ML20134N135

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Insp Repts 50-338/85-18 & 50-339/85-18 on 850708-0804. Violation Noted:Failure to Perform Surveillance Requirements for Dc Distribution Sys in Allowed Time Interval
ML20134N135
Person / Time
Site: North Anna  Dominion icon.png
Issue date: 08/20/1985
From: Branch M, Elrod S, Leuhman J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20134N123 List:
References
50-338-85-18, 50-339-85-18, NUDOCS 8509050015
Download: ML20134N135 (14)


See also: IR 05000338/1985018

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UNITE *J STATES

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NUCLEAR REGULATORY COMMISSION

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101 MARIETTA STREET.N.W.

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ATLANTA. GEORGI A 30323

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Report Nos.: 50-338/85-18 and 50-339/85-18

Licensee: Virginia Electric and Power Company

Richmond, VA 23261

Docket Nos.:

50-338 and 50-339

License Nos.:

NPF-4 and NPF-7

Facility Name: North Anna 1 and 2

Inspection Conducted: July 8 - August 4, 1985

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Inspectors:__

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M. W. Brpcpenior Resident Ins (v'ctor

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Approved by:

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S. v'A.E rroTi, 'Se'ction Chi e f

Date Signe'd

Division of Reactor Projects

SUMMARY

Scope: This routine inspection by the resident inspectors invol/ed 205 inspector-

hours on site in the areas of licensee event reports (LERs), previously identi-

fied items, licensee action on previous inspection findings, engineered safety

features (ESF) walkdown, operational safety verification, monthly maintenance,

monthly surveillance and inspection of spent fuel pool (SFP) reracking.

Results: One violation was identified: failure to properly perform surveillance

requirements, paragraph 9.

Additional . examples of previous violation 338,

339/85-16-02, failure to follow procedures, were identified; paragraphs 5, 6, 11,

13, and 17.

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8509050015 850821

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ADOCK 05000338

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REPORT DETAILS

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1.

Persons Contacted

Licensee Employees

  • E. W. Harrell, Station Manager

A.

G.~ Hogg, Jr. , Quality Control (QC) Manager

  • G. E. Kane, Assistant Station Manager
  • E. R. Smith, Assistant Station Manager

R. O. Enfinger, Superintendent, Operations

  • J. R. Harper, Superintendent, Maintenance
  • 0. E. Hickman, Jr. .. Supervisor, Health Physics (HP)
  • L.

L'. Edmonds, Superintendent, Nuclear Training

J. A. Stall, Superintendent, Technical Services

J. R. Hayes, Operations Coordinator

  • J. P. Smith, Engineering Supervisor

D. E. Thomas, Mechanical Maintenance Supervisor

E. C. Tuttle, Electrical Supervisor

R. A. Bergquist, Instrument Supervisor

"F. T. Termine11a, Quality Assurance (QA) Supervisor

R. C. Sturgill, Supervisor, Engineering

G. H. Flowers, Nuclear Specialist

  • J. H. Leberstein, Licensing Coordinator

Other licensee employees contacted included . technicians, operators,

mechanics, security force members and office _ personnel.

  • Attended exit interview

2.

Exit Interview

The _ inspection scope and findings were summarized on August 2,- 1985, with

those persons indicated in paragraph

1.-

The licensee acknowledged the

inspectors findings.

The' licensee did not identify.as proprietary any of

the material s ' provided to or reviewed by the- inspectors during this

inspection.

3.

Licensee Action on Previous Enforcement Matters

-(Closed) Violation . 338,339/84-41-03:

Failure to Include Containment Purge

. Test Valves in Independent Verification Checklist. , The inspectors reviewed

the licensee's response, serial number 85-034, dated February 12, 1985, and

determined that the specified corrective action appeared to be prudent and

proper.

Additionally,_ the inspectors _ reviewed- 1(2)-PT-61.3.1 -dated

March 14, 1985, . and verified the revision was completed as specified in the

' licensee's1 response.

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(Closed) Infraction 339/80-31-01:

Failure of Station Nuclear Safety and

Operating Committee (SNSOC) to Review a Temporary Modification Prior to

Implementation.

The inspectors reviewed the licensee's response dated

January 12, 1981, and based on the licensee response and current licensee

practice, contained . in Station Administrative Procedure ( ADM) 14.1 dated

May 9, 1985, find the corrective action acceptable.

(Closed) Infraction 338/80-26-01 and 339/80-31-05:

Failure of SNSOC to

Review Vendor Manuals When Referenced as Part of a Station Procedure. In a

letter dated February 19, 1981, Mr. R. C. Lewis of the NRC withdrew the

infraction stating that, although it was not a requirement to include vendor

manuals in the procedure approval process, .it was the NRC's position that

vendor manuals must be controlled. Control of vendor manuals continues to

be of concern to the NRC.

Generic Letter 83-28, which addressed the

anticipated transient without scram event at Salem, includes a section on

control of vendor manuals and VEPC0 has committed to improvements in this

area.

(Closed) Violation (339/80-39-05):

Failure to Implement Fire Protection

Modification Requirements of Operating License. This item is closed since

it was mistakenly closed-in Inspection Reports 50-338/81-18 and 50-339/81-15

as Item 339/80-39-03.

Iten 339/80-39-03 was legitimately closed in report

339/84-19.

4.

Unresolved Items

An unresolved item (UNR) is a matter about which more information is

required to determine whether it is acceptable or may involve a violation or

deviation.

One unresolved item was identified during this inspection and is discussed

in paragraph 14. Additional information concerning previous unresolved item

338, 339/85-16-03 is discussed in paragraph 13.

5.

Plant Status

Unit 1

Unit 1 operated at or near 100 percent power during the majority of the

inspection period; however, on August 3,1985, the unit was shut down. to

inspect and repair tube leakage in the-1A steam generator.

Earlier in the month on July 22, 1985, the plant developed a primary leak

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that placed it.in the action statement for high unidentified leakage. The

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leak was' subsequently found to be in a primary sample line which -was

-isolated, satisfying the action statement and preventing plant shutdown.

During this event the licensee discovered that a sample system trip valve

1-TV-SS-109B had been left open.

The mispositioning .of this valve allowed

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the licensee to identify the leak, since, if the valve had been shut there

would have been no path from the primary to the sample line failure. This.

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is a further example of failure to follow procedure, see Inspection Report

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Nos. 50-338, 339/85-16-02.

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Unit 2

Unit 2 operated at or near 100 percent power during most of the inspection

period. However, on July 25, 1985, with the unit at full power, the unit

operator noted an increase in containment gaseous activity and requested a

containment . entry be made to determine - the source.

At 6:50 a.m.,

the

inspection team reported that the leak was coming from the A loop room and

at 7:00 a.m., 'a primary leak rate. calculation determined the unidentified

primary leak rate to be 5.25 gallons per minute (gpm). A power reduction

was initiate.d at 7:39 a.m.,

and at 4:48 p.m. the unit was placed in mode 3

after attempts to. repair the leak failed.

The leak was determined to be

coming from the packing' area of valve 2-RC-6 which is a two-inch manual

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isolation valve . in the bypass line around the A cold- leg stop valve.

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Previous repairs were accomplished using furmanite injections, because the

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valve was non-isolable from the reactor vessel, and replacement of the

packing would require going to cold shutdown and draining the loop. Valve

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repairs were completed on July 28, 1985 by reinjection with- furmanite and

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the unit was returned to power on July 29, 1985.

During evaluation of the above event, the inspectors determined that the

reporting requirements of 10 CFR 50.72(b)(1)(A) as clarified on page 33 of

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NUREG-1022, Supplement No. I were not met.

Specifically, the licensee did

not make the one hour- notification to the NRC Operations Center upon the

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initiation of a Technical Specification (TS) required plant shutdown. The

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licensee had previously determined that the initiation of plant shutdown

meant.the point at which the determination is made to actually shut down the

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reactor and not the point when power. reduction is initiated to allow

maintenance.

The determination to actually shut down-the plant did not

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occur until 4:40 p.m.

on July 25, 1985; however, power reduction was

initiated at 7:39 a.m., with the notification being made at 1:00 p.m. of the

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same day.

The inspectors discussed the current interpretation of what

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constitutes initiation of plant shutdown.with the licensee; consequently,

the licensee agreed to apply this criteria to future events.

Additional _1y, during evaluation of reporting requirements for the above

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event, the inspectors reviewed the station ; Emergency Plan (EP) and ques-

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tioned the basis of the EP and Emergency Plan Implementing Procedures (EPIP)

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that ties Notification of Unusual Events (NOVE) -to the moment of plant

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shutdown and not to the initiating event that requires ~ the shutdown.

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Specifically, NUREG-0654, revision 1,'gives examples-of initiating condi-

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tions ,of an unusual event -(UE), one example being exceeding primary leak

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rates specified in TS, another ~ being other plant conditions. requiring

shutdown per TS. However, the North Anna EP and. EPIP 1.01, revision 6,

makes the declaration of UE for several events upon entering mode 3 (i.e.,

plant is shutdown), and not the onset of the condition that requires the

shutdown. This item requires further review and'is identified as Inspector

Followup Item-.(IFI) 338,339/85-18-01.

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6.

Licensee Event Report (LER) Followup

The folicwing LERs were reviewed and closed. The inspector verified that:

reporting requirements had been met, causes had been identified, corrective

actions appeared appropriate, generic applicability had been considered, and

the LER. forms were complete. Additionally, for those reports identified by

an asterisk, a more detailed review was performed to verify that:

the

licensee had reviewed the event, corrective action had been taken, no

unreviewed safety questions were involved, and violations of regulations or

TS conditions had been identified.

  • 338/81-42, Failure of One Volume Control Tank (VCT) Level Transmitter Could

Cause Loss of Suction to Charging Pumps

  • 339/83-16, Containment Isolation Valves Indicating Both Open and Closed

Reservoir Low Level Signal

  • 338/80-08, Control Panel for Control Room Air Conditioning Chiller Units Not

Qualified to Seismic Category I Requirements

338/85-01, Motor Driven Fire Pump Out of Service for Greater Than Seven Days

  • 338/83-42, Momentary Loss of Power to Inverter 1-I Causes Turbine / Reactor

Trip

  • 338/83-58, Incorrect Alignment of High Head Safety Injection Pump Breakers

and Control Switches Due to Inadequate Procedural Guidance

^338/84-02, Inadvertent Single Train Emergency Core Cooling System (ECCS)

Actuation in Mode 5

(0 pen) LER 338/84-13, revisions 0 and 1, Liquid Waste Discharge Without

Demineralizer_ Treatment. This report documented the discharge of liquid

radwaste without treatment, with projected doses to the unrestricted areas

being in excess of the -limits specified in TS 3.11.1.3.

Two specific time

intervals were discussed in the report, July 11, 1984, to September 10,

1984, and September 10, 1984, to September 25, 1984.

During the first

period, the _ liquid waste mixed bed clarifier demineralizers were not in

service as required and, during the second period, a demineralizer was

placed-in service, however,.it did not contain any resin. On June 1,1985,

with projected _ doses to the unrestricted areas within TS limits and, with a

health physics recommendation to use the demineralizers, liquid radwaste was

again discharged without treatment. In this-case, an improper valve lineup

allowed much of the liquid clarifier ~ flow to bypass the operational

demineralizer.

As_a result of the first two problems, the licensee

committed to instructing operations personnel on the importance of verifying

clarifier demineralizer status and reviewing operating procedures _ for

adequacy. The' third incident, though not a violation of TS, reinforced the

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need to complete these actions. The inspectors informed the licensee at the

monthly exit meeting that the implementation of the corrective actions will

be carefully reviewed.

This is a further example of

failure to follow

procedure as identified in Inspection Reports 50-338, 339/85-16-02.

(Closed) LER 338/81-42, Failure of One VCT Level Transmitter Could Cause

Loss of Suction to the Charging Pumps.

The scheduled corrective action

indicated in the report has been taken and resulted in design change (DCP)

82-S21, VCT Level Circuitry Modifications, which has been completed.

(Closed) LER 339/83-16, Containment Isolation Valves Indicating Both Open

and Closed.

In addition to making the required repairs to the valves and

conducting inspections of other containment isolation valves, the licensee

has implemented a preventative maintenance inspection program to detect any

further problems of the kind discussed in the report.

The inspection

program will be performed every refueling outage.

(Closed) LER 338/84-03, Turbine Trip-Reactor Trip From Spurious EHC

Reservoir Low Level Signal.

The licensee conducted a flush of the EHC

system and replaced various components such as filters. The condition of

the system fluid as well as the condition of the removed filters supported

the licensee's conclusion that the unloader malfunction was a result of EHC

fluid particulate contamination. The licensee's inspection of the system

also resulted in some. suggestions for the long-term improvement of system

condition; however, none of these suggestions were felt to need immediate

implementation.

(Closed) LER 338/80-08, Control Panel for the Control Room Air Conditioning

Chiller. Units Was Not Qualified to Seismic Category I Requirements.

In a

letter dated January 31, 1980, Stone and Webster. Engineering Corporation

informed the licensee of the actions that needed to be taken to qualify

these control panels. These recommendations were the basis-for DCP 80-504,

Control Room Chiller-Seismic Modification, which has been completed by the

licensee.

(Closed) LER 338/93-42, Momenta ry loss of Pcwer .to Inverter 1-1 Causes

Turbine / Reactor Trip. The licensee committed to an revising the Abnormal

Procedure associated with loss of power to an inverter; however,-after more

evaluation, -it was felt that it would be more effective to revise the

Operating Procedure (0P). The inspectors have reviewed 1 and 2-0P-26.5 and

verified that a note has been added to alert the operator of -the conse-

quences of removing an inverter power supply from service.

(Closed) LER 338/83-58, Incorrect Alignment of High Head Safety Injection

Pump Breakers and Control Switches. Due to : Inadequate Procedural Guidance.

'The inspectors have verified that the licensee has revised the~ OP associated

with the alignment of breakers and control switches with these pumps (1 and

2-0P-8.1).

Additionally, the licensee.has revised the associated Mainte-

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nance Operating Procedures.

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(Closed) LER 338/84-02, Inadvertent Single Train ECCS Actuation in Mode 5.

The licensee has developed a procedure for the removal of the Solid State

Protection System (SSPS) output fuses, IMP-P-SSPS-01, SSPS Fuse Removal and

Replacement, and has implemented the procedure by specifically referencing

the removal of the fuses in the appropriate OP. Replacement of the fuses is

verified.by performance of SSPS performance-tests.

7.

Followup of Previously Identified Items

(0 pen) IFI 338/81-05-05:

Installation of Larger Cable for Pressurizer

Heater Power Supply.

The licensee has formulated an engineering work

request (EWR) to- accomplish the work.

Presently, EWR 81-348B is scheduled

to be implemented during the upcoming Unit I refueling outage.

(Closed) IFI 338/80-30-01 and 339/80-29-05: Lamp Testing of Safety-Related

Displays. The inspectors reviewed this issue and are satisfied that lamp

testing presently . being performed by the licensee is consistent with

existing equipment or will be modified as part of the detailed control room

design review specified in Supplement I to NUREG 0737.

(Closed) IFI 338/80-30-02 and 339/80-29-06: Need for QA Review of Construc-

tion Work Accomplished During the Operational Phase. During routine design

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change and plant maintenance reviews, the inspectors verified that adequate

GC inspection requirements for the verification of construction activities

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were specified.

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(Closed) IFI 339/80-31-02:

Completion sof Design Change 80-S49.

The

inspectors verified through review of QA records that the design change was

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completed and forwarded to station records on February 26,-1982. Addition-

ally, the condition that the design change was to correct no longer existed

after the modification.

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(Closed)' IFI 339/80-31-03:

Control of Setpoint' Changes. The inspectors

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reviewed the current practice of requesting and implementing changes to the

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North Anna Setpoint Document as specified in ADM 6.8 dated August 31, 1983,

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and found it ' met current- industry and regulatory requirements.

(Closed) IFI 339/80-31-04:

Scheduling of 18 Month Surveillance Tests. The

inspectors, during the monthly surveillance review, verified that the

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requirements of TS were met. Additionally, during 1984, VEPC0 contracted an

independent consultant to accomplish a review of the surveillance program to

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ensure the requirements of TS are being met.

(Closed) IFI 338/80-26-02 and 339/80-31-06:

Followup Licensee Action on

Unqualified Level Transmitter for Containment Sump - LER 338/80-71. Through

a review:of QA records, the inspectors verified that equipment specifiod as

being _ not qualified for' a harsh environment was ~ relocated by design change

DC'80-S64'to the rack rooms which are outside the accident envelope.

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(Closed) IFI 50-338/80-21-20 and 50-339/80-22-20:

Determination of Sample

Hood Face Velocities. After evaluating this. item in the Regional Office and

utilizing the results of the latest region based inspection, this item was

determined to require no additional specific NRC followup.

8.

Monthly Maintenance

Several station maintenance activities affecting safety-related systems and

components were observed / reviewed to ascertain that the activities were

cor. ducted in accordance with approved procedures, regulatory guides and

industry codes or standards, and in conformance with TS.

Maintenance

activities . observed included:

transferring spent fuel pool filters to

casks, corrective ~ maintenance of system . radiation monitors, repair of the

packing in valve 2-RC-6, and mechanical cleaning of service water piping.

No violations or deviations were identified in this area.

9.

Monthly Surveillance

The . inspectors observed / reviewed TS required testing and verified that

testing was performed in accordance with - adequate procedures, that test

instrumentation was calibrated, that limiting conditions for operation (LCO)

were met and that any deficiencies identified were properly , reviewed and

resolved.

The inspectors observed the performance of 1-PT-36.1A, Reactor

Protection and Engineered Safeguards Function Logic Test (Train A), and had

two comments: First, the procedure has recently been revised and the rough

draft of the ' newly approved procedure is presently being used by the

technicians to perform the test. The inspectors' understood the need to use

the draft procedure while a final is being typed; however, the SNSOC needs

to be sensitive to the quality of the draft procedures they approve for

temporary use.

In this case, there were numerous lineouts and steps added

with arrows directing where new steps should be added to the procedure-

making the procedure very hard to follow. The second comment concerns the

required values for the undervoltage coil voltage meter reading.

In the

notes following steps 4.3 and 4.9, it is.specified as 40 plus or minus two

Vdc; while in step 4.5.2, it .is required to be- 42 plus or minus two Vdc.

The. voltage, 40 Vde, required by this procedure is a target voltage which is

not that critical. However, the licensee agreed to alter the procedure to

reflect the 40 plus or minus two Vdc.

On July 9, 1985,-licensee personnel performed 1 and 2-PT-85, DC Distribution

. System. These performance tests are required to be performed every seven

days to meet the surveillance requirements of TS 4.8.1.1.3.a.

Due to a

scheduling error, these tests were not performed again until July 19, 1985.

The time elapsed exceeds that allowed under Units 1 and 2 TS 4.0.2 which

requires, 'in part, that each' surveillance requirement be _ performed within

the_ specified interval with the max! mum extension not to exceed 25-percent

of the interval. The failure to perform the surveillance requirements in

the allcwed time interval is identified as Violation 338,339/85-18-02.

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10.

ESF System Walkdown

The following selected ESF ' systems were verified operable by performing a

walkdown 'of the accessible and essential portions of the systems on

August 1, 1985.

Unit 1-

RWST (1-0P-7.7A dated May 3,1985) and NA0H Chemical Addition (1-0P-7.8A

dated June 11,1985)

Unit 2

RWST (2-0P-7.7A dated May 3,1985) and NA0H Chemical Addition (2-0P-7.8A

dated June 11,1985)

No violations or deviations were identified in this area.

11. -Routine Inspection

By observations during the inspection period, the inspectors verified that

the control room manning requirements were t,Wng met.

In addition, the

inspectors observed shift turnover to verify _that continuity of system

status was maintained.

The inspectors periodically questioned shift

personnel relative to their awareness of plant conditions.

Through log review and plant tours, the inspectors verified compliance with

selected TS and LCO.

During the course of the inspection, observations relative to Protected and

Vital Area security were made,_ including access controls, boundary integ-

rity, search, escort and badging.

On a regular basis, radiation work permits (RWP) were reviewed, and the

specific work activity was monitored to assure the activities were being

conducted per the RWP.

Selected radiation protection instruments were

periodically checked, and equipment operability and calibration frequency

were verified.

The inspectors kept informed, on a daily basis, of overall status of both

units and of any significant safety matter related to plant' operations.

Discus'sfons . were held with plant inanagement and various _ members of the

operations staff on a regular basis. Selected portions of operating logs

.and data-sheets were reviewed daily.

-The_ inspectors conducted various plant-tours and made frequent visits to the

control room.

Observations'. included:

witnessing work activities in

progress; verifying the status of operating and standby safety systems and

equipment; confirming valve positions, instrument and recorder readings,

annunciator alarms, and housekeeping.

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~ During a routine inspection of the plant, the inspectors found a piece of

measuring equipment marked NQC-PSE 2676. The calibration sticker indicated

the equipment had been due for calibration March 7,1985.

This resulted

from a failure to follow ADM 12.0 (August 23,1983) and is a further example

of failure to follow procedure as identified in Inspection Reports 50-338,

339/85-16-02.

No violations or deviations were identified in this area.

12. Nuclear Instrumentation System Flux Rate Trip Setpoints

A potential problem with compliance to the guidance of Westinghouse

Technical Bulletin NSID-85-13, dated may 28, 1985, was identified by the

licensee.

This bulletin informed Westinghouse plants with positive and

negative flux rate reactor trips that there appeared to be a problem with

the way licensees were setting these trips. The licensee has requested

further information from Westinghouse concerning this bulletin.- The

licensee's present position is that they are conforming with the TS dealing

with the flux rate trip setpoints. However, as a precautionary measure, the

present core loads were re-analyzed and _it was determined that adequate

safety margins exist despite the fact that the flux rate trip setpoints are

not set in accordance with this new vendor guidance.

This issue is being

evaluated on a generic basis by both NRC Region II and NRC Headquarters.

No violations or deviations were identified in this area.

13. Administrative Procedures

During this inspection period. selected Station Administrative Procedures

were reviewed.

Based on the review, the inspectors had the following

comments:

a.

ADM 2.19,

ISI' [ Inservice Inspection] Personnel Certification and

Training for Visual Examinations VT-2, VT-3, . and VT-4 (September 27,

1984), -in part requires that the station maintain the' qualification

records of the visual inspectors and those of the ISI supervisor. A

review of selected training records revealed that some inspection

qualification records were missing or incomplete.

The subject of

training records is discussed further in paragraph 14.

b.

ADM 19.27, Control and Use of Operator Aids (August 8,1983), requires

quarterly audits of the operator aid -log and prescribes the required

documentation of these audits. The audits are not being documented as

required, making it impossible to determine if the audits are being

done.

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c.

ADM 20.32, 10 CFR 19 Posting Requirements. In addition to the required-

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posting locations of this procedure, NRC Form 3s are posted in other

areas of the plant including the training ' building. and - records

building.

In.the case of the records building,'the posted form was

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-found to be outdated, subsequently, licensee management committed to

removing or updating the form.

d.

ADM 19.17,

Incore Moveable Detector Background Characterization

(October 31, 1983), _ specifies a required use of the axial power

distribution monitoring system (APDMS).

By Technical Specifications

the APDMS .is utilized only when reactor power is above Pm (defined in

TS as ",surv'eillance power level" - it is used in a mathematical

formula) because of problems with the APDMS. Core reloads are designed

to ensure Pm > 100 percent power, thus, eliminating the need for the

monitoring system.

In order to maintain the number of ADM at a

minimum, the inspectors have recommended to the licensee that this

procedure be cancelled or placed in reserve until needed.

e.

ADM 6.28, Control of -Vendor Manuals, Vendor Files and Interface

(October 25, 1984), and the referenced Document Control Procedure

(DCM-41), cover the updating of vendor manuals and imply the require-

ment to update drawings as part of the manual. This item will be

looked at further as part of Unresolved Item 338,339/85-16-03.

Items a. and b. are further examples of the violation for failure to follow

procedure identified in Inspection Reports 50-338, 339/85-16-02.

14.

Training Records

The inspectors, in reviewing completed copies of 1-PT-79.1, Hydraulic

Snubber Accessible for Visual Inspection During Reactor Operations, and

1-PT-79.2, Snubber Not Accessible for Visual Inspection, checked the

training records of selected visual inspection personnel. The inspectors

found that some visual inspection qualification records were satisfactory

while others were incomplete or missing.

Based on these findings, the

inspectors reviewed the licensee's commitments in the area of collection and

storage of records.

The licensee is committed - to ANSI N45.2.9-1974 as

endorsed by Regulatory Guide 1.88 (Rev. 2,

10/76) and as clarified by

Virginia Electric and Power Company Topical Report, Quality Assurance

Program Operations Phase (VEP-1-4A) Amendment Four, October 1982.

ANSI

N45.2.9-1974Property "ANSI code" (as page type) with input value "ANSI</br></br>N45.2.9-1974" contains invalid characters or is incomplete and therefore can cause unexpected results during a query or annotation process. requires that the current individual plant staff member

qualifications, experience, training and retraining records be maintained as

lifetime records. The standard further requires, in Section 5.3, the method

of storage to have a specified filing system and a method of verifying

records received and removed. Section 5.7 of the standard specifies the

records should be audited periodically.

a.

A review of North Anna Power Station Training Administrative Guideline

6.2.14,

dated December 30, 1985, Records Management for Nuclear

Training Records, found that this procedure does not appear to be

prescriptive enough in setting guidelines for the maintenance of

individual training . records.

Review of additional training records

'found that training instructors in individual disciplines maintain

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their own filing system. For example, in the area of General Employee

Training, it appears that all records are placed in the individual's

file.

In the chemistry area some records are kept in the individual's

file, while others are kept in the Chemistry Department retraining

records. Neither method is incorrect; however, in order to comply with

the standard and make training records auditable, one documented and

approved method should be used,

b.

The Training Department has a formal system for documenting the records

placed in an individual's training records.

Interviews conducted by

the inspectors revealed that though this receipt system exists, formal

and timely transmittal of training documentation from individual

station departments is not always occurring.

By Administrative

Procedures the Training Department is tasked with maintaining indivi-

dual training records, but the records will only be useful if indivi-

duals and their supervision forward all required documentation for

proper storage. A major problem area in this regard appears to be the

documentation of training received by licensee personnel at vendor and

other offsite training facilities.

The prevalent practice in these

types of training is that the individual receives his or her training

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completion certificate,.a copy of which may or may not be forwarded to

tne Training Department.

Further, if a copy of such a record is

forwarded to the Training Department, the established formal trans-

mittal system used by the station for other quality records is frequ-

ently not used.

Finding no. two of the licensee's Quality Assurance

Audit 83-16 touched on this subject but did not examine it closely. In

that instance, it was found that various records were missing from

individual training records. The resolution was to obtain copies of

the missing records and bring the training records up to date. This

resolution solved the individual problems; however, it did not address

the larger question of formal overall records accountability which is

needed to ensure such instances are not repeated.

Overall accountability is currently being addressed by some individual

training instructors and, based on the inspector's comments, the

licensee's Training Department intends to make this a comprehensive

program.

c.

Both VEP-1-4A and the North Anna Power Station Updated Final Safety

Analysis Report, Appendix 3A, need to be revised to include the

training building records storage area as an approved storage area for

quality records. Presently, only the station records building inside

the Protected Area is addressed.

The .above items are of concern to the inspector and is identified as

Unresolved Item 338, 339/85-18-05 pending further information to be

provided by the licensee and investigation by the inspectors.

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15. Station Emergency Plan

North Anna EP, Table 4.1A, no.12 and EPIP 1.01, Tab E, specify 2.4 E5

counts per minute (cpm) as the Notification of Unusual Event initiating

condition for the clarifier effluent and 6.8 E4 cpm as the same initiating

condition for the condenser air ejector monitor.

The present radiation

monitor alarm settings for the clarifier effluent monitor place the

initiating condition level between the high and high-high alarm setpoints.

In the case of the air ejector radiation monitor, the -initiating condition

value is below both the high and high-high alarm setpoints. The air ejector

alignment could create a situation where the plant reaches the threshold for

NOUE without even an alarming radiation monitor. It should be noted that at

the time the .present air ejector alarm setpoint values were input, the

recorded monitor value was 9.0 E4 cpm, which was above the EP initiating

condition for NOUE and below the alarm setpoints.

In. a related matter, the North Anna TS states that . radioactive liquid

effluent monitoring instrumentation channel alarm / trip setpoints shall be

determined and adjusted in accordance with the OFFSITE DOSE CALCULATION

MANUAL (0DCM). Using the methodology in the ODCM, the inspectors calculated

the maximum alarm / trip setpoint for the clarifier effluent radiation monitor

and compared that value with the setpoint presently in use.

The setpoint

presently being used is about two orders of magnitude higher than that

allowed by .the ODCM method.

Licensee HP personnel explained to the

inspectors that high background radiation levels in the area of the detector

were the reason the present setpoint did not agree with the calculated

value. The inspectors then explained to the licensee that the approved

methodology of the ODCM was what. Technical Specifications required and, if

it was found to be incorrect or unusable, it should be formally changed.

Correction of these problems associated with radiation monitor setpoints 'is

identified as Inspector Followup Item 338,339/85-18-03.

North Anna EP, Table 4.1A, no. 4, and EPIP 1.01, Tab A, state in part that

placing a unit in mode 3 or a lower mode as a result of meteorological

monitoring instrumentation less than minimum required to perform offsite

dose calculations per Unit 1 TS 3.3.3.4 is an initiation condition of NOVE.

Unit 1 TS 3.3.3.4 does not require plant shutdown on loss of meteorological

monitoring capability, nor does any other plant TS. Based on that fact, the

inspectors asked the licensee how the plant could ever get' into the

condition outlined above. Additionally, the inspectors pointed out to the

licensee that NUREG 0654, revision I guidance calls for the Notification of

Unusual Event based solely on loss- of all meteorological instrumentation

(page 1-5 no.11).

Revision of the procedures concerning NOUE of loss

meteorological monitoring instrumentation is identified as Inspector

Followup Item 338,339/85-18-04.

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No violations or deviations were identified in this area.

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16.

Spent Fuel Storage Racks (50095)

During this inspection period the inspectors observed some of the work done

as part of DCP 82-19. The activities witnessed included:

preliminary SFP

diving operations, removal of existing racks from the SFP, decontamination

of the removed racks and transfer of those racks to shipping containers. In

addition, the inspectors observed licensee inspection of the vehicles used

to ship the racks (including radiation surveys), reviewed selected shipping

documentation and observed preliminary, cleaning of some of the new spent

fuel storage racks.

At present, 11 racks have been removed from the SFP (10 have been shipped

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offsite). . One additional rack remains in the SFP in an area being worked

and cannot be removed at this time due to an obstruction along.the SFP wall.

Four new spent fuel storage racks have been transferred into the fuel

building with others being readied for transfer from the storage area to the

fuel building staging area.

No violations or deviations were identified in this area.

17. Compliance with Station Procedures

On July 19, 1985, NRC Region II issued a Notice of Violation for failure to

follow procedures against North Anna 1 and 2 (338,339/85-16-02).

This

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report contains further examples of that violation.

The failure to close

the sample trip valve discussed in paragraph 5 is failure to follow

1-OP-12.1.

In paragraph 6, the discussion of a followup problem similar to

those discussed in LER 338/84-13 is.another example of failure to follow an

Operating Procedure.

The out-of-calibration: NQC device referenced in

paragraph 11 is an example of failure to follow ADM 12.0 (August 23, 1983).

Finally, paragraph 13 discusses failures to follow the requirements of both

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ADM 2.19 and ADM 19.27.

The inspectors discussed with the licensee the

above failures to follow plant procedures and requested the licensee address

these items when specifying corrective action for the violations discussed

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above.

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