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Category:ABNORMAL OCCURRENCE REPORTS (SEE ALSO LER & RO)
MONTHYEARML20086G2701976-01-0808 January 1976 AO 75-79:on 751229,local Leak Test Identified through- Leakage of B Loop RHR Torus Spray Valve MO-3-10-38B & Torus Cooling Return Valve MO-3-10-34B.Cause Under Investigation ML20086G2721976-01-0505 January 1976 AO 75-78:on 751226,drywell Radiation Monitor Inoperative. Caused by Flow Blockage in on Stream Sample Line.Sample Point Changed to Reestablish Sample Flow to Drywell Radiation Monitor ML20086G2741975-12-30030 December 1975 AO 75-76:on 751220-21,local Leak Rate Test Identified through-leakage on Loop a & B RHR Outboard Injection Valves MO-3-10-154A & B.Cause Not Determined.Inboard Isolation Valves Verified as Leaktight & Closed ML20086H0411975-12-0505 December 1975 AO 75-72:on 751126,core Spray 3A Full Flow Test Valve MO-3-14-26A Failed to Close.Caused by Broken Wire on Closing Torque Switch in Valve Operator.Broken Wire Repaired & Proper Valve Operator Verified ML20086F8431975-12-0505 December 1975 AO 75-77:on 751126,LS-4223 Failed to Operate RHR Head Spray Line High Point Vent SV-4223 on Low Accumulator Level.Caused by Blown Fuse in Solenoid Valve Circuit.Grounded Wire Repaired & Vent Valve Returned to Svc ML20086F8491975-12-0101 December 1975 Telecopy AO 75-77:on 751126,LS-4223 Failed to Operate SV-4223 on Low Accumulator Level.Caused by Blown Fuse in Solenoid Valve Circuit.Operator Manually Vented Accumulator to Ensure Head Spray Line Maintained Filled ML20086F8711975-11-26026 November 1975 AO 75-75:on 751117,reservoirs of Two Hydraulic Snubbers Found Empty.Caused by Leaking O-rings & Gaskets.Defective gaskets,seals,O-rings & Fittings Will Be Replaced & Snubbers Will Be Checked ML20086F8551975-11-26026 November 1975 AO 75-76:on 751117,rigid Pipe Support Found Broken on RHR Shutdown Cooling Suction Line.Caused by Component Failure. Pipe Support Replaced.Investigation Continuing ML20086F8801975-11-26026 November 1975 AO 75-74:on 751116,setpoint of RCIC Steam Supply Line Area High Temp Switch TE-TS 4939A Found Less Conservative than Specified by Tech Specs.Caused by Slight Setpoint Drift. Switch Recalibr,Tested & Returned to Svc ML20086H0461975-11-26026 November 1975 Telecopy AO 75-72:on 751126,core Spray Full Flow Test Valve MO-3-14-26A Failed to Close.Caused by Broken Wire on Closing Torque Switch in Valve Operator.Broken Wire Repaired & Proper Valve Operation Verified ML20086F8961975-11-21021 November 1975 AO 75-73:on 751113,leak Observed on RHR Sys Relief Valve RV-35B.Caused by Throttling of MO-2-10-154B Valve Resulting in Crack.Weld Repairs Will Be Made to Relief Valve in Accordance W/Approved Procedures ML20086F8611975-11-18018 November 1975 Telecopy AO 75-76:on 751117,rigid Pipe Support Found Broken on RHR Shutdown Cooling Suction Line.Cause Under Investigation.Corrective Action to Be Determined After Investigation ML20086F8741975-11-18018 November 1975 Telecopy AO 75-75:on 751117,two Outside Drywell Snubbers Found to Have Empty Reservoirs.Cause Under Investigation. Corrective Action to Be Determined After Investigation ML20086F8901975-11-17017 November 1975 Telecopy AO 75-74:on 751116,setpoint of RCIC Steam Supply Line High Temp Switch TE-TS 4939A Found Less Conservative than Allowed by Tech Specs.Caused by Slight Setpoint Drift. Switch Recalibr & Returned to Svc ML20086F9061975-11-17017 November 1975 AO 75-71:on 751107,cracked Weld on 1-inch Line to Relief Valve RV-35B Observed.Caused by Throttling MO-2-10-154B Resulting in Cracked Weld.Repairs Completed in Accordance W/Approved Procedure ML20086F9181975-11-14014 November 1975 AO 75-70:on 751104,reservoirs of Five Hydraulic Snubbers Found Empty.Caused by Leaking O-rings & Gaskets.Defective Gaskets & O-rings Will Be Replaced ML20086F9021975-11-14014 November 1975 Telecopy AO 75-73:on 751113,leak on Body of RV-35B RHR Sys Relief Valve Observed.Caused by Throttling of MO-2-10-154B Valve Resulting in Crack.Rhr Loop B Shut Down in Preparation for Repair of Relief Valve ML20086F9111975-11-10010 November 1975 Telecopy AO 75-71:on 751107,cracked Weld on Line to RV-35B Observed.Caused by Throttling Down on MO-2-10-154B Resulting in Weld Crack.Repairs Completed.Pipe Vibration Readings Taken to Determine If Mods Required ML20086H0521975-11-0707 November 1975 AO 75-71:on 751030,drywell Oxygen Analyzer Sample Sys Outer Isolation Valve SV-3978B Failed.Caused by Dirt on Seat & in Body of Valve.Valve Internals & Seat Cleaned.Valve Disc, Piston Rings & Bonnet O-ring Replaced ML20086F9231975-11-0505 November 1975 Telecopy AO 75-70:on 751104,reservoirs of Five Hydraulic Snubbers Found Empty.Cause Under Investigation.Corrective Action to Be Determined After Investigation ML20086H0621975-11-0303 November 1975 AO 75-70:on 751024,drywell Purge Supply Isolation Valve A0-3520 Operated W/O Manual Initiation.Caused by Incorrect Implementation of Mod.Piping Corrected & Will Be Monitored ML20086H0751975-10-31031 October 1975 AO 75-68:on 751021,torus Makeup Supply Isolation Valve AO-3523 Found to Leak in Excess of 2,000 Cc/Minute.Caused by Closing Spring Not Providing Sufficient Force to Fully Close Valve.Closing Spring Adjusted ML20086H0561975-10-31031 October 1975 Telecopy AO 75-71:on 751030,isolation Valve SV 3978B Failed. Cause Under Investigation.Corrective Action to Be Determined ML20086F9291975-10-31031 October 1975 AO 75-69:on 751021,nitrogen Found to Leak Out of Test Connection on Inboard Flange of AO-2519.Caused by Use of Wrong Connection for Testing Double O-ring Seal.Connection Capped & Leak Checked Successfully ML20086H0851975-10-31031 October 1975 AO 75-67:on 751021,torus Makeup Supply Isolation Check Valve 276Y Found Leaking in Excess of 2,000 Cc/Minute.Caused by Valve Piston Being Hung Up During Operation.Check Valve Repaired & Local Rate Test Repeated ML20086F9381975-10-31031 October 1975 AO 75-68:on 751021,O-ring Gasket Leak Discovered on Torus Purge Supply Valve AO-2521B.Caused by Use of Improper Connection for Testing Double O-ring Seal.Connection Capped & Leak Checked Successfully ML20086F9521975-10-30030 October 1975 AO 75-66:on 751020,APRM B Flow Bias Signal Failed Upscale. Caused by Internal Ground in Channel Flow Transmitter D Combined W/Installed Instrument Loop Ground,Lowering Total Loop Resistance.Defective Components Replaced ML20086F9661975-10-24024 October 1975 AO 75-65:on 751015,setpoints on Reactor High Pressure Scram Switches Found Less Conservative than Specified by Tech Specs.Caused by Instrument Setpoint Shift.Channel D Switch Recalibr,Tested & Returned to Svc ML20086H0741975-10-24024 October 1975 Telecopy AO 75-69:on 751023,O-ring Gasket Leak Found on Drywell Purge Supply Valve AO-3505.Cause Under Investigation.Corrective Action to Be Determined After Investigation ML20086H0681975-10-24024 October 1975 Telecopy AO 75-70:on 751024,drywell Purge Supply Isolation Valve AO-3520 Operated W/O Manual Initiation.Caused by Incorrect Implementation of Mod.Valve Failed Closed & Will Be Repaired ML20086F9331975-10-21021 October 1975 Telecopy AO 75-69:on 751021,O-ring Gasket Leak Discovered on Drywell & Torus Inerting Nitrogen Supply Valve AO-2519.Cause Under Investigation.Corrective Action to Be Determined After Investigation ML20086F9491975-10-21021 October 1975 Telecopy AO 75-67:on 751021,diesel Generator Breaker E-4 Inoperable.Caused by Inoperative Charging Motor Failing Due to Brush Wear.Breaker Replaced ML20086H0901975-10-21021 October 1975 Telecopy AO 75-67:on 751021,torus Makeup Supply Isolation Check Valve 276Y Found Leaking in Excess of 2,000 Cc/Minute. Cause Under Investigation.Corrective Actions to Be Determined After Investigation ML20086H0811975-10-21021 October 1975 Telecopy AO 75-68:on 751021,torus Makeup Sys Isolation Valve AO-3523 Found to Leak in Excess of 2,000 Cc/Minute.Cause Under Investigation.Corrective Action to Be Determined After Investigation ML20086F9581975-10-21021 October 1975 Telecopy AO 75-66:on 751020,logic Aprm/Rbm B Flow Bias Signal from FT-2-2-110D Failed Upscale.Caused by Failure of Second Ground on Recirculation Drive Flow Transmitter Signal Loop.Flow Signal Corrected ML20086F9441975-10-21021 October 1975 Telecopy AO 75-68:on 751021,leak Found on O-ring Gasket on Torus Purge Supply Valve AO 2521A.Cause Under Investigation. Corrective Action to Be Determined After Investigation ML20086H0961975-10-16016 October 1975 AO 75-66:on 751006,RCIC Inboard Steam Supply Isolation Valve MO-3-13-15 Failed to Close.Cause Not Identified.Valve Stroked Successfully.Failure Not Repeatable ML20086F9701975-10-16016 October 1975 Telecopy AO 75-65:on 751015,setpoint on Reactor High Pressure Scram Switches Found to Be Less Conservative than Specified by Tech Specs.Caused by Instrument Setpoint Shift. Channel D Switch Recalibr,Tested & Returned to Svc ML20086H1061975-10-10010 October 1975 AO 75-65:on 751002,drywell Radiation Monitor Inoperable. Caused by Rust Blockage of Pressure Control Valve.Valve Cleaned,Reassembled & Returned to Svc ML20086F9811975-10-10010 October 1975 AO 75-64:on 751002,upper Isolation Valve to LS-2-3-231C Found Closed.Caused by Technician Error.Technicians Involved Interviewed & Seriousness of Error Stressed ML20086H1171975-10-0909 October 1975 AO 75-64:on 750929,main Steam Line High Flow Switch DPIS-3-2-116A Found to Trip at Value Slightly Higher than Tech Spec.Caused by Setpoint Shift.Device Checked for Setpoint Repeatability & Recalibr ML20086H1011975-10-0707 October 1975 Telecopy AO 75-66:on 751006,RCIC Inboard Steam Supply Isolation Valve MO-3-13-15 Failed to Close.Cause Under Investigation.Corrective Action to Be Determined After Investigation ML20086F9741975-10-0303 October 1975 Telecopy AO 75-65:on 751015,alarm Received Indicating Sampling Sys Exhaust Pump Suction Low.Cause Under Investigation.Corrective Action to Be Determined After Investigation ML20086H1111975-10-0303 October 1975 Telecopy AO 75-65:on 751002,drywell Radiation Monitor Inoperable.Cause Under Investigation.Corrective Action to Be Determined After Investigation ML20086F9861975-10-0303 October 1975 Telecopy AO 75-64:on 751002,upper Isolation Valve to LS-2-3-231C Found Closed.Caused by Technician Error. Technicians Involved Interviewed & Seriousness of Error Stressed ML20086F9891975-09-30030 September 1975 Telecopy AO 75-63:on 750929,outer Isolation Valves 86C & 86D Closed in 1.7 & 2.3 S,Respectively.Caused by Insufficient Hydraulic Fluid in Valve Actuator.Hydraulic Fluid Added & Adjustments Made to Closing Speed ML20086G4221975-09-30030 September 1975 AOs 50-277-75-62 & 50-278-75-61:on 750920,main Stack Flow Transmitters Failed.Caused by Lightning Strike.Damaged Components Replaced.Util Begun Study to Provide Permanent Resolution of Problem ML20086H1201975-09-29029 September 1975 Telecopy AO 75-64:on 750929,main Steam Line High Flow Switch DPIS-3-2-116A Found at Value Slightly Higher than Specified by Tech Spec.Caused by Setpoint Shift.Device Checked for Setpoint Repeatability & Recalibr ML20086H1301975-09-22022 September 1975 Telecopy AO 75-62:in 750921,RHR Head Spray Stay Fill Vent LS-5223 Found Inoperable.Caused by Binding in Switch Float Assembly.Stay Fill Tank Refilled & Switch Will Be Repaired ML20086G4261975-09-22022 September 1975 Telecopy AOs 50-277-75-62 & 50-278-75-61:on 750920,main Stack Flow Transmitters Failed.Caused by Lightning Strike. Damaged Components Replaced 1976-01-08
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K9931999-10-14014 October 1999 Safety Evaluation Supporting Amend 234 to License DPR-56 ML20217B4331999-10-0505 October 1999 Safety Evaluation Supporting Amend 233 to License DPR-56 ML20217G3541999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Pbaps,Units 2 & 3. with ML20216H7091999-09-24024 September 1999 Safety Evaluation Supporting Amends 229 & 232 to Licenses DPR-44 & DPR-56,respectively ML20212D1281999-09-17017 September 1999 Safety Evaluation Supporting Proposed Alternatives CRR-03, 05,08,09,10 & 11 ML20212A5871999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Peach Bottom,Units 2 & 3.With ML20211D5501999-08-23023 August 1999 Safety Evaluation Supporting Amends 228 & 231 to Licenses DPR-44 & DPR-56,respectively ML20212H6311999-08-19019 August 1999 Rev 2 to PECO-COLR-P2C13, COLR for Pbaps,Unit 2,Reload 12 Cycle 13 ML20210N7641999-07-31031 July 1999 Monthly Operating Repts for Jul 1999 for PBAPS Units 2 & 3. with ML20209H1121999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Pbaps,Units 2 & 3. with ML20195H8841999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Pbaps,Units 2 & 3. with ML20206N1661999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Pbaps,Units 2 & 3. with ML20206A2921999-04-20020 April 1999 Safety Evaluation Concluding That Proposed Changes to EALs for PBAPS Are Consistent with Guidance in NUMARC/NESP-007 & Identified Deviations Meet Requirements of 10CFR50.47(b)(4) & App E to 10CFR50 ML20205K7411999-04-0707 April 1999 Safety Evaluation Supporting Amends 227 & 230 to Licenses DPR-44 & DPR-56,respectively ML20205P5851999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Peach Bottom Units 2 & 3.With ML20207G9971999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Peach Bottom Units 2 & 3.With ML20199E3471998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Peach Bottom,Units 1 & 2.With ML20205K0381998-12-31031 December 1998 PECO Energy 1998 Annual Rept. with ML20206P1651998-12-31031 December 1998 Fire Protection for Operating Nuclear Power Plants, Section Iii.F, Automatic Fire Detection ML20206D3651998-12-31031 December 1998 1998 PBAPS Annual 10CFR50.59 & Commitment Rev Rept. with ML20206D3591998-12-31031 December 1998 1998 PBAPS Annual 10CFR72.48 Rept. with ML20196G7021998-12-0202 December 1998 SER Authorizing Proposed Alternative to Delay Exam of Reactor Pressure Vessel Shell Circumferential Welds by Two Operating Cycles ML20196E8261998-11-30030 November 1998 Response to NRC RAI Re Reactor Pressure Vessel Structural Integrity at Peach Bottom Units 2 & 3 ML20198B8591998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Pbaps,Units 2 & 3. with ML20206R2571998-11-17017 November 1998 PBAPS Graded Exercise Scenario Manual (Sections 1.0 - 5.0) Emergency Preparedness 981117 Scenario P84 ML20198C6751998-11-0505 November 1998 Rev 3 to COLR for PBAPS Unit 3,Reload 11,Cycle 12 ML20195E5341998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Pbaps,Units 2 & 3. with ML20155C6071998-10-26026 October 1998 Safety Evaluation Supporting Amend 226 to License DPR-44 ML20155C1681998-10-22022 October 1998 Safety Evaluation Accepting Proposed Alternative Plan for Exam of Reactor Pressure Vessel Shell Longitudinal Welds ML20155H7721998-10-12012 October 1998 Rev 1 to COLR for Peach Bottom Atomic Power Station Unit 2, Reload 12,Cycle 13 ML20154J2401998-10-0505 October 1998 Safety Evaluation Supporting Amends 224 & 228 to Licenses DPR-44 & DPR-56,respectively ML20154H4771998-10-0505 October 1998 Safety Evaluation Supporting Amends 225 & 229 to Licenses DPR-44 & DPR-56,respectively ML20154G6821998-10-0101 October 1998 SER Related to Request for Relief 01A-VRR-1 Re Inservice Testing of Automatic Depressurization Sys Safety Relief Valves at Peach Bottom Atomic Power Station,Units 2 & 3 ML20154G6631998-10-0101 October 1998 Safety Evaluation Supporting Amends 223 & 227 to Licenses DPR-44 & DPR-56,respectively ML20154H5541998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Pbaps,Units 2 & 3. with ML20153B9651998-09-14014 September 1998 Safety Evaluation Supporting Amend 9 to License DPR-12 ML20151Y2901998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Pbaps,Units 2 & 3. with ML20238F2661998-08-24024 August 1998 Safety Evaluation Supporting Amend 222 to License DPR-44 ML20237B9531998-08-10010 August 1998 Specification for ISI Program Third Interval,Not Including Class Mc,Primary Containment for Bpaps Units 2 & 3 ML20237A7761998-08-10010 August 1998 SER Accepting Licensee Response to NRC Bulleting 95-002, Unexpected Clogging of RHR Pump Strainer While Operating in Suppression Pool Cooling Mode ML20237A5351998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Pbaps,Units 2 & 3 ML20236R8281998-07-15015 July 1998 Safety Evaluation Approving Proposed Alternative (one-time Temporary non-Code Repair) Pursuant to 10CFR50.55a(a)(3) (II) ML20236M3471998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Pbaps,Units 2 & 3 ML20249C4791998-06-0202 June 1998 Rev 6 to COLR for PBAPS Unit 2 Reload 11,Cycle 12 ML20248F4781998-06-0101 June 1998 Corrected Page 1 to SE Supporting Amends 221 & 226 to Licenses DPR-44 & DPR-56,respectively.Original Page 1 of SE Had Three Typos ML20248F7441998-05-31031 May 1998 Reactor Vessel Working Group,Response to RAI Regarding Reactor Pressure Vessel Integrity ML20248M3001998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Pbaps,Units 2 & 3 ML20247N5351998-05-11011 May 1998 SER Accepting Third 10-year Interval Inservice Program for Pump & Valves for Plant,Units 2 & 3 ML20249C4751998-05-0707 May 1998 Rev 5 to COLR for PBAPS Unit 2 Reload 11,Cycle 12 ML20247G0721998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Pbaps,Units 2 & 3 1999-09-30
[Table view] |
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, i- September 14, 1973 Mr. A. Giambusso Deputy Director of Reactor Projects United States Atomic Energy Commission Directorate of Licensing Washington, D. C. 20545
Reference:
Peach Bottom Atomic Power Station - Unit #2 Facility Operating License DPR-44 Docket No. 50-277
Subject:
Abnormal Occurrances
Dear Mr. Giambusso:
During the week of September 3, 1973, surveillance tests were performed on instrument systems required for both the shutdown as well es power operating condition. Certain set point deviation and switch deficiencies were noted snd reported to Regulatory Operations, at the present time the reactor is in the shutdown condition -- having just received the initial fuel load. The reactor has not yet been brought to the critical condition, therefore, safety problems associated with heat removal and -
radiation do not exist. y The following items were reported to Mr. T. Shediowsky, AEC Region 1 Regulatory Operations Office on .the dates indicated: .
PB-2-14-44A Setpoint Shift 9/5/73 dPIS-2-2-119A Functional Failure 9/7/73 l(Isf IRM Chan C Setpoint Shift 9/7/73 3h) LB-2-3-231 D Functional Failure 9/9/73
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, In accordance with Section 6 7.2.A of the Technical Specification
(,[ Appendix A of DPR-44 for Unit #2 Peach Bottom Atomic Power Station, these fail-T, ures are being reported to the Directorate of Licensing as Abnormal Occurrances, ys-
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_ . . . _ _ _ _ . - ~ _ __ E=d n G O V PS-2-14-44A 9/4/73 During routine instrument surveillance testing on 9/4/73, pressure switch PS-2-14-44A was found to be out of calibration. The acceptable range for this switch is 185 + 5 psig. The "as found" setpoint was 191.7 psig, which is less than 2 PSI out of limit. This switch is used in the Automatic Depressuri-zation System logic to provide the " Core Spray Pump Running" interlock permissive (at 185 + 5 psig, Tech. Spec. Table 3 2.8) .
The switch was recalibrated, retested according to the same instrument surveillance procedure ST 2.1.04A, and found to be within acceptable limits.
Inve st i gati on Investigation of this setpoint shif t f ailed to disclose any specific reason for this shif t.
The remainder of the switches used in this same type of application were checked and found to be satisfactory. This consists of four en the Core Spray System and eight on the Residual Heat Removal System.
Corrective Action No further corrective action was deemed necessary.
Safety Implicatiens The f ailure of this switch presents no safety hazard to the plant under the present conditions in that the reactor contains no irradiated fuel and has no decay heat. Additionally, the Technical Specifications indicate (Section 3.5.E.1) that the Automatic Depressuri zation System of which this switch is a part is not needed to be operable if there is no irradiated fuel in the reactor or the reactor pressure is less than 105 psig. The plant presently meets both of these conditions. -
2 dPIS-2-2-119A 9/6/73 During routine instrument surveillance te' sting on 9/6/73, differential pressure switch dPIS-2-2-Il9A was found to be inoperative. This switch is used in the main steam line leak detection circuit to provide the main steam line High Flow signa! to the Primary Containment Isolation System Logic to initiate Main Steam Line Isolation Valve Closure.
Investigation It was found that the switch could be actuated at the setpoint by tapping the case. Internal inspection revealed that the linkage was binding slightly at the first pivot point. Straightening of the hold down plate at the pivot allowed the linkage to then operate freely.
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N e 4 O.e O 3- l The calibration was rechecked and the instrument returned to service.
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Corrective Action The remaining switches of this type are being investigated for binding and for proper se'tpoint to preclude repetition of this type failure.
Safety Implications Since the requirement for primary containment integrity (Tech.
Spec., Limiting Conditions for Operation, 3 7.A.2) does not exist at this time, no safety hazard exists because of this failure.
IRM Channel C 9/7/73 During routine neutron monitoring system surveillance testing on 9/7/73, both the HI and the HI-HI setpoints on IRM Channel C were found- to be out of calibration. The acceptable setpoints are as follows:
- a. HI, which provides a rod block, ~
108 indicated on scale (Tech.
Spec. Table 3 8.0)
- b. HI-HI, which provides a scram input, - 120/125 of full scale (Tech. Spec. Tabic 3.1.1)
The "as found" setpoints were:
- a. HI trip at 109
- b. 'HI-HI trip at 120 5 The Dual Trip Unit was recalibrated, and re-tested using the same surveillance test ST 3 2.1, found to be within acceptable limits, and returned to service. ,
e Investigation ~"
The setpoint drif t was found to be wholly within the G. E. Qual Trip Unit which has exhibited drif ting in the past. The observed drift has been in the range of less than 1% per month. No component f ailures were evident.
Corrective Action Since there is no requirement to have these setpoints this close to the upper limit, the ' Instrument Group was directed to reset the trip points to 116% for the HI-HI trip (Scram) and 104% for a HI trip (Rod Block) . This permits a greater drift in the trip unit before a setpoint limit is reached.
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i Safety Implications The Plant Operations Review Committee agreed that this minor drif t in setpoint did not have any safety effect in that with the non-coincident i scram circuits presently installed, the required scram would have occurred on the other channels which were correctly calibrated.
LB-2-3-231D 9/8/73
' During routine instrument surveillance testing on 9/8/73, level switch LB-2-3-2310 was found to be inoperative. This switch is one of four which pro-vide scram inputs on Scram Discharge Volume High Level.
4 Investigation Internal investigation showed that the switch mechanism was binding slightly. Readjustment of the float mechanism succeeded in freeing the switch movement. The trip calibration was then checked using the " calibration check" surveillance procedure ST 2.4.110, and the instrument returned to service.
Corrective Action -
j The other three level switches which provide the same reactor pro-
- tection system input (scram) were checked for binding and for proper
- setpoint and found to be free and acceptable.
! Safety Implications
, According to the Technical Specifications, note 7 to Table 3.1.1, the Scram Discharge Volune High Level switches are one of the four-scram functions required to be operable when the reactor is subcritical and the reactor water temperature is less than 2120F. The other oper- ,
able switches in the scram circuit would have properly-caused a reactor
- scram should discharge volume high level have occured. ?
4 l Very truly yours,. ,,
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- .'h' . Coo mG(ney /
Ass't General Superintendent j G4neration Division 4
i cc: J. P. O'Reilly Director, Region 1 l
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