ML20135A440

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Insp Repts 50-373/96-10 & 50-374/96-10 on 960803-960913. Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support
ML20135A440
Person / Time
Site: LaSalle  
Issue date: 11/26/1996
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20135A422 List:
References
50-373-96-10, 50-374-96-10, NUDOCS 9612030222
Download: ML20135A440 (11)


See also: IR 05000373/1996010

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U.S. NUCLEAR REGULATORY COMMISSION

REGION 111

Docket No:

50-373, 50-374

License No:

NPF-11, NPF-18

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Report No:

50-373/96010, 50-374/96010

Licensee:

Commonwealth Edison Company

Facility:

LaSalle County Station, Units 1 and 2

Location:

2601 N. 21st Road

Marseilles, IL 61341

Dates:

August 3 - September 13, 1996

Inspectors:

M. Huber, Senior Resident Inspector

K. Ihnen, Resident Inspector

H. Simons, Resident Inspector

J. Roman, Illinois Department of Nuclear Safety

Approved by:

Bruce Jorgensen, Acting Chief

Reactor Projects Branch 5

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9612030222 961126

PDR

ADOCK 05000373

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PDR

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EXECUTIVE SUMMARY

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LaSalle County Station, Units 1 and 2

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NRC Inspection Report 50-373/96010; 50-374/96010(DRP)

This inspection report included aspects of licensee operations, maintenance,

engineering and plant support. The report covers a 6-week period of

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inspection conducted by the resident inspectors.

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Plant Operations

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Comed took good initiative to perform a review of their Technical

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Specification (TS) interpretations. However, they found that 17 of 43

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interpretations were not fully compatible with the licensing or design

basis of the plant.

The licensee initiated corrective actions including

upgrading their process for review and approval of TS interpretations.

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Maintenance

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Materiel condition problems continued to challenge the operations,

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maintenance, and engineering organizations.

Emergent equipment problems

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resulted in difficulties for the maintenance organization in

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accomplishing scheduled work. These problems challenged operations in

that, in several cases, the plant was placed in short-duration limiting

conditions for operations.

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Enaineerina

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The conduct of root cause analyses for both the 0 diesel generator (DG)

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output breaker failure and reactor core isolation cooling (RCIC) rupture

disc event were weak.

In both cases, the root cause team made non-

conservative recommendations to the plant operations review committee

(PORC) regarding the operation of plant equipment.

In one case, they

recommended bypassing a protective relay on the DG.

In the RCIC event,

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they recommended preconditioning the plant equipment.

In both cases,

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PORC performed their function and did not approve the root cause team

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recommendations.

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ReportDetails

Summary of Plant Status

Unit 1 operated at or near full power for the entire inspection period.

Unit 2 entered the period at 96% power, derated because of thermal limit

concerns due to power suppression in the area of two previously identified

leaking fuel assemblies. On August 18, 1996, main turbine control valve (TCV)

  1. 2 partially closed and then reopened. The valve position continued to

oscillate.

The decision was made to close the valve and limit power to 83%.

The unit operated at the reduced power for the remainder of the period.

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Doerations

01

Conduct of Operations

01.1 General Comments (71707)

The inspectors conducted frequent reviews of ongoing plant operations.

Walkdowns were performed in the main control room, emergency diesel

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generator rooms, auxiliary electrical equipment rooms, safety related

pump rooms, the reactor building, and the turbine building. The

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inspectors also discussed plant status and pending evolutions with shift

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personnel in the control room.

01.2 Shift Operatina Activities

a. Insoection Scope

On several occasions, the operating shift was required to respond to

indications of equipment performance problems.

For each event, the

inspector reviewed the symptoms, causes and consequences, along with

licensee response and decisionmaking.

On August 8, Operations identified that the lake makeup line was not

supplying makeup water as designed. A search revealed a break in this

5-mile concrete supply pipe approximately a mile from its source at the

Illinois river.

Repairs to the makeup line were pursued on a high-

priority basis, to ensure the absence of lake makeup would not impact

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adversely on the cooling lake, particularly on the capability to

maintain level in the ultimate heat sink well above the necessary

minimum.

On August 18, the #2 turbine control valve (TCV) on the Unit 2 main

turbine unexpectedly closed.

It immediately re-opened. Operations had

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done nothing to precipitate the erratic TCV behavior, so they

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immediately focused closely on this valve.

Small oscillations continued

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to occur, leading to a decision to manually close the valve and keep it

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closed. This decision resulted in a need to reduce reactor power to

about 83% of full power for the last several weeks of the plant

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operating cycle leading up to a scheduled refueling outage. The

decision provided protection from TCV-induced transients and was

considered prudent by the inspectors.

The shared, "0" emergency diesel-generator was found to have a failed-

open backwash valve during a routine operator round on September 6,

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1996. This led operations to declare the diesel-generator inoperable

and enter a 72-hour LCO. The inspector received the circumstances and

found the licensee correctly applied the LCO.

On September 7, operations encountered difficulty in maintaining the

required reactor building differential pressure.

Prompt diagnosis of

the problem indicated the control system was malfunctioning, so the

operators decided to switch the ventilation system to manual control.

The inspector noted good coordination with engineering in the

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installation of a temporary alteration to provide manual control

capability. This restored differential pressure to the required level.

In addition, the inspector verified that the correct LC0 was applied.

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b. Conclusions

Operations correctly diagnosed the problems encountered and applied the

correct Limiting Condition for Operation or other prudent control to

successfully overcome each difficulty.

Coordination with maintenance

and/or engineering was good.

01.3 Licensee Review of Technical Soecification (TS) Clarifications

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a. Inspection Scope (71707)

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The inspectors reviewed the licensee's efforts to verify that the TS

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clarifications written by the licensee conform to the current licensing

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and design basis of the plant. The inspector discussed several of these

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clarifications with the licensee staff and attended the Plant Operations

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Review Committee (PORC) meeting which reviewed the issue.

b. Observations and Findinas

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Comed assigned a review team to conduct a complete review of their TS

clarifications. These clarifications were written interpretations

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provided to the control room personnel to assist in interpreting TSs.

There were a total of 43 TS clarifications. The review team determined

that 17 of the TS clarifications were not compatible with the current

licensing or design basis.

Fourteen of the 43 clarifications were in

accordance with the licensing and design basis; however, the safety

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evaluations associated with these clarifications had been performed

several years ago and the quality was not in accordance with Comed's

current standards. As a result, the licensee decided to re-perform the

50.59 evaluations and have the PORC review the upgraded 50.59s. Seven

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of the 43 clarifications were determined to be valid; however, the

licensee determined that these clarifications should be controlled via

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other administrative methods such as in procedures. The safety

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evaluations for these clarifications will be reviewed by PORC as the

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clarifications are moved to other administrative controls.

Five of the

43 were determined to be acceptable by the review team with respect to

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the licensing and design basis, and they had an appropriate safety

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evaluation. These five clarifications were retained with no further

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actions.

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The problems with the TS clarifications were discussed at a PORC meeting

on August 30, 1996. The PORC decided to cancel the 17 questionable

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clarifications and approve the five clarifications that the review team

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identified as meeting the design and licensing basis. The other

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clarifications and the upgraded safety evaluations will be reviewed by

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PORC at a later date.

In addition to initiating corrective actions to

address the immediate concerns identified by the TS interpretation

reviews, the licensee initiated corrective actions to upgrade their

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process for review and approval of TS clarifications.

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At.the end of the inspection period, the licensee was reviewing the

clarifications that were canceled to evaluate if there were any events

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involving these clarifications that were required to be reported in

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accordance with 10 CFR 50.72 and 50.73.

c. Conclusion

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Comed took good initiative to perform a review of their TS

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interpretations, and the review criteria and depth were of good quality,

iiowever, they found that 17 of 43 interpretations were not compatible

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with the licensing or design basis of the plant. The licensee has

initiated corrective actions including upgrading their. process for

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review and approval. of TS interpretations. The licensee's initial

review determined that a Licensee Event Report (LER) would be required.

The inspectors will follow this issue through the LER.

II.

Maintenance-

M1

Conduct of Maintenance

The inspectors observed several maintenance and surveillance activities

during this inspection period in accordance with inspection procedure

62703 and 61726.

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M1.1 Routine Activities

a. Insoection Scone (62703. 61726)

The inspectors observed routine (typically, monthly) maintenance and

surveillance activities as they were being performed or conducted in the

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plant and discussed the activities with the personnel performing them.

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b. Observations and Findinas

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The routine surveillance of emergency diesel generator IA was observed

and reviewed against criteria established in the UFSAR, the technical

specifications and the controlling test procedure.

The personnel-

performing the test were closely following the test procedure.

Communications and coordination among involved personnel were good. The

test results met all the required criteria.

Surveillance testing of the Unit I standby gas Treatment system was

observed in detail. The inspector reviewed the applicable procedure,

technical specifications and UFSAR information and discussed system

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performance with personnel conducting the test.

Knowledge and

understanding of the involved personnel were good; the test was

successfully completed in conformance to all specified performance

criteria.

c Conclusions

Routine test activities were successfully performed in accordance with

applicable controls by personnel who were knowledgeable and who

coordinated their activities well. No significant problems were

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observed in the conduct of these activities.

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M2

Maintenance and Material condition of Facilities and Equipment

M2.1 Materiel Condition Continued to Impact Operation and Scheduled Work

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a. Insoection ScoDe (71707. 62703)

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The inspectors followed the daily scheduled work and emergent

equipment problems to assess materiel condition.

b. Observations and Findinas

As noted above, during this inspection, several equipment failures

occurred which continued to challenge operations and affect the conduct

of scheduled work.

For example, operations identified that there was a break in the lake

makeup line on August 8, 1996. The lake makeup line is a 5-mile stretch

of concrete pipe which connects the LaSalle cooling lake (ultimate heat

sink) to the Illinois River. As a result of this failure, significant

engineering and mechanical maintenance resources were diverted to repair

the line. The licensee has experienced previous breaks of the lake

makeup line. The inspectors periodically monitored the work activities

associated with this job. The work was completed in good time to ensure

the cooling lake and the ultimate heat sink always had more than

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adequate water level.

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On September 6,1996, the licensee identified', during a system walkdown,

that the backwash valve on the 0 DG cooling water strainer had failed

open with a potential stem to disc separation. The 0 DG was declared

inoperable and a 72-hour Limiting Condition for Operation (LCO) was

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entered. The' resultant emergent work challenged the operations,

maintenance, and engineering departments. The inspector observed work,

monitored progress and schedule and followed return-to-service

activities. Although challenging,' the work was properly completed

within the limits of the LCO.

On September 7,1996, operations experienced problems with the reactor

building differential pressure. - A temporary alteration was installed to

operate the reactor building ventilation manually such that

troubleshooting could be done on the control system where the problem

apparently originated. The problem was traced to a failed controller.

This problem challenged operations by placing them in a 4-hour LCO for

secondary containment and it also challenged the maintenance

organization because of its emergent nature. The inspector reviewed the

activity and the control system history, and found the work was

completed properly and in compliance with LCO requirements.

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c. Conclusion

Materiel condition problems continued to challenge the operations,

maintenance, and engineering organizations.

Emergent equipment problems

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were handled successfully, but they resulted in difficulties for the

maintenance organization to. accomplish scheduled work and caused the

engineering organization to focus on reactive rather than proactive

activities. These problems also' challenged operations in that, in

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several cases, the plant was placed in short duration LCOs.

In each

case, LC0 requirements were met.

III.

Enaineerina

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Conduct of Engineering

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El.1 Enaineerina Root Cause Analysis of 0 DG Failure

a. Scone (37551)

The inspectors observed the troubleshooting activities for the 0 DG

after the output breaker for Unit I failed to close during surveillance

testing following maintenance. The inspectors also observed the root

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cause analysis effort.

b. 0bservations and Findinas

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On August 14, 1996, the 0 DG was being run in accordance with LOS-DG-M1,

"O Diesel Generator Operability Test," Revision 31, when the output

breaker failed to close on Unit 1.

Operations personnel notified system

engineering and maintenance of the problem.

The initial troubleshooting was not performed using the available

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procedure. The purpose of LTP-500-1, " Diesel Generator Output Breaker

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Troubleshooting Procedure," Revision 6, as stated in the procedure, is

to determine the failure mode in the event that a DG output breaker

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fails to close during its monthly operability surveillance.

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engineer and electrician did not use this procedure; instead they

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performed troubleshooting based on their personal knowledge using a

controlled electrical print. The system engineer and electrician were

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unaware that LTP-500-1 existed. This failure to follow procedures is a

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violation of 10 CFR 50, Appendix B, Criterion V (VIO 373;374/96010-01).

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As a result, the troubleshooting w'as not well documented. The next day

most of the initial troubleshooting had to be re-performed because of

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the uncertainty of the tests that had already been conducted. At that

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time, there were only about 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> left of the 72-hour LCO.

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While the troubleshooting was taking place, a root cause team assembled

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to assist in identifying the root cause. This team became narrowly

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focused on one component during the troubleshooting activities. The

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team was focused on the synchronization check (HACR) relay as the root

cause, partly due to past equipment problems with this relay. This

relay provides a protective function when paralleled with an outside

source in that it requires the DG to be in-phase in order to close the

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output breaker.

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The root cause team recommended jumpering out the relay even though

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there were spare calibrated relays onsite. Also, by early afternoon on

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August 15, troubleshooting had ruled out the possibility of a problem

with the HACR relay.

Even after troubleshooting ruled out the HACR

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relay as the cause, the root cause team took a procedure change to the-

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PORC for approval. This procedure change allowed jumpering out the HACR

relay. The PORC made the good decision to disapproved the proposed

procedure change.

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Further troubleshooting identified a failed component in the starting

circuitry, specifically, the interposing relay. This component was

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replaced and the DG was tested satisfactorily.

c. Conclusigni

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The PORC decision was a good decision, because the root cause team did

not present a' valid reason for needing the procedure.

In addition, it

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was viewed as a non-conservative action to bypass the DG's protective

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equipment.

El.2 Enaineerina Root Cause Analysis of Reactor Core Isolation Coolina (RCIC)

Ruoture Disc Event

a. Scope (37551)

The inspectors reviewed the licensee's root cause analysis efforts,

maintenance recovery efforts, and management involvement in the RCIC

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rupture disc event.

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b. Observations and Findinas

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On August 19, 1996, while performing LOS-RI-Q5, " Reactor Core Isolation

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Cooling (RCIC) System Pump Operability, Valve Inservice Tests in

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Conditions 1, 2, 3, and Cold Quick Start," Revision 8,,on Unit 1, the

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RCIC exhaust line rupture discs blew. No one was injured or

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contaminated. The licensee immediately began a root cause

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investigation.

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The licensee determined that the most likely cause of the rupture disc

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failure was plugging of the steam. drain line causing water to collect

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in the exhaust.line and turbine casing. When RCIC'was started for the

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monthly run, the water in the turbine casing was displaced downstream to

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the drain pot where this excessive water created a loop seal and

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overpressure condition. As a result, the rupture discs-blew. The

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licensee determined that the most probable cause for the water in the

exhaust drain line was a marginal drain line design such that the drain

line was unable to pass expected corrosion products or foreign material.

When the licensee inspected _the drain line piping, they did not find any

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significant amount of corrosion products or foreign material. The

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licensee assumed the overpressure condition cleared any obstruction of

the drain line.

Overall, the root cause effort was unorganized with weak management

oversight. There was a disconnect between the root cause team,

management, and the workers in the field. As a result of this

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disconnect,' the root cause analysis and repair work did not proceed

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smoothly. Over 12 problem identification forms were generated during

the repair of the rupture discs. On day 10 of the 14-day LCO, the

Maintenance Superintendent stopped all work on RCIC because of the

disorganization of the recovery efforts.

Finally, the repair work was

completed on day 13 of the 14. day LCO.

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The root cause report was not final at the end of this inspection

period.

However, the inspectors attended the PORC meeting on August 30,

1996, where the root cause team presented their preliminary root cause

and short term corrective actions. The root cause team presentation to

PORC was largely administrative until the members of the PORC began

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asking detailed technical questions and challenging the conclusions of

the root cause team. The' root cause team was unable to answer many

technical questions to support the bases for their' conclusions. The

root cause team was not completely forthcoming in their discussions; for

example, when discussing the long term corrective actions from the

previous RCIC rupture disc event in 1994, they were very non-specific

about whether or not all the long term corrective actions had been

implemented.

The. root cause team's recommendations for immediate corrective actions

were considered weak. One of the immediate corrective actions was to

put a drain line on the drain pot such that the drain pot could be

manually checked for water. The root cause team recommended only

checking this drain line before and after scheduled RCIC runs. The

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Operations Manager, a member of the PORC, quickly questioned the root

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- cause team on the acceptability of this practice and whether it was

preconditioning.

The root cause team did not view this as preconditioning as they felt

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the first action to take if water was found would be to declare RCIC

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inoperable.

However, the PORC asked the root cause team to re-evaluate

the frequency at which the drain line should be checked.

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Another corrective action was to put a strainer in the drain line to

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catch any foreign material which could potentially clog the downstream

orifice. The root cause team recommended that this strainer be checked

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every refueling cycle. However, they could not present any basis for

this. The PORC asked that they also re-evaluate the frequency of this

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activity.

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This PORC meeting lasted approximately 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and the PORC members

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asked the root cause team to re-evaluate specific recommendations and

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reconvene the PORC to discuss specific actions. The PORC reconvened the

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next day, August 31, to discuss these issues; however, no one from the

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root cause team was at the PORC to present the additional information.

The PORC relied on the system engineer to make the presentation although

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this was not his responsibility as he was not a member of the root cause

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team.

The PORC members again asked technical questions which could not

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be answered. As a result, the PORC made decisions and solved the

problems rather-than maintaining an oversight function.

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The inspectors will track the final corrective actions for the RCIC

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rupture disc event as an Unresolved Item (URI 373;374/96010-02).

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to be reviewed by the inspector prior to closure include:

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the final root cause report,

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work packages associated with the repair of the rupture

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disc, and

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implementation of corrective actions from the 1994 rupture

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disc event.

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El.3 Conclusions on the Conduct of Root Cause Analyses

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The root cause analyses conducted for.both the 0 DG and RCIC events were

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weak in that the root cause teams were either narrowly focused or

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unorganized.

In both cases, the root cause team made non-conservative

recommendations to the PORC regarding the operation of plant equipment.

In one case, they recommend bypassing a protective relay on the DG,

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the RCIC event, they recommended preconditioning' plant equipment.

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both cases, PORC performed their function and did not approve the root

cause team recommendations.

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IV.

Plant Support

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The inspectors reviewed plant support activities in accordance with inspection

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procedure 71750 as part of their daily inspections. These activities included

verifying plant personnel were complying with radiological protection

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procedures, observing the ALARA principle, and generally knowledgeable of

plant conditions.

No problems were observed in the areas of radiation

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protection, security, or emergency preparedness.

V.

Manaaement Meetinas

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Exit Meeting Summary

The inspectors presented the results of these inspections to Comed

management at an exit meeting on September 13, 1996.

Comed acknowledged

the findings presented.

The inspectors asked the licensee if any materials examined during the

inspection should be considered proprietary

No proprietary information

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was identified.

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PARTIAL LIST OF PERSONS CONTACTED

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  • W. Subalusky, Site Vice President
  • D. Ray, Station Manager
  • L. Guthrie, Operations Manager
  • A. Magnafici, Acting Maintenance Superintendent

R. Fairbank, System Engineering Supervisor

  • P. Antonopoulos, Site Engineering Manager

D. Boone, Health Physics Supervisor

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  • R. Crawford, Work Control Superintendent

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J. Burns, Regulatory Assurance Supervisor

  • Present at evit meeting on September 13, 1996.

INSPECTION PROCEDURES USED

IP 37551

Onsite Engineering

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IP 40500

Effectiveness of Licensee Controls in Identifying, Resolving, and

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Preventing Problems

IP 61726

Surveillance Observation

IP 62703

Maintenance Observation

IP 71707

Plant Operations

IP 71750

Plant Support Activities

ITEMS OPENED,~ CLOSED, AND DISCUSSED

Opened

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373;374/96010-01 VIO

Failure to follow a troubleshooting procedure

373;374/96010-02 URI

Followup of the root cause of the RCIC rupture disc

failure

LIST OF ACRONYMS USED

ALARA As Low As Reasonably Achievable

DG

Diesel Generator

DRP

Division of Reactor Projects

DRS

Division of Reactor Safety

IDNS Illinois Department of Nuclear Safety

IR

Inspection Report

IFI

Inspection Follow-up Item

LC0

Limiting Condition for Operation

LER

Licensee Event Report

LOP

LaSalle Operating Procedure

NRC

Nuclear Regulatory Commission

PIF

Problem Identification Form

PORC Plant Operations Review Committee

PDR

NRC Public Document Room

RCIC Reactor Core Isolation Cooling System

TCV

Turbine Control Valve

TS

Technical Specification

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