ML20135E099

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Insp Repts 50-313/96-09 & 50-368/96-09 on 961222-970201. Violations Noted.Major Areas Inspected:Aspects of Licensee Operations,Engineering,Maint & Plant Support
ML20135E099
Person / Time
Site: Arkansas Nuclear  Entergy icon.png
Issue date: 02/28/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20135E089 List:
References
50-313-96-09, 50-313-96-9, 50-368-96-09, 50-368-96-9, NUDOCS 9703060260
Download: ML20135E099 (25)


See also: IR 05000313/1996009

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ENCLOSURE 2

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U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

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Docket Nos: 50-313;50-368

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License Nos: DPR-51; NPF-6

Report No:

50-313/96-09:50-368/96-09

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Licensee:

Entergy Operations, Inc.

Facility:

Arkansas Nuclear One, Units 1 and 2

Location:

1448 S.R. 333

Russellville, Arkansas 72801

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Dates:

December 22,1996, through February 1,1997

Inspectors:

K. Kennedy, Senior Resident inspector

J. Melfi, Resident inspector

S. 8urton, Resident inspector

Approved by: Larry Yandell, Acting Chief, Project Branch C

Division of Reactor Projects

ATTACHMENT: Supplemental information

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9703060260 970229

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EXECUTIVE SUMMARY

Arkansas Nuclear One, Units 1 and 2

NRC Inspection Report 50-313/96-09:50-368/96-09

This routine announced inspection included aspects of licensee operations, engineering,

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maintenance, and plant support. The report covers a 6-week period of resident inspection.

Operations

Walkdown of the control room ventilation systems revealed that they were properly

aligned, in good material condition, and capable of supplying the required air to the

control room (Section 01.2).

The licensee loaded their second ventilated storage cask in accordance with

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procedures and met the requirements of the Certificate of Compliance. Lessons

learned from the loading of the first cask were effectively implemented, which

shortened the time needed to complete the activity (Section 01.3).

For the Unit 1 EDG fuel oil system, the associated procedure provided misleading

guidance for determination of diesel operability during degraded fuel system

conditions. Followup and corrective actions were appropriate for the deficiencies

identified (Section 01.4).

A Unit 1 control room supervisor failed to verify that electricians had completed

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work and authorized clearance of a hold card and closure of a breaker while work

on a 480 volt breaker was in progress. This was determined to be a violation.

Although no personnel were injured, this error created the potential for a personnel

injury or fatality. Significant weaknesses were noted in the lack of communications

between the control room supervisor and shift superintendent and the failure of an

auxiliary operator to question the work being performed by the electricians in a

panel that he knew was energized (Section 01.5).

Maintenance

The inspectors found that the maintenance and surveillance activities were correctly

performed in accordance with the applicable procedures and work instructions.

Personnel were knowledgeable and demonstrated effective communications,

self-checking, and peer checking. When conducted, prejob briefs were

comprehensive. Proper radiological work practices were observed (Section M1).

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Instrumentation and controls technicians properly investigated and diagnosed

circuitry problems associated with a control element assembly timer malfunction

alarm. Technicians utilized a working model, located in the maintenance shop, prior

to actual troubleshooting, to pre-empt problems at the work location. Deficiencies

were properly resolved or dispositioned (Section M1.3).

The inspectors identified a vulnerability in the licensee's independent verification

process in that an individual involved in the closure of a valve also performed the

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independent verification that the valve was closed and locked. As a result, errors

made in the initial component manipulation may not be identified if one of the

individuals performing this manipulation performed the independent verification

(Section M1.4).

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The licensee incorrectly determined that the f ailure of the Unit 2 reactor coolant

pump breaker to open was not a functional f ailure of the 6.9 kV switchgear system.

The failure did not result in the system exceeding any of its four performance goals

and the licensee stated that the error would have been identified during the next

periodic assessment of the system performance (Section M8.2).

Enaineerina

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During a period where a Unit 2 containment recirculation sump isolation valve

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bonnet relief valve was out of service, the containment recirculation sump isolation

valve remained operable. A proposed change to the Safety Analysis Report (SAR)

associated with the sump isolation valves was inadvertently fiied and not forwarded

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for incorporation in the next revision (Section E1.1).

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The licensee f ailed to update the Unit 1 SAR to incorporate the installation of

fibrous insulation on reactor coolant pumps. This was identified as a violation

(Section E1.2),

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Implementation of Option 8 to 10 CFR Part 50, Appendix J, waa accomplished in

accordance with the submitted license amendment. Engineering had established

methods to track and identify problems above those required by the scope of their

program. One change updating a reference had not been submitted for the next

revision of the SAR (Section E2.1).

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The licensee's procedure for setting the underload setpoints on the Unit 1 refueling

mast and spent fuel crane was incorrect and resulted in nonconservative setpoints.

This was determined to be a noncited violation (Section E8.1).

Plant Support

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The inspectors concluded that personnel demonstrated very good radiological work

practices during the conduct of plant activities, including operator rounds and

maintenance and surveillance activities. The requirements of radiation work permits

were followed, health physics technicians provided support to plant activities, and

proper consideration was shown to maintain dose as low as is reasonably

achievable (ALARA) (Sections M1 and R1).

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Report Details

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Summary of Plant Status

Unit 1 began the inspection period at 100 percent power. On January 5,1997, Unit 1

operators reduced power to 88 percent to perform a tu-Sine valve / governor valve test and

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returned power to 100 percent on January 6. Unit 1 operated at 100 percent power for

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the remainder of the inspection period.

Unit 2 began the inspection period at 97 percent power, where it remained throughout the

inspection period,

l. Operations

01

Conduct of Operations

01.1

General Comments (71707)

The inspectors reviewed ongoing plant operations. In general, the conduct of

operations was professional and safety conscious; specific events and notewnrthy

observations are detailed below:

01.2 Units 1 and 2 - Enaineered Safety Feature Walkdown of the Emeraency Control

Room Ventilation System

Units 1 and 2 share a common control room, which is required to be maintained

following a loss of coolant accident to minimize doses to control room operators.

The control room air is continuously monitored for high radiation, smoke, and

chlorine. On reaching predetermined setpoints, the control room will be isolated

from its normal supply of air and use the f mergency ventilation system.

Penetrations into the control room are designed and maintained to limit air infeakage

into the control room. Further, a safety-related ventilation system supplies filtered,

conditioned air at a higher relative pressure than surrounding areas to ensure that air

leakage is out of the control room. Both units share equipment that is necessary to

maintain this control room pressurization boundary.

To keep the control room supplied with filtered, conditioned air following an

accident, there are two 100 percent capacity filtration trains and two 100 percent

capacity cooling trains. Unit 1 has one filtration train and Unit 2 has the other

filtration train. Each filtration train has a roughing filter, high efficiency particulate

air filter and carbon filter, and a ventilation supply fan. Each train has an air

flowrate into the control room of 2000 cfm, of which 1667 cfm is recirculated from

the control room and 333 cfm is makeup from outside air. The makeup air assures

that air leakage through the control room pressurization boundary is out of the

control room.

The cooling for the control room is supplied by separate cooling trains, located in

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the Unit 2 side of the control room. The cooling units receive air from the control

room, cool it, and recirculate 9900 cfm back into the control renm.

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a.

inspection Scope (71707)

The inspectors performed a detailed walkdown of accessible portions of the control

room emergency ventilation system to verify its operability.

b.

Observations and Findinas

The inspectors walked down accessible portions of the control room ventilation and

cooling systems. The inspectors found that the system was aligned correctly, the

system appeared to be wel! maintained, and hangers and supports were made up

properly.

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The power to various f ans, valves, and other components is supplied by a

combination of Units 1 and 2 safety-related power. The inspectors reviewed the

power sources and determined that a single failure of a power supply would not

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degrade the system effectiveness.

The inspectors noted that the Seismic Category i Fan 2VSF-9 emergency filter unit

had an unsecured, wheeled charcoal filter hopper cart stored on top of the cabinet.

The inspectors asked to review the seismic qualification test for the emergency filter

unit to determine if this was an analyzed configuration. The licensee was not able

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to locate the qualification report and, rather than continue looking for the test

report, evaluated the condition in Engineering Request 973696E301. The

evaluation determined that nothing would be adversely affected from the cart failing

off of Fan 2VSF-9. The licensee intends to secure the hopper , srt to the cabinet to

preclude it from rolling off.

c.

Conclusions

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The inspectors concluded that the control room ventilation systems were proparty

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aligned, in good material condition, and capable of supplying the required air to the

control room.

01.3 Loadina of Second Ventilated Storaae Cask

a.

Insoection Scope (60855)

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The inspectors observed portions of the loading of the second ventilated storage

cask with Unit i spent fuel to verify that the cask was loaded in accordance with

procedural and Certificate of Compliance requirements. The licensee began loading

the cask on January 19,1997, and placed it on the storage pad on January 28.

b.

Observations and Findinas

The inspectors observed that the licensee followed their procedures and satisfied

the Certificate of Compliance requirements during the process of cask loading and

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movement. The inspectors found that the licensee effectively incorporated lessons

learned from the loading of the first cask, resulting in a more efficient process which

allowed them to complete the movement of the second cask in a shorter period of

time. The licensee was not able to significantly reduce the time it took to

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vacuum-dry the cask, which took approximately 3 days to complete, and planned to

evaluate the process further.

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Conclusions

The licensee loaded their second ventilated storage cask in accordance with

procedures and met the requirements of the Certificate of Compliance. Lessons

learned from the loading of the first cask were effectively implemented, which

shortened the time needed to complete the activity.

01.4 Unit 1 - Emeraency Diesel Operability

a.

Inspection Scone (71707)

On December 26,1996, during the inspector's review of the Unit 1 control room

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turnover sheet, it was noted that the Emergency Diesel Generator A fuel oil return

sight glass was observed by operators to be half full. The normal condition for this

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sight glass is full. The inspectors were concerned that the loss of level was caused

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by leakage of fuel into a cylinder which could damage the diesel during a diesel start

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or result in a loss of prime to the fuel oil pump which would delay the diesel from

starting in the required amount of time. Inspection was conducted to assess the

licensee's evaluation of diesel generator operability.

b.

Observations and Findinas

The system engineer was interviewed to assess the impact of a loss of level in the

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fuel oil sight glass on diesel operability. Procedure 1104.036, Revision 36,

" Emergency Diesel Generator Operation," indicated that while shutdown the diesel

would be considered inoperable and a condition report (CR) written "if there is no

fuel in the ' return fuel' sight glass."

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The inspectors questioned the system engineer about two standpipes within the

sight glass and asked if the sight glass was effectively empty when the level was at

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the top of the standpipes. The inspectors were concerned that, in the event of a

leak in the fuel oil system, the level in the sight glass would only drop to the top of

the standpipes and would not result in an empty sight glass. Thus, there would

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always be some indication of fuelin the sight glass and the operability guidelines

contained in Procedure 1104.036would not be correct. The system engineer

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investigated this and concurred that the sight glass would be effectively empty

when fuel oil was at the top of the standpipes, which corresponded to a sight glass

level of 3/4 full.

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The inspectors noted that the operations shift turnover sheet indicated that the

sight glass was 1/2 full. The system engineer had been monitoring the

accumulation of bubbles in ti.a sight glass but was not aware of the indications

reported on the shift turnover sheet. During interviews with the operator, the

inspectors found that, although operations was reporting the level as 1/2 full, the

level was actually above the top of the standpipes. Operators believed that the

accuracy of the level report was not critical since the procedure indicated that diesel

generator operability was not affected until the sight glass was empty.

To address the level decrease in the sight glass, operators periodically operated the

fuel oil priming pump to refill the sight glass. No records were kept as to the

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amount of leakage or the frequency for repriming the fuel oil system. System

engineering was not aware of how frequently operators were priming the fuel oil

system. The periodic operation of the fuel oil priming pump was not controlled or

logged as an operator work around.

In response to the inspectors' findings, the licensee revised Procedure 1104.36 to

require the diesel to be declared inoperable if fuel oil level in the return sight glass is

at the top of the standpipes and cannot be restored with the priming pump.

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The inspectors observed the fuel oil level in the supply sight glass and confirmed

the slow accumulation of air bubbles in the dome. Subsequent observations by the

inspectors indicated no significant loss of level. The inspectors reviewed the

system design and possible leakage paths with the system engineer. Although the

licensee had not identified the source of the fuel oilleakage by the end of the

inspection period, they determined that fuel oil was not leaking into the cylinders.

Further investigation was planned to locate the source of the leak. The inspectors

concurred with the system engineer that the diesel remained operable because fuel

was not found to be leaking into the cylinders, only minor leakage was observed,

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and the priming pump was able to restore level in the sightglass.

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Conclusions

The associated procedure provided misleading guidance for determination of diesel

operability during degraded fuel system conditions. Followup and corrective actions

were appropriate for the deficiencies identified.

01.5 Unit 1 -Imorocer Clearance of Hold Card (71707)

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inspection Scope

The inspectors conducted a review of the circumstances surrounding the improper

clearance of a hold card from an electrical breaker which created the potential for a

personnel injury or fatality. The inspectors reviewed paperwork associated with the

actual hold card, conducted interviews, and reviewed CRs related to hold card

issues for the last 2 years.

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b.

Observations and Findinas

On January 13,1997, electricians were preparing to perform a scheduled

maintenance activity to remove and recalibrate Breaker B-1415, a 480 volt breaker,

which provides power to a main chiller. The lead craftsman entered the Unit 1 shift

superintendent's office at approximately 7:15 p.m. and requested that operators

hang the necessary tag to de-energize the power supply to Bus B-14. The lead

craftsman exited the office while operators tagged open Breaker A-104. At

approximately 8:15 p.m., the lead craftsman returned to the shift superintendent's

office to sign the Hold Card Authorization form, signifying that he considered the

system adequately isolated. The shift superintendent placed the Hold Card

Authorization form on his desk. The lead craftsman then left the office to

commence work on the breaker with two other electricians.

Concurrent with the lead craftsman signing in on the authorization form, the control

room supervisor entered the shift superintendent's office from the control room and

saw the lead craftsman signing the form. Because he thought that the lead

craftsman had previously signed in on the authorization form, the control room

supervisor believed that he was witnessing the lead craftsman sign the form to

release control of the hold card, signifying that tags were no longer required for the

work activity. There was no communication between the control room supervisor

and the shift superintendent or the lead craftsman. The control room supervisor

retrieved the hold card authorization form from the shift superintendent's desk and

took it into the control room to authorize the removal of the hold card. The shift

superintendent assumed the control room supervisor had retrieved the authorization

form to place it in the hold card book located in the control room. Because the

control room supervisor assumed that he had just witnessed the lead craftsman sign

for the release of the hold card, he did not adequately review the Hold Card

Authorization form and thus did not identify that the " Released By Lead Craftsman"

signature block had not been signed. The control room supervisor authorized

removal of the hold card from Breaker A-104 and directed operators to close the

breaker from the control room. Procedure 1000.027, Revision 22, " Hold and

Caution Card Control," Step 6.9.2, required the shift superintendent / control room

supervisor to verify that the " Released By Lead Craftsman" signature block was

completed prior to authorizing the removal of the hold card and system restoration.

The electricians had begun work on the breaker and removed one bus bar bolt from

the breaker when they saw an auxiliary operator taking voltage readings on the

switchgear in which they were working. The electricians also heard the humming

sound at the transformer. The electricians determined that the bus was energized

as indicated by the 500 volt reading on the bus voltage meter and with

measurements using their own voltmeter. The electricians stopped their work and

notified the control room that the bus on which they were working was energized.

No personnel were injured. The control room supervisor notified the shift

superintendent of the error. CR 1-97-009 was wntten to document the error.

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in response to this event, night orders were issued to Units 1 and 2 operators, who

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discussed the event and added a requirement to obtain a second verification that

the " Released by Lead Craftsman" signature block was properly completed prior to

authorizing clearance of the hold cards.

The licensee established an Event investigation Team to determine the root cause

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for the event and recommend corrective actions. The inspectors reviewed the

findings of the team and found them to be thorough and comprehensive. The team

determined that the root cause was the failure of the control room supervisor to

follow Procedure 1000.027in that he did not verify that the lead craftsman had

signed the Hold Card Authorization form to release the hold card. The team

identified additional weaknesses in the hold card process, communications, and

personnel work practices. The inspectors found that the lack of communications

between the control room supervisor and shift superintendent, and the failure of the

auxiliary operator to question the work being performed by the electricians in a

panel that he knew was energized, were significant weaknesses.

The investigation team recommended, and the licensee planned to implement, a

number of corrective actions to address the root cause of the event and the

additionalidentified weaknesses. These included revising Procedure 1000.027 to

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permanently implement a second verification that the craft had released the hold

card; evaluating the use of additional controls in the hold card process; conducting

all hands meetings to discuss the event and the potential consequences; and

discussing the event during continuing training with the appropriate personnel. In

addition, the team recommended reviewing the hold card process to identify all

single failure points in the hold card process which could result in an error and

determining the appropriate actions to address these single failure points.

The inspectors reviewed licensee CRs written in the last 2 years and did not identify

any corrective actions taken as a result of previous hold card issues which would

have precluded this event from occurring. The inspectors did note that, of the CRs

reviewed,11 were classified as significant by the licensee. The inspectors

categorized these significant CRs as: (1) personnel failing to verify the adequacy of

hold cards prior to commencing work; (2) inadequate hold card boundaries

established for work activities; (3) and failure to properly position components when

establishing hold card boundaries. Although the licensee had taken corrective

actions for these previous CRs, the inspectors found similarities between

weaknesses identified during this recent event and those identified in previous CRs.

These similarities included inadequate communications, auxiliary operators unaware

of activities occurring in their areas, and inadequate self-checking. The inspectors

found that, at the time of this inspection, the licensee was continuing to implement

corrective actions in response to previous CRs.

The inspectors determined that the failure of the control room supervisor to verify

that the lead craftsman had signed the Hold Card Authorization form, signifying

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release of the hold cards for his work activity, as required by Procedure 1000.027,

Revision 22, " Hold and Caution Card Control," Step 6.9.2, was a violation of Unit 1

Technical Specification (TS) 6.8.1(50-313/9609-01).

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Conclusions

A Unit 1 control room supervisor f ailed to verify that electricians had completed

work and authorized clearance of a hold card and closure of a breaker while work

on a 480 volt breaker was in progress. This was determined to be a violation.

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Although no personnel were injured, this error created the potential for a personnel

injury or fatauty. Significant weaknesses were noted in the lack of communications

between the control room supervisor and shift superintendent and the failure of an

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auxiliary operator to question the work being performed by the electricians in a

panel that he knew was energized.

01.6 Unit 2 - Tour With Auxiliarv Operator

On January 22 the inspectors accompanied the Unit 2 waste control operator on a

tour of the auxiliary building. The inspectors found that the operator was very

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knowledgeable, conducted a thorough tour of the auxiliary building, and took the

required logs. The operator maintained awareness of activities performed in his

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watch station by questioning personnel he encountered to determine the activities

they were performing.

01.7 Review of Institute of Nuclear Power Operations (INPO) Evaluation (71707)

The inspectors reviewed the results of an INPO evaluation performed in July and

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of licensee performance. Based on this review, no additionalinspections were

planned.

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Miscellaneous Operations issues

08.1

(Closed) Inspection Followun item (IFI) 50-368/9602-01." Unexpected Drop in Fuel

Pool Level" (92700)

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On March 20,1996, a mechanical failure of a Unit 2 spent fuel pool purification

filter drain valve resulted in a loss of level in the fuel pool. This followup item was

opened to track the resolution of the generic concern associated with other valves

used in the plant made by the same manuf acturer. The licensee wrote

CR 2-96-0129 to address the concern about generic valve f ailure and remote (reach

rod) operators. The licensee determin3d that the valve f ailure was caused by a

broken stem nut. Corrective actions incbded: (1) identifying critical valves and

reach rods; (2) defining management's expectations for initiating valve or reach rod

maintenance; (3) discussing expectations for acceptable performance and initiation

of maintenance on valves or reach rods; and, (4) modifications to reach rod position

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indications susceptible to malfunction or inaccurate readings. The inspectors

concluded that actions taken to address the issues associated with the valve failure

were appropriate.

08.2 Review of TS Interoretations (92901)

The inspectors conducted a survey of the licensee's TS interpretations and

determined that none of the documents contained informal references to NRC

review and approval. The inspectors emphasized to the licensee that any informal

reference to NRC review and approvalin a TS interpretation is not recognized by the

Commission and is not an acceptable practice,

11. Maintenance

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Conduct of Maintenance

M 1.1 General Comments

a.

inspection Scope (62707)

The inspectors observed all or portions of the following work activities:

Unit 1 - Job Order 00958408," Replacement of NNI Signal Conditioner,"

performed on January 7,1997.

Unit 1 - Job Order 00959141," Bearing flush of P7-B Outboard Bearing and

Bolt Torque Check," performed on January 28.

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Unit 1 - Job Order 00959946," Troubleshoot DROPS System," performed on

January 29.

Unit 2 - Job Order 00958216," Repair Gas Collection Header Flush

Connection Valve 2GH-5008," performed on January 10.

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Unit 2 - Job Order 00958001," Troubleshoot Control Element Assemblies,"

performed on January 14.

Unit 2 - Procedure 1412.001, Revision 8, " Preventive Maintenance of

Limitorque SB/SMB Motor Operators," performed on Valve 2CV-5076-2,the

safety injection system header Number 2 shut-off isolation valve. This

maintenance was conducted en January 23 under Job Order 00958306.

b.

Observations and Findinas

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The inspectors found that the maintenance activities were correctly performed in

accordance with the applicable procedures and work instructions. Personnel were

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knowledgeable and demonstrated effective communications, self-checking, and peer

checking. When conducted, prejob briefs were comprehensive. Proper radiological

work practices were observed.

In addition, see the specific discussions of maintenance observed under

Sections M1.2 and M1.3, below.

M1.2 Unit 2 - Repair of Gaseous Radwaste Flush Connection isolation Valve

a.

Inspection Scoce (62707,71750)

On January 10,1997, the inspectors observed maintenance performed on Gas

Collection Header Flush Connection isolation Valve 2GH-5008in accordance with

Job Order 00958216. Maintenance was performed because the valve would not

close and was believed to be clogged with resin beads that accumulated during

system operation. Mechanical maintenance and radiological practices were

observed.

b.

Observations and Findinas

The prejob briefing included a discussion of the tools and equipment necessary for

maintenance, radiological concerns, contamination, and cleanliness aspects of the

activity. Unexpected mechanical and radiological conditions were also considered.

A 55 gallon lined drum was stationed to collect the contents of the piping when the

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valve flange was opened. Health physics established containment bags to direct

any resin or liquids into the 55 gallon drum. The inspectors determined that the

mechanics appropriately considered pipe sizes and lengths to determine the volume

of water and foreign material that would need to be collected. Health physics

personnel were questioned about the possibility of unknown radiological conditions

in the piping and what precautions would be taken if the radiological conditions

changed during the maintenance. Health physics personnel stated that the piping

had only been surveyed as high as someone could reach and that, if radiological

conditions changed, the job would be terminated and personnel would leave the

area and conditions re-evaluated. Subsequent to the inspectors' questions, a

survey was conducted to determine the radiological conditions in the c,verhead

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piping. The survey indicated no abnormal radiological conditions and that dose

rates due to the resin clog ended about 4 feet up the pipe from the valve.

Precautions were taken by operations, maintenance, and health physics in

anticipation of a ventilt

ilineup change that could affect airborne radiological

conditions. Mechanics and health physics showed concern for ALARA during

anticontamination clothing changing, maintenance prestaging, and the performance

of maintenance as indicated by discussions about radiological postings, staging

locations, and other health physics questioning. The inspectors observed that the

valve maintenance was performed in accordance with the work package.

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c.

Conclusions

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Maintenance of the gaseous radwaste flush connection isolation valve was

conducted safelv and in accordance with approved procedures. Proper radiological

precautions were taken to minimize the spread of contamination and ALARA was

considered during all aspects of the maintenance. However, initial radiation surveys

of the affected piping were conducted only as high as a technician could reach and

conditions in the overhead piping were not assessed.

M1.3 Unit 2 - Troubleshootina of Control Element Assembly (CEA)

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a.

Insoection Scoce (62707)

On January 14,1997, the inspectors observed instrument and control technicians

troubleshoot CEA's under Job Order 00958001 to determine the cause of an

intermittent timer failure alarm.

b.

Observations and Findinas

inspectors observed the technicians investigate the circuitry associated with the

affected CEA. Troubleshooting methods were practiced in the shop on a working

model of the circuitry before field troubleshooting was accomplished. Additional

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testing was conducted in the shop to determine if oscilloscope grounds would

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affect the circuitry when used in the field. Technicians worked with system

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engineering to utilize controlled wiring diagrams to investigate possible sources for

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the f ailure. An integrated circuit card was believed to be the cause of the timer

failure alarm and it was replaced. The new card did not resolve the problem and

further troubleshooting revealed that an intermittent ground in the circuitry caused

the new card to f ailin the same manner. The intermittent ground could not be

reproduced. The integrated circuit card was again replaced and it functioned

correctly. The system was returned to service and a job order written to investigate

the circuitry when the system is out of service during the upcoming outage. The

inspectors observed peer checks, three-way communications, and a good

questioning attitude throughout the troubleshooting process.

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Conclusions

Instrument and control technicians properly investigated and diagnosed circuitry

problems associated with a CEA timer malfunction alarm. Proper use of three-way

communications, peer checks, and a questioning attitude were observed throughout

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the maintenance process. Technicir.as utilized a working model, located in the

maintenance shop, prior to actual trc'ubleshooting to pre-empt problems at the work

location. The inspectors verified that a failure of the CEA timer would not affect the

ability of the CEA to trip into the core. Deficiencies were properly resolved or

dispositioned.

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M 1.4 General Comments on Surveillance Activities

a.

' Inspectino Scope (61726)

The inspectors observed all or portions of the following surveillance activities:

Unit 1 - Procedure 1104.036, Revision 36, "DG1 Monthly Test," performed

on January 6,1997.

Unit 1 - Procedure 1104.004, Revision 60, Supplement 1, " Low Pressure

injection (Decay Heat) Pump (P-34A) & Components Quarterly Test,"

performed on January 9.

Unit 2 - Procedure 2304.237, Revision 0, " Calibration of Emergency

Feedwater Flow and Pressure Inst. Red Channel," performed on January 6

and 7.

Unit 2 - Procedure 2104.036, Revision 41, " Emergency Diesel Generator

Operations," Supplement 18, "2DG1 Month ly Test (Slow Start), performed

on January 8.

Unit 2 - Procedure 2104.005, Revision 36, " Containment Spray System,"

Supplement 1, "2P-35A Quarterly Test With SDC Secured," performed on

January 9.

Unit 2 - Procedure 2106.006, Revision 44, " Emergency Feedwater System

Operations," Supplement 7, " Quarterly EFW Check Valve Test," performed

on January 10.

b.

Observations and Findinas

The inspectors found that the surveillances were correctly performed in accordance

with the applicable procedures. Personnel were knowledgeable and demonstrated

effective communications wlf checking, and peer checking. When conducted,

prejob briefs were compreber sive. Proper radiological work practices were

e

observed.

During the performance of Procedure 2104.005, Revision 36, " Containment Spray

System," Supplement 1, "2P-35A Quarterly Test With SDC Secured," the

inspectors observed the operators perform valve manipulations as set forth in the

procedure. Due to the size of some of the valves, two operators were used to

reposition the valves. The inspectors observed the operators close Valve 2SI-5A,

as required by the procedure. The inspectors observed self-checking and peer

checking used to verify that they were manipulating the correct valve and that the

j

valve was properly closed and locked. At the completion of the test, the procedure

required independent verification that the valve was in the locked closed position.

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The inspectors noted that the operator who assisted in closing the valve, but did

not sign the initial verification, was going to perform the independent verification

required by the procedure. He was going to leave the area of the valve to perform

another step of the procedure, then return to perform the independent verification.

It did not appear to the inspectors that this practice would provide an independent

verification of valve position since the operator was involved in the initial closure of

the valve.

The inspectors found that Procedure 1015.035," Valve Operations," which provided

guidance on how to perform independent verification, did not prohibit this method

of independent verification. The procedure stated that independent verification was

the act of confirming, by an independent means or by a second individual at a

i

separate time other than the initial verihcation, that actions were correctly

performed. The licensee stated that the method of independent verification used

during the surveillance was acceptable. Although the inspectors concluded that the

independent verification was done in conformance with Procedure 1015.035, they

determined that the practice observed during the performance of this test created a

vulnerability in the independent verification process in that errors made in the initial

component manipulation may not be identified if one of the individuals performing

i

this manipulation performed the independent verification.

M1.5 Conclusions on Conduct of Maintenance

The inspectors found that the maintenance and surveillance activities were correctly

performed in accordance with the applicable procedures and work instructions.

Personnel were knowledgeable and demonstrated effective communications,

self-checking, and peer checking. When conducted, prejob briefs were

,

comprehensive. Proper radiological work practices were observed.

,

The inspectors identified a vulnerability in the licensee's independent verification

process in that an individual involved in the closure of a valve also performed the

independent verification that the valve was closed and locked. As a result, errors

eJe in the initial component manipulation may not be identified if one of the

fividuals performing this manipulation performed the independent verification.

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M8

Miscellaneous Maintenance issues (92902)

M8.1 (Closed) Violation 50-313/9512-01033." Installation of the Cy.e Suocort Assembly

Was Not Classified as an Infreauentiv Performed Test or Evolution"

(Closed) Violation 50-313/9512-01043."A Comotete Briefina includina All

Personnel Involved With the Replacement of the Core Support Assembly Was Not

Conducted Prior to Performina the lift"

(Closed) Violation 50-313/9512-01053." Failure to Establish the Reauired Fuel

Transfer Canal Water Level Prior to Movina the Core Suocort Assembiv"

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(Closed) Violation 50-313/9512-01063 "Inadeauate Procedure for the Removal and

Replacement of the Core Suocort Assembiv"

(Closed) Violation 50-313/9512-01073," Personnel Exceeded Overtime Limits

Without Plant Manaaer Acoroval"

The inspectors verified the corrective actions described in the licensee's response

letter, dated August 16,1995, to be reasonable and complete.

'

M8.2 (Closed) Unresolved item (URI) 50-368/96008-01," Failure of RCP Breaker to Open"

s

a.

Inspection Scoce

NRC Inspection Report 50-313/96-08; 50-368/96-08 described the licensee's

response to a failure of the Unit 2 Reactor Coolant Pump (RCP) 2P-32A breaker to

open from the control room on November 17,1996. The licensee determined thit

the breaker failed to open due to grease hardening, which resulted in the binding of

the breaker's trip latch roller bearing, A URI was opened pending review of this

breaker f ailure with respect to the maintenance rule.

b.

Observations and Findinas

,

The inspectors found that the 6.9kV switchgear system was included in the

licensee's maintenance rule program. However, the licensee had not classified the

f ailure of the RCP breaker as a functional failure. In response to questions by the

inspectors, the licensee reviewed this decision and determined that the failure

should have been classified as a functional f ailure due to the fact that the breaker is

.

'

required to trip to provide containment penetration overcurrent protection. The

licensee reclassified this f ailure as functional . failure; however, the failure did not

l

cause the 6.9kV switchgear system to exceed any of its four system performance

,

critena.

System performance and maintenance rule evaluations are normally conducted by

the cognizant system engineer. The licensee found that, due to vacation, the CR

,

describing the RCP breaker failure was reviewed by someone other than the system

engineer for the 6.9kV switchgear. This contributed to the error. In discussions

with the inspectors, the system engineer stated that he would have identified the

error during his next periodic assessment of system performance conducted at the

end of the current cycle. The inspectors verified that the scope of the periodic

assessment, as described in the "ANO System Engineering Desk Guide," included a

review of system performance against the performance criteria. The inspectors

verified that the assessment of system performance included a review of CRs

written on the systems. The inspectors also found that the licensee had

incorporated industry experience into their maintenance plans for the

6.9kV switchgear.

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c.

Conclusions

The Unit 2 6.9kV switchgear was included in the licensee's maintenance rule

program. The licensee incorrectly determined that the failure of a Unit 2 RCP

breaker to open was not a functional failure. However, the licensee stated that the

error wLuld have been identified during the next periodic assessment of system

performance at the end of the current refueling cycle.

Ill. Enaineerina

E1

Conduct of Engineering

E1.1

Unit 2 - Containment Recirculation Sumo isolation Valve

a.

Insoection Scope (37551)

On December 14,1996, the low pressure safety injection suction header was

pressurized during the performance of a routine surveillance. This caused the

overpressurization of the bonnet area of containment recirculation sump isolation

Valve 2CV-5649 and resulted in Bonnet Relief Valve 2PSV-56031ifting. The

licensee subsequently found that Valve 2PSV-5603 leaked and isolated the valve.

Bonnet Relief Valve 2PSV-5603 was installed to address concerns related to

'

pressure locking of containment recirculation sump isolation Valve 2CV-5649. The

inspectors reviewed the effects of isolating Valve 2PSV-5603 on the operability of

the containment sump isolation valve. The inspectors were also concerned about

the potential for Valve 2PSV-56031eakage during accident conditions.

t

b.

Observations and Findinas

i

The inspectors were concerned that, with Valve 2PSV-5603 isolated, the

containment recircu!ation sump isolation valve would be susceptible to pressure

locking / thermal binding and could be rendered inoperable. Interviews with

engineering and reviews of operability analysis demonstrated that the sump isolation

valve would remain operable during periods when the relief valve was isolated.

The licensee determined that the relief valve was leaking due to debris in the valve.

Maintenance history indicated that Valve 2PSV-5603 was in a location that

contained debris which could cause the valve to stick open upon actuation. The

'

inspectors questioned the susceptibility of the relief valve to open during accident

conditions and subsequently leak, resulting in increased off-site doses. The licensee

indicated that Valve 2PSV-5603 was susceptible to lifting when Valve 2CV-5649

stroked to the closed position, but not when stroked to the open position, its

required position during the recirculation phase. Thus,it was unlikely that the relief

valve would leak during accident conditions and affect off-site doses. Plant Impact

Evaluation (PIE) 95-0057 determined that water maintained in the header between

the sump and the isolation valve was sufficient to preclude pressure loc. king of the'

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valves. In addition, the licensee's calculations demonstrated that increases in room

temperature would not cause pressure locking of the valves. The licensee installed

the relief valves to increase the margin to prevent pressure locking of the valves.

The inspectors reviewed the Safety Analysis Report (SAR) to determine what

revisions were made as a result of the modification to add the relief valves to the

containment recirculation sump isolation valves. The inspectors found that a

proposed change to the SAR, written in response to an action item from a previous

condition report (CR 2-95-0116),had not been incorporated in the SAR. The

proposed revision to SAR Section 6.2.2.2.1, " Containment Spray System," stated

that water was required to be maintained in the piping between the sump isolation

valve and the recirculation sump to preclude pressue locking / thermal binding.

Although the change was not required to be made until the next revision of the

SAR, the licensee could not locate the proposed change. Subsequently, the

licensee determined that the proposed change had been inadvertently filed with the

closure documentation for the CR. As a result of the inspectors' questions, the

licensee included this change in the next amendment package.

c.

Conclusions

During a period when the containment recirculation sump isolation valve bonnet

relief valve was out of service, the containment recirculation sump isolation valve

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remained operable. Recommended revisions to facility documentation and

I

procedures associated with the original mod;fication were properly incorporated

with one exception. A proposed revision to the SAR, which the licensee had

intended to incorporate, was inadvertently filed and not fcrwarded to licensing.

E1.2 SAR Discrecancy Associated with Reactor Coolant System (RCS) Insulation

,

a.

jnspection Scoce (92903)

Inspection was performed to followup on a discrepancy identified in the Unit 1 SAR,

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Section 4.2.2.7, " Reactor Coolant Equipment Insulation."

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b.

Observations and Findinas

During walkdowns of the RCS following a fire in the Unit 1 reactor building on

October 17,1996, the licensee identified fibrous insulation installed on the bowls of

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RCPs A and B (see NRC Inspection Reports 50-313/96-07:50-368/96-07and

50-313/96-27:50-368/96-27). The inspectors later discovered Section 4.2.2.7 of

the Unit 1 SAR stated that "due to fire protection concerns, fiberglass insulation

materials are not permitted on, adjacent to, or immediately below the RCP bowls."

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The inspectors determined that Limited Change Package (LCP) 92-5005A installed

this fibrous insulation around the RCP bowls, and the SAR was not updated due to

the timing of the review of LCP 92-5005A. The following table shows the relevant

timeline.

1

Date

Description

Mar 92

LCP 92-5005, "RCS Insulation Upgrade," installed, adding new fibrous

1

insulation on the RCS to improve thermal performance. As part of

,

LCP 92-5005, SAR change to Section 4.2.2.7 was drafted, noting new

'

insulation and adding a caution not to have fibrous insulation around

the RCP bowls.

Jun 93

LCP 92-5005A, " Install RCS Insulation," written to add fibrous

insulation to RCPs.10 CFR 50.59 review of LCP 92-5005 A performed.

Jul 93

SAR updated from LCP 92-5005

Nov 93

LCPs 92-5005 and 92-5005A closed

LCP 92-5005 upgraded insulation around the RCS during Refueling Outage 1R12

(March 1992)to improve thermal performance of the RCS Mirror insulation was

placed around RCP A and B bowls. The RCP bowl fibrous insulation was installed

during Refueling Outage 1R13 (October 1993) per LCP 92-5005A. When

LCP 92-5005A was in final review (June 93), the SAR had not yet been updated for

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the changes from LCP 92-5005. When performing a 10 CFR 50.59 review for

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LCP 92-5005A,the reviewer did not look at pending SAR changes, and the SAR did

'

not prohibit the use of fibrous insulation on the RCP bowls. The 10 CFR 50.59

evaluation did conclude that fibrous insulation was acceptable for use on the RCP

,

bowls due to the existence of the RCP oil collection system.

)

10 CFR 50.71(e) states, in part, that each person licensed to operate a nuclear

power reactor shall update, periodically . . . the Final Safety Analysis Report (FSAR)

originally submitted as part of the application for the operating license to assure that

the information included in the FSAR contains the latest material developed . . . .

The updated FSAR shall be revised to include the effects of all changes made in the

facility or procedures as described in the FSAR . . . .

The f ailure to revise the FSAR to incorporate the installation of fibrous insulation on

RCPs A and B was identified as a violation of 10 CFR 50.71(e)(50-313/9609-02).

c.

Conclusions

The licensee f ailed to update the Unit 1 SAR to incorporate the installation of

fibrous insulation on RCPs. This was identified as a violation.

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E2

Engineering Support of Facilities and Equipment

E2.1

Unit 2 - Performance Based Reauirements for Con, ta_inment Leakaae Testina

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a.

insoection Scooe (37551)

The inspectors reviewed the licensee's implementation of Option B to Appendix J of

10 CFR Part 50 which was incorporated into the SAR and TSs with License

Amendment 176. This option allows licensees to establish performance based

inspection criteria for containment leakage testing. Included was a review of the

applicable TSs and conformance of the new program to Regulatory Guide 1.163,

" Performance-Based Containment Leak-Test Program," September 1996.

The following licensee documents were reviewed for the inspection:

,

Unit 2 SAR

Unit 2 TSs, Amendment 176

HES-02, Revision 4, " Arkansas Nuclear One Engineerina Standard For

Containment Leak Rate Testing Program"

Procedure 2304.015," Arkansas Nuclear One - Unit 2 Electrical Penetration

Local Leak Rate Tests"

Procedure 2104.009," Arkansas Nuclear One - N Systems Operations"

2

CR 2-96-0375," Increased Electrical Penetration Room Leakage"

b.

Observations and Findinas

TSs properly incorporated documentation submitted to NRC for the referenced

license amendment. The SAR did not require any changes to content because TSs

were referenced for local leak-rate test requirements.

HES-02, Revision 4, " Arkansas Nuclear One Engineering Standard for Containment

Leak Rate Testing Program," was reviewed. This procedure referenced the

associated commitments and contained methodology to monitor the performance of

those items previously covered by TSs. In addition to the leak rate testing program,

the licensee had established a database to track and trend associated components.

The database included several methods for trending both frequency of evaluation

and root causes for degradation. In addition, future procedural revisions were

planned to bettet quantify performance and testing frequency requirements.

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c.

Conclusions

implementation of Option B to 10 CFR Part 50, Appendix J, was accomplished in

accordance with the submitted license amendment. Additionally, engineering had

established methods to track and identify problems above those required by the

scope of their program.

,

E8

Miscellaneous Engineering issues (92903)

E8.1

(Closed) URI 50-313/9607-01:50-368/9607-01,"Cause of Fuel Pin Failure.

Nonconservative Crane Setooints, and Verification of Correct Setooints for Both

Units' Refuelina Masts and SFP Cranes"

a.

Inspection Scone

During the Unit 1 reieeling outage, the licensee identified damage to their fuel

assembly grid straps, damage on one fuel rod, and nonconservative underload

setpoints on the Unit 1 refueling mast and spent fuel cranes. This URI was opened

to review the licensee's actions with respect to these items and also verify the

underload settings on the Unit 2 spent fuel pool mast,

b.

Observations and Findinos

At the start of the refueling outage, the licensee had indications of fuelleakage.

Due to problems at other plants with grid strap movement, the licensee also

inspected the fuel assemblies. As a result of this inspection, the licensee noted

damage on the grid straps' corners and one grid strap that was torn along the side.

i

The licensee also found that one end cap weld on one fuel pin had a full

,

circumferential crack.

The licensee noted that the fuel pin damage was due to an improper weld done by

the fuel vendor (Framatome). The vendor changed their welding procedure to

improve the process and preclude further problems.

!

Most of the damage to the grid straps was on the corners of the grid straps, which

the licensee believed was due to the fuel upender not being vertical. This was fixed

during the previous refueling outage. The licensee also observed that some damage

was not attributable to the upender, which included a torn grid strap on a

once-burned fuel assembly. In conjunction with the torn grid straps, the licensee

identified that the refueling bridge and spent fuel pool mast had underload setpoints

that were approximately 15 pounds nonconservative. The licensee determined that

the underload setpoints on the Unit 1 refueling mast and spent fuel crane were

incorrect due to inaccurate weights of the control rod assemblies used in the

determination of the setpoint. It was not clear whether this slight amount of

nonconservatism could have caused the damage observed. The licensee believed a

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combination of factors caused the grid strap damage and implemented corrective

actions to prevent recurrence. The licensee revised their procedure to include the

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approprhte underload setpoints.

The licensee found that Procedure 1502.003, Revision 17, " Refueling Equipment

I

and Operator Checkouts," provided an incorrect value for setting the underload

1

setpoints for the Unit 1 refueling mast and spent fuel crane. This was determined

"

to be a violation of 10 CFR Part 50, Appendix B, Criterion V, in that the procedure

was not appropriate to the circumstances. This licensee-identified problem was

promptly corrected and the licensee's corrective actions for the grid strap damage

were appropriate. Based on the above, this is being treated as a noncited violation,

consistent with Section Vll.B.1 of the NRC Enforcement Policy (50-313/9609-03).

The inspectors also reviewed the methodology used to set the underload and

.

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overload limits for the Unit 2 refueling bridge and spent fuel pool. The inspectors

found that the licensee set the Unit 2 underload and overload limits appropriately.

c.

Conclusions

The licens90's procedure for setting the underload setpoints on the Unit 1 refueling

i

mast and spent fuel crane was incorrect and resulted in nonconservative setpoints.

'

This was identified as a noncited violation.

E8.2 (Closed) Licensee Event Reoort (LER) 50-313/94003-00/01."SurveillanceTestina of

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Some Enoineered Safeauards Components Did Not Verifv Operability Due to

Procedural Deficiencies" (92700)

1

LER 94-003 was written by the licensee to report inadequate surveillance testing of

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some engineered safeguards components. These inadequacies were described in

NRC Inspection Report 50-313/94-08;50-368/94-08 and were determined to be a

'

noncited violation. A task force, established as a result of this and similar findings,

identified an additionalinstance of inadequate testing related to the autostart

function of the high pressure injection auxiliary lubricating oil pumps. The

'

inspectors reviewed the licensee's corrective actions and found them to be

thorough and complete.

,

,

E8.3 (Closed) Violation 50-368/9408-02."Inadeauate Intearated ES Feature Tests"

(92903)

(Closed) LER 50-368/94-004." Surveillance Test of HPSI Pumo Did Not Verifv

Operability by Technical Specifications" (92700)

These two items concern the same issue, and the licensee wrote LER 50-368/94-

004 for this violation of Technical Specifications. The inspectors verified the

corrective actions described in the licensee's response letter, dated December 9,

1994, to be reasonable and complete.

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IV. Plant Support

R1

Radiological Protection and Chemistry Controls

'

R1.1 Unit 2 - Reoair of Leakina inspection Cover on Deboratina lon Exchanaer

1

a.

Inspection Scope (71750)

On January 15,1997, the inspectors monitored radiological practices for the repair

of an inspection cover on the deborating ion exchanger Tank 2T-70, conducted

under Job Order 00942776. Radiological Work Permit 1997-0052 was established

for the maintenance on Tank 2T-70, which was located in a locked high radiation

area.

b.

Observations and Findinas

Prebriefings were held that ensured minimal exposures were received. Rotation of

workers and prestaging of materials ensured that exposure times were minimal.

Health physics technicians showed proper concern for exposure by closely

monitoring entry times and ensuring that maintenance workers remained in low

dose areas while standing by to perform tasks. A dose goal of 0.100 person-rem

l

was set for the performance for this task. Total dose for the performance of this

task was 0.058 person-rem.

c.

Conclusions

The inspectors concluded that radiological work practices conducted for the repair

of the inspection cover on the deborating ion exchanger were conducted in

<

accordance with the radiological work permit. Proper consideration was shown for

ALARA and the total dose for the performance of the task was less than the dose

goal.

F2

Status of Fire Protection Facilities and Equipment

F2.1

Units 1 and 2 - Self-Contained Breathina Apoaratus (SCBA)

.

The inspectors conducted annualinspections of SCBAs. The SCBAs were checked

for test dates and supply bottle inspections. All apparatus were within their

inspection dates and bottles were Deing checked on a monthly basis as required.

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SUPPLEMENTAL INFORMATION

,

ATTACHMENT

PARTIAL LIST OF PERSONS CONTACTED

I

1

.

Licensee

P. Allen, System Engineering, Unit 2

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C. Anderson, Plant Manager, Unit 2

J. Clement, Assistant Manager, Unit 1 Operations

,

D. Denton, Director, Support

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P. Diet rich, Superintendent, Unit 1 Mechanical Maintenance

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R. Edington, General Manager Plant Operations

B. Gordon, Supervisor, Unit 2 System Engineering

R. Hutchinson, Vice President, Operations

R. Lane, Director, Design Engineering

D. McKenney, Acting Manager, Unit 1 System Engineering

D, Millar, Supervisor, Unit 2 Operations Standards-

D. Mims, Director, Licansing

T. Mitchell, Manager, Unit 2 System Engineering

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F. Philpott, Superintendent, Reactor Engineering

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T. Russell, Manager, Unit 2 Operations

M. Smith, Supervisor, Licensing

A. South, Licensing

J. Veglia, Supervisor, Modifications

D. Wagner, Supervisor, Quality Assurance

C. Zimmerman, Plant Manager, Unit 1

Framatome Technoloaies. Inc.

D. Scott, Resident Engineer

NRC

S. Burton, Resident inspector

K. Kennedy, Senior Resident inspector

J. Melfi, Resident inspector

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INSPECTION PROCEDURES USED

37551

Onsite Engineering

61726

Surveillance Observations

62707

Maintenance Observations

71707

Plant Operations

71750

Plant Support Activities

92700

Onsite Followup of I.ERs

92901

Followup - Plant Operations

92902

Followup - Maintenance

92903

Followup - Engineering

ITEMS OPENED CLOSED, AND DISCUSSED

Ooened

50-313/9609-01

VIO

Clearance of Hold Card Prior to Completion of Work

50-313/9609-02

VIO

Failure to Update SAR Due to the inadequate Design

Package Closecut

50-313/9609-03

NCV inadequate Procedure For Setting the Underload

Serpoints on the Unit 1 Refueling Mast and Spent Fuel

Crane

Closed

50-368/9408-02

VIO

Inadequate integrated ES Feature Tests

50-313/94003-00/01

LER

Surveillance Testing of Some Engineered Safeguards

Did Not Verify Operability Due to Procedural

Deficiencies

50-368/94-004

LER

Surveillance Test of HPSI Dump Did not Verify

Operability by TSs

50-313/9512-01033

VIO

Installation of the Core Support Assembly was not

Classified as an Infrequently Performed Test or

Evolution

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50-313/9512-01043

VIO

A Complete Briefing including All Personnel involved

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with the Replacement of the Core Support Assembly

was not Conducted Prior to Performing the Lif t

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f

50-313/9512-01053

VIO

Failure to Establish the Required Fuel Transfer Canal

Water Level Prior to Moving the Core Support Assembly

50-313/9512-01063

VIO

Inadequate Procedure for the Removal and Replacement

,

of the Core Support Assembly

'

50-313/9512-01073

VIO

Personnel Exceeded Overtime Limits without Plant

Manager's Approval

50-368/9602-01

IFl

Unexpected Drop in Fuel Pool Level

50-313:368/9607-01

URI

Cause of Fuel Pin Failure, Nonconservative Crane

,

Setpoints, and Verification of Correct Setpoints for Both

Units Refueling Masts and SFP Cranes

50-368/9608-01

URI

Failure of the RCP Breaker to Open from the Control

Room

50-313/9609-03

NCV Inadequate Procedure For Setting the Underload

Setpoints on the Unit 1 Refueling Mast and Spent Fuel

Crane

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. LIST OF ACRONYMS USED

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ALARA

as low as is reasonably achievable

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CEA

control element assembly

.

CR

condition report

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-FSAR.

Final Safety Analysis Report'

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IFl .

inspection followup item

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INPO

Institute of Nuclear Power Operations

.

LCP-

Limited Change Package

LER

Licensee Event Report

NCV

noncited violation

RCP

reactor coolant pump

RCS

reactor coolant system

SAR

' Safety Analysis Report

SCBA

self-contained breathing apparatus

SFP

spent fuel pool

TS

Technical Specification

URI

Unresolved item

VIO

violation

VSF

ventilation safety fan

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