ML20129D767

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Insp Rept 50-382/96-11 on 960721-0831.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support
ML20129D767
Person / Time
Site: Waterford Entergy icon.png
Issue date: 09/20/1996
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20129D731 List:
References
50-382-96-11, NUDOCS 9609300183
Download: ML20129D767 (20)


See also: IR 05000382/1996011

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ENCLOSURE 2

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket No.:

50 382

License No.:

NPF-38

Report No.:

50-382/96-11

Licensee:

Entergy Operations, Inc.

Facility:

Waterford Steam Electric Station, Unit 3

Location:

Hwy.18

Killona, Louisiana

Dates:

July 21 through August 31,1996

Inspectors:

L. A. Keller, Senior Resident inspector

T. W. Pruett, Resident inspector

D. L. Proulx, Resident inspector, River Bend Station

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Approved By:

P. H. Harrell, Chief, Project Branch D

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ATTACHMENTS-

Attachment 1:

Partial List of Persons Contacted

List of Inspection Procedures Used

List of items Opened, Closed, and Discussed

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List of Acronyms Used

9609300183 960920

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ADOCK 05000302

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EXECUTIVE SUMMARY

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Waterford Steam Electric Station, Unit 3

NRC Inspection Report 50-382/96-11

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This routine, announced inspection included aspects of licensee operations, maintenance,

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engineering, and plant support. The report covers a 6-week period of resident inspection.

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Operations

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All observed operations activities were conducted professionally and were

consistent with safe operation of the facility (Section 01.1).

A licensee audit revealed that the appropriate Limiting Conditions for Operation

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(LCO) was not entered for two Component Cooling Water (CCW) valves on the

Equipment out-of-service (EOS) List, due to the failure of operators to recognize that

the valves had a closed safety function. The inspectors determined that the valves

were always capable of performing their closed safety function, the valves'

condition did not require LCO entry and, therefore, this error was administrative in

nature (Section 04.1).

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A nuclear auxiliary operator's inadvertent addition of the wrong type of oil to the

CCW Pump A outboard bearing was a result of a lack of attention to details and is

considered a noncited violation (Section 04.2).

Maintenance

The licensee's maintenance scheduling process did not include provisions for

quantitative assessments of unscheduled maintenance. Additionally, the qualitative

assessments of maintenance on engineered safety features systems, concurrent

with switchyard maintenance, was not implemented by the on-shift operations staff

consistent with established practices. The adequacy of the licensee's risk

assessments for unscheduled maintenance is an unresolved item (Section M1.2).

As a result of not returning a manual / automatic station setpoint to its original state

following maintenance, Auxiliary Component Cooling Water (ACCW) Pump B

inadvertently started when power was returned to the pump. The unexpected start

of the ACCW pump caused a waterhammer in the system. The failure to provide

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written instructions appropriate to the circumstances for returning the

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manual / automatic station to service is a violation of Technical Specification (TS) 6.8.1.a (Section M4.1).

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A licensee self-assessment team questioned whether degraded CCW flows through

the containment fan coolers indicated the coolers were not in compliance with a TS

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surveillance requirement. The licensee concluded that there was adequate CCW

flow to meet all design basis requirements and that the coolers were in compliance

with TS. The issue of compliance with TS Surveillance Requirement 4.6.2.2.b.2

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and the adequacy of the 1325 gpm value is unresolved pending review by the

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NRC's Office of Nuclear Reactor Regulation (NRR) (Section E4.1).

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' .The engineering self-assessment finding that CCW flows experienced during

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full-flow conditions might indicate noncompliance with TS Surveillance

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Requirement 4.6.2.2 for the containment f an coolers was a positive example of

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questioning attitude. Overall, the self-assessment provided good findings and

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recommendations (Section E7).

Rosemount transmitter calibrotion errors were found to be of minor safety

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significance. The failure to appropriately calibrate certain Rosemount transmitters is

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identified as a noncited violation (Section E8).

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The licensee's corrective actions related to the latest Reactor Coolant Pump

(RCP) 2B baffle bolt failures were adequate (Section E8.4).

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Plant Suocort

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Allowing Emergency Operating Facility (EOF) diesel generator fuel oil storage tank

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level to decrease below 50 percent and not providing a user's guide for EOF plant

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monitoring computer terminals were identified as poor emergency planning practices

(Section P2.1).

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Reoort Details

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Summarv of Plant Status

The plant began this inspection period in mid-loop operations due to RCP 2B seal problems.

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On July 30,1996, RCP 2B seal replacement activities were completed and the plant was

placed in Mode 4. The plant reentered Mode 5 later that day due to RCP 2B exhibiting

similar seal problems that initiated the forced outage, on July 16, to replace the seal

package. The seal was replaced and the plant entered Mode 4 on August 3. Mode 1 was

entered on August 5 and the plant operated at or near full power throughout the rest of

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this inspection period.

I. Operations

01

Conduct of Operations

01.1 General Comments (71707)

Using Inspection Procedure 71707, the inspectors conducted frequent reviews of

ongoing plant operations, control room board walkdowns, and plant tours. All

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observed activities were conducted professionally and were consistent with safe

operation of the facility. Operators displayed good knowledge of plant status and

understood the reason why control room annunciators were in alarm.

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04

Operator Knowledge and Performance

04.1 Failure to Recoanize Closed Safetv Function of CCW Valves

a.

Inspection Scoce (71707)

On July 3,1996, the inspectors were informed that two CCW valves with closed

safety functions had been previously declared out of service without closing the

valves or entering the appropriate LCO. The inspectors reviewed the background

and circumstances associated with the valves being out of service and reviewed the

EOS list to determine if there were generic problems in this area. The EOS list is

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maintained by the licensee to track the status of equipment that has been removed

from service. This list is used by the operations crews to ensure that any system

affected by the equipment out of service will be declared inoperable and the

appropriate TS LCO entered.

b.

Observations and Findinas

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During a review of the EOS list on July 3, the licensee noted that Valves CC-620

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(spent fuel pool heat exchanger temperature control valve) and CC-636 (letdown

heat exchanger temperature control valve) have a closed safety function per the

inservice testing program design basis documentation. Although these valves were

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on the EOS list, they were in service and operating appropriately to throttle CCW

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through the respective heat exchangers. The personnel performing the EOS list

review noted that if Valves CC-620 and -636 were truly out of service then the

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valves should either be closed or the appropriate TS LCO entered. Upon discovery

of this problem on July 3, the licensee entered 1S 3.7.3 for CCW Train A.

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Valve CC-620 was placed on the EOS list on February 6,1996, for replacement of

the manual handwheel stem actuator coupling key. The valve was tagged out, but

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the work was never performed and the clearance was restored. Although the valve

was returned to service, it remained on the EOS list as a result of the limit switch

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being inoperable. The licensee determined that the limit switch problem did not

prevent Valve CC-620 from fulfilling its safety function and removed Valve CC-620

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from the EOS list on July 3.

Valve CC-636 was placed in the EOS list on October 9,1995, in order to perform a

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modification to the valve in accordance with Design Change 3430. The

modification involved replacing the existing butterfly valve with a smaller globe

valve. The clearance tags were subsequently removed and the valve was returned

to service; however, since a portion of this modification was not completed, the

valve remained on the EOS list. The licensee determined that the unfinished portion

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of the modification did not prevent Valve CC-636 from fulfilling its safety function

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and removed it from the EOS list on July 3. TS 3.7.3 was exited, on July 3, after

Valves CC-620 and -636 were removed from the EOS list.

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The inspectors determined that Valves CC-620 and -636 were returned to service,

but left on the EOS list, due to the failure of operators to recognize that these

valves had a closed safety function. The inspectors independently confirmed that

Valves CC-620 and -636 were always capable of performir.g their closed safety

function, and would not have required LCO entry. Therefore, this error was

administrative in nature. The inspectors reviewed the other items on the EOS list

and determined that there were no other items that would require the licensee to

enter a TS LCO action statement. The inspectors noted that the Procedure

OP-100-10, " Equipment Out Of service," Revision 7, was in the process of being

revised to assist the operators in determining if entry into a TS LCO was appropriate

after taking a component out of service.

c.

Conclusions

The inspectors determined that Valves CC-620 and -636 were always capable of

performing their closed safety function, the valves' condition did not require LCO

entry and, therefore, this error was strictly administrative in nature.

04.2 Addition of incomoatible Oil to CCW Pumo

a.

Insoection Scoce (71707)

The inspectors reviewed the licensee's response to their identification that a nuclear

auxiliary operator added incompatible oil to the CCW Pump A outboard bearing,

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b.

Observations and Findinos

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On August 23,1996, while investigating a CCW Pump A outboard bearing oil leak,

the licen'see noted from the lube oil addition records that a nuclear auxiliary operator

added 215 milliliters of SHC 626 (motor bearing oil) instead of DTE-MED (pump

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bearing oil) to the CCW Pump A outboard bearing on August 19. The licensee

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determined the cause to oe human error in that the individual misread the type of oil

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to be used from the computerized equipment database.

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Maintenance engineering determined that the oils were incompatible in that mixing

of the different oils in the pump bearing could result in sludge formation. The

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licensee's immedime corrective actions included draining, flushing, and placing the

correct oil in the bearing; performing a satisfactory inservice test; and counseling

the individual. The licensee estimated that there was not enough incompatible oil

added to result in bearing failure under any accident scenario. The licensee

performed checks to verify that the proper oil had been added to other pumps and

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motors and identified no additional problems.

Procedure UNT-005-007, " Plant Lubrication Program," Section 5.4.2, stated that

only lubricants specified on the information sheet in the Station Information

Management System shall be used in lubrication tasks. The f ailure to ensure the

correct oil was added to the CCW Pump A outboard bearing is a violation of

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TS 6.8.1.a. This licensee-identified and corrected violation is being treated as a

noncited violation, consistent with Section Vll.B.1 of the Enforcement Policy.

Specifically, the violation was identified by the licensee, was not willful, actions

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taken as a result of a previous violation should not have corrected this problem, and

appropriate corrective actions were completed by the licensee (50-382/9611-01).

c.

Conclusions

A nuclear auxiliary operator inadvertently read the wrong line item off a

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computerized database which resulted in the addition of the wrong type of oil to the

CCW Pump A outboard bearing. This error was a result of a lack of attention to

details and is considered a noncited violation.

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II. Maintenance

M1

Conduct of Maintenance

M1.1 General Comments

a.

Inspection Scope (61726,62707)

The inspectors observed all or portions of the following activities:

  • WA01149811:

Replace RCP 2B mechanical seal

  • WA01149346:

Troubleshoot / check calibration of Valve ACC-126B

  • WA01147321:

VOTES testing of Valve SI-125B in accordance with

ME-007-047

  • PE-005-004:

Control room envelope integrity test

  • OP-903-068:

Emergency Diesel Generator A monthly surveillance

  • STP-115-0154: Special test procedure - CCW system flow balance

b.

Observations and Findinas

in general, the inspectors found the work performed to be adequate. All work

observed was performed with the work authorization (WA) package and/or test

procedure present and in active use. Technicians were experienced and

knowledgeable of their assigned tasks. When applicable, appropriate radiation

control measures were implemented. However, certain maintenance activities

appeared to be in violation of NRC requirements or indicate problem areas, as

discussed below in Sections M1.2 and M4.1.

M1.2 On-Line Maintenance Risk Assessment for Unscheduled Work

a.

Inspection Scoce (62707)

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The inspectors performed a review of the licensee's process for ensuring that the

assessment of equipment removed from service considered the impact on the

performance of safety functions.

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b.

Observations and Findinos

During a review of scheduled maintenance activities performed on August 12-14,

1996, the inspectors noted that the licensee removed portions of the low-pressure

safety injection (LPSI), high-pressure safety injection (HPSI) and containment spray

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(CS) Train B systems from service in conjunction with the performance of

switchyard maintenance affecting batteries and a phase comparison relay.

Scheduling personnel performed a quantitative analysis of the on-line maintenance

using the risk monitor and determined that the activities involving LPSI, HPSI, and

CS constituted an ac'ceptable risk (plant safety index of 8.8 and a core damage

frequency increase of 2.79E-5). The inspectors noted that the analysis did not

include the impact of performing concurrent switchyard maintencnce. The risk

inonitor is a computer tool maintained by safety and engineering analysis and

utilized by planning and scheduling to quantitatively determine core damage

frequencies for on-line maintenance.

The switchyard battery maintenance involved installing and parallelling a temporary

battery, disconnecting the normal battery, performing activities on the normal

battery, and reconnecting the normal battery. The maintenance on the phase

comparison relay was performed in response to a failure causing one of the two

main transformer output breakers to open. The licensee stated that the shift

supervisor was aware of the switchyard maintenance activities and that based on

his understanding, no significant increase in risk occurred as a result of these

activities.

The inspectors noted that switchyard maintenance was not identified on the

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maintenance schedule, that scheduling was unaware of the switchyard maintenance

activities, and that the switchyard maintenance activities had not been factored into

the quantitative risk assessment. In response to the inspectors' concern,

scheduling f actored in the unplanned switchyard work in conjunction with the

planned LPSI, HPSI, and CS maintenance and determined that the resulting plant

safety index (6.1) and a core damage frequency increase (7.04E-4) were in the

"high risk" category. Scheduling stated that they would not have allowed the

performance of the maintenance activities associated with LPSI, HPSI, and CS had

they been aware of the switchyard maintenance activities.

The inspectors noted that the risk monitor enabled the user to select one of four

options for a potential loss of offsite power and that the licensee had not

established specific criteria associated with each of the four options. As of

August 14, scheduling arbitrarily assigned the worst case loss of offsite power

penalty into the risk monitor for any switchyard maintenance activity. The licensee

subsequently determined that the performance of the switchyard maintenance did

increase the risk of a potential loss of offsite power, but not to the degree in which

the scheduling department originally calculated.

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The inspectors questioned the licensee to determine if assessments of emergent or

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unscheduled maintenance activities on the overall effect on performance of safety

functions were being performed. Based on discussions with scheduling,

maintenance, and operations, the inspectors determined that the licensee routinely

did not quantitatively assess the impact of unscheduled maintenance on the

performance of safety functions. However, the licensee did perform a limited

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qualitative assessment in that the on-line maintenance philosophy only allowed

work on selected components within a single safety train and that maintenance on

components in separate safety trains or in conjunction with electrical power source

maintenance would not be performed.

The inspectors noted that the qualitative assessments, which were frequently

performed by the operations shift supervisor, were informal and relied primarily

upon the knowledge level of each individual (i.e., no checklist, matrix, or other tool).

The inspectors questioned several senior reactor operators to determine what

function the switchyard batteries performed. Based on these discussions, the

inspectors determined that the knowledge level of operations personnel regarding

the function of the switchyard batteries varied widely. Specifically, the range o'

responses provided to the inspector was from no knowledge of the battery fur;ction,

to back-up power supply to annunciators, to back-up power supply for protective

relays, to a full understanding of the purpose of switchyard batteries.

The inspectors noted that the shift supervisor's assessment of the qualitative risk

was not consistent with current on-line maintenance practices in that maintensnce

on one train of LPSI, HPSI, and CS were performed concurrently with mainteni nee

on an electric power source.

In response to the inspectors' observations, the lionsee commenced a review of

on-line maintenance controc. Interim corrective actions taken by the licensee

included, in part: (1) operations personnel ncofying scheduling of unscheduled

maintenance activities, (2) providing the operations shift support center with the

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risk monitor capability, and (3) providing personnel with a consistent methodology

to assess the risk of performing switchyard maintenance on a loss of offsite power.

The inspectors questioned the adequacy of the quantitative and qualitative

assessments for maintenance activities involving switchyard maintenance in

conjunction with LPSI, HPSI, and CS maintenance on August 12-14. The

inspectors concluded that the licensee's maintenance scheduling process did not

provide provisions for quantitative assessment of risk of unscheduled maintenance

activities. This issue will be tracked as an unresolved item pending an evaluation of

the licensee's risk assessment process by the NRC maintenance rule review

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committee (50-382/9611-02).

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Conclusions

The licensee's maintenance scheduling process did not include provisions for

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quantitative assessments of risk of unscheduled maintenance. Additionally, the

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qualitative assessments of maintenance on engineered safety features systems,

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concurrent with switchyard maintenance, was not implemented by the on-shift

operations staff consistent with established practices. The adequa.:y of the

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licensee's risk assessments for unscheduled maintenance is an unresolved item.

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M4

Maintenance Staff Knowledge and Performance

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M4.1 Inadvertent ACCW Pumo Start and System Waterhammer

a.

Insoection Scoce (62707)

The inspectors reviewed the circumstances surrounding an inadvertent automatic

start of ACCW Pump B and coincident waterhammer of the ACCW system following

maintenance on a CCW temperature control instrument loop.

b.

Observations and Findinas

On July 29,1996, ACCW Pump B automatically started when control power was

restored to the 4160-volt feeder breaker following maintenance on a CCW

temperature control instrument loop. The unexpected start of the ACCW pump

caused a waterhammer in the system. The susceptibility of the ACCW system to

waterhammer during an ACCW pump start due to void formation in the ACCW

system is discussed in NRC Inspection Report 50 382/95-23. Due to the potential

to damage ACCW system components from waterhammer, the licensee, by

procedure, shuts the pump discharge valve prior to starting the pump. Since this

was an inadvertent start, the discharge valve was open, and as a result, the system

experienced a waterhammer. The licensee walked down the system and

determined that the waterhammer event did not damage the system.

The licensee determined the cause of the inadvertent pump start was the failure to

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restore the CCW temperature control loop manual / automatic Station CC ITIC70708

setpoint to its original setting following maintenance. Manual / automatic Station

CC ITIC7070B provides control signals to Valve ACC-1268 (CCW heat exchanger

outlet temperature control valve), which in turn throttles CCW flow through the

CCW heat exchanger in order to maintain CCW temperature at a predetermined

setpoint. An automatic start signal is sent to the respective ACCW pump when the

CCW train temperature exceeds the manual / automatic setpoint by more than 10 F.

This particular pump start occurred because the manual / automatic station setpoint

was set at 50*F (minimum) when it was returned to service, while CCW water

temperature was 86*F.

As of the end of this inspection period, the licensee had not completed their root

cause assessment for this incident. The inspectors performed an independent

assessment and determined that the written instructions included in the WA

package for the maintenance on the CCW temperature control loop

manual / automatic station were not appropriate to the circumstances. Specifically,

WA01149346 did not address restoring the manual / automatic Station

CC ITIC70708 setpoint to its original setting following maintenance. The inspectors

observed that this activity did not appear to be within the skill of the craft. The

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failure to provide written instructions appropriate to the circumstances for CCW

temperature control loop maintenance is a violation of TS 6.8.1 (50-382/9611-03).

c.

Conclusions

The inspectors concluded that the WA did not provide instructions appropriate to

the circumstances for restoring the CCW temperature control loop to service

following maintenance.

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Miscellaneous Maintenance issues (92902)

M8.1 (Closed) Insoection Followuo item 50-382/9604-01: Review of the licensee's

evaluation on extending replacement scheduie for safety-related relays. The

licensee extended the replacement schedule for numerous safety-related Agastat

relays from 10 to 40 years, despite vendor guidance that the qualified life of the

relays was 10 years. The inspectors reviewed the licensee's evaluation for

extending the replacement schedule and determined that it followed acceptable

practices for determining the life of electric / electronic components; however, it did

not address the vendor's rationale for establishing 10 years as the replacement

interval. The inspectors were unable to clearly establish the relay vendor's basis for

selecting 10 years as the qualified life. However, the inspectors determined that

the vendor had not identified an anticipated failure mechanism for these relays that

would occur after some specific period of operation in excess of 10 years. The

inspector noted that these relays were included in the licensee's maintenance

program and are routinely tested. The inspectors noted that, per the licensee's

testing and corrective action programs, any relay failures that were the result of

age-related phenomenon would require evaluation of the replacement schedule. The

inspectors determined that the licensee's extension of the replacement schedule for

these relays was acceptable.

Ill. Enaineerina

E2

Engineering Support of Facilities and Equipment

E.2.1 Review of Facility and Eouloment Conformr,nce to Uodated Final Safety Analysis

Report (UFSAR) Descrirtion

A recent discovery of a licensee operating a facility in a manner contrary to the

UFSAR description highlighted the need for a special focused review that compares

plant prcctices, procedures and/or parameters to the UFSAR descriptions. While

performing the inspections discussed in this report, the inspectors reviewed the

applicable portions of the UFSAR that related to the areas inspected. The following

inconsistency was noted between the wording of the UFSAR and the plant

practices, procedures and/or parameters observed by the inspectors.

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  • UFSAR Tables 6.2-6,6.2 21, and 9.2-3 specified CCW flow rates thiough the

containment fan coolers and shutdown cooling heat exchangers that were not

consistent with those demonstrated during a special test conducted in

, October 1995 and August 1996. This issue is discussed in Section E4.1.

E4

Engineering Staff Knowledge ind Performance

E4.1

CCW Flow issues

a.

Insoection Scoce (37551)

On August 12,1996, during the ultimate heat sink design basis self-assessment, a

question was identified by the self-assessment team regarding the low flow results

obtained during a CCW flow balance test performed during the last refueling outage

(RFO 7) and the impact on the TS flow requirements. The inspectors reviewed the

flow balance test results, CCW startup testing results, the licensee's operability

analysis, and the applicable UFSAR and TS sections.

b.

Observations and Findinas

TS Surveillance Requirement 4.6.2.2.b.2 requires verifying that, following a safety

injection actuati:.n signal, CCW flow to each containment fan cooler is greater than

or equal to 1325 gpm. The licensee's test to verify flow greater than 1325 gpm is

typically conducted with CCW in its normal alignment and, therefore, flows through

the containment f an coolers are greater than would be expected during a design

basis accident. Tests conducted with CCW in its normal lineup have always

resulted in flows through the coolers greater than 1500 gpm.

On August 12, a licensee self-assessment team noted that a special test, conducted

during RFO 7, with CCW in its accident lineup, demonstrated flows less than

1325 gpm to each containment fan cooler. The licensee generated Condition

Report (CR) 95-0955 to document and evaluate that CCW flow through the

containment fan coolers was less than the value specified in the UFSAR, which was

1350 gpm. The flow through the coolers was:

Train A

Containment Fan Cooler A 1300 gpm

Containment Fan Cooler C 1320 gpm

Train B

Containment Fan Cooler B 1200 gpm

Containment Fan Cooler D 1290 gpm

CR 95-0955 and its attached engineering analysis concluded that the containment

fan coolers remained operable as long as CCW flow was greater than 1100 gpm.

However, the CR did not address the applicability of TS Surveillance Requirement 4.6.2.2.b.2.

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in response to the self-assessment team's concern, the licensee performed an

assessment of the CCW flows through the coolers under accident conditions and

determined that the coolers remained operable and were in compliance with the TS

, operability requirements. The basis for the licensee's position was that the value of

1325 gpm, as specified in the TS, was a design assumption for analysis and not

intended as a minimum flow requirement through the containment fan coolers. The

licensee stated that the intent of TS Surveillance Requirement 4.6.2.2.b.2 was to

verify that the flow control valve for the cooler was fully open and not to verify

minimum accident flow rates would be achieved. The inspectors acknowledged the

licensee's position and the information was forwarded to NRR for a determination of

compliance with the TS.

The inspectors questioned the difference between the UFSAR value of 1350 gpm

and the TS value of 1325 gpm. It was determined by engineering that there is a

25 gpm tolerance for error for instruments used to measure CCW flow through the

coolers. The licensee stated that this tolerance was apparently applied in the wrong

direction to ensure 1350 gpm to each cooler. The inspectors noted that if the

instrument uncertainty had been applied appropriately, the TS value would be

1375 gpm.

CR 95-0955 documented degraded CCW through the shutdown cooling heat

exchangers (2900 gpm vice UFSAR value of 3000 gpm) in addition to the

containment fan coolers. The CR determined the apparent cause of the degraded

CCW flows was increased flow resistance through the dry cooling towers as a

result of fouling. The CR concluded that as long as flow through the containment

fan coolers exceeded 1100 gpm and flow through the shutdown cooling heat

exchangers exceeded 2600 gpm, no operability concern existed. Therefore, the

plant was started up with the expectation that the dry cooling tower tubes would

be cleaned during system outages and the CCW full-flow test would be reperformed

during the next refueling outage, scheduled for the spring of 1997. The dry cooling

tower cleaning was completed in February 1996.

On August 23, the licensee performed a CCW full-flow test after the dry cooling

towers were cleaned. The results of the August 23 test were:

Train A

Containment Fan Cooler A 1340 gpm

Containment Fan Cooler C .1310 gpm

Train B

Containment Fan Cooler B 1250 gpm

Containment Fan Cooler D 1370 gpm

These results indicated that at least one cooler in each train has CCW flow greater

than the TS required a minimum of 1325 gpm. These flowrates satisfied the

requirements for system operability as specified in TS 3.6.2.2.

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The issue of compliance with TS Surveillance Requirement 4.6.2.2.b.2 and the

1325 gpm flow requirement specified in the TS is unresolved pending review by

NRR (50-382/9611-04).

c.

Conclusions

The inspectors acknowledged the licensee's position that they were in compliance

with the TS requirements for CCW flow through the containment fan coolers

following a safety injection actuation signal. The inspectors determined that the TS

value of 1325 gpm through the coolers was the result of applying instrument error

in the wrong direction. The issue of compliance with TS Surveillance

Requirement 4.6.2.2.b.2 and the adequacy of the 1325 gpm value is unresolved

pending review by NRR.

E7

Quality Assurance in Engineering Activities (37551)

From August 12-16,1996, the licensee performed an engineering self-assessment

of the ultimate heat sink (CCW and ACCW systems). The self-assessment team

was composed of offsite engineering personnel (both Entergy and contractors)

knowledgeable in the subject areas. On August 12, the self-assessment team

questioned whether degraded CCW flows through the containment fan coolers

during previous full-flow testing indicated the coolers were not in compliance with

the TS surveillance requirement. The inspectors considered the self-assessment

team's identification of this issue to be a positive example of questioning attitude.

The technical aspects of this issue are discussed in Section E4.1. The issue of

compliance with TS Surveillance Requirement 4.6.2.2.b.2 is unresolved pending

review by NRR.

The inspectors attended the exit meeting for the licensee's ultimate heat sink

self-assessment team and noted the team provided valuable insights into the

ultimate heat sink deign basis, material condition, and operating practices.

E8

Miscellaneous Engineering issues (92700,92903)

E8.1

(Closed) Unresolved item 50-382/9510-03: Rosemount instrument transmitter

calibration errors. On November 2,1995, while reviewing main steam flow

calculations, the licensee discovered that the static pressure correction for some

safety- and nonsafety-related Rosemount differential pressure flow and level

transmitters was in error. The misapplication of the static pressure correction and

subsequent instrument calibrations resulted in safety injection tank (SIT) and steam

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generator indicated levels being higher than the actuallevel. Records indicated that

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the SIT actual levels were below the minimum level allowed by TS 3.5.1 for periods

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longer than the allowed outage time. The licensee submitted Licensee Event Report

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(LER)95-005 to address this issue. The inspectors left this item unresolved until

the licensee reviewed all other calculations associated with Rosemount transmitters

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to determine the extent of the problem and to review the licensee's corrective

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actions.

Subsequently, the licensee submitted LER 96-001, which again concerned

out-of-specification SIT levels. Due to the previous error corrections associated

with LER 95-005, two SIT levels were out-of-specification high, requiring entry into

TS 3.0.3 for 14 minutes. The licensee demonstrated that although the SIT levels

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were outside TS limits, they did not exceed the levels assumed in the safety

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analysis. Therefore, this event was of minor safety consequence.

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The inspectors evaluated the licensee's results of the calculation reviews. The

licensee identified a number of other errors in applying correction factors to

Rosemount transmitter outputs. These errors did not affect operability of any

safety-related Rosemount transmitters and were not safety significant. These items

were corrected upon discovery.

The two examples of f ailure to control SIT levels within the.TS limits is a violation

of TS 3.5.1. This licensee-identified and corrected violation is being treated as a

noncited violation, consistent with Section Vll of the NRC Enforcement Policy.

Specifically, the violation was identified by the licensee, was not willful, actions

taken as a result of a previous violation should not have corrected this problem, and

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appropriate corrective actions were completed by the licensee (50-382/9611-05).

E8.2 (Closed) LER 50-382/95-005: Rosemount instrument transmitter errors. This item

was addressed in Section E8.1 of this report.

E8.3 (Closed) LER 50-382/96-001: Entering TS 3.0.3 due to safety injection tank levels

reading high. This item was addressed in Section E8.1 of this report.

E8.4 (Closed) Insoection Followuo item (IFI) 50-382/9610-02: Review root cause and

corrective actions for RCP baffle bolt f ailures. On July 16,1996, the plant was

shut down when flow through the RCP 2B mechanical seal was lost. The licensee

removed the mechanical seal cartridge and found that all six bolts on the rotating

baffle, located immediately below the seal cartridge, were broken. The bolts are

used to retain the baffle to the RCP shaft. The baffle itself fits over and directs

controlled bleed-off flow through the seal heat exchanger to cool the water prior to

entering the seal cartridge.

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Examination of the mechanical seal found metallic particles within the pressure

breakdown device and between the seal faces. The licensee concluded that these

metallic particles were wear products that resulted from the baffle bolt f ailures. The

cause of the failure of the baffle bolts was determined to be loss of bolt preload.

Loss of preload reduces the clamping force of the joint between the baffle and the

RCP shaft and can result in relative motion between the baffle and bolts, which can

result in fatigue failure of the bolting. The most likely cause of loss of preload was

identified by the licensee as inadequate thread engagement. To prevent future bolt

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failures, the baffle bolts were modified to add 1/2 inch to their length. Additionally,

proper preload was ensured by measuring the elongation of the baffle bolts during

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installation.

  • " On July 29-30, following the initial RCP 2B seal failure outage, the licensee again

experienced seal f ailure shortly after placing RCP 2B in service. The licensee

determined that the cause of this failure was blockage of the mechanical seal from

existing debris. The mechanical seal was again replaced and all potential sources of

debris were thoroughly cleaned and inspected. The pump was returned to service

on August 3 with no further seal problems experienced to date.

IV. Plant Support

P2

Status of Emergency Planning (EP) Facilities, Equipment, and Resources

P2.1

Tour of EOF

a.

Insoection Scooe (71750)

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On July 29,1996, the licensee distributed Inter-Office Correspondence

W3D3-96-0146, "Waterford 3 Technical Support Center (TSC) Staffing." The

correspondence indicated that when access to the control room envelope is limited

to a specified number of persons and an emergency occurs requiring staffing and

activation of the TSC, responders shall report to the EOF. The correspondence was

initiated in response to deficiencies involving leakage of the normal air intake

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Valves HVC-101 and -102 (See NRC Inspection Report 50-382/9621).

On August 14, the inspectors performed a walk through and inventory of the EOF

to ensure that the licensee would be able to accommodate inclusion of TSC

personnel in the EOF.

b.

Observations and Findinas

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The inspector observed that the EOF diesel generator fuel oil storage tank capacity

was 500 gallons and that the level was 225 gallons. EP personnel stated that the

diesel generator operated for 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> every Tuesday which resulted in an

approximate 4 gallon decrease in fuel oil storage tank level. EP personnel also

stated that a task existed that required the fuel oil storage tank be drained and

refilled every year and that the task may not be performed frequently enough to

maintain a desirable quantity of fuel oilin the storage tank. Following the

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inspectors observation, EP personnel initiated a new task to verify the fuel oil

storage tank level once per month and to refill the tank if the level decreased to

300 gallons.

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The inspector observed that a plent monitoring computer user's guide was not

located at each operating station. in October 1995, the licensee replaced the old

plant monitoring computer with a new model. Because the user's guide had not

been approved by the licensee, EP personnel did not provide user instructions for

the ne.w plan't monitoring computer stations in the EOF. Following the inspectors'

observation, emergency planning provided copies of selected attachments from

Procedure OP-004-012, " Plant Computer System," at each operating station.

Emergency planning stated that the user's guide would be placed at each operating

station once the procedure was revised.

The inspectors observed that the licensee had the 1993 version of

NUREG/BR 0150, " Response Technical Manual," instead of the 1996 version. In

response to the inspectors' observation, the licensee obtained several copies of the

1996 NUREG/BR 0150 version. EP personnel stated that updated copies of

NUREG/BR 0150 were normally provided by the NRC when new revisions were

issued and that there had been a delay in the licensee's receipt of the updated

revision.

c.

Conclusions

The inspectors determined that allowing the EOF fuel oil storage tank level to

decrease below 50 percent and not providing a user's guide for the plant monitoring

computer were poor emergency planning practices.

V. Manaaement Meetinas

X1

Exit Meeting Summary

The inspectors presented the inspection results to members of licensee management

at the conclusion of the inspection on September 9,1996. The licensee

acknowledged the findings presented.

The inspectors asked the licensee whether any materials examined during the

inspection should be considered proprietary. No proprietary information was

identified.

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ATTACHMENT 1

PARTIAL LIST OF PERSONS CONTACTED

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Licensee

R. G. Azzarello, Manager, Maintenance

C. M. Dugger, General Manager, Plant Operations

J. J. Fisicaro, Director, Nuclear Safety

T. J. Gaudet, Acting Manager, Licensing

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D. C. Matheny, Manager, Operations

M. B. Sellman, Vice-President, Operations

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D. W. Vinci, Superintendent, System Engineering

A. J. Wrape, Director, Design Engineering

INSPECTION PROCEDURES USED

37551

Onsite Engineering

61726

Surveillance Observations

62707

Maintenance Observations

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71707

Plant Operations

71750

Plant Support Activities

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92901

Followup - Plant Operations

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92902

Followup - Maintenance

92903

Followup - Engineering

ITEMS OPENED. CLOSED, AND DISCUSSED

Opened

50-382/9611-01

NCV

Failure to follow procedures for oil addition to CCW pump

(Section 04.2)

50-382/9611-02

URI

Adequacy of quantitative and qualitative assessments for

risk of switchyard work in conjunction with other work

(Section M1.2)

50 382/9611-03

VIO

Inadequate written instructions for CCW temperature

control loop work (Section M4.1)

50-382/9611-04

URI

Compliance with TS Surveillance Requirement 4.6.2.2.b.2

and adequacy of 1325 gpm value (Section E4.1)

50-382/9611-05

NCV

Rosemount transmitter calibration errors (Section E8.1)

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Closed

50-382/9510-03

URI

Rosemount instrument transmitter calibration errors

(Section E8.1)

50 382/9604-01

IFl

Review licensee's evaluation on extending replacement

schedule for safety-related relays (Section M8.1)

50-382/9611-01

NCV

Failure to follow procedures for oil addition to CCW pump

(Section 04.2)

50-382/9611-05

NCV

Rosemount transmitter calibration errors (Section E8)

50-382/9610-02

IFl

Review root cause and corrective actions for RCP baffle

bolt failures (Section E8.4)

50-382/95-005

LER

Rosemount instrument transmitter errors (Section E8.2)

50-382/96-001

LER

Entering TS 3.0.3 due to safety injection tank levels

reading high (Section E8.3)

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LIST OF ACRONYMS USED

ACCW

Auxiliary Component Cooling Water.

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CCW

Component Cooling Water

CR

Condition Report

CS

Containment Spray

EO'F

Emergency Operating Facility

EOS

Equipment Out-of Service

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EP

Emergency Planning

gpm

Gallons Per Minute

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HPSI

High Pressure Safety injection

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IFl

Inspection Followup item

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LCO

Limiting Conditions for Operation

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LER

Licensee Event Report

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LPSI-

Low Pressure Safety injection

NRC

- Nuclear Regulatory Commission

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NRR

Office of Nuclear Reactor Regulation

PDR

Public Document Room

P

RCP

Reactor Coolant Pump

RFO

Refueling Outage

SIT

Safety injection Tank

TS

Technical Specifications

TSC

Technical Support Center

UFSAR

Updated Final Safety Analysis Report

WA

Work Authorization

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