Proposed Tech Specs 3/4.4.5,adding Footnote Specifying Repair Criteria for Top of Tube Sheet Indications If Found as Part of Reviewing Previous Unit 1 Oct 1995 EC SG DataML20117K376 |
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Braidwood ![Constellation icon.png](/w/images/b/be/Constellation_icon.png) |
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08/30/1996 |
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COMMONWEALTH EDISON CO. |
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Shared Package |
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ML20117K317 |
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NUDOCS 9609110246 |
Download: ML20117K376 (7) |
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Category:TECHNICAL SPECIFICATIONS
MONTHYEARML20210J1751999-07-30030 July 1999 Marked-up TS Pages for Proposed Changes Re Upper Temp Limit for UHS ML20209B7411999-06-30030 June 1999 Proposed Tech Specs Section 3.8.5, DC Sources - Shutdown, Correcting LCO & Braidwood TS Section 3.8, Electrical Power Systems, Deleting Various References to At&T Batteries ML20204H9781999-03-23023 March 1999 Proposed Tech Specs,Revising Sections 3.7.15,3.7.16,4.3.1 & 4.3.3 to Support Installation of New Boral high-density SFP Storage Racks at Byron & Braidwood Stations ML20204H4291999-03-22022 March 1999 Proposed Tech Specs 3.9.3,allowing Use of Gamma-Metrics post-accident Neutron Monitors to Provide Neutron Flux Info During Operational Mode 6 ML20198N3471998-12-29029 December 1998 Proposed ITS Tables 3.3.1-1 & 3.3.2-1,revising Twelve Allowable Values ML20198K5841998-12-23023 December 1998 Revised Tech Spec Pages 3/4 3-53,3/4 3-53a,6-27 & 6-27a,for Rv LI Sys ML20198A0811998-12-14014 December 1998 Proposed Rev T to Improved Tech Specs Section 3.4, Reactor Coolant Sys ML20196G6611998-11-30030 November 1998 Proposed Rev to Improved Tech Specs Section 3.1 ML20196B4101998-11-25025 November 1998 Proposed Tech Specs Facilitating Replacement of 125 Vdc At&T Batteries with New 125 Vdc C&D Batteries While in Mode 1-4 ML20155J2051998-11-0505 November 1998 Proposed TS Converting to Its,Rev R ML20155J0041998-10-30030 October 1998 Proposed Tech Specs Section 5.6.2, Fuel Storage Drainage, to Identify Sf Pool Level Sufficient to Ensure SRP Acceptance Criteria ML20154S5011998-10-18018 October 1998 Proposed Rev N to Improved TS Section 3.7 ML20154M5281998-10-15015 October 1998 Revisions K,O & P of 961213 ITS Submittal ML20154A8881998-10-0202 October 1998 Proposed Rev L to Improved Tech Specs Section 3.8 Closeout ML20153G4331998-09-25025 September 1998 Revs J & M to Tech Specs Sections 3.6 & 5.0,converting to Improved Tech Specs (Its),Final Closeout Package ML20236W5851998-07-31031 July 1998 Proposed Rev G to Sections 3.1 & 3.2 of Improved Tech Specs ML20237B6391998-07-30030 July 1998 Proposed Rev H to Section 3.5 of Improved Tech Specs ML20237E9971998-07-21021 July 1998 Rev I to Proposed Improved Tss,Section 3.9 Re Final Closeout ML20237B7021998-07-0909 July 1998 Proposed Improved TS (ITS) Section 3.3 Issued as Result of Removing Generic Change Traveler TSTF-135,Rev E from ITS Submittal ML20236H6531998-07-0202 July 1998 Rev F to 961213 Improved TS Submittal,Containing Final Package Closeout for Improved TS Sections 1.0,2.0 & 3.0 ML20248M1491998-06-0101 June 1998 Proposed Tech Specs Bases Page B 3.8-58b,converting to Improved Tech Specs ML20248C5511998-05-29029 May 1998 Proposed Tech Specs Bases Section 3/4.4.4, Relief Valves, Specifically Crediting Automatic Function of PORVs to Provide Mitigation for Inadvertent Operation of ECCS at Power Accident ML20217B2681998-02-14014 February 1998 Proposed Rev D to ITS ML20198L8811998-01-14014 January 1998 Proposed Tech Specs Pages,Revising TS Section 3/4.8.2 & Bases,To Allow Replacement of 125 Volt Dc At&T Batteries W/New Charter Power Sys,Inc (C&D) Batteries ML20198L8131998-01-14014 January 1998 Proposed Tech Specs Pages Revising TS 3.4.8, Specific Activity, Figure 3.4-1,Table 4.4-4 & TS Bases 3.4.8 ML20198C3181997-12-30030 December 1997 Proposed Tech Specs 3.7.1.3 Re Condensate Storage Tank ML20203M5921997-12-17017 December 1997 Proposed Tech Specs,Rev C Changes Improved TSs 3.0,3.3,3.7, 3.8 & 5.0 as Result of Removing Generic Change Traveler TSTF-115 from Improved TS Submittal ML20203D0361997-12-0909 December 1997 Proposed Tech Specs Pages Correcting Errors Discovered in Current TS W/Regards to Total RCS Volume & Correction to Increase in RCS Volume Associated W/Unit 1 Replacement SGs Accounting for Hot Conditions ML20199A4751997-11-0707 November 1997 Proposed Tech Specs Pages Revising TS Surveillance Sections 4.6.1.1.c,4.6.1.2.a,4.6.1.2.c & Bases to Allow Performance of 10CFR50 App J,Type a Testing ML20217K4461997-10-21021 October 1997 Proposed Tech Specs Re Boron Credit in SFP ML20202F4561997-10-10010 October 1997 Proposed Tech Specs,Deleting Lower Flow Rate Requirement Associated W/Nonaccessible Area Exhaust Filter Plenum & Fuel Handling Bldg Ventilation Sys ML20211D9421997-09-24024 September 1997 Proposed Tech Specs Revising Allowable Time Interval for Performing Turbine Throttle Valve & Turbine Valve SRs Requirements from Monthly to Quarterly ML20216G8541997-09-0808 September 1997 Proposed Tech Specs Change to TS 4.5.2.b & Associated Bases Bringing Byron Unit 1 & Braidwood Unit 1 Requirement in Conformance W/Unit 2 Requirements Approved by NRC in ML20216F1351997-09-0202 September 1997 Proposed Tech Specs 3.4.8 Re Specific Activity ML20148P7721997-06-30030 June 1997 Proposed Tech Specs,Revising TS 3.9.11,5.6.1.1 & 6.9.10 to Allow Util to Permanently Take Credit for Soluble B in Spent Fuel Storage Pool Water to Maintain Acceptable Margin of Subcriticality ML20141F3081997-06-24024 June 1997 Proposed Tech Specs,Changing TS for ECCS Venting ML20141B7781997-06-17017 June 1997 Proposed Tech Specs Revising TS Sections 3/4.6.1.6,4.6.1.2, 6.8.4 & 6.9.1.11 to Support New Requirements in 10CFR50.55a, Which Requires Utils to Update Existing Containment Vessel Structural Integrity Programs ML20148J3231997-06-0909 June 1997 Proposed TS Reflecting Latest Rev of Waste Gas Decay Tank Rupture Accident Dose Calculation ML20141K8991997-05-24024 May 1997 Proposed Tech Specs Revising TS Surveillance Requirement 4.5.2.b to Encompass non-operating ECCS Pumps & Discharge Piping Which Are Provided W/High Point Vent Valves ML20141K8931997-05-23023 May 1997 Proposed Tech Specs Revising TS Surveillance Requirement 4.5.2.b.1 for Unit 1 as It Relates to Requirement to Vent ECCS Pump Casings & Discharge Piping High Points Outside Containment ML20141K3381997-05-23023 May 1997 Proposed Tech Specs Requesting Enforcement Discretion from Compliance W/Ts 4.5.2.b.1 Requirements of Venting of Emergency Core Cooling Sys Pump Casings & Discharge Piping High Points Outside of Containment ML20148D6861997-05-23023 May 1997 Proposed Tech Specs Revising TS Surveillance Requirement 4.5.2.b.1 for Unit 1 as It Relates to Requirement to Vent ECCS Pump Casings & Discharge Piping High Points Outside Containment ML20141K0011997-05-21021 May 1997 Proposed Tech Specs Relocating Reactor Vessel Surveillance Program Capsule Withdrawal Schedules IAW GL 91-01 ML20196G0501997-04-25025 April 1997 Proposed Tech Specs Revising Primary Containment & Reactor Coolant Sys Volume Associated W/Unit 1 Steam Generator Replacement ML20137P0081997-03-24024 March 1997 Proposed Tech Specs Removing Values of cycle-specific Core Operating Limits from TS & Relocating Values to Operating Limits Rept ML20135E6851997-02-28028 February 1997 Proposed Tech Specs,Replacing Original W D4 SG at Byron & Braidwood W/B&W International SGs ML20138N6841997-02-24024 February 1997 Proposed Tech Specs Changing TS from Current TS to Improved TS Consistent w/NUREG-1431,Rev 1, STS - W Plants, Dtd Apr 1995 ML20134N8481997-02-18018 February 1997 Proposed Tech Specs Table 2.2-1 & Table 3.3-4 Re Sys Instrumentation Trip Setpoints,Ts 3.4.1.2 Re Reactor Coolant Sys & TS 4.4.1.2.1 Re Surveillance Requirements ML20134E8661997-01-30030 January 1997 Proposed Tech Specs Revising TS 1.0, Definitions, 3/4.6.1, Primary Containment & Associated Bases & 5.4.2, Reactor Coolant Sys Volume, for Bs & Bs to Support SG Replacement ML20134A1551997-01-21021 January 1997 Proposed Tech Specs 3/4.7.1.1 to Clarify That Values Calculated from New Equation for Reactor Trip Setpoint Reductions Were Adjusted 1999-07-30
[Table view] Category:TECHNICAL SPECIFICATIONS & TEST REPORTS
MONTHYEARML20210J1751999-07-30030 July 1999 Marked-up TS Pages for Proposed Changes Re Upper Temp Limit for UHS ML20209B7411999-06-30030 June 1999 Proposed Tech Specs Section 3.8.5, DC Sources - Shutdown, Correcting LCO & Braidwood TS Section 3.8, Electrical Power Systems, Deleting Various References to At&T Batteries ML20211C3311999-04-30030 April 1999 Rev 2.0 to Generic ODCM for Dresden,Quad Cities,Zion, Lasalle,Byron & Braidwood ML20204H9781999-03-23023 March 1999 Proposed Tech Specs,Revising Sections 3.7.15,3.7.16,4.3.1 & 4.3.3 to Support Installation of New Boral high-density SFP Storage Racks at Byron & Braidwood Stations ML20204H4291999-03-22022 March 1999 Proposed Tech Specs 3.9.3,allowing Use of Gamma-Metrics post-accident Neutron Monitors to Provide Neutron Flux Info During Operational Mode 6 ML20198N3471998-12-29029 December 1998 Proposed ITS Tables 3.3.1-1 & 3.3.2-1,revising Twelve Allowable Values ML20198K5841998-12-23023 December 1998 Revised Tech Spec Pages 3/4 3-53,3/4 3-53a,6-27 & 6-27a,for Rv LI Sys ML20198A0811998-12-14014 December 1998 Proposed Rev T to Improved Tech Specs Section 3.4, Reactor Coolant Sys ML20196G6611998-11-30030 November 1998 Proposed Rev to Improved Tech Specs Section 3.1 ML20196B4101998-11-25025 November 1998 Proposed Tech Specs Facilitating Replacement of 125 Vdc At&T Batteries with New 125 Vdc C&D Batteries While in Mode 1-4 ML20155J2051998-11-0505 November 1998 Proposed TS Converting to Its,Rev R ML20155J0041998-10-30030 October 1998 Proposed Tech Specs Section 5.6.2, Fuel Storage Drainage, to Identify Sf Pool Level Sufficient to Ensure SRP Acceptance Criteria ML20154S5011998-10-18018 October 1998 Proposed Rev N to Improved TS Section 3.7 ML20154M5281998-10-15015 October 1998 Revisions K,O & P of 961213 ITS Submittal ML20154A8881998-10-0202 October 1998 Proposed Rev L to Improved Tech Specs Section 3.8 Closeout ML20153G4331998-09-25025 September 1998 Revs J & M to Tech Specs Sections 3.6 & 5.0,converting to Improved Tech Specs (Its),Final Closeout Package ML20153C0351998-08-31031 August 1998 Revs to ODCM for Plant,Including Rev 2 to Chapters 10 & 11, Rev 4 to Chapter 12 and Rev 3 to App F ML20238F8221998-08-25025 August 1998 Rev 2 to Braidwood Station Units 1 & 2 Second Interval ISI Program Plan ML20236Y5481998-08-0303 August 1998 Rev 1 to Braidwood Station Units 1 & 2 Second Interval ISI Program Plan ML20236W5851998-07-31031 July 1998 Proposed Rev G to Sections 3.1 & 3.2 of Improved Tech Specs ML20237B6391998-07-30030 July 1998 Proposed Rev H to Section 3.5 of Improved Tech Specs ML20237E9971998-07-21021 July 1998 Rev I to Proposed Improved Tss,Section 3.9 Re Final Closeout ML20237B7021998-07-0909 July 1998 Proposed Improved TS (ITS) Section 3.3 Issued as Result of Removing Generic Change Traveler TSTF-135,Rev E from ITS Submittal ML20236H6531998-07-0202 July 1998 Rev F to 961213 Improved TS Submittal,Containing Final Package Closeout for Improved TS Sections 1.0,2.0 & 3.0 ML20248M1491998-06-0101 June 1998 Proposed Tech Specs Bases Page B 3.8-58b,converting to Improved Tech Specs ML20248C5511998-05-29029 May 1998 Proposed Tech Specs Bases Section 3/4.4.4, Relief Valves, Specifically Crediting Automatic Function of PORVs to Provide Mitigation for Inadvertent Operation of ECCS at Power Accident ML20216C1011998-03-26026 March 1998 Revs to ODCM for Braidwood,Including Rev 1.9 to Chapter 10 & Rev 3 to Chapter 12 ML20217B2681998-02-14014 February 1998 Proposed Rev D to ITS ML20217C3011998-01-31031 January 1998 Rev 0 to Inservice Testing Program Plan Pumps & Valves Braidwood Nuclear Generating Station,Units 1 & 2 ML20198L8131998-01-14014 January 1998 Proposed Tech Specs Pages Revising TS 3.4.8, Specific Activity, Figure 3.4-1,Table 4.4-4 & TS Bases 3.4.8 ML20198L8811998-01-14014 January 1998 Proposed Tech Specs Pages,Revising TS Section 3/4.8.2 & Bases,To Allow Replacement of 125 Volt Dc At&T Batteries W/New Charter Power Sys,Inc (C&D) Batteries ML20216H4321997-12-31031 December 1997 Revs to OCDM for Braidwood,Including Rev 1.8 to Chapter 10, Rev 1.9 to Chapter 11,rev 2 to Chapter 12 & Rev 2 to App F ML20198C3181997-12-30030 December 1997 Proposed Tech Specs 3.7.1.3 Re Condensate Storage Tank ML20203M5921997-12-17017 December 1997 Proposed Tech Specs,Rev C Changes Improved TSs 3.0,3.3,3.7, 3.8 & 5.0 as Result of Removing Generic Change Traveler TSTF-115 from Improved TS Submittal ML20203D0361997-12-0909 December 1997 Proposed Tech Specs Pages Correcting Errors Discovered in Current TS W/Regards to Total RCS Volume & Correction to Increase in RCS Volume Associated W/Unit 1 Replacement SGs Accounting for Hot Conditions ML20199A4751997-11-0707 November 1997 Proposed Tech Specs Pages Revising TS Surveillance Sections 4.6.1.1.c,4.6.1.2.a,4.6.1.2.c & Bases to Allow Performance of 10CFR50 App J,Type a Testing ML20217K4461997-10-21021 October 1997 Proposed Tech Specs Re Boron Credit in SFP ML20198P1601997-10-20020 October 1997 Rev 1.5 to Odcm,Chapter 12 ML20202F4561997-10-10010 October 1997 Proposed Tech Specs,Deleting Lower Flow Rate Requirement Associated W/Nonaccessible Area Exhaust Filter Plenum & Fuel Handling Bldg Ventilation Sys ML20211D9421997-09-24024 September 1997 Proposed Tech Specs Revising Allowable Time Interval for Performing Turbine Throttle Valve & Turbine Valve SRs Requirements from Monthly to Quarterly ML20216H7011997-09-10010 September 1997 Revised Procedures,Including Rev 2 to Bwzp 2000-18, Post- Accident Sampling Sys (Primary Responsibility - Chemistry Director) & Rev 2 to Bwzp 2000-18A1, PASS Sample Collection Procedures ML20216G8541997-09-0808 September 1997 Proposed Tech Specs Change to TS 4.5.2.b & Associated Bases Bringing Byron Unit 1 & Braidwood Unit 1 Requirement in Conformance W/Unit 2 Requirements Approved by NRC in ML20216F1351997-09-0202 September 1997 Proposed Tech Specs 3.4.8 Re Specific Activity ML20148P7721997-06-30030 June 1997 Proposed Tech Specs,Revising TS 3.9.11,5.6.1.1 & 6.9.10 to Allow Util to Permanently Take Credit for Soluble B in Spent Fuel Storage Pool Water to Maintain Acceptable Margin of Subcriticality ML20141F3081997-06-24024 June 1997 Proposed Tech Specs,Changing TS for ECCS Venting ML20141B7781997-06-17017 June 1997 Proposed Tech Specs Revising TS Sections 3/4.6.1.6,4.6.1.2, 6.8.4 & 6.9.1.11 to Support New Requirements in 10CFR50.55a, Which Requires Utils to Update Existing Containment Vessel Structural Integrity Programs ML20148J3231997-06-0909 June 1997 Proposed TS Reflecting Latest Rev of Waste Gas Decay Tank Rupture Accident Dose Calculation ML20141K8991997-05-24024 May 1997 Proposed Tech Specs Revising TS Surveillance Requirement 4.5.2.b to Encompass non-operating ECCS Pumps & Discharge Piping Which Are Provided W/High Point Vent Valves ML20141K8931997-05-23023 May 1997 Proposed Tech Specs Revising TS Surveillance Requirement 4.5.2.b.1 for Unit 1 as It Relates to Requirement to Vent ECCS Pump Casings & Discharge Piping High Points Outside Containment ML20141K3381997-05-23023 May 1997 Proposed Tech Specs Requesting Enforcement Discretion from Compliance W/Ts 4.5.2.b.1 Requirements of Venting of Emergency Core Cooling Sys Pump Casings & Discharge Piping High Points Outside of Containment 1999-07-30
[Table view] |
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ATTACHMENT B MARKED UP PAGES FOR PROPOSED CHANGES TO APPENDIX A TECHNICAL SPECIFICATIONS OF FACILITY OPERATING LICENSES NPF-72, AND NPF-77 BRAIDWOOD STATION UNITS I & 2 REVISED PAGES:
i 3/4 4-16 1
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9609110246 960830 PDR ADOCK 05000456 P PDR o efsypW6040 doc
REACTOR COOLANT SYSTEM )
- I SURVEILLANCE REOUIREMENTS (Continued)
. 1 4.4.5.4 Acceptance Criteria
- a. As used in this specification:
- 1) Imoerfection means an exception t1FThe dimensions, finish or 4 contour of a tube or sleeve from that required by fabrication drawings or specifications. Eddy-current testing indications !
i below 20% of the nominal tube or sleeve wall thickness, if detectable, may be considered as imperfections;
)
- 2) 'Deoradation means a service-induced cracking, wastage, wear or general corrosion occurring on either inside or outside of a tube or sleeve;
- 3) Deoraded Tube means a tube or sleeve containing unrepaired imperfections greater than or equal to 20% of the nominal tube or sleeve wall thickness caused by degradation; l
- 4) % Dearadation means the percentage of the tube or sleeve wall I l
thickness affected or removed by degradation; l
- 5) Defect means an imperfection of such severity that it exceeds l the plugging or repair limit. A tube or sleeve containing an i
unrepaired defect is defective;
! 6) Plucoina or Reoair Limit means the imperfection depth at or beyond which the tube shall be removed from service by plugging or repaired by sleeving in the affected area. The plugging or I repair limit imperfection depth for the tubing and laser welded sleeves is equal to 40% of the nominal wall thickness. The plugging limit imperfection depth for TIG welded sleeves is //
equal to 32% of the nominal wall thickness. For Unit 1, this
/
definition does not apply to defects in the tubesheet that meet the criteria for an F tube. For Unit 1 Cycle 6, this l definition does not apply to the tube support plate intersections for which the voltage-based repair criteria are being applied. Refer to 4.4.5.4.a.11 for the repair limit applicable to these intersections; f
- 7) i Unserviceable describes the condition of a tube if it leaks or l contains a defect large enough to affect its structural integ-l rity in the event of an Operating Basis Earthquake, a loss-of-coolant accident, or a steam line or feedwater line break as i
specified in 4.4.5.3c., above;
- 8) Tube Insoection means an inspection of the steam generator tube !
from the point of entry (hot leg side) completely around the U-bend to the top support of the cold leg. For a tube that has been repaired by sleeving, the tube inspection shall include the sleeved portion of the tube, and f $nierf b i
BRAIDWOOD - UNITS 1 & 2 3/4 4-16 AMENDMENT NO.
I Insert A l
For Unit 1, Cycle 6, operation may continue provided that the projected distribution of indications found in the top of tubesheet roll transition resulting from the re-analysis of previous NDE data results in a probability of burst ofless than 1 x 10-2 and predicted leakage is less than the site allowable leak limit. Otherwise, Unit I will shutdown and top of tubesheet roll transition indications will be plugged or repaired.
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l EVALUATION OF SIGNIFICANT IIAZARDS CONSIDERATIONS FOR l PROPOSED CHANGES TO APPENDIX A l TECHNICAL SPECIFICATIONS OF
- FACILITY OPERATING LICENSES NPF-72, AND NPF-77 l
Commonwealth Edison is:: evaluated this proposed amendment and determined that it involves
% significant hazards consideratione Aarding to Title 10 Code of Federal Regulations Section 50 Subsection 92 Paragraph c (10 CFR 50.92 (c)), a proposed amendment to an operating license involves no significant hazards considerations if operation of the facility in accordance with the proposed amendment would not: j l
- 1. Involve a significant increase in the probability or consequences of an accident j previously evaluated; or
- 2. Create the possibility of a new or difTerent kind of accident from any accident previously evaluated; or l
- 3. Involve a significant reduction in a margin of safety.
A. INTRODUCTION Commonwealth Edison (Comed) proposes to revise Technical Specification Surveillance ;
Requirement (TSSR) 4.4.5.4.a 6) " Plugging or Repair Limit," of TS 3.4.5, " Steam Generators."
This revision will provide guidance on actions to be taken based on the results of a review of previous Braidwood Steam Generator (SG) Non-Destructive Examination (NDE) data for top of tube sheet cracking indications.
Over the past eleven months Comed has conducted a significant program to evaluate the safety significance of Top of Tubesheet (TTS) roll transition circumferential ODSCC cracks at not only Braidwood and Byron but at other units world wide. The results from this program clearly demonstrate:
! . Steam Generators must be inspected periodically for the presence of TTS roll transition circumferential ODSCC cracks.
. First time use of techniques to identify circumferential indications insure that the largest j indication will be repaired. In subsequent inspections the size of the most limiting indications l found will be smaller.
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. If circumferential indications are found, the scope of the inspection must be increased to 100%
of the tubes.
. All TTS circumferential ODSCC cracks have been shown to have the same morphology.
. All circumferential indications which have been in operation for 2 one cycle afler an initial inspection has been performed have been within the structural integrity limit.
Results of the program indicate that if circumferential cracks are detected using approved inspection techniques and repaired, then indications which were not identified during the inspection are shown to be small in size and will not grow to exceed the structurallimit in the subsequent cycle of operation.
Therefore, the establishment of acceptance criteria to assess structural integrity and leakage potential during accident conditions, ensure that the requirements of General design Criteria (GDC) of 10CFR, Part 50 Appendix A are met, specifically GDC-14 " Reactor Coolant System Boundary."
B. NO SIGNIFICANT llAZARDS ANALYSIS
- 1. The proposed change does not involve a significant increase in the probability or consequences of an accident previously evaluated.
The previously evaluated applicable accidents are steam generator tube burst, and Main Steam Line Break (MSLB). The postulated MSLB outside of containment but upstream of the Main Steam Isolation Valve (MSIV) represents the most limiting radiological condition for this proposed change. This change requires that tube burst probability must be shown to be less than 1 x 10 2 for the projected distribution ofindications resulting from the proposed re-analysis of previous NDE data. Otherwise, Unit I will be shutdown and top of tube sheet indications will be l plugged or repaired. The presence of circumferential cracks in SG tubing does not afTect the probability of occurrence of a MSLB, or the failure of the MSIV. Regarding SG tube rupture, the probability of burst ofless than 1 x 10-2 has been previously accepted as providing an appropriate level of safety against tube burst for an individual tube degradation mechanism, and is consistent with the requirements of Generic Letter 95-05, " Voltage Based Repair Criteria for Westinghouse Steam Generator Tubes Affected By Outside Diameter Stress Corrosion Cracking." Additionally, Draft Regulatory Guide X.XX, " Steam Generator Tube Integrity," provides further support for a tube burst probability intersections of 1 x 10-2 as being acceptable for modes of degradation other than ODSCC. Thus, this proposed change does not result in a significant increase in the probability of an accident previously analyzed.
The changes proposed in this amendment request require that the predicted leakage be shown to be less than the site allowable leakage limit for the projected EOC distribution ofindications resulting from the proposed re-analysis of previous NDE data. Otherwise, Unit I will be shutdown and top of tube sheet indications will be plugged or repaired. Thus, all offsite dose calculation assumptions remain satisfied and these proposed changes do not result in an increase in the consequences of an accident previously analyzed.
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- 2. The proposed change does not create the possibility of a new or different kind of accident from any accident previously evaluated.
The changes proposed in this amendment request will not result in the installation of any new equipment or systems or the modification of any existing equipment or systems.
, No new operating procedures, conditions or modes will be created by this proposed amendment.
Thus, this proposed change does not create the possibility of a new or different kind of accident from any accident previously evaluated.
- 3. The proposed change does not involve a significant reduction in a margin of safety.
1 1 The accidents of concern for this proposed amendment are SG tube burst and MSLB. The I i changes pro I than 1 x 10This posed in this amendment request require that tube burst probability be main value has been previously accepted in Generic Letter 95-05 as providing an acceptable level of safety against tube burst and is consistent with Drafl Regulatory Guide X.XX
" Steam Generator Tube Integrity". The changes proposed in this amendment request also require j 4
that site allowable leakage limits be maintained. Otherwise, Unit I will be shutdown and top of i tube sheet indications will be plugged or repaired. Thus, all design basis and offsite dose calculation assumptions remain satisfied and the proposed change does not result in a significant reduction in a margin of safety.
This amendment request increases the safety margin to leak and burst in the event of a MSLB because it defines clear acceptance criteria in the Technical Specific for operation of a Steam Generator in which circumferential ODSCC at TTS has been identified.
1 Therefore, based on the above evaluation, Commonwealth Edison has concluded that these changes involve no significant hazards considerations.
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ATTACHMENT D !
ENVIRONMENTAL ASSESSMENT FOR PROPOSED CHANGES TO APPENDIX A TECHNICAL SPECIFICATIONS OF FACILITY OPERATING LICENSES NPF-72, AND NPF-77 Commonwealth Edison Company (Comed) has evaluated this proposed license amendment request against the criteria for identification oflicensing and regulatory actions requiring environmental assessment in accordance with Title 10, Code of Federal Regulations, Part 51, Section 21 (10 CFR 51.21). Comed has determined that this proposed license amendment request meets the criteria for a categorical exclusion set forth in 10 CFR 51.22(c)(9). This determination is based upon the following:
- 1. The proposed licensing action involves the issuance of an amendment to a license for a reactor pursuant to 10 CFR 50 which changes a requirement with respect to installation or use of a facility component located within the restricted area, as .
defined in 10 CFR 20, or which changes an inspection or a surveillance requirement. This proposed license amendment request revises Technical Specification Surveillance Requirement (TSSR) 4.4.5.4.a 6) " Plugging or Repair q Limit," of TS 3.4.5, " Steam Generators."
This revision will provide guidance on actions to be taken based on the results of the review of previous Braidwood Steam Generator (SG) Non-Destructive Examination (NDE) data for top of tube sheet indications.
- 2. this proposed license amendment request involves no significant hazards considerations;
- 3. there is no significant change in the types or significant increase in the amounts of any efiluent that may be released offsite; and
- 4. there is no significant increase in individual or cumulative occupational radiation exposure.
Therefore, pursuant to 10 CFR 51.22(b), neither an environmentalimpact statement nor an environmental assessment is necessary for this proposed license amendment request.
s
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