Exceeded Tech Spec Limit.Caused by Fuel Element Defects in Reactor Core.Dose Equivalent Monitored Until Less than 1.0 Uci/Cc |
- on 850911,following Reactor trip,I-131 Level Exceeded Tech Spec Limit.Caused by Fuel Element Defects in Reactor Core.Dose Equivalent Monitored Until Less than 1.0 Uci/Cc
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| 05000280/LER-1985-018, :on 850911,turbine Trip/Reactor Trip Occurred Due to Low Condenser Vacuum Signal.Caused by Operation Error.Covers Placed on Inlet Valve Switches & Operator Reinstructed |
- on 850911,turbine Trip/Reactor Trip Occurred Due to Low Condenser Vacuum Signal.Caused by Operation Error.Covers Placed on Inlet Valve Switches & Operator Reinstructed
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| 05000281/LER-1985-018-01, :on 850911,turbine Trip/Reactor Trip Occurred Due to Low Condenser Vacuum Signal.Caused by Operator Inadvertently Closing Four Condenser Inlet Valves While Throttling Four Condenser Outlet Valves |
- on 850911,turbine Trip/Reactor Trip Occurred Due to Low Condenser Vacuum Signal.Caused by Operator Inadvertently Closing Four Condenser Inlet Valves While Throttling Four Condenser Outlet Valves
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| 05000280/LER-1985-019, :on 850927,individual Rod Position Indicator for Two Rods Inoperable.Spurious Incorrect Rod Position Indication Is Generic Westinghouse PWR Concern.Portion of Sys Outside Containment Tested & No Problems Found |
- on 850927,individual Rod Position Indicator for Two Rods Inoperable.Spurious Incorrect Rod Position Indication Is Generic Westinghouse PWR Concern.Portion of Sys Outside Containment Tested & No Problems Found
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| 05000280/LER-1985-020, :on 850927,following Controlled Shutdown Due to Hurricane Gloria,Iodine Spike Discovered.Caused by Known Fuel Element Defects in Reactor Core.Level of Dose Equivalent I-131 Monitored Per Tech Spec Table 4.1-2B |
- on 850927,following Controlled Shutdown Due to Hurricane Gloria,Iodine Spike Discovered.Caused by Known Fuel Element Defects in Reactor Core.Level of Dose Equivalent I-131 Monitored Per Tech Spec Table 4.1-2B
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| 05000280/LER-1985-021, :on 851114,unexpected Start of Auxiliary Feed Pump 2-FW-P-3A Occurred.Caused by Open Coil in Bfd Relay AFP-2XA.Relay Replaced & Tested Satisfactorily |
- on 851114,unexpected Start of Auxiliary Feed Pump 2-FW-P-3A Occurred.Caused by Open Coil in Bfd Relay AFP-2XA.Relay Replaced & Tested Satisfactorily
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| 05000280/LER-1985-022-01, :on 851121,spurious auto-start of Auxiliary Vent Emergency Fans Occurred.Cause Not Determined.Steam Generator Pressure Returned to Normal & Letdown Trip Valve TV-1204 Opened |
- on 851121,spurious auto-start of Auxiliary Vent Emergency Fans Occurred.Cause Not Determined.Steam Generator Pressure Returned to Normal & Letdown Trip Valve TV-1204 Opened
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| 05000280/LER-1985-022, :on 851121, Auxiliary Vent Sys Safety Mode Initiated Alarm Received.Caused by Momentary Decrease of Instrument Air Pressure from Ice Formation.Bypass Valve Adjusted |
- on 851121, Auxiliary Vent Sys Safety Mode Initiated Alarm Received.Caused by Momentary Decrease of Instrument Air Pressure from Ice Formation.Bypass Valve Adjusted
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