ML20132E830

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Insp Repts 50-361/96-15 & 50-362/96-15 on 961020-1130. Violations Noted.Major Areas Inspected:Operations, Maintenance,Engineering & Plant Support
ML20132E830
Person / Time
Site: San Onofre  Southern California Edison icon.png
Issue date: 12/17/1996
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20132E825 List:
References
50-361-96-15, 50-362-96-15, NUDOCS 9612230416
Download: ML20132E830 (21)


See also: IR 05000361/1996015

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ENCLOSURE 2

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U.S. NUCLEAR REGULATORY COMMISSION

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REGION IV

Docket Nos.:

50-361

50-362

License Nos.:

NPF-10

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NPF-15

Report No.:

50-361/96-15

50-362/96-15

Licensee:

Southern California Edison Co.

Facility:

San Onofre Nuclear Generating Station, Units 2 and 3

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Location:

5000 S. Pacific Coast Hwy.

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San Clemente, California

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Dates:

October 20 through November 30,1996

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inspectors:

J. A. Sloan, Senior Resident inspector

J. J. Russell, Resident inspector

D. L. Solorio, Resident inspector

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B. J. Olson, Project inspector

Approved By:

Dennis F. Kirsch, Chief, Branch F

Division of Reactor Projects

ATTACHMENT:

Supplemental Information

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9612230416 961217

PDR

ADOCK 05000361

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PDR

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EXECUTIVE SUMMARY

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San Onofre Nuclear Generating Station, Units 2 and 3

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NRC Inspection Report 50-361/96-15;50-362/96-15

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Operations

The inspector identified that volume control tank (VCT) inlet diversion

Valve 3LV0227A was in " auto" with the block valve to radwaste closed. This was

not in accordance with Abnormal Alignment 3-96-34, in effect at that time, and

was a violation of Technical Specification (TS) 5.5.1.1.a for failure to follow

procedures (Section 01.2). Operations management had previously identified

several component mispositioning events in recent months as a performance

concern, and had performed a self-assessment. The licensee's Nuclear Oversight

Division had also recently raised a concern regarding the large number (47) of

mispositioning events reported in 1996 (Section 07.1).

The licensee was monitoring a slow increase in containment gaseous activity, and

was proactive in planning to reset the Critical Functions Monitoring System (CFMS)

alarms to avoid operator distractions. However, the licensee missed an opportunity

to avoid the Containment Purge Isolation Signal (CPIS) A actuation, primarily

because of a general lack of awareness of the CPIS setpoint. The licensee could

have predicted that the CPIS setpoint would be reached and taken actions to reset

the setpoint (Section 01.4).

Operator actions in response to a dropped control element assembly (CEA) were in

accordance with TS requirements. Oversight by Operations management and

reactor engineering was effective in ensuring activities were coordinated and that

TS and Core Operating Limits Report requirements were accurately understood

(Section 01.3).

A noncited violation was identified after operators failed to follow procedural

controls for removal of a control element assembly calculator (CEAC) from service.

Inattention to these controls by operators led to a surveillance being missed.

Operators missed several opportunities to ensure that the surveillance would be

completed. Operators exhibited weak command and control, in that the control

operator (CO) did not provide direction to the assistant control operator (ACO) to

perform the surveillance, and the control room supervisor (CRS) did not adequately

oversee the activities to ensure operators had initiated a surveillance required by TS

(Section 04.1).

Maintenance

Instrumentation & Control (l&C) technicians lacked sufficient knowledge of licensee

computer systems used to identify and retrieve current drawings, which contributed

to an unplanned core protection calculator (CPC) channel trip (Section E3.1).

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The licensee did not have data to confirm that leakage from the emergency chilled

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water (ECW) system was within the values added to the design basis

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document (DBD) in 1993. Until the inspector identified the issue, Engineering did

not follow up on recommendations made at that time to evaluate the need for

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safety related makeup and for development of a system leakage test, indicating an

isolated weakness in system management (Section E2.2).

The licensee's identification and correction of a methodology error in a vendor

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calculation was an excellent finding demonstrating strength in the licensee's reload

technology transfer program (Section E4.1).

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The nonconformance report (NCR) process used to modify the CPC inputs did not

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ensure that affected procedures were identified and revised. This weakness had

not been fully addressed in recent NCR program changes (Section E3.1).

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Plant Sucoort

The inspector's observation that scaffolding rendered some safe-shutdown

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emergency lighting ineffective revealed a programmatic weakness in the licensee's

program for control of emergency lighting, in that emergency lighting inspections

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were ineffective in identifying the lighting deficiencies and the scaffolding

procedures did not address the effect of scaffolding on the lighting. Licensee

corrective actions were thorough (Section P2.1).

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Report Details

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Summary of Plant Status

Unit 2 operated at essentially 100 percent power from the beginning of this inspection

period until November 23,1996, when the unit began a power coastdown to refueling.

The unit shut down to Mode 3 on November 30,1996, and commenced its Cycle 9

refueling outage. The unit was in Mode 4 at the end of this inspection period.

Unit 3 operated at essentially 100 percent power from the beginning of this inspection

period until October 31,1996, when a CEA dropped into the core (Section 01.3), and

power was reduced to approximately 43 percent. After the CEA was recovered, power

was increased. The unit operated at essentially 100 percent power from November 2,

1996, until the end of this inspection period.

1. Operations

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Conduct of Operations

01.1 General Comments (71707)

Operators were observed to generally carefully monitor control board indications,

refer to procedures frequently during many evolutions, and make conservative

decisions regarding plant safety. Routine control room oversight by Operations

management was evident. Operators were responsive to emergent conditions and

alarms However, several system valve linup problems have been identified

rece" e, demonstrating the need for improved attention to detail (Section 07.1).

01.2 VCT Inlet Diversion Valve Controller in an incorrect Mode - Unit 3

a.

Inspection Scone (71707)

On October 18,1996, the inspector inspected the Unit 3 main control boards and

observed that the VCT inlet diversion Valve 3LV0227A controller was not in the

correct position per an abnormal alignment in effect at that time. The inspector

reviewed documents and interviewed personnel associated with this observation,

b.

Observations and Findinas

On October 18,1996, the inspector identified that VCT inlet diversion

Valve 3LV0227A was in " auto," with the block valve to radwaste, Valve 3MU924,

closed. This was not in accordance with Abnormal Alignment 3-96-34 in effect at

that time. The inspector notified Unit 3 operators, who repositioned the controller

to " manual /VCT" and initiated Action Request (AR) 961001022. Abnormal

Alignment 3-96-34 had been initiated on April 25,1996, because Valve 3LV0227A,

which is a three-position valve, leaked fluid to radwaste when positioned to the

VCT. Abnormal Alignment 3-96-34 required that Valve 3MU924 be closed, except

as needed to divert to radwaste, and that Valve 3LV0227A be maintained in

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" manual /VCT," except when diverting to radwaste. A precaution in Abnormal

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Alignment 3 96-34 warned operators not to divert to radwaste without opening

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Valve 3MU924. With Valve 3LVO227A in " auto," the valve would automatically

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reposition to divert letdown flow to radwaste when the VCT level increased to

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78 percent.

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The inspector determined that positioning Valve 3LVO227A to divert to radwaste,

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while Valve 3MU924 was shut, would result in a loss of letdown flow. Letdown

system pressure would increase, causing the backpressure regulating valves to

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close and the pressure relief valves in the system to lift. The intermediate pressure

letdown relief valve,3PSV9206, had a setpoint of 650 psig, and the low pressure -

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letdown relief valve,3PSV9208, had a setpoint of 200 psig. Operators would then

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have had to take prompt action to restere letdown flow. The plant was designed to

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withstand 100 loss of letdown flow transients.

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The inspector determined that, during steady-state operations, operators generally

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controlled reactor coolant system (RCS) inventory, such that additions to the RCS

did not result in VCT level changes, by simultaneeusly diverting letdown to

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radwaste. Operators did not normally rely on the automatic VCT water level control

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capability, and Valve 3LVO227A would not normally shift position automatically

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without a plant transient causing an approximate 8 degree elevation in RCS

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temperature or a control system failure,

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Licensee corrective actions addressed incorporating instructions from long-standing

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abnormal alignments into permanent operating procedures. The licensee also

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counseled the operators involved.

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The failure to have Valve 3LVO227A aligned as required by Abnormal-

Alignment 3-96-34 was a violation of TS 5.5.1.1.a for failure to fellow procedures

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(Violation 50-362/96015-01). Although the safety consequence of this violation

was low, the inspector found that the condition existed during a shift turnover (the

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mispositioning was a result of not changing the controller mode after performing a

water inventory balance the preceding day) and should have been noted by

operators at that time. The inspector also found that the abnormal alignment,

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despite having been in effect for approximately 6 months, placed the controller in a

mode that was different from the mode called for in permanent procedures and no

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measures were in effect to resolve the opportunities this created for the controller

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to be mispositioned.

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Operations management had previously identified several component mispositioning

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events in recent months as a performance concern, and had performed a self-

assessment. Additionally, Nuclear Oversight recently addressed an observed high

number of such events by various line divisions, including Operations

(Section 07.1).

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The inspector also observed that the Updated Final Safety Analysis Report (UFSAR)

states, in Section 9.3.4.2.1.2, that an automatic system maintains the water level

in the VCT, and that the letdown flow is automatically diverted to the boric acid

recycle system when the highest permissible water level is reached in the VCT.

The licensee initiated AR 961100216 to review the accuracy of this statement in

the UFSAR.

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The inspector found that the UFSAR description of VCT operation was misleading in

that it stated that VCT level was maintained by the automatic system when, in fact,

during normal steady-state operations, operators manually controlled VCT level.

However, the VCT level control capability was normally selected for automatic

control. Licensee changes to the UFSAR will be reviewed as a followup item

(Inspector Followup item 50-361(362)/96015-02).

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c.

Conclusion

The failure to have Valve 3LV0227A aligned as required by Abnormal

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Alignment 3-96-34 was a violation. A followup item was created to review licensee

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changes to the UFSAR because of a discrepancy identified by the inspector.

01.3 Drocoed CEA - Unit 3

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Insoection Scooe (71707)

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At 7:17 p.m. on October 31,1996, while Unit 3 was operating at approximately

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99 percent power, Shutdown Group A CEA 49 dropped fully into the core. The

inspector responded to the site and reviewed the circumstances of the event.

b.

Observations and Findinas

Operators responded by initiating a power reduction in accordance with TS Limiting

Condition for Operation (LCO) 3.1.5, Condition C (one shutdown CEA misaligned

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greater than 7 inches), to meet the requirements of the Core Operating Limits

Report, which required an 18 percent power reduction. However, azimuthal power

tilt increased to 0.30 as a result of the dropped CEA, which was near the periphery

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of the core. TS LCO 3.2.3, Condition C, required that power be reduced to less

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than 50 percent within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> with tilt greater than 0.10; thus, operators

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continued the downpower, reaching approximately 43 percent power by

approximately 10:30 p.m.

A plant equipment operator observed that indications in the CEDMCS cabinets were

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abnormal for CEAs 49 and 53, both in Shutdown Group A Subgroup 13. He also

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observed that a toggle switch at the bottom of the cabinet, controlling blowers in

the cabinet, was in the "off" position. He turned the blowers on. Additionally, one

of the two CEDMCS room coolers was out of service for maintenance, with work in

progress, at the time the CEA dropped.

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At 9:17 p.m., operators entered TS LCO 3.1.5, Condition D, requiring shutdown to

Mode 3 within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />, as the result of the CEA misalignment not having been

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corrected within 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> (Condition C).

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l&C technicians and the system engineer responded to troubleshoot and repair the

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cause of the dropped CEA. They took coil traces and determined that all four CEAs

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in Shutdown Group A Subgroup 13 were missing at least one phase of power.

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Further inspection identified that six optical isolator chips were loose in their

sockets. The technicians tested the chips, determined that they were functional,

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and reseated them. Additional coil traces showed that all four CEAs were still

missing one phase. This condition was determined to be caused by a blown fuse.

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The fuse was replaced and the system was retested satisfactorily.

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At approximately 10:33 p.m., CEA 49 was relatched and operators i;cgan to fully

withdraw it to align it with the rest of Shutdown Group A. A reactor engineer and

the Operations superintendent were present to advise and monitor operator actions.

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CEA 49 was aligned at approximately 11:53 p.m. Power was slowly increased, and

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was restored to 100 percent on November 2,1996.

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The licensee initiated AR 961100003 to document the event, the root cause

determination, and associated corrective actions. The licensee's preliminary

determination was that high temperature in the CEDMCS cabinet caused the CEA to

drop. As of the end of this inspection period the licensee had not determined how

or when the blower switch had been turned off.

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Conclusions

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Operator actions in response to the dropped CEA were in accordance with TS

requirements. Oversight by Operations management and reactor engineering was

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effective in ensuring activities were coordinated and that TS and Core Operating

Limits Report requirements were accurately understood.

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01.4 CPIS - Unit 3

a.

Insoection Scope (71707. 71750)

The inspector reviewed licensee activities surrounding a CPIS A actuation that

occurred in Unit 3 on October 25,1996.

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b.

Observations and Findinas

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The CPIS was initiated by containment gaseous Radiation Monitor (RM) 3RE7807C

reaching its setpoint (900 cpm). Because a purge was not in progress at the time,

no equipment changed state.

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The licensee had been aware of, and had been actively monitoring, an increasing

trend in containment gaseous activity since approximately October 20. The

increased activity was approximately linear between October 20 ar.d October 25.

The trend was also apparent on Train B containment gaseous RM 3RE7804C. The

licensee had initiated AR 961001168 on October 24, stating that the CFMS alarm

point for RM 3RE7804C should be increased to avoid nuisance alarms and to

provide an alarm based on approximately 1.0 gpm RCS leakage. This sensitivity

was described in the UFSAR and was in accordance with NRC Regulatory

Guide 1.45.

AR 961001168 documented that the increased gaseous activity was apparently due

to approximately 0.1 gpm of RCS leakage from the pressurizer steam space, since

particulate activity was not increasing.

After the return to full power on November 2, following a dropped CEA (see

Section 01.3), the containment gaseous activity again increased. The licensee

made a containment entry on November 5 and observed that the vent to

containment from the pressurizer, Valve 3HV0298 was leaking at approximately

0.05 gpm. This was consistent with observed gaseous activity. In the days

following the containment entry, the activity level stabilized at approximately

1000 cpm.

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Conclusions

The licensee was monitoring a slow increase in containment gaseous activity, and

was proactive in planning to reset the CFMS alarms to avoid operator distractions.

The license missed an opportunity to avoid the CPIS A actuation primarily because

of a general lack of awareness of the CPIS setpoint. The licensee could have

predicted that the CPIS setpoint would be reached on October 25, and taken

actions to reset the setpoint.

04

Operator Knowledge and Performance

04.1 Failure to Comolete Surveillance - Unit 2

a.

Insoection Scoce (71707)

The inspector reviewed the circumstances surrounding Operation's failure to

perform a conditional surveillance.

b.

Observations and Findinas

On November 1,1996, Unit 2 operators declared CEAC #1 inoperable for

performance of an 18-month surveillance. The same day the licensee reported to

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the NRC that operators failed to complete a 4-hour surveillance within the required

time period, required by TS 3.3.3, Action A, when they made the CEAC inoperable.

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However, Action B of TS 3.3.3 allowed continued operation in the event Action A

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was not completed within the required 4-hour period, as long as the actions of

Condition B were completed within the next 4-hour period. Because operators

completed the surveillance required by Action A within the second 4-hour period,

the TS allowed continued operation in accordance with the provisions of Action A

until the CEAC was returned to service.

Operators logged the inoperability in the CEAC log book. The book included a

column, that was signed and verified by the CO and ACO, respectively, to ensure

the 4-hour surveillance was initiated when making a CEAC inoperable. However,

the CO did not direct the ACO to initiate the 4-hour surveillance. Additionally, the

ACO did not verify who had initiated the surveillance. This was more significant

since the ACO is normally responsible for performing surveillances such as the

4-hour surveillance for CEA position.

Work Authorization Record 2-9603373 for the CEAC work did not list the 4-hour

surveillance needed to be performed, but did direct the CEAC to be removed from

service in accordance with Procedure SO23-3 2.13c

The CO had made an entry in the CO log at 8:40 a.m. stating that CEAC #1 was

removed in accordance with Procedure SO23-3-2.13, " Core Protection / Control

Element Assembly Calculator Operation," Revision 7. The CO stated that he had

reviewed the procedure, but had failed to review Section 6.5.2, which directed the

4-hour surveillance to be initiated when a CEAC was removed from service.

At the time the CO and ACO were making the CEAC inoperable the CRS was in the

control room. The CO stated that the CRS was not observing their activities

directly. Procedure SO123-0-2, "CRS Authority, Responsibilities, and Duties,"

Revision 3, Step 6.2.3, required the CRS to direct and coordinate the activities of

the operating crew with approved procedures, TS, and Licensee Controlled

Specifications (LCS). The procedure also required the CRS to review the TS when

removing equipment from service. The CRS dM not direct and coordinate the

activities of the crew nor review the TS when equipment was removed from

service. Procedure SO123-0-3, "CO's Responsibilities and Duties," Revision 1,

Step 6.2.4.1, also required the CO to " ensure control room round sheets or shift

relief status and surveillances are completed in the assigned time frame." The CO

did not ensure the surveillance was completed within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />.

Shortly af ter the CEAC was taken out of service the operators became involved in a

long evolution to support a pump retest. Following completion of the pump retest,

approximately 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> after removing the CEAC from service, operators realized

they had missed the 4-hour surveillance.

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TS 3.3.3, Action A.1, required that if one CEAC was inoperable, to perform a

SR 3.1.5.1 once every 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />. SR 3.1.5.1 required verification that the position of

each full and part length CEA was within 7 inches of all other CEAs in its group. At

3:15 p.m. the CO made a log entry that position verification required by the TS had

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been completed. However, Condition B stated that, if the required action for

Condition A was not met within its required completion time, to verify that the

departure from nucleate boiling ratio requirement of LCO 3.2.4 was met within

4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />. Because operators completed this verification within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />, the TS

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requirements were met.

The licensee briefed all operators regarding this event, emphasized the need to

ensure that a timer is started to ensure that the surveillances are performed.

c.

Conclusions

The 4-hour surveillance required by Action A of TS 3.3.3 was not completed 'within

the required time frame; however, the licensee complied with Action B within the

required time frame, which was provided in the event Action A was not completed.

Therefore, TS requirements were met.

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Operators failed to follow procedural controls for removal of a CEAC from service.

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Operators missed several opportunities to ensure that the surveillance would be

completed. The licensee's administrative controls for roles and responsibilities for

operators were sufficiently detailed to ensure operators understood they should

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follow TS and perform surveillances required when removing equipment from

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service, inattention to these controls by operators led to the surveillance being

missed. While the operators were aware of the requirement to perform the

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surveillance, they did not take action to ensure that it would be performed. The

failure to follow the procedures was a violation of TS 5.5.1.1.a. This

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licensee-identified and corrected violation is being treated as a noncited violation,

consistent with Section Vll.B.1 of the NRC Enforcement Policy

(NCV 50-361/96015-03).

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Operators exhibited weak command and control, in that the CO did not provide

direction to the ACO to perform the surveillance, and the CRS did not adequately

oversee the activities to ensure operators had initiated a surveillance required by TS.

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07

Quality Assurance in Operations

07.1 Component Miscositionina Events

Recently, the licensee had experienced certain valve mispositioning situations

(i.e., RCS head vent valve in Unit 3 and pressurizer spray line drain valves in

Unit 2). These situations were of concern to the NRC and the mispositioned head

vent valve was the subject of a recent special NRC inspection.

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Operations management maintained an ongoing list and analysis of performance

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issues. In this program, component mispositioning by operators had been identified

as a concern. Operations had performed a self-assessment in this area in about

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July 1996.

On November 5,1996, Nuclear Oversight sent a memorandum to the Vice

President, Nuclear Generation, requesting action regarding 47 component

mispositioning events that had been reported in ARs in 1996, validating NRC

concerns in this area. The events involved personnel from Operations and other

divisions. In the memorandum, Nuclear Oversight requested identification of a

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responsible manager to address the broad issue, including establishing appropriate

metrics for evaluating and tracking progress in improving performance in this area.

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The inspector considered Nuclear Oversight's assessment to be significant and

timely in that it established a larger scope to this important issue.

08

Miscellaneous Operations issues (71707, 92700)

08.1 (Closed) Licensee Event Report (LER) 50-362/96006-00: containment purge

isolation actuation. This issue is discussed in Section 01.

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08.2 (Closed) LER 50-362/96004-00: RCS pressure boundary leakage due to a failed

resistance temperature detector (RTD) thermowell. This issue was previously

discussed in NRC Inspection Report 50-361(362)/96011.

08.3 Institute of Nuclear Power Operations Report

The inspector reviewed the Institute of Nuclear Power Operations report of its

periodic evaluation of performance of San Onofre. The report had been received by

the licensee in September 1996.

II. Maintenance

M1

Conduct of Maintenance

M 1.1 General Comments

a.

Insoection Scope (62707)

The inspector observed all or portions of the following work activities:

Replace spent fuel pool cooling branch connection with new style fitting -

Unit 2

Install flat bar support brackets on refueling water storage tanks - Unit 3

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b.

Observations and Findinas

The inspectors found the work performed under these activities to be thorough. All

work observed was performed with the work package present and in active use.

Technicians were knowledgeable and professional. The inspectors frequently

observed supervisors and system engineers monitoring job progress, and quality

control personnel were present whenever required by procedure. When applicable,

appropriate radiation controls were in place.

In addition, see the specific discussions of maintenance observed under

Section E3.1, below.

M1.2 General Comments on Surveillance Activities

a.

Insoection Scooe (61726)

The inspector observed all or portions of the following surveillance activities:

Engineered safety feature group relay K-112A, K-625A, and K-725A

semiannual test - Unit 3

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Main and auxiliary feedwater valve testing - cold shutdown and refueling

interval - Unit 2

b.

Observations and Findinas

The inspectors found all surveillances performed under these activities to be

thorough. All surveillances observed were performed with the work package

present end in active use. Technicians were knowledgeable and professional. The

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inspectors frequently observed supervisors and system engineers monitoring job

progress, and quality control personnel were present whenever required by

procedure.

M8

Miscellaneous Maintenance issues (92902)

M8.1 (Closed) Violation 50-361(362)/96008-01: performance of maintenance activities

on the wrong components. This violation involved two instances where technicians

performed work on wrong components after being briefly interrupted in their work.

The licensee's corrective actions for the violation were identified in a letter to the

NRC dated September 11,1996. The inspector reviewed licensee documents and

determined that the corrective actions were either completed or scheduled for

completion. The inspector also spoke with Maintenance technicians and determined

that management was emphasizing self and cross checking to ensure that correct

components are worked on.

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M8.2 (Closed) Inspector Followuo item 50-361/93016-02: differences in ultrasonic

testing wall thickness measurements. This item was opened after repetitive

measurements indicated that component wall thickness had changed by more than

five percent, which was the accuracy range of the test equipment. The licensee

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evaluated the measurements and determined that wall thickness was greater than

the code specified minimum thickness. The licensee also determined that the

measurement differences were attributable to operator technique and component

variability. The inspector discussed the issue with licensee personnel and agreed

with their evaluation of the issue. The inspector also noted that the licensee's

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program required an examination of the entire grid area if one measurement was

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less than the manufacturer's minimum wall thickness.

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Ill. Enaineerina

E2

Engineering Support of Facilities and Equipment

E2.1

Review of Facility and Eouloment Conformance to UFSAR Descriotion

A recent discovery of a licensee operating its facility in a manner contrary to the

UFSAR description highlighted the need for a special focused review that compares

plant practices, procedures and/or parameters to the UFSAR description. While

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performing the inspections discussed in this report, the inspectors reviewed the

applicable sections of the UFSAR that related to the inspection areas inspected.

The following inconsistency was noted between the wording of the UFSAR and the

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plant practices, procedures and/or parameters observed by the inspectors:

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The description of the method used to control VCT level, in UFSAR

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Section 9.3.4.2.1.2, was found to be inconsistent (Section 01.2 ).

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E2.2 ECW System Leakaoe Detection

a.

Inspection Scope (37551)

The inspector interviewed cognizant ec.gir'sers and walked down portions of the

(common to both units) ECW system * srder to determine leakage detection

methods in place. The inspector also reviewed DSD SO23-800, " Auxiliary Building

Emergency Chilled Water System," Revision 0,

b.

Observations and Findinos

The ECW system is a closed-loop safety-related system that supplies chilled water

for cooling safety-related equipment tsuch as emergency core cooling pump room

coolers and charging pump room coolers) and to provide habitability. The system

automatically starts on various engineered safety signals. Two emergency chiller

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units provide chilled water to both units. A nominal 60-gallon compression tank

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provides for compression and contraction of the chilled water, maintains suction

head to the chilled water pump, and prevents voiding in the system high points.

The system normally contains approximately 1200 gallons of water with 42

separate cooling coils located throughout both units. Tank pressure is provided by

a closed volume of air. The tank has an automatic makeup, based on low tank

pressure, that comes from nonsafety-related nuclear service water. There is no

control room indication of initiation of automatic makeup.

If an event occurred, and the nonsafety automatic makeup for the system was lost,

and if system leakage was sufficient, the system compression tank could lose level.

Air from the compression tank could then enter the suction of the pump, and the

system could fail.

The licensee logged compression tank level locally, in addition it was normal

practice for operators and the cognizant engineer, if they observed leakage during

normal plant tours, to evaluate the amount of the leakage, and generate ARs for

Maintenance to repair the leakage. However, the inspector found that although

these methods would detect some leakage, they did not quantify system leakage

with reasonable assurance at any one time. The inspector found that operators had

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no ready means to determine, nor did they determine, the amount of makeup taking

place. However, the inspector found that these monitoring methods did provide

some assurance that significant undetected leaks would not occur.

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Immediately after inspector questioning during October 1996, Station Technical

personnel discovered, and Maintenance personnel repaired, a 60 cc/hr leak in a

compression tank drain line. The licensee had determined in 1993, as a result of

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DBD in 1992, that with a low compression tank level, 200 cc/hr leakage was

acceptable; with a high tank level,950 cc/hr leakage was acceptable. The licensee

also generated ARs 961000554 and 961200136 to reevaluate the acceptable

leakage numbers and to initiate a test for leakage.

The inspector also observed that Revision 0 to DBD SO23-800, completed in 1992,

left as an open item for engineering to resolve the need to install a safety-related

makeup source and the need of performing a system leakage test. The inspector

found thr.t acceptable leakage amounts had been developed, but that these other

issues ht d not been addressed as of this inspection report period,

c.

Concitsion

The licensee did not have data to confirm that leakage from the ECW system was

within the values added to the DBD in 1993. Until the irspector ider.tiNd the

issue, Engineering did not follow up on recommendations made at that time to

evaluate the need for safety-related makeup and for development of a system

leakage test, indicating an isolated weakness in system management.

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E2.3 Charoino Pumo 2P190 Breaker Failure - Unit 2

a.

Insoection Scope (37551)

The inspector reviewed the licensee's response to the failure of the safety-related

480 volt breaker for Charging Pump 2P190.

b.

Observations and Findinos

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On October 22,1996, the breaker for Charging Pump 2P190 failed to close on

demand from the control room. it failed to close on a second attempt, and on a

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third attempt it closed and then tripped open after approximately 3 minutes. The

licensee documented these failures in AR 961001008.

The licensee determined that the cause of the failures was that the roller assembly

was sticking, resulting in the breaker not being properly aligned in the cubicle and

the secondary contacts not being fully engaged.

The roller assembly was not included in the preventive maintenance program, and

had not been lubricated since assembly by the manufacturer. The vendor manual

for the breaker did not address preventive maintenance for the roller assembly.

The licensee contacted the vendor to determine the appropriate lubricant, and

intended to add inspection and lubrication of the roller assembly to the preventive

maintenance program for similar breakers.

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The licensee replaced the breaker with a spare and restored the system to service.

c.

Conclusion

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The licensee's resolution of a failed 480 voit safety-related breaker was prompt and

thorough.

E3

Engineering Procedures and Documentation

E3.1

RCS Temperature Element Wirina Modification - Unit 3

a.

Insoection Scoce (37551. 717071

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During a review of the Unit 3 CO logs, the inspector determined that l&C

technicians caused a trip of CPC Channel A while performing a surveillance of RCS

cold leg temperature Indicator 3TI-0925-1. The inspector reviewed the

circumstances leading up to the event,

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b.

Observations and Findinas

RTD 3TE-0925-1 once had been only used as the input to Indicator 3TI-0925-1.

However, because of a failure of another RTD in 1994, wiring changes and

modifications were made, in accordance with NCR 941100027, resulting in

RTD 3TE-0925-1 also supplying an input to CPC Channel A.

l&C technicians calibrating Indicator 3TI-0925-1 caused the trip of CPC Channel A

(on departure from nucleate boiling ratio and linear power density) during the

calibration activities. Work Authorization Record 3-9603339 referenced

Maintenance Order (MO) 96052709, which referenced Procedure S023-11-9.657,

" Surveillance Requirement Qualified Safety Parameter Display System A (OSPDS-A)

Calibration," Revision 6, for calibration of Indicator 3TI-0925-1. The procedure did

not mention that the RTD feeding indication 3TI-0925-1 performed a dual purpose.

The inspector considered that under other licensee design modification processes

the impact to the l&C procedure would have normally been evaluated.

Apparently, the technicians did not obtain the drawing change showing that the

RTD for Indication 3TI-0925-1 also supplied a temperature signal to CPC Channel A.

l&C supervision stated that the drawing change documents were not obtained

because the technician was unfamiliar with the software application used to obtain

drawings and missed the information in the computer system that stated there were

changes outstanding against the drawing.

The inspector determined that Maintenance personnel had received no training on

the used of the computer application used to obtain drawings. Apparently, the

technicians learned it on their own. In response to this weakness, the licensee

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planned to conduct training of Maintenance personnel and to evaluate

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enhancements to the computer application.

The inspector reviewed Procedure SO123-XV-5, " Nonconforming Material, Parts, or

Components", Temporary Change Notice 3-22, which was in effect when the

modification was made. The procedure did not require review of Operations or

Maintenance procedures when making a design modification, as the licensee's other

design change processes would. As a result, the inspector considered that the

opportunity was missed to identify that the modification of the RTD inputs could

affect the unit in an adverse manner.

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The inspector reviewed the current procedure for NCRs and noted that it still

allowed plant modifications if operational instructions and drawings were reviewed

for impact. However, the inspector determined that the process still did not require

an impact review of surveillance and maintenance procedures, in response to this

programmatic weakness, the licensee agreed to revise the NCR process.

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c.

Conclusions

l&C technicians lacked sufficient knowledge of licensee computer systems used to

identify and retrieve current drawings. which contributed to an unplanned CPC

channel trip.

The NCR process used to make modify the CPC inputs did not ensure that affected

procedures were identified and revised. This weakness had not been fully

addressed in recent NCR program changes.

E4

Engineering Staff Knowledge and Performance

E4.1

Reload Analvsis Error

a.

Insoection Scooe (37551)

The inspector reviewed licensee performance in the identification and resolution of

an error in the fuel reload analysis.

b.

Observation Findinas

While reviewing vendor calculations as part of the reload technology transfer

program, licensee engineers identified a discrepancy in the data related to core

power distributions for dropped part-length CEAs (PLCEAs). Because the PLCEAs

are not uniform along their length, they introduce an axial asymmetry when inserted

into the core. The asymmetry was not properly addressed in the calculations,

resulting in a nonconservative acceptable operating region being included in the

LCS. The curve affected was LCS Figure 3.1.105-3, " Required Power Reduction

after Single PLCEA Deviation," which is part of the Core Operating Limits Report.

The licensee contacted the vendor, who confirmed the error as identified by the

licensee.

The licensee determined that TS operating limits prior to issuance of the LCS were

more conservative than required, and that the units had never operated in what was,

now determined to be an unacceptable region.

Had the licensee operated in the unacceptable region, which was applicable after a

PLCEA dropped over halfway into the core, departure from nucleate boiling limits

could have been exceeded.

The licensee d'ocumented the condition in AR 961100053, and implemented

immediate corrective action to require operators to comply with LCS

Figure 3.1.105-2, " Required Power Reduction After Single Group 6 Full Length CEA

Deviation," if a PLCEA dropped. LCS Figure 3.1.105-2 was more conservative than

required for plant safety for a dropped PLCEA.

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c.

Conclusions

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The licensee's identification and correction of a methodology error in a vendor

calculation was an excellent finding demonstrating strength in the licensee's reload

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technology transfer program.

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E8-

Miscellaneous Engineering issues (92712) .

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E8.1

(Closed) LER 50-362/96002-00.01: potential decalibration of log power level

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- instrumentation. On February 9,1996, the licensee was notified by Asea-Brown

Boveri Combustion Engineering (CE) that a potential nonconservatism in the

calibration of logarithmic power channels reported by Waterford may exist at San

Onofre Units 2 and 3. The potential decalibration was attributed to physics effects,

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which may cause the log power indication to vary significantly from actual plant

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power during low power operation due to factors such as CEA position, temperature

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shadowing, boron changes, etc. CE estimated that the effects had the potential to

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cause'the log power trip to be high by a factor of two, but less than a factor of 10.

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In response, the licensee reduced the high logarithmic power trip setpoints, in both

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units on all four channels, by a factor of 10, while CE performed a reanalysis to

determine the actual effect of the nonconservatisms. The inspector verified that the

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licensee initiated MOs to change the setpoints.

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.The inspector reviewed portions of the reanalysis performed by CE, which

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concluded that the total of the decalibration effects was a factor of two. Based on

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the calculated decalibration effect the log power trip setpoint was reanalyzed. The

results demonstrated that the previously installed setpoints would have allowed the

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fog power trips to perform their intended safety functions. Following receipt of the

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reanalysis, the licensee restored the trip setpoints to their previous values. The

licensee submitted Revision 1 of the LER to document that, based on the results of

CE's analysis, the condition previously reported was no longer reportable.

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The inspector concluded that the !icensee's actions were conservative.

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IV. Plant Suonort

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R8

Miscellaneous Radiological Protection and Chemical lasues (92904)

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R8.1

(Closed) Insoector Followuo item 50-362/96009-05: steam generator (SG)

blowdown RM valve misalignment. The licensee found an open bypass valve for.

SG 3E088 blowdown RM 3RE6759 that was unidentified on plant drawings. The

-licensee also found similar bypass valves for the other three SG blowdown RMs;

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however, those bypass valves were in the closed position. The four bypass valves

were not depicted on plant drawings or specified in plant procedures.

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The inspector discussed this item with Engineering, Operations, and RM personnel.

The inspector also reviewed alarm response instructions, abnormal operating

instructions, and emergency operating instructions applicable to the SG blowdown

RMs. The SG blowdown RMs are used in conjunction with other RMs and sample

results to diagnose a SG tube rupture. While the open bypass valve rendered the

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RM inoperable, the inspector concluded that operators could have diagnosed a SG

tube rupture using the other RMs and sample results. The inspector found that the

SG blowdown RMs were not required to be operable by TS. In addition, the

inspector reviewed the UFSAR and determined that the SG blowdown RMs were

not covered by the quality assurance provisions of 10 CFR Part 50, Appendix B.

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Although the unidentified valves represented a configuration control problem, the

inspector concluded that no violation of NRC requirements occurred. A field change

was performed to remove the four bypass valves from the SG blowdown RMs. The

licensee inspected other RMs and found no other unidentified valves.

P2

Status of Emergency Preparedness Facilities, Equipment, and Resources

P2.1

Safe Shutdown Emeroency Liahts Olocked By Scaffoldino - Unit 2

a.

Insoection Scoce (71707. 71750)

The inspector walked down portions of Unit 2 during an electrical outage and

observed that some emergency lights were blocked by scaffolding. The inspector

evaluated licensee controls for temporary scaffolding erected in the Unit 2 main

steam safety valve (MSSV) area.

b.

Observations and Findinas

On October 17,1996, during a plant walkdown of the MSSV area, the inspector

observed that temporary scaffolding, erected for painting, was blocking safe

shutdown 8-hour emergency lights illuminating an access and egress path to safe

shutdown components and illumination of two safe shutdown components,

atmospheric dump Valve 2HV8421, and turbine auxiliary feedwater pump steam

supply Valve 2HV8200. The inspector informed the licensee of the degradation of

the emergency lighting and determined that the licensee had been previously

unaware of the condition. The inspector determined that plant equipment operators

routinely, at least once per shift, toured the MSSV areas on both units.

The inspector reviewed the LCS for safe shutdown emergency lights, LCS 3.7.114,

and determined that the LCS required that when a light was made inoperable,

operators were directed to utilize portable lanterns after a 14-day time period.

However, since the operators were previously unaware of the degradation, no

tracking mechanism was initiated to ensure that after 14 days portable lanterns

would be used in the affected areas. However, the inspector observed that plant

operators routinely carried flashlights. The inspector verified that, in the safe

shutdown from outside the control room, backpacks given to all operators during

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implementation of the emergency operating instruction for safe shutdown outside

the control room contained portable lanterns. In addition, as discussed below, the

inspector also could not determine that the lights were blocked for more than

14 days. Once the operators were aware that the lights were blocked, tracing was

initiated in accordance with LCS 3.7.114.

The inspector determined that the procedure controlling scaffolding erection did not

provide guidance to sensitize craft personnel that the illumination path of emergency

lights should not be blocked. In addition, the inspector determined that the

Emergency Preparedness procedure for weekly plant inspections did not sensitize

fire inspectors to the poter.tial of scaffolding blocking emergency lights. The

inspector verified that a weekly inspection of the MSSV had been performed;

however, because the fire inspection procedure did not state the need to look for

degradation of emergency lighting, the licensee inspectors did not identify the

scaffolding problem. As a result, the licensee revised these program procedures to

reflect the need to prevent scaffolding from blocking emergency lighting or to take

the appropriate compensatory actions if not preventable.

The inspector reviewed the " work done" section of MO 96052477, used for control

of the scaffolding activities. The scaffolding blocking the lighting i!!uminating safe

shutdown Valvos 2HV8200 and 2HV8421 was documented as being built less than

14 days prior.to the observation. The date for when the scaffolding blocking the

access and egress paths to the area was built could not be determined.

c.

Conclusions

The scaffolding that was blocking the safe shutdown emergency lights was not

documented as being erected for more than 14 days. Therefore, no LCS violation

occurred. The inspector considered that even though operators were not tracking

the inoperability of the emergency lights to ensure that at 14 days they needed to

utilize portable lanterns, the safety consequence was minimal because, during a

shutdown from outside the control room, emergency supply kits provided to

operators contained portable lanterns. While the root cause was a programmatic

breakdown in the programs for control of scaffolding erection and inspection of fire

protection equipment, the licensee corrective actions were thorough.

V. Manaaement Meetinas

X1

Exit Meeting Summary

The inspectors presented the inspection results to members of licensee management

at the exit meeting on December 4,1996. The licensee acknowledged the findings

presented.

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The inspectors asked the licensee whether any materials examined during the

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inspection should be considered proprietary. No proprietary information was

identified.

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ATTACHMENT

PARTIAL LIST OF PERSONS CONTACTED

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Licensee

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D. Brieg, Manager, Station Technical

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J. Fee, Manager, Maintenance

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G. Gibson, Manager, Compliance

D. Herbst, Manager, Site Quality Assurance

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P. Knapp, Manager, Health Physics

R. Krieger, Vice President, Nuclear Generation

D. Nunn, Vice President, Engineering and Technical Services

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T. Vogt, Plant Superintendent, Units 2 and 3

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R. Waldo, Manager, Operations

M. Wharton, Manager, Nuclear Engineering Design

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INSPECTION PROCEDURES USED

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IP 37551:

Onsite Engineering

IP 61726:

Surveillance Observations

IP 62707:

Maintenance Observations

IP 71707:

Plant Operations

IP 71750:

Plant Support Activities

IP 92700:

On Site LER Review

IP 92712:

Inoffice Review of LER

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IP 92902:

Followup - Maintenance

IP 92904:

Followup - Plant Support

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ITEMS OPENED AND CLOSED

Ooened

50-362/96015-01

VIO

VCT inlet diversion valve controller in incorrect mode

50-361 (362)/96015-02

IFl

UFSAR changes to VCT operation

Ooened and Closed

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50-361/96015-03

NCV missed CEAC surveiPar.ca

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Closed

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50-361/93016-02

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differences in ultrasonic testing wall thickness

measurements

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50-361/96008-01

VIO

performance of maintenance activities on wrong unit

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50-362/96006-00

LER

containment purging isolation actuat!on

60-362/96004-00

LER

RCS pressure boundary leakage

50-362/96002-00, 01

LER

potential decalibration of log powei level

instrumentation

50-362/96009-05

IFl

SG blowdown RM misalignment

LIST OF ACRONYMS USED

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ACO

assistant control operator

AR

action request

CE

Combustion Engineering

CEA

control element assembly

CEAC

control element assembly calculator

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CEDMCS

control element drive mechanism control system

CFMS

critical functions monitoring system

CO

control operator

CPC

core protection calculator

CPIS

containment purge isolation signal

CRS

control room supervisor

DBD

design basis document

ECW

emergency chilled water

l&C

instrumentation and controls

LCO

limiting condition for operation

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LCS

licensee-controlled specifications

LER

licensee event report

MO

maintenance order

MSSV

main steam safety valve

NCR

nonconformance report

PDR

Public Document Room

PLCEA

part-length control element assembly

RCS

reactor coolant system

RM

radiation monitor

RTD

resistance temperature detector

SG

steam generator

TS

technical specification

UFSAR

Updated Final Safety Analysis Report

VCT

volume control tank

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