ML20117M763

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SALP Rept 50-285/85-07 for Sept 1983 - Feb 1985
ML20117M763
Person / Time
Site: Fort Calhoun Omaha Public Power District icon.png
Issue date: 05/14/1985
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML20117M768 List:
References
50-285-85-07, 50-285-85-7, NUDOCS 8505170196
Download: ML20117M763 (37)


See also: IR 05000285/1985007

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SALP BOARD REPORT

.U.S.. NUCLEAR REGULATORY COMMISSION

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a

REGION IV

.

SYSTEMATIC APPRAISAL OF LICENSEE PERFORMANCE-

50-285/85-07

Omaha Public Power District

Fort Calhoun Station

September 1, 1983 --February 28, 1985

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INTRODUCTION

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The Systematic Assessment of Licensee Performance (SALP) program is an

integrated NRC staff effort to collect available observations and data on

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a periodic basis and to evaluate licensee performance based upon this

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information. SALP is supplemental to normal regulatory processes used to

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ensure compliance to NRC rules and regulations. SALP is intended to be

sufficiently diagnostic to provide a rational basis for allocating NRC

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resources and to provide meaningful guidance to the licensee's management

to promote quality and safety of plant operation.

An NRC SALP Board, composed of the staff members listed below, met on

April 16, 1985, to review the collection of performance observations and

data to assess the licensee performance-in accordance with the guidance in

NRC~ Manual Chapter 0516, " Systematic Assessment of Licensee Performance."

A summary of the guidance and evaluation criteria is provided in

Section II of this report,

,

This report is the SALP Board's assessment of the licensee's safety

performance at Fort Calhoun Station for the period September 1, 1983,

through February 28, 1985.

SALP Board for Fort Calhoun Station:

R. P. Denise, Director, Division of Reactor Safety and Projects

(Chairman)

'

R. L. Bangart, Director, Division of Radiation Safety and Safeguards

L. E. Martin, Section Chief, Project Section A, Reactor Project

Branch 2

L. A. Yandell, Senior Resident Inspector

J. R. Miller, Chief, Operating Reactors Branch 3

E. G. Tourigny, Project Manager

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Attendees at all or part of the SALP Board Meeting were:

R. E. Hall, Chief, Emergency Preparedness and Radiological

Protection Branch

W. C. Seidle, Technical Assistant

J. B. Baird, Chief, Emergency Preparedness Section

,

R. J. Everett, Chief, Nuclear Materials Safety Section

R. E. Baer, Regional Inspector

II. CRITERIA

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Licensee performance was assessed in 11 selected functional areas.

Each

functional area normally represents areas significant to nuclear safety

and the environment, and are normal programmatic areas.

One or more of the following evaluation criteria were used to assess each

functional area.

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1.

Management involvement and control in assuring quality.

2.

_ Approach to resolution of technical issues from a safety standpoint.

3.

Responsiveness to NRC initiatives.

4.

Enforcement history.

5.

Reporting and analysis of reportable events.

6.

Staffing (including management).

7.

Training effectiveness and qualification.

.

However,. the SALP Board is not limited to these criteria and others may

have'been used where appropriate.

Based upon the SALP Board assessment each functional area evaluated is

classi'ied into one of three performance categories. The definition of

-these performance categories is:

Categoryj.

Reduced NRC attention may be appropriate. Licensee

management attention and involvement are aggressive and oriented toward

nuclear safety; licensee resources are ample and effectively used so that

a high level of performance with respect to operational-safety is being

achieved.

Category 2.

NRC attention should be maintained at normal levels.

Licensee management attention and involvement are evident and are

concerned with nuclear safety; licensee resources are adequate and are

reasonably effective so that satisfactory performance with respect to

operational safety is being achieved.

Category 3.

Both NRC and licensee attention should be increased.

Licensee management attention or involvement is acceptable and considers

nuclear safety, but weaknesses are evident; licensee resources appear to

be strained or not effectively used so that minimally satisfactory

performance with. respect to operational safety is being achieved.

The SALP Board has also categorized the performance trend over the course

of the SALP assessment period. The trend is meant to describe the general

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or prevailing tendency (the performance gradient) during the SALP period.

This categorization is not a comparison between the current and previous

SALP ratings; rather the categorization process involves a review of

performance during the current SALP period and categorization of the trend

of performance during that period only.

The performance trends are

defined as follows:

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' Improved: Licensee performance has generally improved over the course of

the SALP assessment. period.

.Same:

Licensee performance has remained essentially constant over the

" course of. the SALP assessment period.

Declined: Licensee performance has generally declined over the course of

the.SALP assessment period.

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IIIT SUMMARY OF RESULTS

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In summary,. the ' licensee has exhibited significant-strength in the areas

of' plant operations, radiological controls, maintenance, fire protection,.

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surveillance, refueling, and licensing activities. Weak areas identified

included security and safeguards, and. training. The licensee's

performance and trend are summarized in the table below along with the

performance category-from the previous SALP evaluation period:

Previous

Present

Trend During

Performance

Performance

Latest

Category

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Category

-Functional Area-

(9/1/82 to 8/31/83) (9/1/83 to 2/28/85).

SALP

Period

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A.

~ Plant Operations

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1

Declined

B..

Radiological Controis-

1

Improved

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1.. Radiation Protection

2

N/A

2.

Chemistry / Radiochemistry

and Confirmatory

Measurements

3

N/A

3.

Radwaste Management,

Effluent Releases, and

Effluent Monitoring

2

N/A

4..

Transportation / Solid

Radwaste

3

N/A

5.

Environmental Monitoring

2

N/A

C.

Maintenance

2

1

Improved

D.

Surveillance

1

1

Same

. ' Fire Protection

2

1

Same

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F.

. Emergency Preparedness

2

2

Improved

' G.

~ Security and Safeguards

2

3

Improved

~H.

' Refuel.ing

1

1

Same

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Quality Programs and

Administrative Controls

Affecting Quality *-

3

2

Improved

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Licensing Activities

2

1

Improved

K.

Training-

3

3

Improved

  • This category-was divided into two individual categories in the

previous SALP report.

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The total NRC inspection effort during this'SALP evaluation period

consisted of.44 inspections including resident inspector. inspections'and-

emergency exercises for a total of 3,241 direct inspection man-hours.

LIV. PERFORMANCE ANALYSIS'

A.

Plant Operations

1.

Analysis-

This area was inspected on a continuing basis.by the NRC

resident inspector. .Four violations and no deviations were

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identified in this functional area during the appraisal period:

. Failure-to properly terminate a containment pressure

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.. reduction.when the limiting X/Q was exceeded.

(Severity

Level IV, 8407-01)

Failure to provide an adequate procedure requiring

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independent verification of tag-outs to_ ensure that

equipment was properly isolated.

(Severity Level IV,

8412-01)

Failure of shift supervisor to document review of

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maintenance orders.

(Severity Level IV, 8412-02)

Failure to install the locking device.on a closed valve as

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required by the procedure lineup.

(Severity Level IV,

8429-02)

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~ The four Licensee Event Reports (LERs) listed below involved

activities in the area af plant operations:

Inadvertent opening of breaker supplying power to a control

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room DC panel. (LER 84-003)

Unplanned actuation of VIAS while shifting to the high

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alert / alarm setpoints.

(LERs84-014, 84-019, and 84-024)

Fort Calhoun Station maintains an experienced group of senior

operators and reactor operators.

The plant manager, three of

the five technical area supervisors, three training supervisors,

and the plant engineer all hold and maintain senior reactor

operator licenses and provide support and technical expertise to

the operations department. Operating personnel exhibit a strong

commitment to procedural compliance and a good understanding of

technical issues associated with plant operations. These

strengths have been observed by NRC inspectors during emergency

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preparedness drills, routine operations, and abnormal plant

situations. The Fort Calhoun Station completed 302 days of

continuous operation (the longest in the plant's history) during

this evaluation period which is indicative of the high caliber

of onshift personnel. The plant experienced only one reactor

trip this SALP period, the first since December 1982.

The operations department has experienced a net loss of licensed

personnel during this appraisal period. Attrition due to

resignations, retirement, and one transfer to another department

prevents the licensee from manning a full six-shift rotation as

they did on January 1, 1984, when the new manning regulations

went into effect. Additional burden was placed on the licensed

operators due to long term disabilities, hospitalizations, and

the removal of one senior operator from the shift rotation for

training following his failure of the annual requalification

examination. A review of licensee statistics for the last

quarter of this appraisal period indicated that overtime work

hours are increasing.

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The licensee continued their program of upgrading the Fort

Calhoun Station annunciator system to eliminate nuisance alarms

and to h?vo no annunciators lit during power operation.

Significant progress was made during the last refueling outage

wfth work continuing in this area as part of the overall control

room design review being done in accordance with Supplement I to

NUREG-0737 (Generic Letter 82-33), Item 1.D.1.

Portions of the

safety parameter display system were energized this report

period and are available for use by the operators.

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2.

Conclusions

The overall performance level of the operations department has

'been excellent during this appraisal period. The net loss of

licensed personnel and the lack of qualified replacements are a

concern to the NRC.

The licensee is considered to be in Performance-Category 1 in

this area.

Trend: Declined

3.

' Board Recommendations

a.

Recommended NRC' Actions

The NRC inspection effort in this functional area could be

reduced.

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Recommended Licensee Actions

Licensee' management should give priority to reversing the

declining trend related to staffing and staff-qualifica-

tions to ensure that the licensee meets Fort Calhoun

Station staffing objectives.

Efforts to improve the

control room annunciator system and to implement the

recommendations of the control room design review should be

continued.

B.

Radiological Controls

1.

Analysis

Eight inspections were conducted during the assessment period by

region-based inspectors concerning radiological controls. These

eight inspections covered the following areas:

radiation-

protection-normal operations; radiation protection-refueling

outage; radwaste management, effluent releases, and effluent

monitoring; chemistry / radiochemistry and confirmatory

measurements; and transportation / solid radwaste. One violation

and no deviations were identified:

Failure to Follow Procedures.

(Severity Level V, 83-31)

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Radiation Protection

This area was inspected twice during normal plant

operations and once during a refueling outage.

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The-person-rem for 1983 was 433 as compared to the PWR

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national _ average of 592.

In 1984, 544 person-rem was

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expended. .The 1984 national averages have not been

tabulated,Ebut the 1984 values are expected to be near the

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1983clevels. The licensee's person-rem average between

_1978 and 1983 was 385 which is below the PWR national

average of 556 for the same time-period.

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-The-radiation protection staff was stable during the _

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assessment period. .All. members of the radiation protection

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staff _ met the ' ANSI N18.1-1971 qua11fication requirements as

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. senior radiation protection technicians: The radiation-

. protection staff consisted of.12' technicians, 2-

supervisors, and 2 ALARA coordinators. The licensee had

' decreased reliance on contractor. technicians; only one

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contractor technician was included in the radiation

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protection staff.

The lack of a. full-time ALARA coordinator was noted as a

concern in the previous assessment.

In this assessment

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. period,_the Itcensee established and filled an'ALARA-

coordinator and an assistant ALARA coordinator position.

.The implementation _of an extensive decontamination program

.in the auxiliary building corridors, that allowed access-

.into these areas without the need~for protective clothing,

was noted as;a program improvement in the previous

assessment. .The licensee had continued to expand this

decontamination effort to include additional areas and

rooms in the auxiliary building. The lack of timely action

to resolve open items was identified as a major concern in

the previous assessment.

In this assessment period, good

progress had been made toward the resolution of outstanding

open items.

A comprehensive training program has not been implemented-

for the radiation protection staff.

b.

Chemistry / Radiochemistry and Confirmatory Measurements

This area was inspected once during the assessment period

which included onsite. confirmatory measurements with the

Region M mobile laboratory. The following LERs concerning

this area were submitted:

Boron concentrations in the Safety Injection and

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Refueling Water Tank below Technical Specification

limits. (LERs84-012'and 84-021)

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An overall improvement was noted in the percent agreement

between the NRC's and the licensee's measurements in this

assessment period.

Considerable improvement was made in

the percent agreement concerning the comparative analyses

of gaseous samples. The percent agreement for gaseous

samples.in this assessmrat was about 70 percent as compared

to less than'50 percent in the previous-assessment period.

The licensee had implemented a quality control cross-check

program with an offsite: independent laboratory.

An approximate _60 percent turnover rate was noted among the

chemistry / radiochemistry staff in the assessment period.

A comprehensive training program had not been implemented

for radiochemistry personnel,

c.

Radwaste Management, Effluent Releases, and Effluent

Monitoring

This area was inspected once in the assessment period. The

following LERs concerning this area were submitted:

Exceeded Technical Specification Limits for I-131 Dose

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Equivalent in Reactor Coolant.

(LER 84-004)

Unplanned actuation of Ventilation Isolation Actuation

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Signal (VIAS) due to instrument error.

(LERs84-005,

006, 007, 010, 017, 018, and 023)

Disconnection of sample line from auxiliary building

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ventilation duct to gaseous effluent monitor.

(LER

84-011).

Gaseous leak in the waste gas vent header caused stack

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iodine monitor to initiate VIAS.

(LER 84-025)

The licensee had a well established program for sampling

and analyses of liquid and gaseous samples to assure

compliance with Technical Specification requirements.

Improvements noted in this area included:

installation of

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low-background steam generator blowdown radiation monitors;

in place calibration of liquid and gaseous effluent

monitors with liquid and gas standards; and an in place

testing program for the auxiliary building HEPA filters.

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Approximately 20 unplanned actuations of the VIAS related

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to instrument. error were reported in LERs during the

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assessment period.

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d.

Tr&nsportation/ Solid Radwaste

This area was inspected twice during the assessment period.

The licensee had updated their program to include the

revisions to Department of Transportation regulations

effective July 1, 1983, and revisions to 10 CFR Part 20.311,

10 CFR Part 61.55, and 10 CFR Part 61.56 effective

December 27, 1983.

Improvements noted in this area

included: assignment of a full-time radwaste coordinator;

development of detailed shipping procedures and records;

impler...tation of a QA/QC program concerning the packaging

.of radioactive materials; and establishing a procedure to

evaluate the amount of radwaste generated.

A comprehensive training program had not been established

for personnel involved with transportation / solid radwaste

activities.

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e.

Enviror, mental Monitoring

The radiological environmental monitoring program was

inspected once during the assessment period. No

significant problems were identified. There had been no

turnover in the onsite staff responsible for the program

during the past several years. Improvements noted in this

area included the use of persons with expertise in

environmental monitoring on the team responsible for

auditing the radiological environmentai monitoring program

and implementation of comprehensive procedures for

identification, collection, and shipping of environmental

samples.

A formal training program had not been established for

persons involved with.the radiological environmental

monitoring program.

2.

Conclusions

Improvements were noted in the area of radiological controls in

this assessment period as compared to the previous assessment

and these improvements reflect strong management attention to

weaknesses previously identified. The licensee had made good

progress toward resolution of outstanding open items.

During

the assessment ~ period, 31 open items were resolved and only one

new open item was identified. A high turnover rate was noted

among the chemistry / radiochemistry staff. -Comprehensive

training programs had not been established that included

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schedules, goals and objectives, full-time instructors, lesson

plans, and. training aids.

No problems were noted concerning enforcement history,

resolution of technical issues, management involvement, and

responsiveness to NRC initiatives.

The licensee is considered to be in Performance Category 1 in

this area.

Trend:

Improved

3.

Board Recommendations

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a.

Recommended NRC Actions

The NRC. inspection effort in this functional area could be

reduced.

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b.

Recommended Licensee Actions

Management attention is needed to ensure that comprehensive

training programs are established. Management should

investigate the cause of the high turnover rate in the

chemistry / radiochemistry staff and establish any

appropriate remedial actions.

C.

Maintenance

1.

Analysis

This area was inspected by region-based NRC inspectors and on a

continuing basis by the NRC resident inspector.

Four violations

and no deviations were identified in this functional area during

the appraisal period:

Failure to have proper receipt inspection of material

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performed prior ~to installation by maintenance personnel.

(Severity Level V, 8415-01)

Failure by maintenance craftsman to properly verify and use

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the correct revision of a surveillance test.

(Severity

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Level IV, 8418-02)

Failure to provide adequate procedures:

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to identify and resolve nonconformances associated

with plant process instrumentation, survei.llance test

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instrumentation, and pressure gauges when found to be

out-of-tolerance at calibration; and

b.

to implement the cleaning requirements for fluid

systems and associated components in accordance with

ANSI N45.2.1-1973.

(Severity Level V, 8421-01)

Failure to follow procedures:

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a.

by failing to perform investigation to determine the

effect of secondary standards being out-of-tolerance;

and

b.

by failing to provide minimum calibration schedules

for oscilloscopes and electrical current measuring

standards.

(Severity Level IV, 8421-02)

The twelve LERs listed below involved activities in the area of

maintenance:

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Diesel generator field failed to flash during surveillance

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test.

(LERs83-008 and 83-011)

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Reactor Coolant Loop RC-2A flow indicator loop failed high.

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-(LER 83-009)

Low pressure safety injection pump sequencer timer failed

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during monthly ESF surveillance test.

(LER 83-010)

Failed power supply fuse in RPS channels. (LER 83-012)

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Containment pressure switches were found

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out-of-tolerance during surveillance test.

(LER 83-013)

Main steam safety valves failed to lift within setpoint

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values during surveillance test.

(LER 84-002)

Steam Generator RC-28 tube failure.

(LER 84-008)

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Electrical penetration assemblies failed under

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environmental qualification testing being conducted by the

test laboratory to fulfill the requirements of

10 CFR Part 50.49.

(LER 84-009)

Noise spikes caused tripping of the "A" and "C" Thermal

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Margin Low Pressure reactor protective system trip circuits

which resulted in a reactor trip.

(LER 84-013)

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High alarm setpoint for stack noble gas monitor was found

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out-of-tolerance during surveillance test.

(LER 84-016)

Hydrogen analyzers failed to indicate proper concentration

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during calibration.

(LER 84-020)

The major maintenance efforts accomplished this appraisal period

occurred during the refueling outage March 5 to July 8,1984.

Maintenance activities accomplished included eddy current

testing of both steam generators, sludge lancing of the

secondary side of both steam generators, repair of the reactor

coolant pump gaskets, work on the Quality Safety Parameters

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Display System (QSPDS), and replacement of the high pressure

turbine rotor.

Extensive management involvement at the planning

level and expanded use.of the computerized tracking system

enabled these activities to be accomplished essentially on

schedule.

Three additional, events caused an extension to the originally

planned outage.

The first was the removal of the drilled tube

support plate rim in both steam generators to reduce the

potential for tube " denting" caused by stresses in the support

plate. This " rim cut" was accomplished by contract boilermakers

under the direct supervision of OPPD personnel and completed

within two weeks. The licensee utilized mockup training for all

craftsmen, and this contributed to the timely completion of the

job and to the less than anticipated overall man-rem exposure.

The second event was-the steam generator tube failure in RC-28

that occurred on May 16, 1984, during the reactor coolant system

leak test. The licensee had identified a small tube leak prior

to shutdown, and had expended considerable effort to identify

the cause prior to startup. This effort included an extensive

eddy current test program, helium leak checks before and after

sludge lancing, and dye leak tests, but no positive indication

of a leak was identified prior to the reactor coolant system

leak test.

Following the tube failure, the licensee removed the

failed tube from RC-28, performed eddy current testing on all

accessible tubes on both steam generators, performed a lab

analyses on the failed tube, initiated more restrictive limits

on the primary to secondary leak rate, and instituted vendor

recommended chemistry control procedures. The third event was

precipitated when a testing laboratory informed OPPD that

containment penetration lead wire insulation could fail under

the harsh environment of a Large Break Loss of Coolant Accident

(LBLOCA) . To correct this problem, the licensee developed a

cable splice using qualified sleeves that shielded the lead wire

insulation from the harsh environment. A total of 638 splices

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. involving 48 cables were reworked during this 2-week extension

'of the outage. With' regard to all three of these events, the

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licensee management responded quickly to address these matters

and to provide the necessary resources and support to these

activities.

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Another major maintenance effort undertaken by' Fort Calhoun

during1this_ appraisal period.was the installation of new spent

fuel. storage racks by an outside. contractor. Whi.le removing the

old racks,_there were instances where plant QC personnel stopped

. work because of the improper way the ~ job was being performed and

controlled. During the removal of one spent fuel rack, the wire

rope sling broke.and the rack became wedged.in the pool. OPPD-

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failed initially to exercise appropriate management control by

providing adequately trained people to direct this work.and

sufficient QC coverage to monitor contractor activities.

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The licensee's system-for tracing measuring and test equipment

(M&TE) usage was found to be weak and lacked adequate procedures.

to identify all items inspected,-. tested,' or measured to specific

M&TE. Adequate procedures were not established to make

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disposition of possible nonconformances of those items when M&TE

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was found to be out-of-tolerance. The licensee revised plant

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procedures and expanded the M&TE program during this SALP period

to address those concerns identified in NRC Inspection

Reports 50-285/84-12 and_50-285/84-21.

The previous SALP identified that.several long term electrical

' jumpers. dating back to 1973 were still outstanding. The

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licensee made significant progress during this SALP period at

closing out these items and incorporating them'as permanent

design changes in accordance with the plant standing order.

The tracking of maintenance. orders (MOs) was another item of -

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concern discussed in the previous SALP. A computerized M0

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system is now in effect that works in conjunction with a

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computerized tracking. system to provide current. status

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information.

The tracking and closeout of design changes was a-third item of-

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concern discussed in the. previous SALP report. The efforts of

the update team were completed this SALP period, and all

modifications through December 31, 1980, have been reviewed. A

computerized listing of all outstanding Design Change Requests

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and Engineering Evaluation and Assistance Requests was

established and Itcensee management now has the capability of

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assessing the status of the design change program.

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The licensee implemented a Qualified Life Program (QLP) during

this appraisal period to " establish and maintain the qualified

life of safety-related equipment installed in a harsh

environment." Although the QLP was established in April 1984,

the licensee was slow in fully implementing the program and

delegating appropriate. responsibility to the various crafts. A

full-time coordinator was assigned to this effort in order to:

(1) review Electrical Equipment Qualification (EEQ)

documentation since the QLP started, (2) review QLP entries for

accuracy in the computer data base used in the maintenance

. program, and (3) provide comprehensive training of the QLP/EEQ

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program.

2.

. Conclusions

The licensee has initiated additional management control

programs to strengthen the maintenance area, and has established

a better working interface between the plant and design groups

at the Jones Street office. The resolution of items mentioned

in previous SALP reports indicates OPPD's commitment in

maintenance, but poor control of the new spent fuel rack

installation and delays in full implementation of the EEQ

program suggest areas that require additional management

attention.

The plant has a stable, well qualified maintenance staff that

has seen little turnover the past three SALP periods.

The licensee is considered to be in Performance Category 1 in

this area.

Trend:

Improved

3.

Board Recommendations

a.

Recommended NRC Actions

The NRC inspection. effort in this functional area could be

reduced.

b.

Recommended Licensee Actions

The licensee should continue the increased management

attention being given to the EEQ program in preparation-for

a site verification inspection by the NRC in 1985.

D.

Surveillance

1.

Analysis

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This area was inspected on a continuing basis by the NRC

resident inspector. No violations or deviations were identified

in this area.

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Fort Calhoun maintains a well-developed and effectively managed

surveillance test program. A monthly surveillance testing

- schedule is published to ensure that all required tests are

. assigned as to due date and responsible department. The program

is set.up to verify that the current revision to the test is

being used, that QC verification is obtained where required, and

that calibrated test equipment is used and identified on the

procedure. .During the last refueling outage, the master

schedule was updated and the applicable surveillance tests were

written or modified to reflect new Technical Specification

requirements.

2.

Conclusions

The licensee maintains a well-developed and effectively managed

surveillance test program.

The licensee is considered to be in Performance Category 1 in

this area.

Trend: Same

3.

Board Recommendations

a.

Recommended NRC Actions

.The NRC inspection effort in this functional area should

remain at the reduced level.

b.

Recommended Licensee Actions

The Board recommends that the licensee continue to exercise

strong management control of the surveillance program.

E.

' Fire Protecti'on

1.

Analysis

This area was inspected on a continuing basis by the NRC

resident inspector. No violations or deviations were identified

in this area.

The one LER listed below involved activities in

the functional area of fire protection:

. Temporary fire barrier failed to meet design criteria.

.

(LER 84-022)

A major activity in this area by OPPD during this appraisal

period was the resolution of items identified by the NRC special

inspection team and documented in NRC Inspection

Report 50-285/83-12 dated July 1, 1983.

.

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-16-

'Another major effort by the licensee this report period was the

upgrading of_ temporary fire barriers into permanent barriers and

to grout conduit penetrations. This 3-month effort utilized a

qualified outside contractor and resulted in approximately 350

fire barriers being upgraded. The licensee is presently

developing a program to enable OPPD personnel to install new

fire barrier penetrations and perform maintenance on permanent

fire barriers.

2.

Conclusions

The licensee has made significant progress at resolving the

items identified in the fire protection audit report and is

working toward compliance with the requirements of

10 CFR Part 50, Appendix R, Sections III.G and III.L.

The licensee is considered to be in Performance Category 1 in

this area.

.

-Trend: Same

3.

Board Recommendations

a.

Recommended NRC Actions

The NRC inspection effort in this functional area should

remain at the present level.The NRC should complete the-

review and processing of OPPD's exemption requests,

b.

Recommended Licensee Actions

The licensee management should continue their efforts to

resolve all identified items pertaining to compliance with

Appendix R.

F.

Emergency Preparedness

1.

Analysis

During the assessment period, five routine emergency

preparedness inspections were conducted. Three of the

inspections were routine reviews of the implementation status

for various elements of the emergency preparedness program.

Two emergency _ exercise inspections were also conducted during

the assessment period in conjunction with the licensee's annual

emergency exercises held December 6-7, 1983, and October 24,

1984. No violations or deviations were observed by the NRC

inspectors.

~

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-17-

Most of the open items identified during inspections in the

previous assessment periods were closed during this assessment

period based on timely licensee actions.

For concerns

identified during the reporting period, corrective action was

noted for most items during the next review of that item.

During the October 24, 1984, emergency exercise, the Federal

Emergency Management Agency (FEMA) evaluated offsite emergency

preparedness of states and local agencies. As a result of this

evaluation, FEMA identified a Category A deficiency in regard to

agreements for ambulance services in two counties of the state

of Iowa side of the 10 mile emergency planning zone. Plans for

resolution of this deficiency included agreements between Iowa

and the ambulance services, training for ambulance personnel,

and a drill to demonstrate this capability. The licensee has

been active in this matter and is cooperating with state and

local authorities to achieve resolution of this offsite

preparedness concern.

.

Management involvement and control of the emergency preparedness

program during the period appeared to be adequate for

implementation of an effective program.

Staffing of the emergency preparedness program was also

considered to be adequate during this reporting period. No

reportable events in the. emergency preparedness area were

received during this reporting period.

2.

Conclusions

The licensee has maintained an acceptable level of emergency

preparedness during the period and demonstrated adequate

capability to protect the health and safety of the public by

conducting two successful emergency exercises. Management

-involvement and control has been adequate for implementation of

an effective program.

Responses to NRC concerns have been

timely, thorough, and acceptable in most cases. Overall, the

licensee's program appeared to have increased in effectiveness

since the previous assessment period.

The licensee is considered to be in Performance Category 2 in

this area.

Trend:

Improved

3.

Board Recommendations

a.

Recommended NRC Action

The NRC inspection effort in this functional area should

continue at a normal level.

_

-

- - - .

$

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b.

Recommended Licensee Action'

A more aggressive level .of management attention to

implementation of-the emergency preparedness program should

be pursued. Additional management attention should be

given to resolution of.each of the NRC identified concerns

in a timely manner.

G .~

Security and Safeguards

1.

Analysis

The physical security staff performed five inspections during

this SALP period.

Twelve violations were identified in this functional area

during the appraisal _ period.

Failure to demonstrate that the microwave system _is tested

.

quarterly against the manufacturer's design specifications.

(Severity Level IV, 8417-02)

Failure to take proper compensatory action when the

.

perimeter intrusion detection system coverage was

discovered to be ineffective.

(Severity Level iV, 8417-03)

. Failure to provide authorized escort.

(Severity

.

Level IV, 8418-01)

' Failure to report facility modification.

(Severity

.

Level *, 8420-01)

Inadequate key control.

(Severity Level *, 8420-02)

.

Failure to provide an adequate barrier for part of one

.

vital area.

(Severity Level IV, 8420-03).

Inadequate compensatory measures.

(Severity Level *,

.

8420-04)

Inadequate surveillance television coverage.

(Severity-

.

Level *, 8420-05)

Failure to provide adequate access control for a vital

.

-

area. _(Severity Level IV, 8420-06)

Insufficient search at access control point.

(Severity

.

Level *, 8420-07)

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Failure to maintain operable assessment aids.

(Severity

.

Level *, 8420-08)

Inadequate compensatory measures following failure of-

.

search equipment.

(Severity Level *, 8420-09)

  • Violations 8420-01, 02, 04, 05, 07, 08, and 09 were

categorized individually at Severity Level IV or V, but were

considered in the aggregate as a Severity Level III

Violation.

Three deviations were identified in this functional area during

the appraisal period.

Failure to revise security' plan according to commitment

.

made to NRC.

(8326-04)

Failure to provide continuous monitoring.

(8420-10)

.

Failure to perform effectiveness test.

(8420-11)

.

Forty-nine licensee event reports (LER) of physical security

events were submitted in accordance with 10 CFR Part 73.71:

Loss of primary (CPU 1) and secondary (CPU 2) security

.

computers.

(LER's Nos. 83-07 through 12, 84-02 through 27,

84-29 through 34, and 85-01 through 09)

Loss of_ AC power and failure of uninterruptible power

.

source to operate the security computers.

(LER No. 84-01)

Reduction in offsite communications to local law

.

enforcement agencies.

(LER No. 84-28)

The licensee lost use of his primary (CPUI) and secondary (CPL'2)

security computers 47 times during this SALP period. On one

occasion, the licensee lost AC power and his backup source of

uninterruptible power failed to operate automatically.

In

LER 84-28, the licensee lost " normal" offsite communications to

the local area due to an accidental slicing of the underground

cable by an offsite nonutility construction crew.

The licensee was issued a Confirmatory Action Letter (CAL) on

'

August 16, 1984. The CAL was. issued as a result of a Region IV

inspection in July 1984. An enforcement conference was held

October 11, 1984, and documented in NRC Inspection Report

50-285/84-27. The enforcement conference was called to discuss

I

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the apparent violations from the special security inspection

(NRC Inspection Report 50-285/84-20) conducted during the period

August 20-24, 1984. The importance of. management involvement in

establishing an effective security program was emphasized by the

NRC participants. The need to develop and implement an effective

testing and maintenance program for security-related equipment

was discussed. As a consequence of the August special security

inspection, a Notice of Violation and Proposed Imposition of

Civil Penalty (CP) dated February 14, 1985, was issued to the-

licensee. The CP was reduced by 50 percent to $25,000 because

of prior good performance in the area of concern; specifically,

no. previous escalated enforcement actions and repeated ratings

of Category 2 in their (SALP) evaluations.

Subsequent to'the August 20-24,-1984, inspection, OPPD initiated

an extensive security improvement program. OPPD management

approved a Fort Calhoun Station security organizational change

providing for a dedicated security supervisor reporting to the

Supervisor-Administrative Services and Security at Fort Calhoun

Station, a review of: the maintenance and testing program

relating to security equipment, and a review of the entire

physical security plan by a qualified security consultant.

In

addition, Fort Calhoun Station made a commitment to submit a

revised physical security pian to the NRC by May 1, 1985.

2.

Conclusions

The licensee had not placed emphasis and dedication on

maintaining an. effective security program and management

involvement with security matters has been marginal. The result

of management's lack of commitment to security was evidenced by

insufficient training and maintenance, and by improper

compensatory actions resulting in violations.

The licensee is considered to be in Performance Category 3 in

this area.

Trend:

Improved

3.

Board Recommendations

a.

Recommended NRC Actions

Tne NRC inspection effort in this functional area should be

increased. An' evaluation of the licensee's corrective actions

and their impact on the security program should be performed by

August 31,~1985.

b.

Recommended Licensee Action

The level of licensee management attention evidenced during the

last_ quarter of this SALP period should be continued.

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The licensee should increase audit. activity of security

training, maintenance, and requirements of the security plan.

Licensee management should ensure that security resources and

organization are adequate to implement the security plan.

H.

Refueling

1.

Analysis

This area was inspected on a continuing basis by the NRC

resident inspector during the period of refueling April 1-8,

1984.

Fort Calhoun Station was in a refueling outage from

March 5 to July 8, 1984, for Cycle 9 refueling. A total of

40 new bundles were inserted into the core.

No violations or deviations were identified during this

evaluation period.

The licensee continued to utilize a fuel load / shuffle scheme

designed to reduce neutron flux to the reactor vessel as part of

OPPD's efforts to address the pressurized _ thermal shock issue.

The fuel movement was completed without incident and the NRC

inspector verified that Technical Specification requirements

were satisfied.

2.

Conclusions

The licensee management demonstr'ated excellent prior planning

and effective control of refueling activities. The licensee is

considered to be in Performance Category 1 in this area.

Trend: Same

3.

Board Recommendations

a.

Recommended NRC Actions

The NRC inspection effort in this functional area should

remain at reduced levels.

b.

Recommended Licensee Actions

Licensee management should continue its involvement in the

planning of refueling outages, the observation of refueling

activities, and adherence to procedures.

I.

Quality Programs and Administrative Controls Affecting Quality

1.

Analysis

This functional area was inspected on a continuing basis by the

NRC resident inspector and by region-based NRC inspectors. Six

.

.

..

-22-

violations and no deviations were identified in this area during

the appraisal period:

Failure to audit security procedures every 12 months.

.

(Severity Level IV, 8326-01)

Failure to adequately perform the review and approval steps

.

of a CQE piping isometric as part of the post-installation

modification review process.

(Severity Level IV, 8335-01)

Failure to provide procedures to assure that appropriate

.

Fort Calhoun Station personnel were provided with current

lists of CQE equipment.

(Severity Level V, 8410-03)

Failure to properly review OPPD's response to IE

.

Bulletin 82-02 resulting in a material false statement

being made that was contrary to actual practice at the Fort

Calhoun Station.

(Severity Level III, 8412-03)

Failure to take prompt corrective action on the resolution

.

of QA deficiency / quality reports within the required

response period.

(Severity Level IV, 8429-01)

Failure to properly establish, monitor, and closeout

.

temporary CQE storage areas.

(Severity Level IV, 8501-01)

The two LERs listed below involved activities in the area of

administrative controls:

Auxiliary building crane interlocks were left in the bypass

.

position without the crane supervisor being present.

(84-001)

A load of approximately 250 pounds was carried by the~ polar

.

crane over the reactor coolant system when the fluid in the

pressurizer was greater than 225 degrees F.

(84-015)

The licensee submitted the revised OPPD QA Plan to the NRC for

review on August 31, 1984. The program is fully implemented and

the complete set of QA department procedures has been issued.

These items were addressed in the last SALP period and the delay

in implementing the new program was considered a weakness in the

OPPD program.

It was determined during routine inspections by regional

inspectors in the radiological controls area that there were no

QA auditors on the licensee's onsite staff that had any training

or background experience in radiation protection except for

instrument calibration. The NRC determined during another

.-.

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-23-

inspection that the licensee did not have a program established

to audit vendors that are contracted to perform radiochemical

analyses on samples of Fort Calhoun Station radwaste for the

requirements of 10 CFR Part 61.55.

In the area of security and

safeguards the NRC determined that the licensee had failed to

perform an audit of security procedures and practices every 12

months as required by the Fort Calhoun Station Physical Security

. Plan.

During this appraisal period, major management changes were

implemented at the OPPD corporate. level and at the Fort Calhoun

Station. A Nuclear Production Division was formed and a

separate division manager for nuclear matters was established

directly under the assistant general manager. The

reorganization provided increased management attention to the

operation of the-Fort Calhoun Station. The NRC resident

inspector observed that the manager of the Nuclear Production

Division initiated weekly staff meetings at the site, made

routine tours of the plant, and attended all NRC exit interviews

at the site.

The licensee reorganized the site management structure to have

the Quality Control (QC) section report to the Supervisor-

Technical, instead of the Supervisor-Maintenance. Observations

by the resident inspector indicated that this move provided a

greater degree of independence for the QC section from the

Maintenance Department and enhanced their effectiveness onsite.

A Supervisor-Station Training position reporting directly to the

plant manager was established this appraisal period and filled

in February 1985.

This reflects the licensee's commitment to

provide increased management attention to plant training

activities.

An area of continued long standing concern'to the NRC is the

matter of the Fort Calhoun Station construction QA records. An

enforcement conference between OPPD and NRC personnel was held

in the Region IV offices on September 9,1983, to address this

matter and identify the licensee's corrective actions. OPPD

agreed to review "all commitments to the NRC for retention of

design, procurement, manufacturing, installation and

construction records, and all applicable involved codes,

standards, and specifications." The licensee has examined the

available records and identified those which were missing, along

with an evaluation of their significance. A recent inspection

by the NRC indicates that this review and evaluation was not

done to the depth and detail necessary to resolve this matter.

.l

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-24-

In addition to those specific items discussed in the various

functional areas, other items that indicated a lack of

sufficient administrative controls and management attention

during this assessment period include:

The. inadequate review of OPPD's response to IE

.

Bulletin 82-02 and the subsequent escalated enforcement, as

. discussed in Section IV.C of.this report, indicated a-

weakness in the licensee's technical evaluation and review

process. Although the specific incident occurred before

this SALP evaluation period, the investigation during this

SALP period revealed that weaknesses still existed. The

licensee exerted significant effort during the past nine

months to correct these problems.

-The failure to followup on identified deficiencies in a QA

.

audit of the plant security program, and the lengthy times

-involved in ' closing out other deficiency reports / quality

reports indicated that management failed to achieve

appropriate and timely corrective actions.

2.

Conclusions

The licensee has demonstrated improvement in the QA area with

regard to program implementation.

OPPD's administrative

controls and management attention had weaknesses in the specific

areas outlined above and in the other analyses sections. The

= establishment of a separate Nuclear Production Division is a

positive step towards bringing management controls to bear on

those areas that need attention.

The licensee is considered to be in Performance Category 2 in

this area.

Trend:

Improved

3.

Board Recommendations

a.

Recommended NRC Actions

The NRC inspection effort in this functional area should be

maintained at normal levels.

-b.

Recommended' Licensee Actions

The licensee management needs to work toward a timely

resolution of the NRC concerns regarding construction

records and to address the other weaknesses identified.

- _.

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J.

Licensing Activities ~

~1;

Analysis-

\\

-The NRC Office of Nuclear Reactor Regulation has ' performed an

assessment of licensee performance in the functional area of

-

licensing activities.

Refer to Attachment 1 for details.of this-

'

assessment.

-2.

. Conclusions-

As discussed in. Attachment 1, the licensee is considered to be

-in Performance Category 1 in this area.

Trend:

Improved

3.

. Board Recommendations

.

a.

Recommended NRC Actions

Continue to perform 111 censing activities as required.

-

b' .-

Recommended Licensee Actions

The licensee should continue its high level of management

.

involvement in-this area.

-

K.

Training

1.

. Analysis

This functional area was inspected by region-based NRC

inspectors and on a periodic basis by the NRC resident

,.

inspector. Three violations and no deviations were identified

in this functional area during the appraisal period:

Failure to follow approved training and qualification plan-

.

as it pertains to firearms qualification program.

(Severity Level IV, 8326-02)

,

! Failure to complete security training program in accordance

.

with commitment made to NRC.

(Severity Level IV, 8326-03)

4

Failure to' provide training as required by the Fort Calhoun

..

Station Security Plan.

(Severity Level IV, 8417-01)

.

The licensee has devoted much attention to this functional area

-since receiving a Category 3 rating in the previous SALP report.

An outside consultant was brought in for evaluation and

o

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-26-

consultation during the winter of 1983/84, and in May 1984, a

working group was in place preparing training materials. This

group started with about five persons and has grown to 15 during

the past nine months.

Following the failure of all three

license candidates in June 1984, OPPD initiated an evaluation to

identify and correct the specific causes of these failures.

Part of this evaluation included an independent task force

assessment of the existing operator training program. The-

results of this assessment formed the bases for short term and

long term corrective actions to be implemented to ensure that

future license candidates are prepared to pass the NRC

examination and safely operate the plant. OPPD and NRC

personnel met in September 1984, to discuss the licensee's

-

operator licensing program and.the results of this independent

task force assessment. OPPD established the position of

Supervisor-Training Services in July 1984, to head the newly

established offsite Training Services Department. .The NRC

resident inspector reviewed the independent assessment report

and concluded that the observations made represented an accurate

picture of the training program at that time, and that the-

three groups of recommendations set forth would correct the

problems if implemented.

Some results from the efforts

described above that occurred during this evaluation-period

included:

(1) improved and expanded lesson plans and training

packages, (2) the successful licensing of two reactor operator

license candidates, (3) the additio'n of instructors from an

inter plant transfer and outside contractors, and (4) the

appointment of the new Supervisor-Station Training.

The NRC

resident inspector reviewed portions of the revised student

handout material and instructor lesson plans and found them to

be comprehensive, well organized, and clearly written.

Three operator licensing examinations were administered during

this evaluation period as tabulated below:

SR0 Candidates

R0 Candidates

Total Pass Fail

Total Pass Fail

November 29-December 1, 1983

6

3

3

1

1

0

June 5-7, 1984

0

-

-

3

0

3

November 7-8, 1984

0

-

-

2

2

0

One requalification examination was administered as tabulated

below:

-

1

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a

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.

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1

SR0 Candidates

R0 Candidates-

Total Pass Fail

Total Pass Fail

~

November 7, 1984-

5_

2

3

2

2

0

'The first two examination results. continued a downtrend that was

.. identified in the previous.SALP period. _These results were

below the industry norm and reflected a weakness .in the

licensee's training department to adequately screen and' prepare

candidates- for licenses. The intensive training effort. focused

'

on the November 1984, candidates and the successful licensing of

-

.both examinees indicated that this trend may-have been reversed.

License requalification training continued to be a problem area

during-this, evaluation period.

Interviews.by the NRC_ resident

. inspector and a region based NRC inspector with licensed'. .

" operators indicated that actual in-class lecture time was.b'eing

cut short and that the~ quality.of training was suffering because

-

of the limited availability _of experienced licensed instructors.

In addition, the high failure rate for new license ~ candidates

and NRC requalification candidates during this appraisal period

seemed to confirm that the overall. quality of training at the

.

licensed operator level remained marginal. _The NRC resident-

inspector attended selected training lectures during this

,

appraisal period and observed a wide variation in quality of

,

handout material and instructor capabilities.

-

As part of the overall restructuring of the training program, a

_

new " performance based" training. program for newly hired

.

auxiliary operator trainees has been developed and will be

+

implemented during the first quarter of 1985. This program has

clearly defined written goals, a' complete schedule for classroom

_'

and onshift _ time, and a structured. system of lesson plans,

  1. -..

_ qualification cards, and practical factors to be completed.

>

This' program is one of many being developed by the. licensee to

qualify for INPO certification in 1986.

I

The in-house. training program for five inexperienced

-

chemistry / health physics technicians was completed this

.

,

,

evaluation period and all five trainees became qualified to work

shift-technician duties.

It was noted in an NRC inspection

'

report.that the training department did not have an instructor

_ qualified or experienced in nuclear power plant chemistry and

that a comprehensive training' program for radwaste operators did

not exist. The chemistry / radiochemistry training program was

being conducted primarily by the chemistry section senior staff

>

personnel under the supervision of the plant chemist. A review-

-

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_ _ ,

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'

of qualification verification records for Chemistry and

-Radiation Protection supervisory personnel revealed that no

training had been completed in any of the study areas listed in

Section 6.1 of the Fort Calhoun Station Training Manual.

The NRC resident inspector noted that the training manual

prepared for Cycle 9 modifications was the'most complete and

informative of those issued to date. The~ licensee provided

acceptable training on short notice in response to the steam

generator tube failure incident and covered the applicable

emergency procedures, the lessons learned from the Ginna tube

rupture incident, and the revised Technical

' Specification / Surveillance Tests.

2.

Conclusions

The licensee has done an excellent job of identifying and

evaluating the problems in this functional area, and has

expressed a strong commitment to resolve these matters. The

initial results of their-efforts have been positive, but the

overall training program has not yet seen the benefits of OPPD's

commitments and plans.

During this evaluation period the

licensee's record in licensee examinations and requalification

examinations remained poor. Many of the personnel changes to

the training department and the appointment of the

Supervisor-Station Training occurred too late in this SALP

evaluation period to have had a significant impact on

performance.

The' licensee is considered to be in Performance Category 3 in

this' functional area.

Trend:

Improved

3.

Board Recommendations

a.

Recommended NRC Actions

=The NRC inspection effort'in this functional area should be

.

increased. An evaluation of the licensee's corrective

actions and their impact on the training program should be

performed by August 31, 1985.

b.

Recommended Licensee Actions

Licensee management should provide aggressive action to

ensure control of the training program in order to maintain

the positive trend that appears to have been established

toward the end of this evaluation period. The effort at

. _ _ -

. - -

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upgrading lesson plans and student material needssto be

carried through to completion. The need for an expanded

training staff remains and this shortcoming should be

resolved as soon as possible. The licensee should further

-consider the benefits of obtaining access to a

site-specific simulator for training of the Fort Calhoun

Station operators.

The quality of instructors should be evaluated and training

provided as required to increase the effectiveness of the

training staff. Training in the areas of security,

chemistry, and radiation protection needs to be better

coordinated and administered under the training department.

'V.

SUPPORTING DATA AND SUMMARIES

A.

Licensee' Activities

1.

Major Outages

-The refueling outage occurred during the period March 5 to

July 8, 1984.

In addition to the insertion of 40 new fuel

bundles into the core, major planned maintenance activities

included eddy current testing of both steam generators, sludge

lancing of the secondary side of both steam generators, repair

of the reactor coolant pump gaskets, work on the QSPDS, and

replacement of the high pressure turbine rotor. Three

additional activities that occurred during this outage included

the " rim cut" on the steam generator's tube support. plate,

plugging of the failed tube in Steam Generator RC-2B, and rework

,'

of 638 containment penetration lead wires to protect them from

the harsh environment of a LBLOCA.

Fort Calhoun Station experienced a 2-week outage from

November 18 to December 3,1984, to repair a body-to-bonnet

flange leak on a pressurizer spray valve.

2.

Power Limitations

The reactor was not limited in power level below the licensed

limits during this appraisal period.

3.

License Amendments

Amendment No. 75

-Authorized Spent Fuel Pool Rerack,

September 9,-1983

Amendment No. 76

Administrative Changes, January 26, 1984

... ..

.

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' Amendment No. 77

Cycle 9 Restart, April 26, 1984

Amendment No. 78

Shift Manning and QC Personnel Changes,

May 16, 1984

Amendment No. 79

Snubber Changes, May 23, 1984

Amendment No. 80

Add Operability and Surveillance

Requirements for RCS Vents and

Administrative Requirements for Analysis of

Plant Effluents, July 9,1984

Amendment No. 81

Add Operability and Surveillance

Requirements for Containment Wide Range

Radiation Monitors, Wide Range Noble Gas

Monitors, and Main Steam Lines Radiation

Monitor, July 12, 1984

Amendment No. 82

Add Operability and Surveillance

Requirements for Containment Hydrogen,

Water, and Pressure Monitors, August 2, 1984

Amendment No. 83

Update Surveillance Capsules Removal

Schedule, September 7, 1984

Amendment No. 84

Plant Support and Plant Organization

Changes, September 7, 1984

Amendment No. 85-

Limit Overtime and Report PORV/SV

Failures and Challenges, October 11, 1984

4.

Significant Modifications

Major modifications completed during this appraisal period

included the installation of new spent fuel racks, removal of

steam generators drilled tube support plate rim, implementation

of new secondary chemistry control in response to the failed

tube in Steam Generator RC-2B, and the upgrading of

instrumentation, limit switches, containment penetrations, etc.

to meet EEQ requirements.

B.

Inspection Activities

1.

Violations

See Table 1.

2.

Major Inspections

During this appraisal period, one special inspection was

conducted in the area of security and safeguards. The

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inspection was performed by a team of three inspectors and one

observer from outside Region IV and involved a total of 235

direct inspection man-hours.

(NRC Inspection

Report 50-285/84-20)

C.

Investigations and Allegations Review

One investigation was conducted during this appraisal period and it

addressed the material false statement made by the licensee in their

response to IE Bulletin 82-02, " Degradation of Threaded Fasteners in

Reactor Coolant Pressure Boundaries of PWR Plants." It was confirmed

by the investigation that the OPPD response to the NRC was false in

that " Super-Moly" (molybdenum disulfide) was used on the reactor

vessel and reactor coolant pump studs and that a mixture of 50

. percent oil and 50 percent graphite was designated for use on manway

studs. These failures by the licensee to perform an adequate review

of the related documentation, to coordinate the response with

knowledgeable personnel, and to identify the false statement during

.

the OPPD required procedural review, resulted in a Severity Level III

Violation. An enforcement conference was held on December 20, 1984,

between the NRC and the licensee to discuss this matter.

One allegation was received during this appraisal period that

identified certain incidents which had occurred over the past five

years and alleged poor management practices in the area of

supervision and discipline that could affect the safety and health of

the public. The review and followup of this allegation was still in

progress at the close of this appraisal period, and is expected to be

resolved during the first quarter of the next SALP period.

D.

Escalated Enforcement Actions

1.

Civil Penalties

Two notices of violation with proposed imposition of civil

penalties were issued to the licensee during this appraisal

period.

A Severity Level III Violation and a proposed civil penalty

.

of $40,000 were issued as a result of the material false

statement made by the licensee in their response to IE

Bulletin 82-02, " Degradation of Threaded Fasteners in

Reactor Coolant Pressure Boundaries of PWR Plants." In

consideration of OPPD's prior good performance in this

area, and their prompt and extensive corrective actions,

the Regional Administrator determined that the civil

penalty should be fully mitigated.

-

1

!

  • -

.

!

-32-

A Severity Level III Violation was issued in the area of

.

security and safeguards that comprised a composite of seven

Severity Level IV and V Violations and reflected an overall

weakness in the Fort Calhoun Station security program. A

civil penalty of $50,000 was proposed, but this amount was

mitigated to $25,000 on the basis of the licensee's

previous good enforcement history in this. area.

E.

Management Conferences Held During Appraisal Period

1.

Conferences

The following conferences were held between Region IV and the

licensee during this appraisal period:

Enforcement conference of September 9, 1983, at the Region

.

IV office to discuss NRC concerns related to construction

QA records and the QA records file room.

The bases for

.

this meeting were the findings described in NRC Inspection

Report 50-285/83-17.

Management meeting of September 21, 1984, at the Region IV

.

office to discuss the licensee's operator licensing program

in response to Mr. J. T. Collins letter of August 13, 1984,

to Mr. W. E. Miller of OPPD.

Enforcement conference of October 11, 1984, at the Region

.

IV office to discuss the results of NRC Inspection

Report 50-285/84-20 which documented nine violations and

two deviations identified by the special inspection team.

Enforcement conference of December 20, 1984, at the Region.

.

IV office to discuss the licensee's response to IE

Bulletin 82-02 and the associated material false-statement

cited in NRC Inspection Report 50-285/84-12.

2.

Confirmation of Action Letters (CALs)

The following CALs were issued by Region IV during this

appraisal period:

J. T. Collins letter of June 5,1984, to W. C. Jones of

.

OPPD to confirm the actions and conditions required of OPPD

in relation to the failed tube in Steam Generator RC-2B.

J. T. ' Collins letter of August 16, 1984, to Mr. R. L.

.

p

Andrews of OPPD to confirm the actions required of OPPD in

-

response to security matters identified in NRC Inspection

Report 50-285/84-17.

r

!

L-

j

' ~

..

-33-

_

-

F.

' Review of Licensee Event Reports and 10 CFR Part 21 Reports

Submitted by the Licensee

1,

Licensee Event Reports (LERs)

The SALP Board reviewed the LERs for the period September 1,

1983, through February 28, 1985. This review included

LERs83-008 through 83-013, and 84-001 through 84-025. The SALP

Board reviewed the licensee's cause classification for these

LERs and did not identify any significant differences between

those made by the licensee and those made independently by the

board.

Due to the. revised LER rule that went into effect on January 1,

1984, the licensee was required to report a significant number

of unplanned VIAS actuations that were not performing a safety

function.

This resulted in an increase of LERs this appraisal

period even though the new rule was intended to eliminate

inconsequential reports.

The licensee is considering a

Technical Specification revision to modify this specific LER

requirement.

The NRC Office for Analysis'and Evaluation of Operational Data

performed a review of licensee LERs, focusing on the accuracy

P

and completeness of the reports. Refer to Attachment 2 for

details of this review.

7

b

2.

Part 21 Reports

None

G.

NRR Activities

1.

NRR License Meetings

December 20, 1983

SALP

March 23, 1984

Environmental Qualification

April 17, 1984, and

Radiological Effluent Technical

October 11 & 13, 1983

Specifications

~

May 29, 1984

Steam Generator 8 Major Leakage

Event

December 13, 1984

Plant Security

February 5-8, 1985

In-Progress Audit of Licensee's

Detailed Control Room Design Review

t

,

,

, .

,.

-34-

2.

NRR Site Visits

October 11 & 14, 1983

Discussed Licensing Actions with

Resident Inspector and Visited Local-

PDR

May 23-26, 1984

. Emergency Trip to Address Steam

Generator 8 Major Leakage Event

August 27-29, 1984

Toured Plant, Reviewed TMI Related

Modifications, and Discussed Licensing

Actions with Resident Inspector

February 6-7, 1985

Toured Control Room and Remote

Shutdown Panel and Discussed Licensing

Actions with Resident Inspector

3.

Commission Briefings

.

None-

- 4.

Schedular Extensions Granted

IST 2nd 10 year program, interim schedular relief for 1 year,

September 30, 1983

IST 2nd 10 year program, interim schedular relief for 1--year,

October 9, 1984

EQ Schedular-Extension, May 18, 1984

5.

Reliefs-Granted

ISI 1st 10 year program, 2 reliefs, November'14, 1984

ISI 2nd 10 year program, I relief, September 30, 1983

ISI 2nd 10 year program,'8 reliefs, April 6, 1984

6.

Exemptions Granted

None

7.

Emergency Technical Specifications Issued

None-

L.

j

.

.

.

.

.._

. -

.

.

. . .-.

e.

.

I

pp .c

.~

-35-

- 8.

- Orders Issued

Order confirming licensee commitments on emergency response

capability.as. required by Supplement l'to NUREG-0737,

,

- February 22, 1984.

.

9.

NRR/ Licensee Management Conferences

None-

.

'

i

4

.

Y

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li

,

i.

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-36-~

'

TABLE 1

. INSPECTION ACTIVITY AND ENFORCEMENT

'

,

,j;j

FUNCTIONAL

NO OF VIOLATIONS IN EACH SEVERITY LEVEL-

- ~ -

AREA

V

IV.

III'

II

I

DEVIATIONS.

,

'

o

'A.' l Plant Operations

4

B.

Radiological Controls

1

.C.~

Maintenance'

2

2

-

,,

10.

Surveillance

E.

' Fire Protection

.

'F.

Emergency Preparedness-

G.

Security and Safeguards

5

1*

3

-

H. : Refueling

.I.

Quality Programs and

1

4

1

.,

Administrative Controls.

'

,:Affecting Quality

.J.

Licensing Activities'

,

'

- K.

Training

3

. TO TA'L '

.4

18

2*

0

0

3

2

.

'

'*This. comprises seven Severity Level IV and V Violations identified in NRC

Inspection Report 285/84-20.

,

. - - -

.

-

-