ML20135D412

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Insp Repts 50-282/97-02 & 50-306/97-02 on 970108-0220. Violation Noted.Major Areas Inspected:Operations, Maintenance,Engineering & Plant Support
ML20135D412
Person / Time
Site: Prairie Island  Xcel Energy icon.png
Issue date: 02/25/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20135D385 List:
References
50-282-97-02, 50-282-97-2, 50-306-97-02, 50-306-97-2, NUDOCS 9703050227
Download: ML20135D412 (21)


See also: IR 05000282/1997002

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U.S. NUCLEAR REGULATORY COMMISSION

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REGION 111

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Docket Nos:

50-282, 50-306

License Nos:

DPR-42, DPR-60

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Report No:

50-282/97002, 50-308/97002

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Licensee:

Northern States Power Company

Facility:

Prairie Island Nuclear Generating Plant

Location:

1717 Wakonade Drive East

Welch, MN 55089

Dates:

January 8 - February 20,1997

Inspectors:

S. Ray, Senior Resident inspector

R. Bywater, Resident inspector

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Approved by:

J. Jacobson, Chief, Projects Branch 4

Division of Reactor T':clects

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9703053227 970225

PDR

ADOCK 05000282

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EXECUTIVE SUMMARY

Prairie Island Nuclear Gencrating Plant, Units 1 & 2

NRC Inspection Report 50-282/97002, 50-306/97002

This inspection included aspects of licensee operations, maintenance, engineering, and

plant support performed by the resident inspectors.

Ooerations

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No significant problems were noted with routine plant operations and the conduct

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of operations was generally good. (Section 01.1)

A project engineer showed awareness and a good questioning attitude in identifying

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that the auxiliary building crane was not operating as expected. (Section 01.2)

Failure to identify wiring change in the auxiliary building crane controls during the

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purchasing process, receipt inspection, or preventative maintenance prior to its use

for moving a spent fuel cask, indicated weaknesses in the licensee's programs and

was considered a Non-cited Violation. (Section 01.2)

Operations performance during refueling operations was excellent. Significant

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improvements were noted, especially in fuel handling operations, compared to the

previous refueling outage. There were several examples of operators averting

problems by the use of self-checking and a questioning attitude. (Section 01.3)

The inspectors noted that the licensee had implemented a new fuel movement log

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with significant human-factors improvements in its format. (Section 08.1)

Maintenance

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The inspectors identified questions regarding whether the January diesel cooling

water pump surveillance met the requirements of Technical Specifications. The

issue was considered an Unresolved item. (Section M1.1)

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The inspectors identified questions regarding whether the diesel cooling water

pumps needed to be tested from the control room to demonstrate that they could

meet their design basis. The issue was considered an inspection Followup item.

(Section M1.1)

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The inspectors identified a main steam safety relief, ready to be installed, that was

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missing a piece. The inspectors concluded that the system engineer would have

identified the missing piece before the valve was put into service. However, the

finding indicated a potential weakness in the control of salvaging parts from

equipment in the warehouse. (Section M1.1)

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The licensee identified that they had moved a heavy load over irradiated fuel

without meeting the requirements of their procedures. The event was considered

an Apparent Violation. (Section M1.2)

The inspectors concluded that refueling outage planning, scheduling, and execution

continued to be a licensee strength. (Section M1.3)

The inspectors identified that the licensee's heavy load procedure was inadequate

because it did not contain instructions or controls for moving heavy loads using of

mobile cranes near or over safe shutdown equipment. This was considered a

Violation. (Section M3.1)

Enaineerina

' The inspectors concluded that system engineer support of the outage activities was

excellent. (Section E2.2)

Plant Suonort

The licensee was adequately monitciing a major roa>. construction project that

could have an effect on emergency evacuation from the area and emergency

response to the plant. (Section P1)

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Report Details

Summarv of Pl ant Status

Unit 1 operated at or near full power for the entire inspection period except for brief power

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reductions for various testing and maintenance activities. Unit 2 operated in a gradual

power coastdown from full power to about 86% power. On January 24,1997, Unit 2

was taken off line for a refueling outage and remained in cold shutdown for the remainder

of the inspection period. During this inspection period the sixth dry cask was transported

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to the Independent Spent Fuel Storage Insta!.ation (ISFSI) and the seventh dry cask was

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loaded with spent fuel and also transported to the ISFSI.

I. Operations

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Conduct of Operatiens

01.1 General Comments

a.

Insoection Scone (71707)

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Using Inspection Procedure 71707, the inspectors conducted frequent reviews of

plant operations. These reviews included observations of control room evolutions,

shift turnovers, operability decisions,logkeeping, etc. Updated Safety Analysis

Report (USAR) Section 13, " Plant Operations," was reviewed as part of the

inspection.

b.

Observations and rindinas

The inspectors noted that control ronm operators were attentive to their panels and

knowledgeable of plant conditions and activities in progress. Communications were

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consistently clear. Shift turnover briefings were thorough but concise. Pre-job

briefings for infrequent or complex evolutions were excellent. No significant

. problems were noted with routine plant operations.

c.

Conclusions

The inspectors observed that the conduct of routine plant operations was generally

good. Additional comments on the conduct of refueling operations is contained in

Section 01.3 of this report.

01.2 Auxiliarv Buildina Crane Protective Features Defeated by Wirina Chances

a.

jnicethun Scooe (93702)

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On January 8,1997, the licensee reported via the Emergency Notification System

that they had discovered that the auxiliary building crane was used to move a spent

fuel cask when it may have been in a condition that prevented it from meeting its

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single failure proof design. The inspectc,rs reviewed the circumstances of the event

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and reviewed associated Licensee Event Report (LER) 282(306)/97-01. The

inspectors also reviewed Updated Safety Analysis Report Sections 10.2.1.2.2,

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' Major Equipment Required for Fuel Handling," and 12.2.12.1.3, " Auxiliary Building

Crane Evaluation."

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b.

Observations and Findinas

As discussed in the LER, the licenese purchased a replacement radio control

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transmitter for the crane and did not realize that the vendor had changed the wiring

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of the critical /non-critical switch from the design of the old transmitter. Thus an

emp'- spent fuel cask was moved into the spent fuel pool and then the loaded cask

was moved out of the pool while the crane was actually in the non-critical

condition. In that condition two of the crane protective features, the main hoist

drum overspeed protection and the spent fuel pool slot limit switch interlock, were

defeated. However, the licensee determined that the crane was still considered

single failure proof in the non-critical mode.

Other drum overspeed protection features were still active and there were

alignment lights that were used to verify the crane remained within the spent fuel

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pool roof slot. Thus the event was of minor safety significance. Since the new

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wiring scheme was an improvement over the old, the licensee's corrective action

included incorporating the new design into their procedures, obtaining updated

drawings from the vendor, and changing the old transmitter to match it. Other

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corrective actions were discussed in the LER.

Failure of the licensee to adequately verify the new radio control box conformed to

the expected design was a violation of 10 CFR 50, Appendix B, Criterion Vil,

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" Control of Purchased Material, Equipment, and Services." However, this licensee-

identified and corrected violation is being treated as a Non-Cited Violation,

consistent with Section Vll.B.1 of the NRC Enforcement Policy. (282/97002-01)

c.

Conclusions

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The difference between the critical and noncritical functions of the crane were

subtle and the fact that the project engineer identified the condition showed

awareness and a good questioning attitude. However, failure to identify the wiring

change during the purchasing process, receipt inspection, or preventative

maintenance prior to its use for moving the spent fuel cask, pointed out

weaknesses in the licensee's programs which were being addressed by the

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corrective actions in the LER. LER 282(306)/97-01 associated with this event will

remain open pending completion of the remaining corrective actions.

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01.3 Refuelino Operations

a.

Insoection Scope (71707)

The inspectors observed portions of several refueling operations and procedures

during the Unit 2 outage. Performance of the following procedures was observed:

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2C1.3

' Unit 2 Shutdown, Revision 38

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2C1.6

Shutdown Operations - Unit 2, Revision 7

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2C12.2

Unit 2 Purification & Chemical Addition, Revision 1

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2C15

Residual Heat Removal System - Unit 2, Revision 13

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C17

Fuel Handling System, Revision 24

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C19.10

Containment Airlock Door Control at Shutdown, Revision 4

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2D2

RCS Reduced Inventory Operation, Revision 6

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D5.2

Reactor Refueling Operations, Revision 20

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D61

Containment Penetration Outage Preparation, Revision 13

in addition, the inspectors reviewed Updated Safety Analysis Report,

Section 10.2.1, " Fuel Storage and Fuel Handling Systems."

b.

Observations and Findinos

Operations performance during refueling operations was excellent. Significant

improvements were noted, especially in fuel handhng operations, compared to the

previous refueling outage. Communications sad "n ependent verifications regarding

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fuel movements, were excellent. Pre-job briefings and training in fuel handling

procedures for each crew was beneficial. Control of the plant during the crucial

draining of the reactor coolant system for steam generator nozzle dem installation

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was good. There were several examples of operators averting problems by the use

of self-checking and a questioning attitude.

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Conclusions

As operations observed by the inspectors associated with the refueling outage were

conducted in an excellent manner with significant improvements noted since the

last refueling outage.

03

Operations Procedures and Documentation

03.1 Licensee Review of Technical Soecifications Interoretations

a.

Insoection Scone (9900)

in response to the NRC-identified issue with failure to test the redundant diesel

. generator discussed in inspection Report 282(306)/96014, Section 01.2, as well as

findings at other plants, the licensee conducted a detailed review of their Technical

Specifications (TS) Interpretation book to see if any interpretations were contrary to

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-a literal reading of the TS. The inspectors reviewed the effort.

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b.

Observations and Findinas

The licensee maintained a book of interpretations for use by operators and others to

clarify the meaning of certain TS. Most of the interpretations were intended to be

temporarily in place until TS amendments could be processed. However, little

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effort had been made recently to submit individual amendments to replace the

interpretations because they were in the process of preparing a significant

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amendment to implement improved Standardized Technical Specifications (ISTS).

At the start of the review, there were 39 interpretations in effect. The ISTS would

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eliminate the need for most of them.

The licensee eliminated 13 of the interpretations when they determined that their

use could not be supported by the current literal wording of the TS. They

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submitted license amendment requests to replace some of the interpretations and

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were working on prioritizing other amendment requests. In addition, the licensee

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identified other interpretations to be eliminated but delayed canceling them until

supporting procedures could also be revised to avoid have conflicting operator

guidance in place,

c.

Conclusions

While the licensee's efforts to eliminate questionable TS interpretations was a good

idea, it was necessary due to the large number of interpretations in effect. The

inspectors reminded licensee management, in accordance with NRC Inspection

Manual Part 9900, that only TS interpretations in writing from the Office of Nuclear

Reactor Regulation were considered binding on the NRC and the license amendment

process was the normal method of clarifying TS.

06

Operations Organization and Administration

06.1 Manaaement Chanaes

The licensee announced the following management changes effective February 3,

1997:

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Doug Antony, President NSP Generation, retired,

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Ed Watzl was selected as President NSP Generation,

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Mike Wadley was selected as Vice President, Nuclear,

Joel Sorensen was selected as Prairie Island Plant Manager,

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Pete Valtakis was designated as acting General Superintendent Plant

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Operations until a permanent selection could be named.

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Miscellaneous Operations issues (92700,92901)

08.1 (Closed) Violation 282/96002-01: Four Examples of Operators Failing to Follow

Procedures During a Refueling Outage. These issues were.previously discussed in

inspection Reports 282(306)/96002, Sections 1.1,1.4, and 1.5 the associated

Notice of Violation: 282(306)/96006, Section 01.4; and 282(306)/96010,

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Section M8.2. The errors were associated with inattention to detail and failure to

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adequately self-check. The licensee responded to the violations in a letter to the

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NRC dated April 18,1996.

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During the Unit 2 refueling outage discussed in this report, the operators performed

the same types of evolutions as those resulting in the violation. The inspectors

noted that performance had improved significantly. During this outage the reactor

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refueling operations were complicated by the fact that extra moves were needed to

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bring the new fuel from the new fuel pit. In the past, the new fuel was placed in

the spent fuel pool prior to the outage. No errors similar to those cited in the

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- violation occurred during the outage activities. In addition, the invectors noted

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several examples of problems avoided by the operators due to increased emphasis

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on self-checking and a questioning attitude. Finally, the inspectors noted that the

licensee had implemented a new fuel movement log with significant human-factors

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improvements in its format.

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08.2 (Closed) Inspection Followun item 282/96008-01: Technical Specification for Shift

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Manning did not meet 10 CFR 50.54 requirements. This issue was previously

discussed in Inspection Report 282(306)/96008, Section 03.2. It was open

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the specification in alignment with the regulation.

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On November 25,1996, the licensee submitted a supplement to a previous license

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amendment request dated December 14,1995, containing the necessary changes

to meet the regulation. NRC approval of the request was still pending.

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08.3 (Closed) Insoection Followuo item 282/96008-02: Maintaining Operator Licenses in

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an Active Status. This issue was previously discussed in Inspection Report

282(306)/96008, Section 05.1. It was open pending licensee submittal of a letter

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clarifying which crew positions would be credited with duiy for the purposes of

maintaining an active license.

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On November 13,1996, the licensee submitted a letter to the NRC stating that

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they had discontinued the practice of crediting duty in the work control center as

meeting the criteria for actively performing the functions of an operator or senior'

operator. The letter also clarified the duties of the shift manager and stated that

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the duties of that position met the requirements for maintaining an active ': cense.

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On November 25,1996, the licensee submitted s supplement to a previous license

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amendment request dated December 14,1995, which added the requirement for

the shift technical advisor (who is also the shift manager) to hold a senior operator

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license. NRC approval of the request was still pending.

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08.4 (Closed) Violation 306/96014-01: Failure to Demonstrate Operability of the

Redundant Diesel Generator with one Diesel Generator inoperable. This issue was

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previously discussed in inspection. Report 282(306)/96014, Section 01.2, and

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Notice of Violation. The licensee responded to the Notice of Violation in a letter

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dated January 27,1997,in which they reported their corrective actions. The

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inspectors determined the corrective actions were completed and acceptable.

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ll. Maintenanca

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Conduct of Maintenance

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M1.1 General Comments

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a.

Insoection Scoos (61726,62707)

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The inspectors observed all or portions of the following maintenance and

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surveillance activities. Included in the inspection was a review of the

surveillance procedures (SP) or work orders (WO) listed as well as the

appropriate Updated Safety Analysis Report (USAR) sections regarding the

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activities.

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SP 1100

12 Motor Driven Auxiliary Feedwater Pump Test

Monthly, Revision 48

SP 1106B

22 Diesel Cooling Water Pump Test, Revision 50

SP 1226A

Containment Hydrogen Monitor Monthly Test,

Revision 8

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SP 1226B

Containment Hydrogen Monitor Quarterly Calibration,

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Revision 8

SP 2305

D6 Diesel Generator Slow Start Test, Revision 8

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SP 2318.1

Source Range Channel Calibration, Revision 4

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SP 2361

Exercising Feedwater Isolation and Feedwater Check

Valves, Revision 5

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WO 960767G

Replace Fan Coil isolation Valve MV-32387

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WO 9607678

Replace Fan Coil isolation Valve MV-32389

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WO 9612068

Replace Loop B Main Steam Safety Valves

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WO 9614755

Investigate 12 Auxiliary Feedwater Pump Lube Oil

Pump

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Monitor input To Room Ventilation Trouble Alarm

WO 9614600

Remove 21 CW Pump for Rebuild

b.

Observations and Findinas

For SP 11068, the inspectors noted that step 1.3 of the monthly test

specified that,in January of each year, the diesel cooling water pump be

started by simulating low cooling water header pressure instead of the

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normal manual start pushbutton actuation that was used the other eleven

months of the year. SP 1106A, "12 Diesel Cooling Water Pump Test,"

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Revision 52, had a similar requirement for the redundant pump.

The inspectors noted that Technical Specification 4.5.B.1.b required that "a

test consisting of a manually-initiated start of each diesel engine, and

assumption of load within one minute, shall be conducted monthly." The

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inspectors questioned whether the low pressure actuation met the literal

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interpretation of the Technical Specifications. The operators were required

to isolate and manually bleed pressure from the low cooling water header

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pressure actuation switch, but actuation of the switch then resulted in an

- automatic start of the diesel-driven pump.

A licensee engineering supervisor informed the inspectors that all monthly

tests were done using the low pressure actuation circuit until about 1991

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when the test was simplified to use the start pushbutton for eleven of

twelve monthly tests. Technical Specifications did not specifically require a

test of the low pressure actuation although Updated Safety Analysis Report,

Section 10.4.1.2, stated that the low pressure start of the pumps was part

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of the design basia response to a loss of offsite power.

For recent tests, the licensee had performed the tests using manual

pushbutton actuation on December 21 and December 20,1996, for the 12

and 22 pumps respectively, and again on February 14,1997, for both

pumps. However, the tests were done using a low pressure actuation on

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January 17 and January 20,1997, for the 12 and 22 pumps respectively.

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The issue was cons'idered an Unresolved item pending an interpretation from

the NRC Office of Nuclear Reactor Regulation of the meaning of the term

" manually-initiated" in the Technical Specification. (282/97002-02)

While reviewing SP 1106B and Updated Safety Analysis Report (USAR),

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Section 10.4.1, " Cooling Water System," the inspectors noted that all

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routine surveillance tests of the diesel-driven cooling water pumps consisted

of starting and stopping the pumps from the local control stations in the

plant screenhouse. USAR Section 10.4.1.1 stated, "The system is

monitored and operated from the Control Room." The inspectors questioned

whether the ability of the pumps to be started and stopped from the control

room, which was part of the design basis, was ever tested. The system

engineer could find no such test and stated that he intended to add a start

and stop, using the control room switch, to the annual preventive

maintenance procedure for the pumps. This issue was considered an

Inspection Followup Item pending completion of the licensee's actions and

review by the NRC of whether demonstration of the ability to operate the

system in accordance with that part of the design basis was a requirement.

(282(306)/97002-03)

For WO 9607676 and WO 9607678, the inspectors noted that the

construction crews had installed the valve label wires through the T-drain

holes on the drains on the Limitorque operator. The inspectors were

concerned that if the valves were environmentally qualified (EO) for a harsh

environment the T-drains needed to be kept free of obstructions for the

valves to meet their design basis.

The inspectors were informed by the system engineer that those particular

valves were not in the EQ program. He had the valve tags moved to a

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proper location on the valve anyway. The EO engineer agreed that is was a

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poor practice to hang tags with wires through T-drains, even on non-EQ

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valves. He wrote a memo to the staff r6 minding them not to do that. The

EO engineer also stated that he did a walkdown near the end of each

refueling outage to examine all EG squipment for any deficiencies that might

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affect their qualification.

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The inspectors found no other valve tag wires through T-drains on any EO or

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non-EO valves. The inspectors had no further concerns it' this area.

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For WO 9612068, the inspectors noted that one of the safety valves that

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the licenses was preparing to install on the relief header was missing its

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release nut. The inspectors contacted the system engineer who agreed that

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the nut should have been present on the valve. The system engineer -

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determined that the valve in question (a used valve kept as a spare) had

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been in storage in the warehouse for some time before being sent to a

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vendor for refurbishment and testing. Apparently the release nut had been

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scavenged while it was in storage. The licensee's quality services

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representative at the vendor during the testing confirmed that the nut was

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not present while the valve was at the vendor.

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The quality services department checked the receipt inspection records but

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the presence of all parts was not one of the attributes checked when the

valve was returned from the vendor. However, the inspectors determined

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that the system engineer was very aware' of NRC Information Notice 96-61,

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" Failure of a Main Steam Safety Valve To Reseat Caused by an improperly

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installed Release Nut," which discussed problems with the release nuts and

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he undoubtedly would have noticed the missing nut before the valve was put

into service.

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The system engineer immediately revised WO 9612068 to add a step to

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ensure the nut was installed before the valve was put into the system. He

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also wrote work order 9700810 to accomplish the installation of the nut.

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That work order was completed the same day using a nut salvaged from a

valve being removed. Quality services added a verification step for the nut's

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installation to the original work order and also wrote an employee

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. observation report to investigate the adequacy of the receipt inspection.

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The missing nut would have had no safety significance because it did not

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affect the ability of the valve to automatically relieve at its set pressure. The

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missing nut would only have prevented manual actuation of the safety valve

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using the actuation lever. Manual actuation was not required for mitigation

of any accident. However, the finding indicated a potential weakness in the

licensee's control of salvaged parts from equipment in the warehouse,

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For WO 9614600, the inspectors observed on February 19,1997, that the

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No. 21 Circulating Water (CW) pump internals were to be lifted from the

casing thorouph the screenhouse roof using a mobile crane. A similar

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situation was observed for WO 9700434 for the No. 22 CW pump motor.

The inspectors were concemed that the load path of the 15000 lb. pump

and 40000 lb. motor was in close proximity to the area of the screenhouse

roof over safe shutdown equipment. However, the inspectors observed

these lifts were performed using a safe load path verbally designated by the

system engineer to the nggers.

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A further discussion of this issue regarding control of heavy loads using

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mobile cranes is discussed in Section M3.1.

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c.

Conclusions

inspector-cbserved maintenance and surveillance activities were generally well

conducted with good communications, proper pre-job planning, safe work practices,

and coordination between departments. The inspectors noted good system

engineer involvement in all phases of maintenance and surveillance activities. With

the exception of the control of heavy loads discussed elsewhere in this report,

activities observed were performed acceptably.

M1.2 Failure to Follow Procedure for Movement of Heavy Load Over the Reactor

a.

Insoection Scone (62703. 92902,92901)

The licensee identified on February 4,1997, that the Unit 2, No. 22 reactor coolant

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pump (RCP) motor rotor and upper bracket had been lifted over the open reactor

vessel containing irradiated fuel, in violation of the heavy loads procedure. The

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inspectors reviewed the circumstances of the event and the licensee's corrective

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actions,

b.

Observations and Findinas

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On February 3, RCP No. 22 rotor and bracket (approximately 21 tons) was lifted

from its vault with the polar crane, transported over the open flooded reactor cavity

(vessel head removed, core filled with irradiated fuel), and placed on the motor

stand on the refueling floor. Both doors of the containment maintenance and

personnel airlocks were open and the inservice purge system was operating.

The purpose of moving the rotor was to perform RCP preventive maintenance per

Work Order (WO) 9608888. This WO implemented Procedure D15.2, Revision 14,

" Reactor Coolant Pump Motor Cleaning Procedure," which directed maintenance

personnel to " follow the instructions and guidelines in D58 on heavy load

movement." Procedure D58, Revision 25, " Control of Heavy Loads," step 5.3.1,

required that with the reactor head removed, loads greater than 2100 lbs. shall not

be moved within 15 horizontal feet of the irradiated fuel without specific written

procedures. Step 5.8 of D58 required having at least one isolation valve closed in

each line which penetrates the containment and provides a direct path from the

containment atmosphere to the outside when a heavy load is moved over the

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reactor vessel. The above requirements in D58 are also identified in USAR

Section 12.2.12.1.4.

Procedure D58 was not referred to prior to the lift. The RCP engineer believed it

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may have been possible to move the load around the vessel, however, it was not.

Riggers and the RCP engineer questioned if it was acceptable to transport the load

across the cavity. The RCP engineer informed the inspectors that a reactor

engineer was consulted and the shift supervisor was consulted and concurred.

Therefore, the riggers performed the lift under the assumption that the shift

supervisor approved it. The shift supervisor informed the inspectors that he told

the engineer Dgi to go over the vessel. He thought that it was acceptable to lift the

rotor around the vessel (along the edge of the refueling cavity), but he did not refer

to D58 for guidance and was not aware of the 15 foot separation distance

requirement.

,

Early during day shift on February 4, maintenance personnel intended to return the

RCP rotor to its vault following completion of maintenance. The inspectors were on

-

the refueling floor to observe fuel handling activities. The Senior Reactor Operator

(SRO) in charge of fuel handling was preparing to initiate core alterations and 'was

consulted by the riggers about the plan to return the rotor to the vault and he

directed the lead rigger to contact the shift supervisor. The SRO in charge of fuel

handling later informed the inspectors that he felt uncomfortable with this lift

occurring during fuel handling and informed the shift supervisor. When the shift

supervisor was contacted, he questioned the appropriateness of the activity with

the outage shift manager. The outage shift manager determined that this lift did

not comply with the requirements of D58. Therefore, the riggers were not allowed

to perform the lift. After further evaluation, the licensee determined that a separate

procedure was required to be written to perform the lift which included the

containment closure requirements. An acceptable procedure was written and

approved by the onsite safety review committee on February 5 and the lift was

performed with the D58 requirements implemented.

An error reduction task force investigation was initiated by the licensee to review

the event, and recommend corrective actions. Short term corrective actions

included conducting training on the requirements of D58 for all riggers and

maintenance repairmen and development of a checklist placed at the controls of

plant cranes as a reminder of heavy load restrictions.

The licensee concluded that it did not meet its commitments in implementing

NUREG-0612 for control of heavy loads inside of containment and also concluded

that the event was reportable as a condition outside of the design basis 9 nause

their analysis for dropping of a heavy load on irradiated fuel assumed ' s

containment would be closed.

10 CFR 50, Appendix B,. Criterion V, stated,in part, that activities affecting auality

shall be prescribed by documented instructions, procedures, or drawings, of a type

appropriate to the circumstances and shall be accomplished in accordance with

these instructions, procedures, or drawings. Procedure D58, Revision 25, " Control

13

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of Heavy Loads," step 5.3.1, required that with the reactor head removed, loads

greater than 2100 lbs. shall not be moved within 15 horizontal feet of the irradiated

fuel without specific written procedures. Step 5.8 of D58 required having at least

one isolation valve closed in each line which penetrates the containment and

provides a direct path from the containment atmosphere to the outside when a

heavy load is moved over the reactor vessel.

On February 3,1997, the No. 22 reactor coolant pump motor rotor and upper

bracket (a heavy load greater than 2100 lbs.) was moved with the Unit 2 polar

crane over the open reactor vessel and irradiated fuel without a written procedure

and without containment closure. This was considered an apparent violation.

(EA 97-073)

c.

Conclusions

An apparent violation was identified for failure to follow the requirements of

Procedure D58. Engineering, maintenance, and operations personnel did not know

or understand the requirements of D58 and did not refer to it as instructed or when

a question was identified. Weak communications were evident between workers in

the field and the main control room. The inspectors previously identified a non-

cited violation in Inspection Report 282(306)/95012 for failure to use a written

procedure for movement of a heavy load in the turbine building over the safeguards

bus rooms.

M1.3 Refuelino Outaae Activities

a.

Insoection Scooe (61726, 62707. 92902)

The inspectors observed planning and scheduling activities for the Unit 2 refueling

outage, daily outage update meetings, and portions of numerous outage work

,

activities.

,

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b.

Observations and Findinos

The inspectors noted that the outage plan was well-developed and comprehensive.

Very few problems were noted with job interferences or scheduling problems. The

licensee used " green, yellow, orange, and red" designations to monitor the status

of five significant shutdown safety parameters. Those were decay heat removal,

'

reactor coolant system inventory control, electrical power availability, reactivity

i

control, and containment integrity. The entire outage schedule contained no

planned entries into " orange or red" conditions of redundancy and capability of

maintaining those parameters in a safe condition. As of the end of this inspection

period, there had been no unplanned entries into " orange or red" conditions either.

The inspectors noted generally good execution of outage work. Time estimates for

jobs in the outage plan were fairly accurate but no pressure to hurry jobs was noted

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when they were behind schedule. Outage scope additions were smoothly

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incorporated into the plan. Teamwork was evident and excellent communications

between all groups involved in the executien contributed to the success,

c.

Conclusions

Careful planning and safe execution of outages has been a significant strength of

the licenses in the past and continued to be strong in the Unit 2 refueling outage

during this inspection period.

M3

Maintenance Procedures and Documentation

M3.1 Control of Heavv Loads with Mobile Cranes

a.

Insoection Scone (62703. 92902)

As discussed in Section M1.1, the inspectors had a concern with the control of

heavy loads using a mobile crane and potential impact on safe shutdown

equipment. The inspectors reviewed the following work orders (WOs) and

procedures:

1

e

WO 9700434

Remove 22 CW Motor for Cleaning and Inspection

i

e

WO 9614599

Remove 21 CW Motor for Cleaning and Inspection

WO 9614600

Remove 21 CW Pump for Rebuild

D58

Control of Heavy Loads, Revision 26

1

b.

Observations and Findinos

'

The WOs addressed the use of a mobile crane to lift the loads from the Unit 2

circulating water (CW) pump area through an opening in the screenhouse roof. The

WOs identified the weight of the loads, however, they did not identify a safe load

path around the area of the roof that covered safe shutdown equipment in

screenhouse. Also, a safe load path area was not marked on the roof of the

screenhouse. Support equipment was located on the roof of the screenhouse and

damage to these components could have impacted operability of safe shutdown

equipment.

The inspectors reviewed Procedure D58 and determined that it did not address the

use of mobile cranes for handling loads in proximity to safe shutdown equipment.

As discussed in NUREG-0612, " Control of Heavy Loads at Nuclear Power Plants,"

safe load paths should be defined for movement of heavy loads to minimize the

potential for heavy loads, if dropped, to impact safe shutdown equipment.

Additionally, procedures should be developed to cover load handling operations for

heavy loads that are or could be handled over or in proximity to safe shutdown

equipment.

10 CFR 50, Appendix B, Criterion V, states,in part, that activities affecting quality

shall be prescribed by documented instructions, procedures, or drawings, of a type

15

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ed

e

appropriate to the circumstances and shall be accomplished in accordance with

these instructions, procedures, or drawings. Procedure D58, " Control of Heavy

Loads," Revision 26, was inadequate for the circumstances in that it did not

contain administrative controls for handling heavy loads over or in proximity to safe

shutdown equipment located in the screenhouse nor instructions for the evaluation

of the use of mobile cranes from reactor safety standpoint in general. This was

i

considered a violation. (306/97002-04)

c.

Conclusions

The actuallifts that the inspectors observed were performed with a load path that

avoided safe shutdown equipment in the screenhouse so this particular evolution

had only minor safety significance. The system engineer who planned the work

reviewed D58, but because it contained no instructions pertaining to the job he was

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planning, he concluded that the administrative controlt;it contained did not apply.

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The inspectors concluded that D58 was too narrowly focused in that it only

addressed permanently installed cranes. Failure to properly control the load paths

of heavy loads using mobile or other temporary cranes could result in a serious

i

event.

M8

Miscellaneous Maintenance issues (92700, 92902)

M8.1 (Closed) Licensee Even Reoort (LER) 282(3061/96-06: Cooling Water Surveillance

Tests Missed as a Result of a Rescheduling Error. This event was previously

discussed in Inspection Report 282(306)/96002, Section 2.7. The inspectors

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verified that corrective actions discussed in the LER had been completed. No

additional events of the same type have occurred since LER 96-06.

M8.2 (Closed) Violation 282/96008-04 and (Closed) Violation 282/96008-05: Failure to

Promptly identify and Correct an Adverse Condition. These issues were discussed

in inspection Reports 282(306)/96008, Sections M1.2, M3.1, and M8.1; the

associated Notice of Violation; and 282(306)/96010, Section M8.4. The licensee

replied to the violations in a letter to the NRC dated November 6,1996. The

'

inspectors verified that corrective actions discussed in the reply had been

completed.

M8.4 (Closed) Violation 282/96008-08: Failure to Make a Timely Report of an Operation

Prohibited by Technical Specifications. This issue was previously discussed in

inspection Report 282(306)/96008, Section M8.1, and the associated Notice of

'

Violation. The licensee replied to the violation in a letter to the NRC dated

November 6,1996. The inspectors verified that corrective actions discussed in the

reply had been completed. Administrative Work Instruction 5AWI 3.6,0,

" Reporting," Revision 6, was issued on December 31,1996. It directed that the

site licensing department be properly informed by the shift manager of events that

will require a Licensee Event Report in accordance with 10 CFR 50.73 but not an

Emergency Notification System callin accordance with 10 CFR 50.72.

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d

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M8.5 (Closed) Violation 282/96010-03: Failure to Adequately Perform Check Valve

Tests. This issue was previously discussed in inspection Reports 282(306)/96010,

Section M3.2: the associated Notice of Violation; and 282(306)/96014,

Section M8.1. The licensee replied to the violation in a letter to the NRC dated

December 5,1996. The inspectors verified that the appropriate changes had been

made to surveillance procedures SP 1355, " Checking Chemical Feed and Auxiliary

Feedwater Check Valves - Unit 1," Revisior; 7, and SP 2355, " Checking Chemical

Feed and Auxiliary Feedwater Check Valves - Unit 2," Revision 3, to prevent

recurrence of the violation. One corrective action in the licenree's reply to the

violation, to conduct procedure walkthroughs, was not yet completed because it

was longer term in nature. However, the inspectors determined that it was

progressing satisfactorily.

M8.6 (Closed) Licensee Event Reoort 282(306)/96-15: Auto-start of No. 22 Diesel

Cooling Water Pump on Low Header Pressure During Surveillance. This event was

previously discussed in inspection Reports 282(306)/96008, Section M3.2, and

282(306)/96010, Section M8.5. The inspectors reviewed Surveillance Procedures

SP 1106A, "12 Diesel Cooling Water Pump Test," Revision 51, SP 1106B, "22

Diesel Cooling Water Pump Test," Revision 49, and SP 1106C, "121 Cooling Water

Pump Test," Revision 8, and noted that they were significantly improved over

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previous revision from a human factors standpoint.

lil. Enoineerina

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E1

Conduct of Engineering (92903)

During this inspection period a detailed inspection of the licensee's inservice inspection

program was conducted by a regional inservice inspection (ISI) specialist and was

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documented in inspection Report 282(306)/97003.

In addition, conference calls, meetings, and correspondence occurred between the NRC

and licensee on the topics of proposed license amendments for F' tube rolling in steam

generators and resolving the unreviewed safety question regarding the emergency cooling

water intake line discussed in inspection Report 282(306)/96015.

E2

Engineering Support of Facilities and Equipment

E2.1

Review of Uodated Safety Analysis Reoort (USAR) Commitments (37551)

While performing the inspections discussed in this report, the inspectors reviewed

the applicable portions of the USAR that related to the areas inspected and used

the USAR as an engineering / technical support basis document. The inspectors

compared plant practices, procedures, and/or parameters to the USAR descriptions

as discussed in each section. One Inspection Followup Item was identified because

there were no tests to demonstrate that the cooling water pumps could be operated

from the control room as described in the USAR (Section M1.1.b).

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E2.2 ' System Enoineer Suonort of Outaae Activates (37551)

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While observing refueling outage operations and maintenance activates described

elsewhere in this report, the inspectors noted strong system engineer involvement

in the work. System engineers were frequently observed at the job sites or

monitoring operations from the control room. Operations and maintenance

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department personnel often consulted system engineers and were consistently

provided with prompt support. The inspectors concluded that system engineering

)

support of the outage was excellent.

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E8

Miscellaneous Engineering issues (92700, 92903)

i

E8.1

(Closed) Violation 282/96007-04: Exceeding Technical Specifications Limiting

Conditions for inoperability of Post Accident Containment Hydrogen Monitors.

This issue was previously discussed in inspection Reports 282(306)/96007,

Section E8.1; the associated Notice of Violation; and 282(306)/96006,

Section M2.2. The licensee replied to the violation in a letter to the NRC dated

i

October 13,1996. The inspectors verified that the appropriate changes had been

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made to maintenance procedure D87, " Containment Hydrogen Monitor Calibration

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Gas Fill," and system technical manual. Training was conducted for technicians

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and engineers on the event, including discussions of the contributing cause;

procedural adherence problems in the work control, post-maintenance testing, and

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technical manual revision process areas. One corrective action to the violation, to

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consider upgrade of the calibration assemblies, was not yet completed because it

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was longer term in nature. However, the inspectors determined that it was

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progressing satisfactorily.

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IV. Plant Suncort

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R1

Radiological Protection and Chemistry Controls (71750)

h

During normal resident inspection activities, routine observaticns were conducted in the

- areas of radiological protection and chemistry controls using Inspection Procedure 71750.

.

No discrepancies were noted. During this inspection period an additional inspection was

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conducted by a regional radiation protection specialist and was documented in inspection

!

Report 282(306)/97004.

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P1

Conduct of Emergency Preparedness Activities (71750)

!

During normal resident inspection activities, routine observations were conducted in the

- area of emergency preparedness using inspection Procedure 71750. No discrepancies

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were noted. The inspectors became aware of the start of major construction work to

upgrade Sturgeon Lake Road. All traffic to and from the plant had to travel on a portion of

the road being worked on. The improvements were to include raising the level of the

i

roadway and widening it to two lanes in each direction. The inspectors were informed

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that the intent of the project managers was to maintain two-way traffic throughout the

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project so that emergency evacuation from the area and emergency response to the plant

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would not be significantly affected. The inspectors concluded that licensee emergency

preparedness personnel were adequ';tely monitoring the project.

S1

Conduct of Security and Safeguards Activities (71750)

During normal resident inspection activities, routine observations were conducted in the

areas of security and safeguards activities using Inspection Procedure 71750. No

discrepancies were noted.

F1

Control of Fire Protection Activities (71750)

During normal resident inspection activities, routine observations were conducted in the

area of fire protection activities using Inspection Procedure 71750. No discrepancies were

noted.

V. Manaaement Meetinas

X1

Exit Meeting Summary

The inspectors presented the inspection results to members of the licensee management at

the conclusian of the inspection on February 20,1997. The licensee acknowledged the

findings prosented.

The insractors asked the licensee whether any materials examined during the inspection

i

should be considered propthtary. No proprietary information was identified.

19

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PARTIAL LIST.0F PERSONS CONTACTED

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Licensee

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- J. Sorensen, Plant Manager

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K. Albrecht, General Superintendent Engineering

J. Goldsmith, General Superintendent Design Engineering

R. Held, Outage Planner

J. Hill, Manager Quality Services

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G. Lenertz, General Superintendent Plant Maintenance

J. Maki, Outage Manager

D. Schuelke, General Superintendent Radiation Protection and Chemistry

M. Sleigh, Superintendent Security

P. Valtakis, General Superintendent Plant Operations (Acting)

INSPECTION PROCEDURES USED

IP 37551:

Onsite Engineering

IP 61726:

Surveillance Observations

IP 62707:

Maintenance Observations

IP 71707:

Plant Operations

IP 71750:

Plant Support Activities

IP 92700:

Onsite Follow-up of Written Reports of Nontoutine Events at Power Reactor

Facilities

IP 92901:

Followup - Operations

IP 92902:

Followup - Maintenance

IP 92903:

Followup - Engineering

Part 9900:

Technical Guidance - Licensee Technical Specifications interpretations

ITEMS OPENED, CLOSED, AND DISCUSSED

Onened

-282/97002-01

NCV Failure to identify a Change to the Design of Purchased

Equipment

282/97002-02

URI

Question Regarding Whether Surveillance Testing of the

Cooling Water Pumps Fulfills a Technical Specification

Requirement

282/97002-03

IFl

No Test to Demonstrate that the Cooling Water Pumps can be

Operated From the Control Room as Described in the Design

Basis

306/97002-04

VIO

_ Inadequate Procedure for the Control Of Heavy Loads

282(306)/97-01

LER

Auxiliary Building Crane Protective Features Defeated by

Wiring Errors

20

a

s

W

Closed

282/96002-01

VIO

Four Examples of Operators Failing to Follow Procedures

During a Refueling Outage

282(306)/96-06

LER

Cooling Water Surveillance Tests Missed as a Revilt of

Rescheduling Error

282/96007-04

VIO

Containment Hydrogen Monitors inoperable

282/96008-01

IFl

Technical Specification for Shift Manning did not Meet

10 CFR 50.54 Requirements

282/96008-02

IFl

Maintaining Operator Licenses in an Active Status

282/96008-04

VIO

Failure to Promptly identify an Adverse Condition

282/96008-05

VIO

Failure to Promptly Correct an Adverse Condition

282/96008-08

VIO

Failure to Make a Timely Report of an Operation Prohibited by

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Technical Specifications

,

282/96010-03

VIO

Failure to Adequately Perform Check Valve Surveillance Tests

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306/96014-01

VIO

Failure to Demonstrate Operability of the Redundant Diesel

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Generator with one Diesel Generator inoperable

282(306)/96-15

LER

Auto-start of No. 22 Diesel Cooling Water Pump on Low

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Header Pressure During Surveillance

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Discussed

None

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LIST OF ACRONYMS USED

i

CFR

Code of Federal Regulations

CW

Circulating Water

EQ

Environmentally Qualified

IFl

Inspection Followup item

IP

inspection Procedure

ISFSI

Independent Spent Fuel Storage Installation

ISI

Inservice Inspection

ISTS

Improved Standardized Technical Specifications

LER

Licensee Event Report

LOCA

Loss of Coolant Accident

NRC

Nuclear Regulatory Commission

NSP

Northern States Power Company

I

PDR

Public Document Room

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RCP

Reactor Coolant Pump

RCS

Reactor Coolant System

SP

Surveillance Procedure

SRO

Senior Reactor Operator

USAR

Updated Safety Analysis Report

TS

Technical Specifications

URI

Unrcsolved item

VIO

Violation

WO

Work Order 21

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)